ML19263D352: Difference between revisions
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LICENSEE EVENT REPORT EXHIBIT A CONTROLBLOCK-l l l l l l lh (PLE ASE PRINT OR TYPE ALL R EOutRED INFORMATION) 7 e i 8 9 j AlRlAl Nl0l 2lglh 0l0 l-l0 l0l 0} 0l0 - l0l0 lgp3 l1 l 1 l1 l l jgl l gg la UC ENSE Novt'E *= 25 20 JO b i C A f bei LICENSEE CODE uctNLE I v ri. | LICENSEE EVENT REPORT EXHIBIT A CONTROLBLOCK-l l l l l l lh (PLE ASE PRINT OR TYPE ALL R EOutRED INFORMATION) 7 e i 8 9 j AlRlAl Nl0l 2lglh 0l0 l-l0 l0l 0} 0l0 - l0l0 lgp3 l1 l 1 l1 l l jgl l gg la UC ENSE Novt'E *= 25 20 JO b i C A f bei LICENSEE CODE uctNLE I v ri. | ||
CON'T 71 1 Sl @p l3Mf'OH1 p 12 l 719 l@ | CON'T 71 1 Sl @p l3Mf'OH1 p 12 l 719 l@ | ||
ol' s!.3"J60LL_)@l0 i s oCOCL 101013 l 6 18l@:1 l1 lEVENT 0 l DATE 7 8 61 E T %MBER -4 63 74 75 CATE 80 EVFNT DESCRIPTION AND PROBAOLE CONSEQUENCES h o 2 i During testing of the Main Steam line code safety valves, executing a i o 2 l coatrolled steam lift, it was disecvered that the varn ring lockpin had I o Ai ibroken on four separate occasions. 2PSV1002 lockpin broke on 11/7/78 and; n s l11/20/78. 2PSV1052 lockpin broke twice on 11/21/78. The relieving ; | ol' s!.3"J60LL_)@l0 i s oCOCL 101013 l 6 18l@:1 l1 lEVENT 0 l DATE 7 8 61 E T %MBER -4 63 74 75 CATE 80 EVFNT DESCRIPTION AND PROBAOLE CONSEQUENCES h o 2 i During testing of the Main Steam line code safety valves, executing a i o 2 l coatrolled steam lift, it was disecvered that the varn ring lockpin had I o Ai ibroken on four separate occasions. 2PSV1002 lockpin broke on 11/7/78 and; n s l11/20/78. 2PSV1052 lockpin broke twice on 11/21/78. The relieving ; | ||
O g, Icapacity of the remaining safety valves exceeded that required for safe , | O g, Icapacity of the remaining safety valves exceeded that required for safe , | ||
Line 29: | Line 28: | ||
7 R 9 SJ S YS I E.M CAUSE CAUSE 8:O"r cAtyt CODE LC CE SUBCODE L's'.*0NE NT CouE v ' .) se ,, aCGt.:E o 9 8 | 7 R 9 SJ S YS I E.M CAUSE CAUSE 8:O"r cAtyt CODE LC CE SUBCODE L's'.*0NE NT CouE v ' .) se ,, aCGt.:E o 9 8 | ||
l C lC l@ [ Bj@ Ql@ l ViA l L JV [ E lX l@ [Pjg [3J@ | l C lC l@ [ Bj@ Ql@ l ViA l L JV [ E lX l@ [Pjg [3J@ | ||
9 10 9 13 | 9 10 9 13 7 11 12 's S E QU E N T t A:. Ocap nr dE CCH r RE s *SiuN | ||
7 11 12 's S E QU E N T t A:. Ocap nr dE CCH r RE s *SiuN | |||
. EVENT VE AR REPORT NG COcc tvpg N3 | . EVENT VE AR REPORT NG COcc tvpg N3 | ||
@ lLE 4g R hO l217 [9 22 l | @ lLE 4g R hO l217 [9 22 l | ||
Line 50: | Line 47: | ||
!i o l Failure va's determined to be a result of the lockpin's fragility. The ; | !i o l Failure va's determined to be a result of the lockpin's fragility. The ; | ||
1i Ii l i lockpins on all Main Steam safety valves vere replaced with cne of a , | 1i Ii l i lockpins on all Main Steam safety valves vere replaced with cne of a , | ||
2 istronger and core reliable design (see Sketch 1 of Attachment). , | 2 istronger and core reliable design (see Sketch 1 of Attachment). , | ||
i 3 1 i i 4 I l | i 3 1 i i 4 I l F ACollTV - | ||
F ACollTV - | |||
