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| ==Subject:== | | ==Subject:== |
| Waterford 3 - FINAL Request for Additional Information (RAIs) RE Relief Request WF3-RR-19-2: Alternate Repair of Degraded Drain Line of Chemical and Volume Control System | | Waterford 3 - FINAL Request for Additional Information (RAIs) RE Relief Request WF3-RR-19-2: Alternate Repair of Degraded Drain Line of Chemical and Volume Control System |
| : Maria, By letter dated July 18, 2019 (Agencywide Documents Access and Management System (ADAMS) Accession No. | | : Maria, By letter dated July 18, 2019 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML19199A708), Entergy Operations, Inc. (Entergy or the licensee) requested relief from certain requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME Code), Section XI, IWA-4000, at Waterford Steam Electric Station Unit 3 (Waterford 3). Pursuant to Title 10 of the Code of Federal Regulations (CFR) 50.55a(z)(2), Entergy submitted Alternative WF3-RR-19-2 proposing an alternate repair of the degraded weld in the drain line of the Chemical and Volume Control System (CVCS) on the basis that complying with ASME Code, Section XI, would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety. |
| ML19199A708), Entergy Operations, Inc. (Entergy or the licensee) requested relief from certain requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME Code), Section XI, IWA-4000, at Waterford Steam Electric Station Unit 3 (Waterford 3). Pursuant to Title 10 of the Code of Federal Regulations (CFR) 50.55a(z)(2), Entergy submitted Alternative WF3-RR-19-2 proposing an alternate repair of the degraded weld in the drain line of the Chemical and Volume Control System (CVCS) on the basis that complying with ASME Code, Section XI, would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety. | |
| To complete its review, the NRC staff requests the following additional information. This Request for Additional Information was discussed with Maria Zamber, Paul Wood, John Schrage, and others of your staff on July 19, 2019. | | To complete its review, the NRC staff requests the following additional information. This Request for Additional Information was discussed with Maria Zamber, Paul Wood, John Schrage, and others of your staff on July 19, 2019. |
| Thank you, April Dr. April L. Pulvirenti Project Manager, Waterford Unit 3 United States Nuclear Regulatory Commission Office of Nuclear Reactor Regulation 301-415-1390 | | Thank you, April Dr. April L. Pulvirenti Project Manager, Waterford Unit 3 United States Nuclear Regulatory Commission Office of Nuclear Reactor Regulation 301-415-1390 |
| -------------------
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| : 1. Section 3, Applicable Code Requirement, of the proposed alternative does not discuss the fact that a flaw will remain inservice, which triggers certain provisions in the ASME Code, Section XI. The 2007 Edition through 2008 Addenda of the ASME Code, Section XI, IWA-4422, addresses defect evaluation and examination. In addition, IWC-3132.2 states that: A component containing relevant conditions is acceptable for continued service if the relevant conditions are corrected by a repair /replacement activity or by corrective measures to the extent necessary to meet the acceptance standards of Table IWC-3410-1. Please discuss if IWA-4422 and IWC-3132.2 should be applicable to the proposed relief request. If not, provide justification. | | : 1. Section 3, Applicable Code Requirement, of the proposed alternative does not discuss the fact that a flaw will remain inservice, which triggers certain provisions in the ASME Code, Section XI. The 2007 Edition through 2008 Addenda of the ASME Code, Section XI, IWA-4422, addresses defect evaluation and examination. In addition, IWC-3132.2 states that: A component containing relevant conditions is acceptable for continued service if the relevant conditions are corrected by a repair /replacement activity or by corrective measures to the extent necessary to meet the acceptance standards of Table IWC-3410-1. Please discuss if IWA-4422 and IWC-3132.2 should be applicable to the proposed relief request. If not, provide justification. |
