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| issue date = 08/22/1996
| issue date = 08/22/1996
| title = LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr
| title = LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr
| author name = MARTIN J T, MECREDY R C
| author name = Martin J, Mecredy R
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:CATEGORY 3 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9608300053 DOC.DATE: 96/08/22 NOTARIZED:
{{#Wiki_filter:CATEGORY 3 REGULATORY INFORMATION DISTRIBUTION SYSTEM                     (RIDS)
NO DOCKET g FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH.NAME AUTHOR AFFILIATION MARTIN,J.T.
ACCESSION NBR:9608300053           DOC.DATE: 96/08/22       NOTARIZED: NO                 DOCKET g FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester                         G 05000244 AUTH. NAME           AUTHOR AFFILIATION MARTIN,J.T.           Rochester Gas a Electric Corp.
Rochester Gas a Electric Corp.MEREDYiR.C.
MEREDYiR.C.           Rochester Gas a Electric Corp.
Rochester Gas a Electric Corp.RECIP.NAME RECIPIENT AFFILIATION
RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 96-009-00:on 960723,determined from leak on piping, sys outside containment greater than program limit.Caused by weld defect.Pipe a socket welds were cut out&replaced.W/960822 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
LER   96-009-00:on 960723,determined from leak on piping, sys outside containment greater than program limit.Caused by weld defect. Pipe a socket welds were cut out & replaced.
05000244 RECIPIENT~ID CODE/NAME PD1-1 PD INTERNAI~G~
W/960822   ltr.
NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN1 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME'ISSINGIG.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR                   ENCL             SIZE:
AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB LITCO BRYCE,J H NOAC POORE,W.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 D U N NOTE TO ALL"RIDS" RECIPIENTS:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
PLEASE HELP US TO REDUCE WASTE CONTACT THE DOCUMENT CONTROL DESK i ROOM OWFN 5D-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25 AND RGCHfSTfR OPS P~D flfCTRIC CCR.CZ47lCiv~'Pr JA'F MST A'IENUf, RCCHfSTfR, N, Y Idol&ml~ARE<COOf 71o S46-2700 v'+)vol August 22, 1996 U.S.Nuclear Regulatory Commission Document Control Desk Attn: Guy Vissing Project Directorate I-1 Washington, D.C.20555  
NOTES:License Exp date       in accordance with 10CFR2,2.109(9/19/72).                     05000244 RECIPIENT           COPIES              RECIPIENT                  COPIES
        ~
ID CODE/NAME          LTTR ENCL          ID CODE/NAME               LTTR ENCL PD1-1 PD                 1      1                          'ISSINGIG.
1    1 INTERNAI~G~                           2      2      AEOD/SPD/RRAB                  1    1 1      1      NRR/DE/ECGB                    1    1 NRR/DE/EELB              1      1      NRR/DE/EMEB                    1    1 NRR/DRCH/HHFB            1      1      NRR/DRCH/HICB                  1     1 NRR/DRCH/HOLB            1      1      NRR/DRCH/HQMB                  1    1 NRR/DRPM/PECB            1      1      NRR/DSSA/SPLB                  1    1 NRR/DSSA/SRXB            1      1      RES/DSIR/EIB                   1    1            D RGN1    FILE  01        1      1 EXTERNAL: L ST LOBBY WARD            1      1      LITCO BRYCE,J     H           2    2 NOAC MURPHY,G.A          1      1      NOAC POORE,W.                   1   1 NRC PDR                  1     1     NUDOCS FULL TXT                1   1 U
N NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE   CONTACT THE DOCUMENT CONTROL DESK i ROOM OWFN 5D-5(EXT. 415-2083) TO ELIMINATE YOUR NAME   FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR             25   ENCL     25
 
AND
                                                                              'Pr JA'F RGCHfSTfR OPS P~D flfCTRICCCR. CZ47lCiv ~ MST A'IENUf,RCCHfSTfR, N, Y Idol&   ml ~ ARE< COOf 71o S46-2700 v '+   )vol August 22, 1996 U.S. Nuclear Regulatory Commission Document     Control Desk Attn:       Guy Vissing Project Directorate I-1 Washington, D.C.           20555


==Subject:==
==Subject:==
LER 96-009, Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit R.E.Ginna Nuclear Power Plant Docket No.50-244  
LER 96-009, Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit R.E. Ginna Nuclear Power Plant Docket No. 50-244
 
==Dear Mr.      Vissing:==
 
In accordance with          10 CFR    50.73, Licensee Event Report System, item (a) (2) (i)      (B), "Any operation            or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 96-009 is hereby 'ubmitted.                                Entry into Limiting Condition for Operation 3.0.3 of Technical Specifications was a conservative action based upon Ginna Station T.S. 5.5.2 "Primary Coolant Sources Outside Containment Program". A further assessment will be provided in a supplement to this LER which will be submitted by September 20, 1996.
This event has in no way affected the public's health safety.
Very truly yours, Robert C. Mecredy JSM:435 xc:    Mr. Guy Vissing (Mail Stop 14C7)
Project Directorate I-1 Washington, D.C.            20555 U.S. Nuclear Regulatory Commission Region I 475  Allendale Road King of Prussia, PA            19406 Ginna Senior Resident Inspector 9608300053 960822 PDR    ADOCK 05000244 8 V LJ  V PDR
 
NRC FORM 366                              U.S. NUCLEAR REGULATORY COMMISSIO                            APPROVED BY OMB NO. 3150.0104 (4-95)                                                                                                              EXPIRES  04/30/96 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER)                                              REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK To INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE (See reverso for required number of                              INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33),
digits/characters for each block)                              U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555.0001, AND To THE PAPERWORK REDUCTION PROJECT FACILITYNAME (11                                                                          DOCKET NUMBER (21                                    PAGE (3)
R.E. Ginna Nuclear Power Plant                                                    05000244                              1  OF 5 TITLE (41 Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit EVENT DATE (5)                  LER NUMBER (6)                REPORT DATE (? I                      OTHER FACILITIES INVOLVED (6)
FACIUTY NAME                              OOCKET NUMBER SEQUENTIAL    REVISION MONTH      DAY    YEAR                NUMBER        NUMBER    MONTH      DAY    YEAR FACILrrY NAME                              OOCKETNUMBER 07        23      96      96        009        00          08      22      96 OPERATING                THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR E: (Chock one or more) (11)
MODE (9)                    20.2201(b)                      20.2203(a)(2)(v)                X 50.73(a)(2)(i)                          50.73(a)(2)(viii)
POWER 20.2203(a) (1)                  20.2203(a)(3)(il                    SO. ?3(a)(2)(ii)                      50.73(a)(2)(x)
LEVEL (10)        100        20.2203(a) l2)(i)              20.2203(a) (3) (ii)                S0.73(a)(2) (iii)                      73.71 20.2203(a)(2)(ii)              20.2203(a) (4)                      50.73(a)(2)(iv)                      OTHER 20.2203(a)(2) (iii)            50.36(c)(1)                        50.73(a)(2)(v)                  Specify In Abstract below or in NRC Form 366A 20.2203(a) (2)(iv)              50.36(c)(2)                        50.73(a) (2) (vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME                                                                                          '(ELEFHONE NUMBER (Inorvde Area Code)
John T. St. Martin - Technical Assistant                                                                (716) 771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DES CRIBFD IN THIS REPORT (13)
REPORTABLE                                                                            REPORTABLE CAUSE        SYSTEM    COMPONENT    MANUFACTURER      To NPRDS                CAUSE      SYSTEM      COMPONENT      MANUFACTURER To NPRDS BE          PSF SUPPLEMENTAL REPORT EXPECTED (14)                                                                    MONTH        DAY        YEAR EXPECTED YES                                                                                              SUBMISSION (II yos, complete EXPECTED SUBMISSION DATE).
NO                        DATE (15)                09          20          96 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines) (16)
On July 23, 1996, at approximately 0857 EDST, it was determined that the leak rate (from a leak on a piping system outside Containment) was greater than the analyzed value of two gallons per hour for a primary coolant source outside Containment.
Immediate corrective action was to conservatively enter Technical Specification Limiting Condition for Operation 3.0.3 and initiate    a plant shutdown,.and to initiate actions to isolate the leak using a freeze seal. Once the leak was isolated, the plant exited Technical Specification 3.0.3 and the shutdown was stopped. The leaking pipe was cut out and replaced.
The underlying cause of the leak was            a  weld defect which dates back to original construction in the 1960's.
This event is NUREG-1022 Cause Code (B).
Corrective action to prevent recurrence is outlined in Section V.B. Additional corrective actions will be identified in a supplement to this LER.
NRC FORM 366 l4-95)


==Dear Mr.Vissing:==
NRC FORM 366A                                                                        U.S. NUCLEAR REGULATORY CONIMISSION (4-95I LICENSEE EVENT REPORT (LER)
In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B),"Any operation or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 96-009 is hereby'ubmitted.
TEXT CONTINUATION FACILITY NAME (1)                                DOCKET        LER NUMBER (6I          PAGE (3I YEAR  SEQUENTIAL REVISION NUMBER    NUMBER R.E. Ginna Nuclear Power Plant                                05000244                              2  OF    5 96    009          00 TEXT llfmore spaceis required, use additional copies of NRC Form 886A/ (17I PRE-EVENT PLANT CONDITIONS:
Entry into Limiting Condition for Operation 3.0.3 of Technical Specifications was a conservative action based upon Ginna Station T.S.5.5.2"Primary Coolant Sources Outside Containment Program".A further assessment will be provided in a supplement to this LER which will be submitted by September 20, 1996.This event has in no way affected the public's health safety.Very truly yours, Robert C.Mecredy JSM:435 xc: Mr.Guy Vissing (Mail Stop 14C7)Project Directorate I-1 Washington, D.C.20555 U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna Senior Resident Inspector 9608300053 960822 PDR ADOCK 05000244 8 PDR V LJ V
On July 22, 1996, the plant was in Mode 1 at approximately 100% steady state reactor power. At approximately 1130 EDST, a Radiation Protection (RP) technician, who was performing a routine weekly survey of the Auxiliary Building, observed water dripping in an area behind the Refueling Water Storage Tank (RWST). The RP technician notified the Control Room operators. Efforts to locate the source of the dripping water and to quantify the leak rate were initiated by Operations and Nuclear Engineering Services (NES). The source of water was determined to be a small leak on a test line for the Containment Spray (CS) system in the Auxiliary Building, which is outside the Containment (CNMT). The leak rate was estimated to be approximately one (1) gallon per nour (GPH).
The Control Room operators did not identify any requirement that would limit plant operations. The Shift Supervisor notified Operations management, maintenance management, and plant and NES staff of the leak. All reached a similar conclusion. The staff worked on developing and implementing an action plan to address the problem. The issues of line integrity and RWST operability were investigated by NES and Laboratory Inspection Services (LIS) personnel LIS personnel measured the amount of pipe cross-section
                                                                  ~
and weld metal remaining, and NES personnel determined that there was ample metal in the affected area to provide system integrity.
The source of the leak was identified as a small pinhole leak on a pipe-to-90 degree forged socket elbow weld on a two (2) inch nominal pipe size Schedule 10 stainless steel test line for the CS system. The leak was in a part-of the CS system that could not be isolated from the RWST by valve manipulations without making both trains of the emergency core cooling system (ECCS) inoperable. The leak was monitored throughout the remainder of the day and night.
An operability assessment had been requested by the Shift Supervisor on July 22. On the 'morning of July 23, 1996, this assessment was reviewed by the Plant Operations Review Committee (PORC). This assessment, which was based on conservative assumptions, concluded that the RWST and ECCS were still operable with the unisolated leak. This conclusion was supported by the fact that there was still ample metal area in the cross-section that can provide integrity of the pipe during a seismic event, and that the total combined stress was less than the yield strength of the material.
PORC requested a more accurate estimate of the leak rate. The leak rate was measured and estimated to be 2.5 GPH. This leak rate is in excess of two (2) GPH, which is specified in Surveillance Test Procedure PT-39, "Leakage Evaluation of Primary Coolant Sources Outside Containment", as the program limit for the maximum integrated leak rate outside CNMT from these sources.             The leak rate exceeded the requirements of procedure PT-39, and it was initially judged to be a violation of the "Primary Coolant Sources Outside Containment Program", as specified in the Ginna Station Improved Technical Specifications (ITS) Section 5.5.2.
The PORC chairman conservatively directed the Shift Supervisbr to enter ITS Limiting Condition for Operation (LCO) 3.0.3, based on the requirements of procedure PT-39 and Administrative Procedure A-52.4, "Control of Limiting Conditions for Operating Equipment", even though the plant was in compliance with all ITS LCOs.
NRC FORM 366A (4-95I


NRC FORM 366 (4-95)U.S.NUCLEAR REGULATORY COMMISSIO LICENSEE EVENT REPORT (LER)(See reverso for required number of digits/characters for each block)APPROVED BY OMB NO.3150.0104 EXPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK To INDUSTRY.FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON.
NRC FORM 366A                                                                            U.S. NUCLEAR REGULATORY COMMISSION (4.95)
DC 20555.0001, AND To THE PAPERWORK REDUCTION PROJECT FACILITY NAME (11 R.E.Ginna Nuclear Power Plant DOCKET NUMBER (21 05000244 PAGE (3)1 OF 5 TITLE (41 Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit EVENT DATE (5)LER NUMBER (6)REPORT DATE (?I OTHER FACILITIES INVOLVED (6)MONTH 07 DAY YEAR 23 96 SEQUENTIAL REVISION NUMBER NUMBER 96-009-00 MONTH 08 DAY 22 YEAR 96 FACIUTY NAME FACILrrY NAME OOCKET NUMBER OOCKETNUMBER OPERATING MODE (9)THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR E: (Chock one or 20.2203(a)(2)(v) 20.2201(b)
LICENSEE EVENT REPORT (LER)
X 50.73(a)(2)(i) more)(11)50.73(a)(2)(viii)
TEXT CONTINUATION FACILITY NAME (1)                                   DOCKET         LER NUMBER (6)          PAGE (3)
POWER LEVEL (10)NAME 100 20.2203(a)
YEAR   SEQUENTIAL REVISION NUMBER     NUMBER OF   5 R.E. Ginna Nuclear Power Plant                                   05000244   96   009           00 TEXT llfmore space is required, use additional copies of NRC Form 366Al (17)
(1)20.2203(a) l2)(i)20.2203(a)(2)(ii) 20.2203(a)(2)(iii)20.2203(a)
DESCRIPTION OF EVENT:
(2)(iv)20.2203(a)(3)(il 20.2203(a)
A.         DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
(3)(ii)20.2203(a)
July 22, 1996, 1130 EDST: A leak is identified on   a line outside of Containment.
(4)50.36(c)(1) 50.36(c)(2)
July 23, 1996, 0857 EDST: Event Date and Time and Discovery Date and Time.
LICENSEE CONTACT FOR THIS LER SO.?3(a)(2)(ii)
July 23, 1996, 0900 EDST: Load reduction is started.
S0.73(a)(2)(iii)50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii)(12)'(ELEFHONE NUMBER (Inorvde Area Code)50.73(a)(2)(x) 73.71 OTHER Specify In Abstract below or in NRC Form 366A John T.St.Martin-Technical Assistant COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DES (716)771-3641 CRIBFD IN THIS REPORT (13)CAUSE SYSTEM BE COMPONENT MANUFACTURER PSF REPORTABLE To NPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE To NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (II yos, complete EXPECTED SUBMISSION DATE).NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR 09 20 96 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines)(16)On July 23, 1996, at approximately 0857 EDST, it was determined that the leak rate (from a leak on a piping system outside Containment) was greater than the analyzed value of two gallons per hour for a primary coolant source outside Containment.
July 23, 1996, 1440 EDST: Integrated leakage outside Containment is determined to be less than two GPH. Load reduction is stopped.
Immediate corrective action was to conservatively enter Technical Specification Limiting Condition for Operation 3.0.3 and initiate a plant shutdown,.and to initiate actions to isolate the leak using a freeze seal.Once the leak was isolated, the plant exited Technical Specification 3.0.3 and the shutdown was stopped.The leaking pipe was cut out and replaced.The underlying cause of the leak was a weld defect which dates back to original construction in the 1960's.This event is NUREG-1022 Cause Code (B).Corrective action to prevent recurrence is outlined in Section V.B.Additional corrective actions will be identified in a supplement to this LER.NRC FORM 366 l4-95)
B.         EVENT:
NRC FORM 366A (4-95I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY CONIMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6I YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-009-00 PAGE (3I 2 OF 5 TEXT llf more spaceis required, use additional copies of NRC Form 886A/(17I PRE-EVENT PLANT CONDITIONS:
On July 23, 1996, at approximately 0857 EDST, with the plant in Mode 1 at approximately 100%
On July 22, 1996, the plant was in Mode 1 at approximately 100%steady state reactor power.At approximately 1130 EDST, a Radiation Protection (RP)technician, who was performing a routine weekly survey of the Auxiliary Building, observed water dripping in an area behind the Refueling Water Storage Tank (RWST).The RP technician notified the Control Room operators.
steady state reactor power, the Plant Operations Review Committee (PORC) conservatively directed the Shift Supervisor to enter ITS LCO 3.0.3. The Shift Supervisor directed the Control Room operators to initiate a plant shutdown. At approximately 0900 EDST, the Control Room operators initiated a plant shutdown per Normal Operating Procedure 0-2.1, "Normal Shutdown to Hot Shutdown".
Efforts to locate the source of the dripping water and to quantify the leak rate were initiated by Operations and Nuclear Engineering Services (NES).The source of water was determined to be a small leak on a test line for the Containment Spray (CS)system in the Auxiliary Building, which is outside the Containment (CNMT).The leak rate was estimated to be approximately one (1)gallon per nour (GPH).The Control Room operators did not identify any requirement that would limit plant operations.
The Mechanical Support group initiated actions to provide a freeze seal to isolate the source of leakage from the RWST. A freeze seal was initiated between the leaking socket and the CS pump suction line from the RWST. At approximately 1440 EDST on July 23, 1996, the freeze seal had isolated the leak. ITS LCO 3.0.3 was exited and the load reduction was stopped. The affected pipe and socket welds were cut out and a new prefabricated spoolpiece was installed. The affected weld was retained for failure mode analysis.
The Shift Supervisor notified Operations management, maintenance management, and plant and NES staff of the leak.All reached a similar conclusion.
A load increase to return the plant to full power was initiated at approximately 1530 EDST on July 23, 1996.
The staff worked on developing and implementing an action plan to address the problem.The issues of line integrity and RWST operability were investigated by NES and Laboratory Inspection Services (LIS)personnel~LIS personnel measured the amount of pipe cross-section and weld metal remaining, and NES personnel determined that there was ample metal in the affected area to provide system integrity.
C.       INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
The source of the leak was identified as a small pinhole leak on a pipe-to-90 degree forged socket elbow weld on a two (2)inch nominal pipe size Schedule 10 stainless steel test line for the CS system.The leak was in a part-of the CS system that could not be isolated from the RWST by valve manipulations without making both trains of the emergency core cooling system (ECCS)inoperable.
None D.       OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
The leak was monitored throughout the remainder of the day and night.An operability assessment had been requested by the Shift Supervisor on July 22.On the'morning of July 23, 1996, this assessment was reviewed by the Plant Operations Review Committee (PORC).This assessment, which was based on conservative assumptions, concluded that the RWST and ECCS were still operable with the unisolated leak.This conclusion was supported by the fact that there was still ample metal area in the cross-section that can provide integrity of the pipe during a seismic event, and that the total combined stress was less than the yield strength of the material.PORC requested a more accurate estimate of the leak rate.The leak rate was measured and estimated to be 2.5 GPH.This leak rate is in excess of two (2)GPH, which is specified in Surveillance Test Procedure PT-39,"Leakage Evaluation of Primary Coolant Sources Outside Containment", as the program limit for the maximum integrated leak rate outside CNMT from these sources.The leak rate exceeded the requirements of procedure PT-39, and it was initially judged to be a violation of the"Primary Coolant Sources Outside Containment Program", as specified in the Ginna Station Improved Technical Specifications (ITS)Section 5.5.2.The PORC chairman conservatively directed the Shift Supervisbr to enter ITS Limiting Condition for Operation (LCO)3.0.3, based on the requirements of procedure PT-39 and Administrative Procedure A-52.4,"Control of Limiting Conditions for Operating Equipment", even though the plant was in compliance with all ITS LCOs.NRC FORM 366A (4-95I NRC FORM 366A (4.95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)DOCKET LER NUMBER (6)PAGE (3)R.E.Ginna Nuclear Power Plant 05000244 YEAR SEQUENTIAL REVISION NUMBER NUMBER 3 OF 5 96-009-00 TEXT llf more space is required, use additional copies of NRC Form 366Al (17)DESCRIPTION OF EVENT: A.DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
Due to the location and size of the leak, an operability assessment determined that no emergency safeguards system function was made inoperable. However, the leak was not isolable from the RWST without valve manipulations that would have resulted in the inoperability of the RWST and both trains of the ECCS.
July 22, 1996, 1130 EDST: A leak is identified on a line outside of Containment.
NRC FORM 366A (4.95)
July 23, 1996, 0857 EDST: Event Date and Time and Discovery Date and Time.July 23, 1996, 0900 EDST: Load reduction is started.July 23, 1996, 1440 EDST: Integrated leakage outside Containment is determined to be less than two GPH.Load reduction is stopped.B.EVENT: On July 23, 1996, at approximately 0857 EDST, with the plant in Mode 1 at approximately 100%steady state reactor power, the Plant Operations Review Committee (PORC)conservatively directed the Shift Supervisor to enter ITS LCO 3.0.3.The Shift Supervisor directed the Control Room operators to initiate a plant shutdown.At approximately 0900 EDST, the Control Room operators initiated a plant shutdown per Normal Operating Procedure 0-2.1,"Normal Shutdown to Hot Shutdown".
 
The Mechanical Support group initiated actions to provide a freeze seal to isolate the source of leakage from the RWST.A freeze seal was initiated between the leaking socket and the CS pump suction line from the RWST.At approximately 1440 EDST on July 23, 1996, the freeze seal had isolated the leak.ITS LCO 3.0.3 was exited and the load reduction was stopped.The affected pipe and socket welds were cut out and a new prefabricated spoolpiece was installed.
NRC FORM 366A                                                                                 U.S. NUCLEAR REGULATORY COMMISSION (4.95)
The affected weld was retained for failure mode analysis.A load increase to return the plant to full power was initiated at approximately 1530 EDST on July 23, 1996.C.INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: Due to the location and size of the leak, an operability assessment determined that no emergency safeguards system function was made inoperable.
LICENSEE EVENT REPORT (LER)
However, the leak was not isolable from the RWST without valve manipulations that would have resulted in the inoperability of the RWST and both trains of the ECCS.NRC FORM 366A (4.95)
TEXT CONTINUATION FACILITY NAME I1)                                   DOCKET           LER NUMBER I6)         PAGE {3)
NRC FORM 366A (4.95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME I1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER I6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-009-00 PAGE{3)4 OF 5 TEXT iif more space is required, use addi rional copies of NRC Form 38&A/(17)METHOD OF DISCOVERY'he leak was first discovered by an RP technician during a routine weekly survey of the Auxiliary Building.He notified the Control Room operators, and the precise location was confirmed by Operations and Engineering.
YEAR   SEQUENTIAL REVISION NUMBER     NUMBER 4 OF    5 R.E. Ginna Nuclear Power Plant                                    05000244      96   009           00 TEXT iifmore space is required, use addi rional copies of NRC Form 38&A/ (17)
Confirmation that the leak rate was above 2 GPH occurred after measurements performed at the direction of PORC.F.OPERATOR ACTION: When notified by PORC, the Shift Supervisor directed the Control Room operators to enter ITS LCO 3.0.3 and to initiate a plant shutdown.The Control Room operators initiated a plant shutdown per procedure 0-2.1.The Shift Supervisor subsequently notified the NRC per 10 CFR 50.72 (b)(1)(i)(A), non-emergency one hour notification, at approximately 0951 EDST on July 23, 1996.When the leak was isolated, ITS LCO 3.0.3 was exited, and the plant was returned to full power.G.SAFETY SYSTEM RESPONSES:
METHOD OF       DISCOVERY'he leak was first discovered by an RP technician during a routine weekly survey of the Auxiliary Building. He notified the Control Room operators, and the precise location was confirmed by Operations and Engineering. Confirmation that the leak rate was above 2 GPH occurred after measurements performed at the direction of PORC.
None III.CAUSE OF EVENT: A;IMMEDIATE CAUSE: The immediate cause of the condition prohibited by Technical Specifications was the conservative determination by PORC to enter ITS LCO 3.0.3 due to the leak.B.INTERMEDIATE CAUSE: The intermediate cause of the leak was a pinhole leak in the weld attaching the pipe to the socket elbow.C.ROOT CAUSE: The affected pipe, socket, and fillet weld were analyzed for the failure mode.The pinhole was determined to be an original installation weld defect (dating from the 1960's)that existed over an area of slag inclusion in the weld.Almost all the slag had been leached from the pinhole channel over the past 25 years.This event is NUREG-1022 Cause Code (B),"Design, Manufacturing, Construction
F.         OPERATOR ACTION:
/Installation".
When notified by PORC, the Shift Supervisor directed the Control Room operators to enter ITS LCO 3.0.3 and to initiate a plant shutdown.               The Control Room operators initiated a plant shutdown per procedure 0-2.1.
The Shift Supervisor subsequently notified the NRC per 10 CFR 50.72 (b) (1) (i) (A), non-emergency one hour notification, at approximately 0951 EDST on July 23, 1996. When the leak was isolated, ITS LCO 3.0.3 was exited, and the plant was returned to full power.
G.         SAFETY SYSTEM RESPONSES:
None III. CAUSE OF EVENT:
A;         IMMEDIATECAUSE:
The immediate cause of the condition prohibited by Technical Specifications was the conservative determination by PORC to enter ITS LCO 3.0.3 due to the leak.
B.         INTERMEDIATE CAUSE:
The intermediate cause of the leak was a pinhole leak in the weld attaching the pipe to the socket elbow.
C.       ROOT CAUSE:
The affected pipe, socket, and fillet weld were analyzed for the failure mode. The pinhole was determined to be an original installation weld defect (dating from the 1960's) that existed over an area of slag inclusion in the weld. Almost all the slag had been leached from the pinhole channel over the past 25 years.
This event is NUREG-1022 Cause Code (B), "Design, Manufacturing, Construction / Installation".
NRC FORM 366A I4-95)
NRC FORM 366A I4-95)
NRC FORM 366A I4-95)LXCENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME I1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-009-00 PAGE I3)5 OF 5 TEXT (if more speceis required, use eddidonel copies of NRC Form 386AI I17)IV.ANALYSIS OF EVENT: This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(8),"Any operation or condition prohibited by the plant's Technical Specifications".
 
The integrated leak rate in excess of 2 GPH outside CNMT resulted in conservative entry into ITS LCO 3.0.3.An assessment will be performed considering both the safety consequences and implications of this event.A supplement to this LER will be submitted with the results of this assessment.
NRC FORM 366A                                                                           U.S. NUCLEAR REGULATORY COMMISSION I4-95)
V.CORRECTIVE ACTION: A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: o The source of the leakage was isolated from the RWST by freeze seal, permitting exit from ITS LCO 3.0.3.o The affected pipe and socket welds were cut out and replaced with a new prefabricated spoolpiece, and the freeze seal was removed.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
LXCENSEE EVENT REPORT             (LER)
o Failure Analysis of the leak in the socket weld has been performed.
TEXT CONTINUATION FACILITY NAME I1)                               DOCKET           LER NUMBER (6)           PAGE I3)
o The adjacent original existing welds were cut out and replaced.o Additional corrective actions will be identified in a supplement to this LER.VI.ADDITIONAL INFORMATION:
YEAR   SEQUENTIAL REVISION NUMBER     NUMBER R.E. Ginna Nuclear Power Plant                                                                          5  OF    5 05000244      96   009           00 TEXT (ifmore speceis required, use eddidonel copies of NRC Form 386AI I17)
A.FAILED COMPONENTS:
IV. ANALYSIS OF EVENT:
The failed component was a 2 inch nominal pipe size Schedule 10 pipe-to-90 degree forged socket elbow weld.The pipe and socket elbow are stainless steel, ASTM A312 Type 304 and A182 F304 (forged)respectively.
This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i)
The socket weld was ar)original installation weld made before 1970.B.PREVIOUS LERs ON SIMILAR EVENT" A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.
(8), "Any operation or condition prohibited by the plant's Technical Specifications". The integrated leak rate in excess of 2 GPH outside CNMT resulted in conservative entry into ITS LCO 3.0.3.
C.SPECIAL COMMENTS: N A A I4.)N}}
An assessment will be performed considering both the safety consequences and implications of this event.
A supplement to this LER will be submitted with the results of this assessment.
V.     CORRECTIVE ACTION:
A.       ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
o         The source of the leakage was isolated from the RWST by freeze seal, permitting exit from ITS LCO 3.0.3.
o         The affected pipe and socket welds were cut out and replaced with a new prefabricated spoolpiece, and the freeze seal was removed.
ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
o         Failure Analysis of the leak in the socket weld has been performed.
o       The adjacent original existing welds were cut out and replaced.
o       Additional corrective actions will be identified in a supplement to this LER.
VI.     ADDITIONALINFORMATION:
A.       FAILED COMPONENTS:
The failed component was a 2 inch nominal pipe size Schedule 10 pipe-to-90 degree forged socket elbow weld. The pipe and socket elbow are stainless steel, ASTM A312 Type 304 and A182 F304 (forged) respectively. The socket weld was ar) original installation weld made before 1970.
B.       PREVIOUS LERs ON SIMILAR EVENT" A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.
C.       SPECIAL COMMENTS:
N N       A   A I4. )}}

Latest revision as of 17:04, 29 October 2019

LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr
ML17264A589
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/22/1996
From: Martin J, Mecredy R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-96-009, LER-96-9, NUDOCS 9608300053
Download: ML17264A589 (8)


Text

CATEGORY 3 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9608300053 DOC.DATE: 96/08/22 NOTARIZED: NO DOCKET g FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION MARTIN,J.T. Rochester Gas a Electric Corp.

MEREDYiR.C. Rochester Gas a Electric Corp.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 96-009-00:on 960723,determined from leak on piping, sys outside containment greater than program limit.Caused by weld defect. Pipe a socket welds were cut out & replaced.

W/960822 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 RECIPIENT COPIES RECIPIENT COPIES

~

ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-1 PD 1 1 'ISSINGIG.

1 1 INTERNAI~G~ 2 2 AEOD/SPD/RRAB 1 1 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 D RGN1 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 U

N NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE CONTACT THE DOCUMENT CONTROL DESK i ROOM OWFN 5D-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25

AND

'Pr JA'F RGCHfSTfR OPS P~D flfCTRICCCR. CZ47lCiv ~ MST A'IENUf,RCCHfSTfR, N, Y Idol& ml ~ ARE< COOf 71o S46-2700 v '+ )vol August 22, 1996 U.S. Nuclear Regulatory Commission Document Control Desk Attn: Guy Vissing Project Directorate I-1 Washington, D.C. 20555

Subject:

LER 96-009, Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit R.E. Ginna Nuclear Power Plant Docket No. 50-244

Dear Mr. Vissing:

In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i) (B), "Any operation or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 96-009 is hereby 'ubmitted. Entry into Limiting Condition for Operation 3.0.3 of Technical Specifications was a conservative action based upon Ginna Station T.S. 5.5.2 "Primary Coolant Sources Outside Containment Program". A further assessment will be provided in a supplement to this LER which will be submitted by September 20, 1996.

This event has in no way affected the public's health safety.

Very truly yours, Robert C. Mecredy JSM:435 xc: Mr. Guy Vissing (Mail Stop 14C7)

Project Directorate I-1 Washington, D.C. 20555 U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna Senior Resident Inspector 9608300053 960822 PDR ADOCK 05000244 8 V LJ V PDR

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSIO APPROVED BY OMB NO. 3150.0104 (4-95) EXPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.

LICENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK To INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE (See reverso for required number of INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33),

digits/characters for each block) U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555.0001, AND To THE PAPERWORK REDUCTION PROJECT FACILITYNAME (11 DOCKET NUMBER (21 PAGE (3)

R.E. Ginna Nuclear Power Plant 05000244 1 OF 5 TITLE (41 Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit EVENT DATE (5) LER NUMBER (6) REPORT DATE (? I OTHER FACILITIES INVOLVED (6)

FACIUTY NAME OOCKET NUMBER SEQUENTIAL REVISION MONTH DAY YEAR NUMBER NUMBER MONTH DAY YEAR FACILrrY NAME OOCKETNUMBER 07 23 96 96 009 00 08 22 96 OPERATING THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR E: (Chock one or more) (11)

MODE (9) 20.2201(b) 20.2203(a)(2)(v) X 50.73(a)(2)(i) 50.73(a)(2)(viii)

POWER 20.2203(a) (1) 20.2203(a)(3)(il SO. ?3(a)(2)(ii) 50.73(a)(2)(x)

LEVEL (10) 100 20.2203(a) l2)(i) 20.2203(a) (3) (ii) S0.73(a)(2) (iii) 73.71 20.2203(a)(2)(ii) 20.2203(a) (4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2) (iii) 50.36(c)(1) 50.73(a)(2)(v) Specify In Abstract below or in NRC Form 366A 20.2203(a) (2)(iv) 50.36(c)(2) 50.73(a) (2) (vii)

LICENSEE CONTACT FOR THIS LER (12)

NAME '(ELEFHONE NUMBER (Inorvde Area Code)

John T. St. Martin - Technical Assistant (716) 771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DES CRIBFD IN THIS REPORT (13)

REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER To NPRDS CAUSE SYSTEM COMPONENT MANUFACTURER To NPRDS BE PSF SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED YES SUBMISSION (II yos, complete EXPECTED SUBMISSION DATE).

NO DATE (15) 09 20 96 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines) (16)

On July 23, 1996, at approximately 0857 EDST, it was determined that the leak rate (from a leak on a piping system outside Containment) was greater than the analyzed value of two gallons per hour for a primary coolant source outside Containment.

Immediate corrective action was to conservatively enter Technical Specification Limiting Condition for Operation 3.0.3 and initiate a plant shutdown,.and to initiate actions to isolate the leak using a freeze seal. Once the leak was isolated, the plant exited Technical Specification 3.0.3 and the shutdown was stopped. The leaking pipe was cut out and replaced.

The underlying cause of the leak was a weld defect which dates back to original construction in the 1960's.

This event is NUREG-1022 Cause Code (B).

Corrective action to prevent recurrence is outlined in Section V.B. Additional corrective actions will be identified in a supplement to this LER.

NRC FORM 366 l4-95)

NRC FORM 366A U.S. NUCLEAR REGULATORY CONIMISSION (4-95I LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6I PAGE (3I YEAR SEQUENTIAL REVISION NUMBER NUMBER R.E. Ginna Nuclear Power Plant 05000244 2 OF 5 96 009 00 TEXT llfmore spaceis required, use additional copies of NRC Form 886A/ (17I PRE-EVENT PLANT CONDITIONS:

On July 22, 1996, the plant was in Mode 1 at approximately 100% steady state reactor power. At approximately 1130 EDST, a Radiation Protection (RP) technician, who was performing a routine weekly survey of the Auxiliary Building, observed water dripping in an area behind the Refueling Water Storage Tank (RWST). The RP technician notified the Control Room operators. Efforts to locate the source of the dripping water and to quantify the leak rate were initiated by Operations and Nuclear Engineering Services (NES). The source of water was determined to be a small leak on a test line for the Containment Spray (CS) system in the Auxiliary Building, which is outside the Containment (CNMT). The leak rate was estimated to be approximately one (1) gallon per nour (GPH).

The Control Room operators did not identify any requirement that would limit plant operations. The Shift Supervisor notified Operations management, maintenance management, and plant and NES staff of the leak. All reached a similar conclusion. The staff worked on developing and implementing an action plan to address the problem. The issues of line integrity and RWST operability were investigated by NES and Laboratory Inspection Services (LIS) personnel LIS personnel measured the amount of pipe cross-section

~

and weld metal remaining, and NES personnel determined that there was ample metal in the affected area to provide system integrity.

The source of the leak was identified as a small pinhole leak on a pipe-to-90 degree forged socket elbow weld on a two (2) inch nominal pipe size Schedule 10 stainless steel test line for the CS system. The leak was in a part-of the CS system that could not be isolated from the RWST by valve manipulations without making both trains of the emergency core cooling system (ECCS) inoperable. The leak was monitored throughout the remainder of the day and night.

An operability assessment had been requested by the Shift Supervisor on July 22. On the 'morning of July 23, 1996, this assessment was reviewed by the Plant Operations Review Committee (PORC). This assessment, which was based on conservative assumptions, concluded that the RWST and ECCS were still operable with the unisolated leak. This conclusion was supported by the fact that there was still ample metal area in the cross-section that can provide integrity of the pipe during a seismic event, and that the total combined stress was less than the yield strength of the material.

PORC requested a more accurate estimate of the leak rate. The leak rate was measured and estimated to be 2.5 GPH. This leak rate is in excess of two (2) GPH, which is specified in Surveillance Test Procedure PT-39, "Leakage Evaluation of Primary Coolant Sources Outside Containment", as the program limit for the maximum integrated leak rate outside CNMT from these sources. The leak rate exceeded the requirements of procedure PT-39, and it was initially judged to be a violation of the "Primary Coolant Sources Outside Containment Program", as specified in the Ginna Station Improved Technical Specifications (ITS) Section 5.5.2.

The PORC chairman conservatively directed the Shift Supervisbr to enter ITS Limiting Condition for Operation (LCO) 3.0.3, based on the requirements of procedure PT-39 and Administrative Procedure A-52.4, "Control of Limiting Conditions for Operating Equipment", even though the plant was in compliance with all ITS LCOs.

NRC FORM 366A (4-95I

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4.95)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 3 OF 5 R.E. Ginna Nuclear Power Plant 05000244 96 009 00 TEXT llfmore space is required, use additional copies of NRC Form 366Al (17)

DESCRIPTION OF EVENT:

A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:

July 22, 1996, 1130 EDST: A leak is identified on a line outside of Containment.

July 23, 1996, 0857 EDST: Event Date and Time and Discovery Date and Time.

July 23, 1996, 0900 EDST: Load reduction is started.

July 23, 1996, 1440 EDST: Integrated leakage outside Containment is determined to be less than two GPH. Load reduction is stopped.

B. EVENT:

On July 23, 1996, at approximately 0857 EDST, with the plant in Mode 1 at approximately 100%

steady state reactor power, the Plant Operations Review Committee (PORC) conservatively directed the Shift Supervisor to enter ITS LCO 3.0.3. The Shift Supervisor directed the Control Room operators to initiate a plant shutdown. At approximately 0900 EDST, the Control Room operators initiated a plant shutdown per Normal Operating Procedure 0-2.1, "Normal Shutdown to Hot Shutdown".

The Mechanical Support group initiated actions to provide a freeze seal to isolate the source of leakage from the RWST. A freeze seal was initiated between the leaking socket and the CS pump suction line from the RWST. At approximately 1440 EDST on July 23, 1996, the freeze seal had isolated the leak. ITS LCO 3.0.3 was exited and the load reduction was stopped. The affected pipe and socket welds were cut out and a new prefabricated spoolpiece was installed. The affected weld was retained for failure mode analysis.

A load increase to return the plant to full power was initiated at approximately 1530 EDST on July 23, 1996.

C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

Due to the location and size of the leak, an operability assessment determined that no emergency safeguards system function was made inoperable. However, the leak was not isolable from the RWST without valve manipulations that would have resulted in the inoperability of the RWST and both trains of the ECCS.

NRC FORM 366A (4.95)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4.95)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME I1) DOCKET LER NUMBER I6) PAGE {3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 4 OF 5 R.E. Ginna Nuclear Power Plant 05000244 96 009 00 TEXT iifmore space is required, use addi rional copies of NRC Form 38&A/ (17)

METHOD OF DISCOVERY'he leak was first discovered by an RP technician during a routine weekly survey of the Auxiliary Building. He notified the Control Room operators, and the precise location was confirmed by Operations and Engineering. Confirmation that the leak rate was above 2 GPH occurred after measurements performed at the direction of PORC.

F. OPERATOR ACTION:

When notified by PORC, the Shift Supervisor directed the Control Room operators to enter ITS LCO 3.0.3 and to initiate a plant shutdown. The Control Room operators initiated a plant shutdown per procedure 0-2.1.

The Shift Supervisor subsequently notified the NRC per 10 CFR 50.72 (b) (1) (i) (A), non-emergency one hour notification, at approximately 0951 EDST on July 23, 1996. When the leak was isolated, ITS LCO 3.0.3 was exited, and the plant was returned to full power.

G. SAFETY SYSTEM RESPONSES:

None III. CAUSE OF EVENT:

A; IMMEDIATECAUSE:

The immediate cause of the condition prohibited by Technical Specifications was the conservative determination by PORC to enter ITS LCO 3.0.3 due to the leak.

B. INTERMEDIATE CAUSE:

The intermediate cause of the leak was a pinhole leak in the weld attaching the pipe to the socket elbow.

C. ROOT CAUSE:

The affected pipe, socket, and fillet weld were analyzed for the failure mode. The pinhole was determined to be an original installation weld defect (dating from the 1960's) that existed over an area of slag inclusion in the weld. Almost all the slag had been leached from the pinhole channel over the past 25 years.

This event is NUREG-1022 Cause Code (B), "Design, Manufacturing, Construction / Installation".

NRC FORM 366A I4-95)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I4-95)

LXCENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME I1) DOCKET LER NUMBER (6) PAGE I3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER R.E. Ginna Nuclear Power Plant 5 OF 5 05000244 96 009 00 TEXT (ifmore speceis required, use eddidonel copies of NRC Form 386AI I17)

IV. ANALYSIS OF EVENT:

This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i)

(8), "Any operation or condition prohibited by the plant's Technical Specifications". The integrated leak rate in excess of 2 GPH outside CNMT resulted in conservative entry into ITS LCO 3.0.3.

An assessment will be performed considering both the safety consequences and implications of this event.

A supplement to this LER will be submitted with the results of this assessment.

V. CORRECTIVE ACTION:

A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:

o The source of the leakage was isolated from the RWST by freeze seal, permitting exit from ITS LCO 3.0.3.

o The affected pipe and socket welds were cut out and replaced with a new prefabricated spoolpiece, and the freeze seal was removed.

ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

o Failure Analysis of the leak in the socket weld has been performed.

o The adjacent original existing welds were cut out and replaced.

o Additional corrective actions will be identified in a supplement to this LER.

VI. ADDITIONALINFORMATION:

A. FAILED COMPONENTS:

The failed component was a 2 inch nominal pipe size Schedule 10 pipe-to-90 degree forged socket elbow weld. The pipe and socket elbow are stainless steel, ASTM A312 Type 304 and A182 F304 (forged) respectively. The socket weld was ar) original installation weld made before 1970.

B. PREVIOUS LERs ON SIMILAR EVENT" A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.

C. SPECIAL COMMENTS:

N N A A I4. )