ME THOD OF STATUS 'L POWE R OTHEM sT ATUS Dr$ cob f HY Ut%QV E H Y DE O(HIP ItQN N 7 | ME THOD OF STATUS 'L POWE R OTHEM sT ATUS Dr$ cob f HY Ut%QV E H Y DE O(HIP ItQN N 7 | ||
iis Lil@ l Oi 0101@l 'sNA ': a I L e | iis Lil@ l Oi 0101@l 'sNA ': a I L e | ||
Line 62: | Line 56: | ||
45 gg | 45 gg | ||
[ | [ | ||
PEH5CNNEL EXPOSURES NUM9 E P TYPE DE SD4rPT*ON i - j | PEH5CNNEL EXPOSURES NUM9 E P TYPE DE SD4rPT*ON i - j 10 I of Oi@LZJ@L..NA | ||
10 I of Oi@LZJ@L..NA | |||
* ' PEnsONNA',Nm'4Es '' so | * ' PEnsONNA',Nm'4Es '' so | ||
~UveEn etSCa,Pno~@ | ~UveEn etSCa,Pno~@ | ||
Line 70: | Line 62: | ||
LCSL GF OA O AV AGE TO F ACiLity tvPE D E SC A'P f lON l i l o11l9[JJ@l10 NA l 7 | LCSL GF OA O AV AGE TO F ACiLity tvPE D E SC A'P f lON l i l o11l9[JJ@l10 NA l 7 | ||
PUBLIC! T Y DESC p.P T EON 46 NNC USI { NLY I 7 I o I '$sVEDLE.181 NA 1 i iiiiiii iiiI | PUBLIC! T Y DESC p.P T EON 46 NNC USI { NLY I 7 I o I '$sVEDLE.181 NA 1 i iiiiiii iiiI | ||
,s.e og ,ng,,n t ,, Chris N. Shively ,,,g, , | ,s.e og ,ng,,n t ,, Chris N. Shively ,,,g, , | ||
551/96S-2519 790327o%fs5 | 551/96S-2519 790327o%fs5 | ||
: 1. Reportable Occurrence Report No. 50-368/79-020 | : 1. Reportable Occurrence Report No. 50-368/79-020 | ||
: 2. Report Date: 03/22/79 3. Occurrence Date: 11/7/78 4 Facility: Arkansas Nuclear One - Unit Two Russellville, Arkansas 72801 | : 2. Report Date: 03/22/79 3. Occurrence Date: 11/7/78 4 Facility: Arkansas Nuclear One - Unit Two Russellville, Arkansas 72801 | ||
Line 86: | Line 74: | ||
The Main Steam Line C cde Safety Valves were being treated by increasing the Main Steam pressure to the valve lift setpoint, thus verifying proper adjustment and blowback. On four separate occasions, it..was discovered that the warn ring lockpin had broken. On 11/7/78 and 11/20/78, the lockpin broke on 2PSV1002. The lockpin in 2PSV1052 broke twice on 11/21/78. | The Main Steam Line C cde Safety Valves were being treated by increasing the Main Steam pressure to the valve lift setpoint, thus verifying proper adjustment and blowback. On four separate occasions, it..was discovered that the warn ring lockpin had broken. On 11/7/78 and 11/20/78, the lockpin broke on 2PSV1002. The lockpin in 2PSV1052 broke twice on 11/21/78. | ||
Reportabic Occurrence Report No. 50-368/79-020 | Reportabic Occurrence Report No. 50-368/79-020 | ||
: 8. Designation of Apparent Cause of Occurrence: | : 8. Designation of Apparent Cause of Occurrence: | ||
Line 98: | Line 84: | ||
:1s sured. The failure occurred during Mode 3 operation, prior to initial criticality. The relieving capacity of the remaining safety valves always exceeded that required for safe operation, as dictated by T.S. Table 3.7.-l. | :1s sured. The failure occurred during Mode 3 operation, prior to initial criticality. The relieving capacity of the remaining safety valves always exceeded that required for safe operation, as dictated by T.S. Table 3.7.-l. | ||
w Reportable Occurrence Report So. 50-368/79-020 | |||
w | |||
Reportable Occurrence Report So. 50-368/79-020 | |||
: 10. Corrective Action: | : 10. Corrective Action: | ||