| : 2. Detail 3 of the proposed alternative provides a drawing of the proposed weld overlay. (a) Provide dimensions of approximate thickness and longitudinal length of the weld overlay (Item No. 6 in the drawing). Specifically, provide the weld overlay thickness above the socket weld (Item No. 1 and the elbow (Item No. 3). (b) Provide thickness of socket weld branch connection (Item No. 1), elbow (item no. 3), and seal weld (item No, 5). (c) Provide the vertical length of the 1 | | : 2. Detail 3 of the proposed alternative provides a drawing of the proposed weld overlay. (a) Provide dimensions of approximate thickness and longitudinal length of the weld overlay (Item No. 6 in the drawing). Specifically, provide the weld overlay thickness above the socket weld (Item No. 1 and the elbow (Item No. 3). (b) Provide thickness of socket weld branch connection (Item No. 1), elbow (item no. 3), and seal weld (item No, 5). (c) Provide the vertical length of the 1 |
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Category:E-Mail
MONTHYEARML24241A1922024-08-27027 August 2024 October 2024 Emergency Preparedness Program Inspection - Request for Information ML24159A2672024-06-0707 June 2024 NRR E-mail Capture - NRC Notice of Acceptance: Waterford Steam Electric Station, Unit 3, Licensee Amendment Request (LAR) to Modify Surveillance Requirements in Support of Surveillance Frequency Control Program ML24137A2702024-05-16016 May 2024 NRR E-mail Capture - Entergy Fleet - Acceptance Review of License Amendment Request to Remove Obsolete License Conditions from Operating Licenses for GGNS, RBS, and WF3 (L-2024-LLA-0062) ML24115A0862024-04-23023 April 2024 NRR E-mail Capture - NRC Notice of Acceptance: Waterford Steam Electric Station, Unit 3, Proposed Alternative WF3-RR-24-01 for Examinations of Pressurizer Circumferential and Longitudinal Shell-to-Head Welds and Nozzle-to-Vessel Welds ML24115A0882024-04-23023 April 2024 NRR E-mail Capture - NRC Notice of Acceptance: Waterford Steam Electric Station, Unit 3, Proposed Alternative WF3-RR-24-02 for Examinations of Steam Generator Pressure-Retaining Welds and Full Penetration Welded Nozzles ML24088A0092024-03-27027 March 2024 NRR E-mail Capture - Entergy Fleet - Final Request for Confirmation of Information (RCI) Re Alternative Request EN-RR-22-001 Concerning ASME Code Case N-752 (L-2022-LLR-0054) ML23348A1222023-12-14014 December 2023 NRR E-mail Capture - Grand Gulf, River Bend, and Waterford, Unit 3 - 2nd Round of Official RAIs for RR EN-RR-22-001, Use ASME Code Case N-752, Risk Informed Categorization for Class 2 and 3 Systems ML23097A0412023-04-0606 April 2023 June 2023 Emergency Preparedness Exercise Inspection - Request for Information ML23076A0552023-03-13013 March 2023 EP Program Inspection RFI Hjs 10132022 ML23072A3672023-03-0909 March 2023 NRR E-mail Capture - Entergy Fleet - Acceptance Review of Quality Assurance Program Manual Reduction in Commitment ML23052A0882023-02-17017 February 2023 Inspection Request for Information ML22336A0202022-12-0101 December 2022 NRR E-mail Capture - Acceptance Review for Waterford Unit 3 - License Amendment Request to Revise Technical Specification 3/4.3.2 ML22335A4802022-12-0101 December 2022 NRR E-mail Capture - NRC Update Completion Date for Waterford 3 LAR to Adopt TSTF-505 ML22329A0152022-11-0202 November 2022 NRR E-mail Capture - NRC Update Completion Date for Waterford 3 LAR to Adopt TSTF-505 ML22290A0442022-10-13013 October 2022 December 2022 Emergency Preparedness Program Inspection - Request for Information ML22215A1492022-08-0303 August 2022 NRR E-mail Capture - Waterford 3 - LAR to Permit the Use of Risk-Informed Completion Times in Accordance with Technical Specifications Task Force (TSTF) Traveler TSTF-505, Revision 2 ML22215A2062022-08-0303 August 2022 NRR E-mail Capture - Waterford 3 - LAR to Adopt Title 10 of the Code of Federal