ML19263D343

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LER 78-015/01T-1 on 781107:following Discovery of Improper Speed Switch in a Emergency Diesel Generator,Instrument Technician Installed Replacement Switch W/O Approved Job Order.Caused by Personnel Error
ML19263D343
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 03/22/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19263D333 List:
References
LER-78-015-01T, LER-78-15-1T, NUDOCS 7903270477
Download: ML19263D343 (4)


Text

NRC FORM 366 U S NUCLE AR REGULATORY COMMISSION (7 77)

LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCC l l l l I I lh (PLEASE PRINT OR TYPE ALL REQQ1 RED INFORMATION)

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s+F #0Ri O ATE gig SG EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h o 2 i Followine the discoverv of an introrer sreed switch in the "A" I g , ; Energency Diesel Generator (see LER 50-363/78-013), an instrument ,

lo l4 l l technician installed the replacement switch without having his Job l c s i Order approved by the shift supervisor as required by Operating i

!o 1s } l Procedure 100h.1h. 'n'ith the shift supervisor unaware of the "A" l 0 , l Diesel being out of service, neither the "A" o. "B" riesels were ,

O , I tested as recuired, violating T.S.3.8.1.(b) Reportable per T.s.6.9.1.j(b) .

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43 a4 er CauSE osSCn.rTicN AND CORREC flVE ACTIONS i O l The instrument technician forgot to obtain the shift supervisor's ,

t i iii 1 antroval before becinning work. He was re-instructed on the i 2 1 trocessing of Job Orders. The "A" Diesel Generatcr was successfully

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1. Reportabic Occurrence Report No. 50-368/78-15
2. Report Date: 03/22/79 3. Occurrence Date: 11/08/78 4 Facility: Arkansas Nuclear One - Unit 2 Russellville, Arkansas
5. Identification of Occurrence:

Diesel generators were not tested as required by Technical Specifications due to non-compliance to operating procedures.

6. Conditions Prior to Occurrence:

Steady-State Power Reactor Power o MWth liot Stand.v Net Output , o MWe Cold Shutdown Percent of Full Power o  %

Refueling Shutdown Load Changes During Routine Power Operation o Routine Startup Operation Routine Shutdown Operation Other (specify) X Preoperational, start-up or pcwer ascension tests

7. Description of Occurrence:

An instrument technician installed a replacement speed switch on the "A" Energency Diesel Generator without having his Job Order approved by the shift supervisor as required. With the shift supervisor unaware of the "A" diesel being out of service, neither the "A" nor "B" diesel were tested.

Reportable Occurrence Report No. 50-368/78-15

8. Designation of Apparent Cause of Occurrence:

Design Procedure hbnufacture Unusual Service Condition Including Environmental Installation / X Const ruction Component Failure (See Failure Data)

Operator Other (specify)

9. Analysis of Occurrence:

The instrument technician forgot to obtain the shift supervisor's approval before beginning vorP., causing a violation of Technical Specification 3.8.1.1.(b). There was no danger to the health and safety of the public.

Reportable Occurrence Report lio. 50-368/78-15

10. Corrective Action:

The technician was re-instructed on the processing of Job Orders and the "A" diesel generator was successfully tested.

11. Failure Data:

There have been no similar occurrences and this is considered an isolated occurrence.