Upon discovery of the failure, the lechpin was replaced with one of similar design until 11/21/78. At the end of testing, 2?SV1052, 2?SV1055 and 2?SV1056 vere gagged because lockpins had been used for replacements in other valves. On 11/28/78, the Icekpins were replaced in all of the Main Steas Line Code Safety Valves with one of a stronger and cere reliable design (see Sketch 1). | Upon discovery of the failure, the lechpin was replaced with one of similar design until 11/21/78. At the end of testing, 2?SV1052, 2?SV1055 and 2?SV1056 vere gagged because lockpins had been used for replacements in other valves. On 11/28/78, the Icekpins were replaced in all of the Main Steas Line Code Safety Valves with one of a stronger and cere reliable design (see Sketch 1). | ||
: 11. Failure Data: | : 11. Failure Data: | ||
Other occurrences involving the Main Stea= Safety Valves are 50-368/79-019 and 50-368/78-010; however, they are not similar. | Other occurrences involving the Main Stea= Safety Valves are 50-368/79-019 and 50-368/78-010; however, they are not similar. | ||
LER To- 368 /79 - ozo | LER To- 368 /79 - ozo | ||
;- ___.$kelcki NEW LocKPlWS Ned lockpins, Were instdied u.nder 70-5011-1 4 tested by (;ftin3 2PSV -t002 wndev 70-5o30-2 The neW . 1 ockpins are a beefed up, neQ desbA Which a.re sbrtger and. Will be more relio.ble. | |||
;- ___.$kelcki NEW LocKPlWS Ned lockpins, Were instdied u.nder 70-5011-1 4 | |||
tested by (;ftin3 2PSV -t002 wndev 70-5o30-2 The neW . 1 ockpins are a beefed up, neQ desbA Which a.re sbrtger and. Will be more relio.ble. | |||
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Latest revision as of 19:36, 1 February 2020
ML19263D352 | |
Person / Time | |
---|---|
Site: | Arkansas Nuclear |
Issue date: | 03/22/1979 |
From: | Shively C ARKANSAS POWER & LIGHT CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
Shared Package | |
ML19263D333 | List: |
References | |
LER-79-020-01T, LER-79-20-1T, NUDOCS 7903270485 | |
Download: ML19263D352 (5) | |
Text
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NRC FORM 366 U. S. NUCLE AR REGUL ATORY COMMISSION (7 77)
LICENSEE EVENT REPORT EXHIBIT A CONTROLBLOCK-l l l l l l lh (PLE ASE PRINT OR TYPE ALL R EOutRED INFORMATION) 7 e i 8 9 j AlRlAl Nl0l 2lglh 0l0 l-l0 l0l 0} 0l0 - l0l0 lgp3 l1 l 1 l1 l l jgl l gg la UC ENSE Novt'E *= 25 20 JO b i C A f bei LICENSEE CODE uctNLE I v ri.
CON'T 71 1 Sl @p l3Mf'OH1 p 12 l 719 l@
ol' s!.3"J60LL_)@l0 i s oCOCL 101013 l 6 18l@:1 l1 lEVENT 0 l DATE 7 8 61 E T %MBER -4 63 74 75 CATE 80 EVFNT DESCRIPTION AND PROBAOLE CONSEQUENCES h o 2 i During testing of the Main Steam line code safety valves, executing a i o 2 l coatrolled steam lift, it was disecvered that the varn ring lockpin had I o Ai ibroken on four separate occasions. 2PSV1002 lockpin broke on 11/7/78 and; n s l11/20/78. 2PSV1052 lockpin broke twice on 11/21/78. The relieving ;
O g, Icapacity of the remaining safety valves exceeded that required for safe ,
a i l operation, as dictated by T.S. Table 3 7.1. ReportableperT.S.6.91.3.({}.