Regulations, Section 50.69: Loe and Completion Date Update ML22206A0172022-07-22022 July 2022 NRR E-mail Capture - Request for Additional Information: Waterford 3 - License Amendment Requests to Adopt 10 CFR 50.69 and TSTF-505 ML22206A0152022-07-21021 July 2022 NRR E-mail Capture - Entergy (Grand Gulf, River Bend, and Waterford-3) - Acceptance Review of the RR EN-RR-22-001, Case N-752, Risk-informed Cat & Treatment for Repair/Replacement Activities in Class 2 & 3 Systems ML22209A1082022-07-15015 July 2022 NRR E-mail Capture - Draft RAIs to License Amendment Request for Application to Adopt 10 CFR 50.69 and Revise Technical Specifications to Adopt TSTF-505, Revision 2 ML22144A1662022-05-24024 May 2022 PI&R Request for Information and Transmittal e-mail ML22108A1792022-04-14014 April 2022 WF3 Cpcs Installation Inspection Plan Email ML22209A1062022-01-20020 January 2022 NRR E-mail Capture - (External_Sender) Options Moving Forward Regarding Waterford TSTF-505 and 50.69 ML22209A1052022-01-0606 January 2022 NRR E-mail Capture - Estimate for Completion of 50.69-TSTF-505 Peer Review ML22012A1592022-01-0505 January 2022 WF3 2022 EP Exercise Inspection RFI Sdh 010522 ML21356A5872021-12-22022 December 2021 NRR E-mail Capture - Acceptance for Review: Waterford 3 - Proposed Revision to Reactor Vessel Surveillance Capsule Withdrawal Schedule ML21349A2242021-12-14014 December 2021 NRR E-mail Capture - (External_Sender) Waterford 3 - Request for One-Time Exemption from 10 CFR 50, Appendix E Biennial EP Exercise ML21312A4792021-11-0505 November 2021 Email: NRC Staff Preliminary Questions Regarding X Energy LLC Xe-100 Topical Report: Risk-Informed Performance-Based Licensing Basis Development ML21308A5602021-11-0404 November 2021 NRR E-mail Capture - Arkansas Nuclear One, Units 1 and 2, Grand Gulf, River Bend, and Waterford, Unit 3 - Acceptance Review of LAR to Adopt TSTF-554, Revise Reactor Coolant Leakage Requirements ML21292A0112021-10-18018 October 2021 NRR E-mail Capture - ANO, 1 and 2, Grand Gulf, River Bend, Waterford, 3 - Acceptance Review of LAR to Adopt TSTF-541, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated Position ML21280A0812021-10-0505 October 2021 Email 10-5-21 - Request for Information_ Waterford EP Inspection (71114.04 & 71151) - Nov-Dec 2021 ML21285A0242021-10-0505 October 2021 Digital Instrumentation and Control Modification Inspection Request for Information ML22112A1512021-08-0606 August 2021 NRR E-mail Capture - for Review: Draft RAIs to LAR to Relocate Chemical Detection Systems Technical Specifications (TS) to Technical Requirements Manual (TRM) ML21216A4562021-08-0404 August 2021 WF3 2021 EP Exercise Inspection Request for Information (RFI) ML21218A0402021-07-26026 July 2021 NRR E-mail Capture - Final RAIs to Entergy Operations, Waterford Steam Electric Station, Unit 3 LAR to Adopt 10 CFR 50.69 ML21201A0062021-07-19019 July 2021 NRR E-mail Capture - Arkansas Nuclear One, Units 1 and 2, and Waterford, Unit 3 - Acceptance Review of LAR to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections ML21173A1082021-06-22022 June 2021 NRR E-mail Capture - Acceptance Review for Waterford Unit 3 - License Amendment Request to Adopt TSTF-563 ML21174A0342021-06-22022 June 2021 NRR E-mail Capture - Entergy Fleet (ANO, Ggulf, Rbend, & Waterford) - Acceptance Review for Relief Request to Use a Provision of a Later Edition of the ASME Code, Section XI for Periodic System Pressure Tests Exemptions ML21160A0852021-06-0404 June 2021 NRR E-mail Capture - (External_Sender) NRC Notification to the State of Louisiana Regarding a Waterford Steam Electric Station, Unit 3 Amendment - Digital Upgrade I&C ML21145A0062021-05-24024 May 2021 NRR E-mail Capture - Supplement Received - Waterford Unit 3 - License Amendment Request for Boration Systems Tech Specs ML21120A1192021-04-30030 April 2021 NRR E-mail Capture - Acceptance Review for Waterford Unit 3 - LAR to Relocate Chemical Detection TSs to TRM ML21105A0512021-04-14014 April 2021 4-14-21 Email - RFI for In-Office Inspection of Recent