ML19323J043

From kanterella
Revision as of 12:15, 10 December 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 80-063/03L-0:on 800513,operator Mistakenly Tripped Normal Feeder from 6.9 Kv Unit Board 2B-B W/O Putting Synchroscope Switches to on Position.Loss of Power to 6.9 Kv Shutdown Board 2A-A Resulted.Caused by Operator Error
ML19323J043
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 06/11/1980
From: Record D
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19323J039 List:
References
LER-80-063-03L, LER-80-63-3L, NUDOCS 8006170691
Download: ML19323J043 (2)


Text

. _ - _ _ _- - - _ _ _ _ _ _ _ _ - - - - _ _ - - _ _ _ _ _ _ _ _ _ - - - _ _

t. .. ..? ..

..

..,

, :, -

,

.

,

  • e, .

.

sene FORtt ::64 . U. S. nucle A.1 REGULATORY coWi$$t0N run LICENSEE EVENT REPORT EXHmita coNTRoLOLoCK: l } l l l l 3 .h l (PLE Ast PRINT oR TYPt ALL neoVIRto 'NFORf/Af tfP.t

.

Io Til lT l NIS l N l PI1 !@4l 010 l -l0 l 0 l Ol 0 l 0 l -l 0(bl Ol@l,64IIl1IlI1l@l I l 7 8 9 tsC4Nast COct 84 EsGE%4 8.Weise 4 LiCt'e54 Tvrt 4J 63 ==. ad @

covr . . . . . . .. ... . . . _

101:1 . U',O [JJ@l0 i s i 0101 o h l *> osl 7GI s i ,1,1 21 n i _.i@l oiREPs 3MTOAft 74 i ll il s t 01@ 43

.

7 8 .60 61 C;,C t t T m.u'.,g i g 4J EvtasT DAf t 75 tvENT otscRipTion ANo eaos AsLe coastcutscts @

o a I During the performance of SMI-1-D/G on D/G 2A-A. the operator 1

~ ~

--*-/ g 1 mistakenly tripie~d 'th'e norm'l 7 a feeder fr'om 6.9-kV unit board 2B-B I

'

ITTTl I without putting the synchroscope switches to "ON" position. This caused I s loss o'f power to 6.9-kV shutdown board 2A-A. The blackout signal I o o l causes all D/G's to start. During the recovery, all D/G's were i io p ,l l made inoperable for sa 10 minutes. LCO 3.8.1.1 l FTm I l

' ' '

54 51 t *J CAW' t CAuit CovP- vatet C004 CC:t SUSCCCf CCv70*,t%T CCot SUSCCCE SueCCCI

  • 0 9 I EI EIO LAj@ (A_j@ l C I Kl T IR I R l K l h [,Bj @ [,Z,j h .

7 8 9 64 13 12 93 a4 13 20 STOvf NTI AL oCCuantNCE RE Poav A IV'S'01 PE PORT NO. C001 TYPt No,

@ .,-(=in so 18 101FtytNT L-J Yt AR 10I6131 L<.J LIJ to_]

L2, l.o lli L. J

,

- .

u n 2 as 2,  : 2, n 2 u i

';.'urr

'

C CN 'nWJ.' o'#ET A., ^L'Mra' ,oT,0. '",'JP.cir '

..R.I#n'L

.

10 I olo @101

'

-

LHj@[ ZJ@ LZJ@ Lll@

3J 38 33 e6 3d LYJ@ lliJ@ LZJ@ Iz l'9 l 919 IC 43 el 42 43 44 4, causs cascRipTion ANo conatenvt AcTicss @

li i a l I Operator error caused blackout signal which started all D/G's. I

  • g ; Operator instructed to'be more attentive while performing system i ml operations. I l

1 i a l I

, FTTTI! I

-

a e , s2 STA 5 MPCwtR QTHtatTATU3 Os Ot:Covinv otscwf.ov h l 8 s [Gj @ l Ol0lOl@l N/A l [A_.j@l Operator observation l l A TiveTV CO* TCPs7 l

. A'.'0"JNY CF ACTtve TV LOCATIO'W O8 Rtttast i r. fittC LZJA*t@o 08 pf tC AttLZJ@l N/A I IN/A I I

'7 8 9 au is 44 43

  • 60 i Pt ATONNat t NPO'.uf st" NU' *3 f p TYPT nt %PnPT'04.

li l i; 10 I O f Ol@L zj@l N/A l

' ' '

, f,.sc. t"..odt.c: "

.

m vitn onC nPfiosh fiTl 10101 d@l !?N/A 7 C 'J It &J

!

ttf,0 0F F GJ OA*.*AC.C 10 F ACst.1 f y TWC f t'.LitP f u)q

  • 8, [z_j@l N/A

. . , - ..,

I

.

  • # pg'gfMV i

'

...oc ..bf!L'C,,4 t w..t V, , ,,r.

r,

. LN_j@l N/A I IIIIi!'!Il

. $ io r. , --

'

Nwc cr eiguua,, Dadd J. Record ,yny,; 615-842-5208

._ . -

~

'

'

.

800617gg

-O s cu ns .- a ..;y na...a..; j

. . ,. Sequoych Nuc10 r P1:nt ]

e,"

  1. ' ~ .

,

-

j LER SUPPLEMENTAL INFORMATION I

-l l

l SQRO-50-327/ 8063- Technical Specification Involved 3.8.1.1 1 Reported Under Technical Specification 6.9.1.13.b i

'

Date of Occurrence: 5/13/80 Time of Occurrence: 1320 Un it 1 Identification and Description of Occurrence:

During the performance of SMI-1-D/G on D/G 2A-A, the operator mistakenly tripped the normal feeder from 6.9-kV unit board 2B-B .without putting the synchroscope switches to "0N" position.

This caused loss of power to 6.9-kV shutdown board 2A-A. The blackout signal caused all 4 D/G's to start. During the recovery all D/G's were made inoperable for GE 10 minutes to reset relays.

Conditions Prior to Occurrence:

Unit 1 in Mode 3 RCS Tavg = 5450 F Pressurizer pressure = 2235 psig.

Apparent Cause of Occurrence:

An unclear specific main:enance instruction directed the operator to inadvertently de-energize the shutdown board. This caused all fcur D/G's to start for a blackout signal. The operator failed to

'

recognize this as a station blackout condition and refer to E0I-5 and he subsequently emergency tripped all four D/G's. A ten minute period when all D/G's were inoperable occurred while all lockout relays were being reset.

Analysis of Occurrence:

There was no danger to the public health and safety because there is no radiated fuel onsite.

  • Corrective Action:

,?..- '-

The SMI is being reviewed and revised to prevent a recurrence of inadvertent de-energizing of a shutdown board. Specific steps and signoff will be inserted to prevent this. A section is being added

  • to shutdown board SOI's adapting the station blackout recovery from E01-5 to be used as'a recovery instruction on any emergency start of the D/G's. This instruction leaves the diesels running until all

' relays are reset.

.

Failure Data:

N/A

.- - - - ,

. -

, - - - , ,_- , - . ,,-,-m . ,_c- _ --- , - . , , . . _ . -