Part 21 Report - Defective Current to Pressure TransducersML16294A264 |
Person / Time |
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Site: |
Calvert Cliffs, Palo Verde, Fermi, Catawba, Oyster Creek, Watts Bar, Grand Gulf, Cooper, Arkansas Nuclear, Three Mile Island, Columbia, River Bend, Waterford, Clinton, Fort Calhoun, 05000470 |
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Issue date: |
10/18/2016 |
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From: |
Rich Smith ITT Enidine |
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To: |
Document Control Desk, Office of Nuclear Reactor Regulation |
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References |
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52300 |
Download: ML16294A264 (5) |
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Similar Documents at Calvert Cliffs, Palo Verde, Fermi, Catawba, Oyster Creek, Watts Bar, Grand Gulf, Cooper, Arkansas Nuclear, Three Mile Island, Columbia, River Bend, Waterford, Clinton, Fort Calhoun, 05000470 |
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Category:Deficiency Report (per 10CFR50.55e and Part 21)
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[Table view]The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Calvert Cliffs]] OR [[:Palo Verde]] OR [[:Fermi]] OR [[:Catawba]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Columbia]] OR [[:River Bend]] OR [[:Waterford]] OR [[:Clinton]] OR [[:Fort Calhoun]] OR [[:05000470]] </code>. |
Text
1011812016 U.S. Nuclear Regulatory Commission Operations Center Event Report Pagel Part 21 (PAR) Event# 52300 Rep Org: ITT ENIDINE INC. Notification Date I Time: 10/18/2016 10:08 (EDT)
Supplier: ITT ENIDINE INC. Event Date I Time: 08/19/2016 (EDT)
Last Modification: 10/18/2016 Region: 1 Docket#:
City: WESTMINSTER Agreement State: Yes County: License#:
State: SC NRC Notified by: RAY SMITH Notifications: CHRISTOPHER CAHILL R1DO HQ Ops Officer: BETHANY CECERE FRANK EHRHARDT R2DO Emergency Class: NON EMERGENCY RICHARD SKOKOWSKI R3DO 10 CFR Section: JOHN KRAMER R4DO 21.21 (d)(3)(i) DEFECTS AND NONCOMPLIANCE PART 21/50.55 REACTORS PART 21 REPORT - DEFFECTIVE CURRENT TO PRESSURE TRANSDUCERS The following was received by facsimile:
"The ITT Conoflow models GT25CA1826 and GT25CD1826 current to pressure (l/P) transducers produce a calibrated 3.0 to 15.0 psi output pressure from a 4.0 to 20.0 mA DC (input) signal. Other dedicated l/P transducer part numbers are available with different output pressure ranges and input signal values.
"On August 19, 2016 a defective model GT25CA 1826 (s/n 628894) was received for evaluation. This transducer would only achieve 0-9 psi output pressure, falling short of the specified 3-15 psi output range. The failure was caused by misalignment of a key internal sub-assembly component as a result of shipping damage (mechanical shock). The product has be~n repaired, calibrated/tested, and is being returned to the customer (Arizona Public Service Co.).
"The following is a list of customers, and the specific l/P transducer part numbers procured from ITT since 2006.
These customers will be notified by November 1, 2016.
"ACSYR SL GT25CA 1826 ALABAMA POWER COMPANY GT25CA 1826 AMERGEN ENERGY, LLC GT25CA1826 ARIZONA PUBLIC SERVICE CO GT25CA1826 ASIAM INT'L (TAIWAN) INC. GT25CA1826 CALVERT CLIFFS NUCLEAR POWER PLANT, INC GT25CD1826 CATAWBA NUCLEAR STATION GT25CA1826 GT25CD1826 CCNPP STOREROOM GT25CD1826
1011812016 U.S. Nuclear Regulatory Commission Operations Center Event Report Page2 CENTRAL NUCLEAR DE ALMARAZ GT25CD1826 CONTROL COMPONENTS INC GT25CD1826 DETROIT EDISON GT25CD1826 DTE ENERGY GT25CD1826 ENERGY NORTHWEST GT25CA 1826 ENERTECH CURTISS-WRIGHT GT25CA1826, GT25CD1826 ENRICO FERMI POWER PLANT 2 GT25CD1826 ENTERGY OPERATIONS GT25CA1826, GT25CD1826 ERGYTECHINC GT25CD1826 EXELON BUSINESS SERVICES GT25CA1826 FLOWSERVE GT25CA 1826 GEFRAN BENELUX NV GT25CA1826 GT25CD1826 KOREA HYDRO & NUCLEAR PWR GT25CA1826 NEBRASKA PUBLIC POWER GT25CA1826 NUCLEAR POWER PLANT KRSKO GT25CA1826 OMAHA PUBLIC POWER DIST GT25CA1826 GT25CD1826 ONTARIO POWER GENERATION GT25CA1826 GT25CD1826 SPX MCKEAN GT25CA1826 TVA NUCLEAR ASSURANCE AND LICENSING GT25CA1826 GT65CD1826 WATTS BAR UNIT 2 CONSTRUCTION GT25CD1826 WEIR VALVES & CONTROLS UK GT25CA1826 ZVONIMIR ZEC GT25CA1826"
Oct. 18. 2016 10:08AM ITT No. 0873 P. 1
.-J, ITT Enidine Inc.
105 Commerce Way ITT Westminster, SC 29693 Phone: (864) 647-3855
. Fax: (864) 647-7993 ENGINEERED FOR LIFE Email: &ymond.smith@itt.com Facsimile Cover Sheet
- Date: 10/18/2016 To the Attention of: NRC operations center Fa:x Number! 301-816-5151 From: Ray Smith Company: ITT Inc.
Phone: 864-647-3855 Email: Raymond.smith@itt.com F:rom Facsimile; 864-647-7993 Number of Pages: 3 Including cover sheet File: GT25CA 1826 Transducer Page 1 ofl
Oct. 18. 2016 10:09AM ITT No. 0873 P. 2
~ITT Enldlne 105 Commerce Way Westminster, SC 29691 Phone:(864}*647-9621
!=ax: (1164)-647-9574 Compact Automation Produet line Turn-Act Product Line Conoflow Product Line Octobsr 18, 2016 Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001
Subject:
USN RC 10CFR Part 21 Notification Gentlemen, This letter is ta notify the US Nuclear Regulatory Commission of a component defect.
Yhe ITT Conoflaw models GT25CA1826 and GT25Cbi826 current to pressure (l/P) transducers produce a calibratsd 3.0 ta 15.0 psi output pressure from a 4.0 to 20.0 mA DC (input) signal. other dedicated l/P transducer part numbers are available with different output pressure ranges and input signal values.
On August 19, 2016 a defective model GT25CA1626 (s/n 628894} was received for evaluation. This transducer would only achieve 0-9 psi output pressure, falling short of the specified 3-15 psi output range.
The failure was caused by misalignment of a key internal sub-assembly component as a result of shipping damage (mechanical shack). The product has been repaired, calibrated I tested, and is being returned to the customer (Arizona Public Service Co.)_
Nuclear facilities which use this product will be advised to examine their stock of uninstalled and/or unverified product for shipping damage through notification and dissemination of a revised installation, operation and maintenance manual. Product which has already been verified (callbrated) and put into service does not have this defect.
Preventive actions will advise customers to verify the condition of the product, prior to placing it into service. Supporting documentation (the instruction, operation and maintenance manual) and packaging
- will be updated to notify facilities ta inspect the packciging and the product, and verify the operation and calibrate the J/P transducer prior ta putting the product in service.
The followlng table (page 2 of this notification} is a list of customers, and the specific l/P transducer part numbers procured from ITT since 2006, These customers will be notified by November 1, 2016.
Respectfully Submitted, Attachments: GT25 series l/P transducer customer list (2006 to present)
Oct. 18. 2016 10:09AM ITT No. 0873 P. 3
)/ I --
ITI GT25 Series customer list (2006 to present) customer Name ltem(s)
ACSYR SL GT25CA1826 ALABAMA POWER COMPANY GT25CA1826 AMERGEN ENERGY, LLC GT25CA1826 ARIZONA PUBLIC SERVICE CO GT25CA1826 ASJAM INT'L (TAIWAN) INC. GT25CA1826 CALVERT CLIFFS NUCLEAR POWER PLANT, INC GT25CD1826 CATAWBA NUCLEAR SlAllON GT25CA1826 GT25CD1826 CCNPP STOREROOM GT25CD1826 CENTRAL NUCLEAR DE ALMARAZ GT25CD1826 CONTROL COMPONENTS INC GT25CD1826 DETROIT EDISON GT25CD1826 DTE ENERGY GT25CD1826 ENERGY NORTHWEST GT25CA1826 ENERTECH CURTISS-WRIGHT GT25CA1826 GT25C01826 ENRICO FERMI POWER PLANT 2 GT25CD1826 ENTERGY OPERATIONS GT25CA1826 GT25CD1826 ERGYTECHINC Gl25CD1826 EXELON BUSINESS SERVICES GT25CA1B26 FLOWSERVE GT25CA1826 GEFRAN BENELUX NV GT25CA1826 GT25CD1826 KOREA HYDRO & NUCLEAR PWR GT25CA1826 NEBRASKA PUBLIC POWER GT25CA1826 NUCLEAR POWER PLANT KRSKO GT25CA1826 OMAHA PUBLIC POWER DIST GT25FA1826 GT65FA1826 ONTARIO POWER GENERATION GT25CA1826 GT25CD1826 SPX MCKEAN GT25CA1826 TVA NUCLEAR ASSURANCE AND LICENSING GT25CD1826 Gl65CD1826 WATTS BAR UNIT 2 CONSTRUCTION GT25CD1826 WEIR VALVES & CONTROLS UK GT25CA1826 ZVONIMIR ZEC GT25CA1826