WF3 Submission of EAL Procedure Revision ML21104A0382021-04-13013 April 2021 NRR E-mail Capture - Acceptance Review for Waterford Unit 3 - License Amendment Request for TSTF-505 ML21084A2552021-03-22022 March 2021 NRR E-mail Capture - Supplement to Audit Plan Dated October 1, 2020 (Waterford 3, L-2020-LLA-0164) ML21088A1512021-03-15015 March 2021 NRR E-mail Capture - Draft Waterford Acceptance Review Letter for TSTF-505 LAR ML21069A1842021-03-0202 March 2021 NRR E-mail Capture - Announcement of QA Inspection ML21040A3892021-02-0808 February 2021 NRR E-mail Capture - Announcement of QA Inspection ML21039A6412021-01-28028 January 2021 NRR E-mail Capture - NRC LIC-109 Acceptance Review Results for Waterford 3 50.69 LAR ML21022A1692021-01-22022 January 2021 NRR E-mail Capture - Entergy Fleet (ANO, Grand Gulf, River Bend, and Waterford) - Acceptance Review for RR EN-20-RR-003, Proposed Alternative to Use ASME Code Case N-711-2 ML20329A1442020-11-20020 November 2020 Terrapower QAPD Preliminary Questions Email 2024-08-27
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARML24150A3852024-06-0404 June 2024 Notification of an NRC Fire Protection Baseline Inspection (NRC Inspection Report 05000382/2024011) and Request for Information ML24088A0092024-03-27027 March 2024 NRR E-mail Capture - Entergy Fleet - Final Request for Confirmation of Information (RCI) Re Alternative Request EN-RR-22-001 Concerning ASME Code Case N-752 (L-2022-LLR-0054) ML23348A1222023-12-14014 December 2023 NRR E-mail Capture - Grand Gulf, River Bend, and Waterford, Unit 3 - 2nd Round of Official RAIs for RR EN-RR-22-001, Use ASME Code Case N-752, Risk Informed Categorization for Class 2 and 3 Systems ML23191A4562023-07-10010 July 2023 Notification of Comprehensive Engineering Team Inspection (050003822023010) and Request for Information ML23097A0412023-04-0606 April 2023 June 2023 Emergency Preparedness Exercise Inspection - Request for Information ML23076A0552023-03-13013 March 2023 EP Program Inspection RFI Hjs 10132022 ML23052A0882023-02-17017 February 2023 Inspection Request for Information ML22290A0442022-10-13013 October 2022 December 2022 Emergency Preparedness Program Inspection - Request for Information ML22206A0172022-07-22022 July 2022 NRR E-mail Capture - Request for Additional Information: Waterford 3 - License Amendment Requests to Adopt 10 CFR 50.69 and TSTF-505 ML22209A1082022-07-15015 July 2022 NRR E-mail Capture - Draft RAIs to License Amendment Request for Application to Adopt 10 CFR 50.69 and Revise Technical Specifications to Adopt TSTF-505, Revision 2 ML22103A1712022-04-13013 April 2022 LAR to Revise TS to Adopt TSTF-505_NRC Request for Additional Information ML22012A1592022-01-0505 January 2022 WF3 2022 EP Exercise Inspection RFI Sdh 010522 ML21285A0242021-10-0505 October 2021 Digital Instrumentation and Control Modification Inspection Request for Information ML21280A0812021-10-0505 October 2021 Email 10-5-21 - Request for Information_ Waterford EP Inspection (71114.04 & 71151) - Nov-Dec 2021 ML22112A1512021-08-0606 August 2021 NRR E-mail Capture - for Review: Draft RAIs to LAR to Relocate Chemical Detection Systems Technical Specifications (TS) to Technical Requirements Manual (TRM) ML21216A4562021-08-0404 August 2021 WF3 2021 EP Exercise Inspection Request for Information (RFI) ML21218A0402021-07-26026 July 2021 NRR E-mail Capture - Final RAIs to Entergy Operations, Waterford Steam Electric Station, Unit 3 LAR to Adopt 10 CFR 50.69 ML21196A5302021-07-19019 July 2021 Wat 2021010 RFI Letter 21N_05 Gap ML21195A0692021-07-13013 July 2021 Staton, Unit 3 - Notification of Digital Instrumentation and Control Modification Inspection and Request for Information ML21125A6522021-05-0606 May 2021 Wat 2021003 Brq RFI- Md, Waterford Steam Electric Station, Unit 3, Notification of Inspection (NRC Inspection Report 05000382/2021003) and Request for Information ML21112A2542021-04-29029 April 2021 Request for Additional Information Digital Upgrade to the Core Protection and Control Element Assembly Calculator