ML16344A118: Difference between revisions

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Enclosure  Interim Part 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker  On October 13, 2016, Arizona Public Service Company (APS) identified an apparent deviation related to a workmanship problem identified during pre-installation testing of a refurbished General Electric (GE)-Hitachi Model AKR-2BE-50 breaker. This interim report is being submitted pursuant to 10 CFR 21.21(a)(2). APS does not have sufficient information to determine if the deviation could result in a substantial safety hazard and is working with the vendor to complete the evaluation.
Enclosure  Interim Part 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker  On October 13, 2016, Arizona Public Service Company (APS) identified an apparent deviation related to a workmanship problem identified during pre-installation testing of a refurbished General Electric (GE)-Hitachi Model AKR-2BE-50 breaker. This interim report is being submitted pursuant to 10 CFR 21.21(a)(2). APS does not have sufficient information to determine if the deviation could result in a substantial safety hazard and is working with the vendor to complete the evaluation.
The evaluation is expected to be completed by February 17, 2017. Pursuant to 10 CFR 21.21(a)(2), the following information is provided related to the apparent deviation:  A GE-Hitachi Model AKR-2BE-50, 250 VDC, 2000 amp circuit breaker exhibited arcing during long-time current injection testing which is used to test the overcurrent trip setpoint prior to breaker installation. The arcing occurred between a loose hex bolt, which anchors a protective trip device (EC-1) to an internal bus bar on the breaker, and the internal bus bar. The loose hex bolt is not observable during external inspection of the breaker. The breaker is used by APS at the Palo Verde Nuclear Generating Station (PVNGS) to provide isolation between the Class 1E 125 VDC batteries and the associated Class 1E 125 VDC electrical distribution system. Information and analysis is needed from the vendor to determine whether the behavior exhibited by the breaker could result in a failure of the breaker to perform its credited safety function. The breaker was refurbished by GE-Hitachi and received by APS and tested on October 13, 2016. The breaker was repaired in consultation with GE-Hitachi staff, satisfactorily retested, and installed in PVNGS Unit 3. The following information is provided:
The evaluation is expected to be completed by February 17, 2017. Pursuant to 10 CFR 21.21(a)(2), the following information is provided related to the apparent deviation:  A GE-Hitachi Model AKR-2BE-50, 250 VDC, 2000 amp circuit breaker exhibited arcing during long-time current injection testing which is used to test the overcurrent trip setpoint prior to breaker installation. The arcing occurred between a loose hex bolt, which anchors a protective trip device (EC-1) to an internal bus bar on the breaker, and the internal bus bar. The loose hex bolt is not observable during external inspection of the breaker. The breaker is used by APS at the Palo Verde Nuclear Generating Station (PVNGS) to provide isolation between the Class 1E 125 VDC batteries and the associated Class 1E 125 VDC electrical distribution system. Information and analysis is needed from the vendor to determine whether the behavior exhibited by the breaker could result in a failure of the breaker to perform its credited safety function. The breaker was refurbished by GE-Hitachi and received by APS and tested on October 13, 2016. The breaker was repaired in consultation with GE-Hitachi staff, satisfactorily retested, and installed in PVNGS Unit 3. The following information is provided:
Vendor: GE-Hitachi Nuclear Energy  3901 Castle Hayne Rd WILMINGTON, NC 28402-2819  Device: Breaker Model AKR-2BE-50, 2000 Amp, 250 VDC Serial No N8682600001  
Vendor: GE-Hitachi Nuclear Energy  3901 Castle Hayne Rd WILMINGTON, NC 28402-2819  Device: Breaker Model AKR-2BE-50, 2000 Amp, 250 VDC Serial No N8682600001}}
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Revision as of 02:36, 19 May 2018

Palo Verde Nuclear Generating Station - Interim 10 CFR 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker
ML16344A118
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 12/09/2016
From: Rash B J
Arizona Public Service Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
102-07393-BJR/DCE
Download: ML16344A118 (3)


Text

(.laps 102-07393-BJR/DCE December 9, 2016 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001

Dear Sirs:

10 CFR 21.21 BRUCE J RASH Vice President Nuclear Engineering Palo Verde Nuclear Generating Station P.O. Box 52034 Phoenix, AZ 85072 Mail Station 7602 Tel 623 393 5102

Subject:

Palo Verde Nuclear Generating Station (PVNGS) Units 1, 2, and 3 Docket No. STN 50-528, STN 50-529, and STN 50-530 License No. NPF 41, NPF 51, and NPF 74 Interim 10 CFR 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker Enclosed please find an interim report for an apparent deviation related to a workmanship problem on a basic component identified during pre-installation testing of a refurbished General Electric Hitachi Model AKR-2BE-50 breaker. This report is being submitted pursuant to 10 CFR 21.21(a)(2). In accordance with 10 CFR 50.4, copies of this notification are being forwarded to the NRC Regional Office, NRC Region IV and the Senior Resident Inspector. Arizona Public Service Company makes no commitments in this letter. If you have questions regarding this submittal, please contact Mark McGhee, Nuclear Regulatory Affairs Department Leader, at (623) 393-4972. Sincerely, BJR/DCE/akf

Enclosure:

Interim 10 CFR 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker cc: K. M. Kennedy S. P. Lingam C. A. Peabody NRC Region IV Regional Administrator NRC NRR Project Manager for PVNGS NRC Senior Resident Inspector PVNGS A member of STARS Alliance LLC Callaway

  • Diablo Canyon
  • Palo Verde
  • Wolf Creek Enclosure Interim 10 CFR 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker

Enclosure Interim Part 21 Report for General Electric Hitachi Model AKR-2BE-50 Breaker On October 13, 2016, Arizona Public Service Company (APS) identified an apparent deviation related to a workmanship problem identified during pre-installation testing of a refurbished General Electric (GE)-Hitachi Model AKR-2BE-50 breaker. This interim report is being submitted pursuant to 10 CFR 21.21(a)(2). APS does not have sufficient information to determine if the deviation could result in a substantial safety hazard and is working with the vendor to complete the evaluation.

The evaluation is expected to be completed by February 17, 2017. Pursuant to 10 CFR 21.21(a)(2), the following information is provided related to the apparent deviation: A GE-Hitachi Model AKR-2BE-50, 250 VDC, 2000 amp circuit breaker exhibited arcing during long-time current injection testing which is used to test the overcurrent trip setpoint prior to breaker installation. The arcing occurred between a loose hex bolt, which anchors a protective trip device (EC-1) to an internal bus bar on the breaker, and the internal bus bar. The loose hex bolt is not observable during external inspection of the breaker. The breaker is used by APS at the Palo Verde Nuclear Generating Station (PVNGS) to provide isolation between the Class 1E 125 VDC batteries and the associated Class 1E 125 VDC electrical distribution system. Information and analysis is needed from the vendor to determine whether the behavior exhibited by the breaker could result in a failure of the breaker to perform its credited safety function. The breaker was refurbished by GE-Hitachi and received by APS and tested on October 13, 2016. The breaker was repaired in consultation with GE-Hitachi staff, satisfactorily retested, and installed in PVNGS Unit 3. The following information is provided:

Vendor: GE-Hitachi Nuclear Energy 3901 Castle Hayne Rd WILMINGTON, NC 28402-2819 Device: Breaker Model AKR-2BE-50, 2000 Amp, 250 VDC Serial No N8682600001