o e 1 No similar occurrences. ;
7 R 9 SJ S YS I E.M CAUSE CAUSE 8:O"r cAtyt CODE LC CE SUBCODE L's'.*0NE NT CouE v ' .) se ,, aCGt.:E o 9 8
l C lC l@ [ Bj@ Ql@ l ViA l L JV [ E lX l@ [Pjg [3J@
9 10 9 13 7 11 12 's S E QU E N T t A:. Ocap nr dE CCH r RE s *SiuN
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!i o l Failure va's determined to be a result of the lockpin's fragility. The ;
1i Ii l i lockpins on all Main Steam safety valves vere replaced with cne of a ,
2 istronger and core reliable design (see Sketch 1 of Attachment). ,
i 3 1 i i 4 I l F ACollTV -
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PUBLIC! T Y DESC p.P T EON 46 NNC USI { NLY I 7 I o I '$sVEDLE.181 NA 1 i iiiiiii iiiI
,s.e og ,ng,,n t ,, Chris N. Shively ,,,g, ,
551/96S-2519 790327o%fs5
- 1. Reportable Occurrence Report No. 50-368/79-020
- 2. Report Date: 03/22/79 3. Occurrence Date: 11/7/78 4 Facility: Arkansas Nuclear One - Unit Two Russellville, Arkansas 72801
- 5. Identification of Occurrence:
Performance of Main Steam Line Code Safety Valves that required remedial action and corrective measures to prevent operation in a manner less conservative than that assumed in the accident analysis in the SAR or T.S. bases. Occurrence is reportable per T.S.6.9.1.8(i).
- 6. Coiditions Prior to Occurrence:
Steady-State Power Reactor Power 0 MWth Hot Standby X Net Output 0 MWe Cold Shutdown Percent of Full Power 0 %
Refueling Shutdown Load Changes During Routine Power Operation Routine Startup Operation Routine Shutdown Operation Other (specify)
- 7. Description of Occurrence:
The Main Steam Line C cde Safety Valves were being treated by increasing the Main Steam pressure to the valve lift setpoint, thus verifying proper adjustment and blowback. On four separate occasions, it..was discovered that the warn ring lockpin had broken. On 11/7/78 and 11/20/78, the lockpin broke on 2PSV1002. The lockpin in 2PSV1052 broke twice on 11/21/78.
Reportabic Occurrence Report No. 50-368/79-020
- 8. Designation of Apparent Cause of Occurrence:
Design X Procedure bbnufacture Unusual Service Condition Including Environmental Installation /
Const ruction Component Failure (See Failure Data)
Operator Other (specify)
Failure was determined to be a result of the lockpin's fragility.
- 9. Analysis of Occurrence:
The lockpin function is to maintain the warn ring adjustment. With the lockpin broken, the relief setpoint for each valve could not be
- 1s sured. The failure occurred during Mode 3 operation, prior to initial criticality. The relieving capacity of the remaining safety valves always exceeded that required for safe operation, as dictated by T.S. Table 3.7.-l.
w Reportable Occurrence Report So. 50-368/79-020
- 10. Corrective Action:
Upon discovery of the failure, the lechpin was replaced with one of similar design until 11/21/78. At the end of testing, 2?SV1052, 2?SV1055 and 2?SV1056 vere gagged because lockpins had been used for replacements in other valves. On 11/28/78, the Icekpins were replaced in all of the Main Steas Line Code Safety Valves with one of a stronger and cere reliable design (see Sketch 1).
- 11. Failure Data:
Other occurrences involving the Main Stea= Safety Valves are 50-368/79-019 and 50-368/78-010; however, they are not similar.
LER To- 368 /79 - ozo
- - ___.$kelcki NEW LocKPlWS Ned lockpins, Were instdied u.nder 70-5011-1 4 tested by (;ftin3 2PSV -t002 wndev 70-5o30-2 The neW . 1 ockpins are a beefed up, neQ desbA Which a.re sbrtger and. Will be more relio.ble.
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