System (EPID L 2020 Lla 0164) - Redacted Version ML20288A2082020-10-0808 October 2020 8Oct2020 Email - Request for Information (RFI) to Support and Prepare for the Emergency Preparedness (EP) Program Inspection at the Waterford 3 Station Scheduled to Occur the Week of December 7, 2020 ML20289A3502020-10-0505 October 2020 NRR E-mail Capture - NRC Request for Additional Information - WF3 EAL Scheme Change - L-2020-LLA-0122 ML20125A3212020-05-0404 May 2020 WAT2020410 Inspection Document Request ML20086M3852020-04-0101 April 2020 Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3/4 8.1, A.C. Sources Operating W3F1-2020-0014, Response to U. S. Nuclear Regulatory Commission Request for Additional Information Regarding Application for Technical Specification Change to Control Room Air Conditioning System2020-03-20020 March 2020 Response to U. S. Nuclear Regulatory Commission Request for Additional Information Regarding Application for Technical Specification Change to Control Room Air Conditioning System ML20049A4102020-02-20020 February 2020 Request for Additional Information Regarding License Amendment Request to Revise Surveillance Requirement 4.7.6.1.d, Control Room Air Filtration System ML19262H0362019-09-0404 September 2019 Ti 2515/194 Request for Information and Email ML19274D4932019-07-24024 July 2019 Request for Information IR 05000382 2019-003 Occupational Radiation Safety Inspection ML19203A0062019-07-19019 July 2019 NRR E-mail Capture - Waterford 3 - Final Request for Additional Information (Rais) Re Relief Request WF3-RR-19-2: Alternate Repair of Degraded Drain Line of Chemical and Volume Control System ML19151A6102019-06-0404 June 2019 Non-Proprietary Second Round RAI Regarding License Amendment Request for Use of the Tranflow Code for Determining Pressure Drops Across the Steam Generator Secondary Side Internal Components ML19172A0852019-05-24024 May 2019 NRR E-mail Capture - Waterford 3 - Final Request for Additional Information (Rais) Re Relief Request W3-ISI-032: Volumetric Examination Requirements ML19035A0412019-02-0101 February 2019 NRR E-mail Capture - Waterford 3 - Final Request for Information Regarding Relief Request WF3-RR-19-001 for Application of Dissimilar Metal Weld Full Structural Weld Overlay ML19018A0102019-01-28028 January 2019 Request for Additional Information Regarding License Amendment Request for Revision of Technical Specification 3/4.7.4,Ultimate Heat Sink ML18320A0902018-11-26026 November 2018 Request for Additional Information Regarding License Amendment Request for Use of the Transflow Code for Determining Pressure Drops Across the Steam Generator Secondary Side Internal Components ML18318A4352018-11-14014 November 2018 NRR E-mail Capture - Waterford 3 - Final Request for Additional Information Regarding Request for Alternative to ASME Code Case N-770-2 ML18299A0862018-11-0707 November 2018 Draft Request for Additional Information License Amendment Request Regarding the Revision of UFSAR Section 3.9 ML18262A0412018-09-25025 September 2018 Request for Additional Information Regarding License Amendment Request to Revise Section 15.4.3.1 of the Waterford 3 Updated Final Safety Analysis Report to Account for Fuel Misload ML18145A2652018-06-0101 June 2018 Supplemental Information Needed for Acceptance of Request for Licensing Action Use of Tranflow Code for Determining Pressure Drops Across Steam Generator Secondary Side Components ML18085A6942018-03-26026 March 2018 Ref: Waterford Steam Electric Station, Unit 3, License Renewal Application - RAI Set 18 ML18058A0572018-02-23023 February 2018 Enclosurequest for Additional Information (Letter to J. Giddens Request for Additional Information Regarding Entergy Operations, Inc.'S Decommissioning Funding Plan Update) ML18039A9722018-02-0808 February 2018 Notification of Evaluations of Changes, Tests, and Experiments Inspection (05000382/2018002) and Request for Information ML17233A2402017-08-14014 August 2017 NRR E-mail Capture - Draft RAI for Waterford Unit 3 Regarding License Amendment Request to Adopt