ML070780615: Difference between revisions

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Trend Type                                      Trend Code CRT=EF PI=SI WP=ST
Trend Type                                      Trend Code CRT=EF PI=SI WP=ST


E--zY                  I                      ADMIN                                  CR-PNP-2003-01411 Initiated Date: 4/19/2003 17:27      Owner Group :Operations Support Mgmt Current Contact: A. SHATAS Current Significance: C - CORRECTION Closed by: Buckley,Patricia A                                                4/26/2003 7:57 Summary
E--zY                  I                      ADMIN                                  CR-PNP-2003-01411 Initiated Date: 4/19/2003 17:27      Owner Group :Operations Support Mgmt Current
 
==Contact:==
A. SHATAS Current Significance: C - CORRECTION Closed by: Buckley,Patricia A                                                4/26/2003 7:57 Summary


== Description:==
== Description:==

Revision as of 13:25, 7 December 2019

CR-PNP-2002-01411, Secondary Containment Leakrate Testing Was Aborted
ML070780615
Person / Time
Site: Pilgrim
Issue date: 04/17/2003
From:
Entergy Corp
To:
Office of Nuclear Reactor Regulation
References
CR-PNP-2003-01411
Download: ML070780615 (4)


Text

Entergy CONDITION REPORT CR-PNP-2003-01411

~~~~~

Originator: Olson,Eric W Originator Phone: 8477 Originator Group: Operations Mgmt Operability Required: N Reportability Required: N Supervisor Name: DietrichSeter T Discovered Date: 04/17/2003 22: 12 Initiated Date: 04/19/2003 17:27 Condition

Description:

Secondary Containment Leakage Testing in accordance with 8.7.3 was aborted when it was noted that the first set of readings taken after the first SBGT fan was placed in service indicated questionable results. Note that the baseline readings taken were outside the suggested parameters. The test was aborted because steam tunnel temperature was rising and with the questionable results the conservative action was to restore normal reactor building ventillation.

Immediate Action

Description:

Aborted the test and established normal reactor building ventilation.

Suggested Action

Description:

TRENDING (For Reference Purposes Only):

Trend Type Trend Code CRT=EF PI=SI WP=ST

E--zY I ADMIN CR-PNP-2003-01411 Initiated Date: 4/19/2003 17:27 Owner Group :Operations Support Mgmt Current

Contact:

A. SHATAS Current Significance: C - CORRECTION Closed by: Buckley,Patricia A 4/26/2003 7:57 Summary

Description:

Remarks

Description:

Closure

Description:

The CA has been reviewed for completeness and meets the requirements for closure per responsible manager.

Entergy ASSIGNMENTS CR-PN'P-2003-01411 Version: 1 Significance Code: C - CORRECTION Classification Code: NON-SIGNIFICANT Owner Group: Operations Support Mgmt Performed By: McWilliams,Dorena C 04/20/2003 02:Ol Assignment

Description:

Responsible Manager: B. Lyons

E n t m I CORRECTIVE ACTION 1 CR-PNP-2003-01411 CA Number: 1

-- - -

1

" ._

I Group i Name Assigned By: CRG Mgmt Assigned To: Operations Support Mgmt Lyons,Brent D Subassigned To :

Originated By: Landeche,David A 4/20/2003 13:5 1:20 Performed By: Lyons,Brent D 4/24/2003 16:32:36 Subperformed By:

Approved By:

Closed By: Lyons,Brent D 4/24/2003 16:32 :36 Current Due Date: 06/20/2003 Initial Due Date: 06/20/2003 CA Type: CORRECTIVE ACTION Plant Constraint: NONE CA

Description:

As the Responsible Manager, validate the problem statement and determine corrective actions as needed to resolve the adverse condition(s). Note: Category 'C' corrective actions may be closed out to MR's without CRG approval provided the M R does not resolve a GL 91-18 deficiency. If a corrective action is closed out to a MR, the responsible manager is responsible to ensure the CR number is included in the M R references section. CA closure statements are expected to confirm this action has been completed.

Response

Revision 41 of 8.7.3 issued on 04/24/03 incorporated appropriate changes to ensure that the Shift Manager is notified prior to proceeding with the test upon observing baseline manometer readings outside acceptable bands specified in the procedure. No additional actions are required. This condition report may be closed.

Subresponse :

Closure Comments: