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  $102 0 50 M _lPREPARER                                                                                                                      _ o u ,,m ,J802)257-7711
 
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05000271 4                                                                                                        LER 81-01/3L                    -
1 a
EVENT DESCRIPTION AND PLOBABLE CONSEQUENCES
'                                                                                        ~
During routine surveillance testing at 38% reactor power, MSIV                                                                          '
80 B and MSIV 86 A were found to close in 5.5 and 5.3 seconds respectively, which exceeds the Tech. Spec. limit of 5 seconds. As required by Tech.
,                    Spec. Section 3.7.D.2, MSIV 80 A and MSIV 86 B were closed.
Additionally, while testing MSIV 80 C, relay SA-K 3F failed to de-energize-i due to a failed limit switch in the closed position on >$IV 80 C.
Vermont Yankee incorrectly reported this occurrence a 24 hour reportable occurrence (LER 81/01/IP). Further investigation has determined that 4 instrument channels per trip system were operable as required by Tech.                                                                              i Spec. Table 3.1.1 since closure of MSIV 86 C did cause relay 5A-K3F to operate. RPS Limit swite'es on MSIV 80 C and MSIV 86 C'are redundant and it was determined that this instrument channel was operable bue                                                                                    ,
degraded. If a Group 1 isolation signal had occurred, a reactor scram would have resulted as required.
Since the second isolation valve in main steam lines A, B and C was
}
operable as required by Tech. Spec., there were no potential consequences
;~
to the health and safety of the general public.. Similar slow MSIV closure times were reported in LER 79-29 and LER 78-32.-
CAUSE DESCRIPTION AND CORRECTIVE ACTION j
The cause of MSIV 80 B slow closure time was due to improper adjustment of the hydraulic dash pot closure time adjustment mechanism. . The valve actuator had been rebuilt and preventative maintenance had been performed
'                during the annual refueling outage. The hydraulic dash. pot had been adjusted with the valve in the cold condition. Valve closure time was within Tech.                                                                                '
Spec. req ~direments in the cold condition but changed slightly in the hot condition. Readjustment of the hydraulic dash pot returned MSIV 80.B to the' required-Tech. Spec. closing. time.
i                              The cauce of MSIV 86 A slow closure time was determined to be due to a                                                                      ;
broken spring in the hydraulic dash pot closure time adjustment mechanism                                                                                '
(a Colorflow Control, 3/8 Range, manufactured by Manatol of Elyria, Ohio).
i                The broken spring was replaced,l the hydraulic dash pot was reassembled and -
adjusted and MSIV 86 A was subsequently retim'ed and determined to close within the required Tech. Spec. closure time.
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Revision as of 05:09, 31 January 2020

LER 81-001/03L-0:on 810101,MSIV 80B & 86A Closing Times Exceeded Tech Spec.Caused by Improper Adjustment of Hydraulic Dash Pot Closure Time Adjustment Mechanism in B & Broken Spring in Mechanism A.Pot Adjusted & Spring Replaced
ML19345E696
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 01/30/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19345E695 List:
References
LER-81-001-03L, LER-81-1-3L, NUDOCS 8102050564
Download: ML19345E696 (2)


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LICENSEE EVENT REPORT LER 81-01/3L CONTROL BLOCK: l l I

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l@ (PLEASE PRINT OR TYPE ALL CEQUIRED INFORMATIONI l0 l1ld 9lV ITLICENSFE 7 lV lYCODE !S l 1 l@l5 0 l0 l- l 0 LICENSE 14 l0 l 0NUMasEM l 0 l 0 l- l0 l 025 l@l4 26

!1 l1 l1 l1 l@lS7 LAI LICENSE TYPE 4J l

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CON T l0l1l 3[03 , l60L l@l0_l 5 l0 l 0 10 l 2 l 7 l1 l@l 0 l1 l 0 II l 8 l Lj@l 0 l 1 l 3 l 0 l 8 l 1 l@

7 8 61 DOCKET NUMSER Ed 63 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROS ABLE CONSEQUENCES h ,

IO ld l l to tal l See attached sheet. l 10141 l l 10161 l l i

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10171! l l

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F $ 3 l 80 S Y S T E *.1 CAUSE CAUSE COYP COCE CGCZ $U8 CODE VALVE I COYPONENT CODE SUSCODE SUSCOO!

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7 8 9 10 )I 12 13 ta is 20 SEOUE N TI AL OCCURRENCE REPORT REVISION

_EVENTYEAR REPOR T NO. CODE TYPE N O.

@ lLER u'[ E RO

_2n l8l1l 22 23 l0 l0 l1 l 24 l/l l 0 l3 l 1L l l-! [Q_j de 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTPOWN A TT ACHY E NT NPRO.4 PRIME COYP TAKEN ACTION ON PLANT METHOD HOURS CCYPONENT SUS VITTE D FORM Wis SUPP LIE R MANLFACTURER

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Sf S *.POWE R OTHER STA TUS IS O HY DISCOVERY CESCRIPTION l1 i S l l C l@ 10 l 3 I 8 l@l NA l lJ_j@l Durin Survoill-inrn To c H ng i ACTIVI TY CO TENT nELEASED OP RELEASE AMOUNT OF ACitVliv LOCATION OF RE LE ASE 7

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PERSQ*.*aE L f RPOSURES NUYllE R

[ i l i j l 0 l 0 l0 j@lZTVl PE @l DESCRIPTION NA l

I d 9 11 12 13 PEPSONNE L INJURIES .

SJ NUYBER DESCnlP TION t -7 li l- Iifl3010101@l 11 12 NA l LOSS OF OR DAYAGE TO SACILITY 80 TvPE DESCDieff0N LLLild JI z l@l 7 to NA l go ISSUE DESCP:P fiON

  • LLL2J I 8 9 tt_[81 m I .I I I I I I I i l'i i 80i li; 10, _

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05000271 4 LER 81-01/3L -

1 a

EVENT DESCRIPTION AND PLOBABLE CONSEQUENCES

' ~

During routine surveillance testing at 38% reactor power, MSIV '

80 B and MSIV 86 A were found to close in 5.5 and 5.3 seconds respectively, which exceeds the Tech. Spec. limit of 5 seconds. As required by Tech.

, Spec. Section 3.7.D.2, MSIV 80 A and MSIV 86 B were closed.

Additionally, while testing MSIV 80 C, relay SA-K 3F failed to de-energize-i due to a failed limit switch in the closed position on >$IV 80 C.

Vermont Yankee incorrectly reported this occurrence a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> reportable occurrence (LER 81/01/IP). Further investigation has determined that 4 instrument channels per trip system were operable as required by Tech. i Spec. Table 3.1.1 since closure of MSIV 86 C did cause relay 5A-K3F to operate. RPS Limit swite'es on MSIV 80 C and MSIV 86 C'are redundant and it was determined that this instrument channel was operable bue ,

degraded. If a Group 1 isolation signal had occurred, a reactor scram would have resulted as required.

Since the second isolation valve in main steam lines A, B and C was

}

operable as required by Tech. Spec., there were no potential consequences

~

to the health and safety of the general public.. Similar slow MSIV closure times were reported in LER 79-29 and LER 78-32.-

CAUSE DESCRIPTION AND CORRECTIVE ACTION j

The cause of MSIV 80 B slow closure time was due to improper adjustment of the hydraulic dash pot closure time adjustment mechanism. . The valve actuator had been rebuilt and preventative maintenance had been performed

' during the annual refueling outage. The hydraulic dash. pot had been adjusted with the valve in the cold condition. Valve closure time was within Tech. '

Spec. req ~direments in the cold condition but changed slightly in the hot condition. Readjustment of the hydraulic dash pot returned MSIV 80.B to the' required-Tech. Spec. closing. time.

i The cauce of MSIV 86 A slow closure time was determined to be due to a  ;

broken spring in the hydraulic dash pot closure time adjustment mechanism '

(a Colorflow Control, 3/8 Range, manufactured by Manatol of Elyria, Ohio).

i The broken spring was replaced,l the hydraulic dash pot was reassembled and -

adjusted and MSIV 86 A was subsequently retim'ed and determined to close within the required Tech. Spec. closure time.

s 4

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