TSTF-501 Relocate Stored Fuel Oil and Lube Oil Volume Values to Licensee Control ML17170A3012017-06-16016 June 2017 Notification of Inspection (NRC Integrated Inspection Report 05000382/2017003) and Request for Information ML17101A4432017-04-17017 April 2017 Requests for Additional Information for the Review of the Waterford Steam Electric Station, Unit 3, License Renewal Application - Set 17 ML17086A5852017-03-28028 March 2017 Request for Additional Information for the Environmental Review of Waterford 3 ML17072A0102017-03-14014 March 2017 Requests for Additional Information for the Review of the Waterford Steam Electric Station, Unit 3, License Renewal Application Set - 15 ML17272A3352017-03-0101 March 2017 Request for Additional Information for the Review of the Waterford Steam Electric Station, Unit 3, License Renewal Application - Set 14 ML17040A5382017-02-14014 February 2017 Requests for Additional Information for the Review of the Waterford Steam Electric Station, Unit 3, License Renewal Application - Set 13 ML17018A3592017-01-26026 January 2017 Requests For Additional Information For The Review Of The Waterford Steam Electric Station, Unit 3, License Renewal Application Set 12 (CAC MF7492.) 2024-06-04
[Table view] |
Text
NRR-DRMAPEm Resource From: Pulvirenti, April Sent: Friday, July 19, 2019 5:36 PM To: Zamber, Maria Cc: Davis, Robert; Tsao, John; Buford, Angela; Wengert, Thomas; Singal, Balwant
Subject:
Waterford 3 - FINAL Request for Additional Information (RAIs) RE Relief Request WF3-RR-19-2: Alternate Repair of Degraded Drain Line of Chemical and Volume Control System
- Maria, By letter dated July 18, 2019 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML19199A708), Entergy Operations, Inc. (Entergy or the licensee) requested relief from certain requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME Code),Section XI, IWA-4000, at Waterford Steam Electric Station Unit 3 (Waterford 3). Pursuant to Title 10 of the Code of Federal Regulations (CFR) 50.55a(z)(2), Entergy submitted Alternative WF3-RR-19-2 proposing an alternate repair of the degraded weld in the drain line of the Chemical and Volume Control System (CVCS) on the basis that complying with ASME Code,Section XI, would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety.
To complete its review, the NRC staff requests the following additional information. This Request for Additional Information was discussed with Maria Zamber, Paul Wood, John Schrage, and others of your staff on July 19, 2019.
Thank you, April Dr. April L. Pulvirenti Project Manager, Waterford Unit 3 United States Nuclear Regulatory Commission Office of Nuclear Reactor Regulation 301-415-1390
- 1. Section 3, Applicable Code Requirement, of the proposed alternative does not discuss the fact that a flaw will remain inservice, which triggers certain provisions in the ASME Code,Section XI. The 2007 Edition through 2008 Addenda of the ASME Code,Section XI, IWA-4422, addresses defect evaluation and examination. In addition, IWC-3132.2 states that: A component containing relevant conditions is acceptable for continued service if the relevant conditions are corrected by a repair /replacement activity or by corrective measures to the extent necessary to meet the acceptance standards of Table IWC-3410-1. Please discuss if IWA-4422 and IWC-3132.2 should be applicable to the proposed relief request. If not, provide justification.
- 2. Detail 3 of the proposed alternative provides a drawing of the proposed weld overlay. (a) Provide dimensions of approximate thickness and longitudinal length of the weld overlay (Item No. 6 in the drawing). Specifically, provide the weld overlay thickness above the socket weld (Item No. 1 and the elbow (Item No. 3). (b) Provide thickness of socket weld branch connection (Item No. 1), elbow (item no. 3), and seal weld (item No, 5). (c) Provide the vertical length of the 1
socket fillet weld (Item No. 4). Approximate or estimated dimensions for these items is acceptable, if the as-built dimensions are not available.
- 3. Page 4 of 9, under heading Structural evaluation, states that the allowable through-wall flaw is 1.7 inches (41% of the pipe circumference). (a) Discuss either how the allowable flaw size is derived or submit the flaw evaluation. (b) The NRC staff assumes that vibration in the drain line will continue after the weld overlay installation and the existing flaw may continue to grow. As such, discuss, in a qualitative manner, the crack growth of the existing pipe between now and refueling outage 23.
- 4. Section 4, Reason for Request, states that the degradation mechanism is attributed to low cycle/high stress (vibration) fatigue. After the weld overlay is applied, the flaw may still grow based on vibration. (a) Discuss whether compensatory measures will be taken to reduce the vibration of the drain line to minimize crack growth. (b) Discuss the operational leakage limits in Technical Specifications for the drain line. (c) Discuss the leakage detection system(s) that can detect potential leakage of the overlaid drain line in case the weld overlay degrades, (d) Discuss whether the drain line is located inside or outside the containment.
- 5. Section 6, Duration of Proposed Alternative, provide the approximate scheduled start date for Refueling Outage 23.
- 6. Table 2 of the calculation in the relief request shows the following minimum required thickness for the weld overlay:
Loading Condition Minimum Required Thickness (inch)
Equation 3- Hoop Stress, Pressure 0.004 Equation 8- Sustained Load-Deadweight 0.008 Equation 9- Occasional Load - OBE, Seismic 0.013 Equation 10- Thermal Expansion 0.021 (a) The licensees analysis shows that the minimum required thickness for the weld overlay is 0.021 inches. The licensee did not calculate the minimum required thickness caused by mechanical vibration. Discuss why the minimum required thickness was not calculated based on mechanical vibration.
(b) The licensee states that the ASME Code,Section III, NC-3652.3 requires only Equation 10 or Equation 11 to be met, not both. The licensee did not calculate the minimum required thickness per Equation 11. If the minimum required thickness per Equation 11 is greater than Equation 10, it seems that the thickness calculated from Equation 11 should be used as the minimum required thickness. Discuss why the minimum required thickness was not calculated using Equation 11.
(c) During the plant normal operation, the drain line will experience stresses caused by pressure, deadweight, temperature, and occasional vibration. It seems that the minimum required thickness of the weld overlay should include the contribution of the required thickness from pressure, deadweight, thermal expansion and vibration.
Discuss whether the minimum weld overlay thickness should be 0.046 inches (0.004 + 0.008 + 0.013 + 0.021).
- 7. Code Case N-666-1, paragraph 5(c) states that: A system leakage test shall be performed in accordance with IWA-4540 The licensee did not take exception to this provision; therefore, the NRC staff assumes that the licensee will perform the system leakage test. However, the NRC staff is not clear how a system leakage test can be performed in accordance with IWA-4540 while the plant is online. Discuss how a system leakage test can be performed in accordance with IWA-4540.
2
Hearing Identifier: NRR_DRMA Email Number: 130 Mail Envelope Properties (BN6PR09MB224260E6D034A9C7BB5049DC8FCB0)
Subject:
Waterford 3 - FINAL Request for Additional Information (RAIs) RE Relief Request WF3-RR-19-2: Alternate Repair of Degraded Drain Line of Chemical and Volume Control System Sent Date: 7/19/2019 5:36:02 PM Received Date: 7/19/2019 5:36:00 PM From: Pulvirenti, April Created By: April.Pulvirenti@nrc.gov Recipients:
"Davis, Robert" <Robert.Davis@nrc.gov>
Tracking Status: None "Tsao, John" <John.Tsao@nrc.gov>
Tracking Status: None "Buford, Angela" <Angela.Buford@nrc.gov>
Tracking Status: None "Wengert, Thomas" <Thomas.Wengert@nrc.gov>
Tracking Status: None "Singal, Balwant" <Balwant.Singal@nrc.gov>
Tracking Status: None "Zamber, Maria" <mzamber@entergy.com>
Tracking Status: None Post Office: BN6PR09MB2242.namprd09.prod.outlook.com Files Size Date & Time MESSAGE 5980 7/19/2019 5:36:00 PM Options Priority: Standard Return Notification: No Reply Requested: No Sensitivity: Normal Expiration Date:
Recipients Received: