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| issue date = 07/19/1989
| issue date = 07/19/1989
| title = LER 89-007-00:on 890619 & 21 Safety Injection Pumps B & C Inoperable Due to Assessed Design Flow Delivery Concerns. Caused by Recirculation Valves Being Full Open.Orifice Plates in Flow Loops Verified to Be correct.W/890719 Ltr
| title = LER 89-007-00:on 890619 & 21 Safety Injection Pumps B & C Inoperable Due to Assessed Design Flow Delivery Concerns. Caused by Recirculation Valves Being Full Open.Orifice Plates in Flow Loops Verified to Be correct.W/890719 Ltr
| author name = BACKUS W H, MECREDY R C
| author name = Backus W, Mecredy R
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:;A,CCELERATED Dl BUTION DEMONS TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RXDS)ACCESSION NBR:8907280303 DOC.DATE: 89/07/19 NOTARIZED:
{{#Wiki_filter:; A,CCELERATED           Dl                     BUTION         DEMONS           TION     SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RXDS)
NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION MECREDY,R.C.
ACCESSION NBR:8907280303                           DOC.DATE: 89/07/19       NOTARIZED: NO           DOCKET g FACIL:50-244 Robert     Emmet                 Ginna Nuclear Plant,   Unit   1, Rochester   G 05000244 AUTH. NAME         AUTHOR AFFILIATION MECREDY,R.C.       Rochester Gas & Electric Corp.
Rochester Gas&Electric Corp.BACKUS,W.H.
BACKUS,W.H.         Rochester Gas & Electric Corp.
Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION DOCKET g 05000244
RECIP.NAME         RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 89-007-00:on 890619,safety injection pumps inoperability concerns due to flow meter calibration errors.W/8 ltr.~DISTRIBUTION CODE: IE22T COPXES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event: Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
LER   89-007-00:on 890619,safety injection pumps                         inoperability concerns due to flow meter calibration errors.
05000244 RECIPIENT XD CODE/NAME PD1-3 LA JOHNSON,A COPIES LTTR ENCL 1 1 1 1 RECIPXENT ID CODE/NAME PD1-3 PD COPIES LTTR ENCL 1 1 INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB DEDRO NRR/DEST/ADE 8H NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NUDOCS-ABSTRACT RES/DSIR/EIB RGN1 FILE 01 EXTERNAL: EG&G WILLIAMS, S L ST LOBBY WARD NRC PDR NSXC MURPHY,G.A 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 4 1 1 1 1 1 1 ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP IRM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/PEB 10 NRR DREP/RPB 10 egREC 02 RES/DSR/PRAB FORD BLDG HOY,A.LPDR NSIC MAYS,G 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 l.1 1 NOTE'IO ALL''RIC6" R1KIPZEÃIS'IZASE HELP US'IO RXXQCB HASTE!CGMI'ACT'IHE DOCGMERI'ONGEAL DESK, RXH Pl-37 (EXT.20079)K)XXi062QTB RX3R MME PBCH DIPZBIBUTXCN LISTS FOR DOCUMENTS KQ DOHiT NEED)R I D S A D D S FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 43 ENCL 42  
W/8         ltr.
$TCR GAS A>VD.I'-CITRIC CORPORATION o 89;=A~;,i,",,:NJ;.,">O',I<;.",'," July 19, 1989 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
DISTRIBUTION CODE: IE22T COPXES RECEIVED:LTR                               ENCL       SIZE:
TITLE: 50.73/50.9 Licensee Event: Report (LER), Incident Rpt, etc.
~
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).                                   05000244 RECIPIENT                           COPIES            RECIPXENT            COPIES XD CODE/NAME                         LTTR ENCL        ID  CODE/NAME        LTTR ENCL PD1-3 LA                               1     1     PD1-3 PD                 1    1 JOHNSON,A                              1     1 INTERNAL: ACRS MICHELSON                             1    1      ACRS MOELLER              2    2 ACRS WYLIE                             1    1      AEOD/DOA                  1    1 AEOD/DSP/TPAB                           1    1      AEOD/ROAB/DSP            2    2 DEDRO                                   1    1      IRM/DCTS/DAB              1    1 NRR/DEST/ADE 8H                         1    1      NRR/DEST/ADS      7E      1    0 NRR/DEST/CEB 8H                        1    1      NRR/DEST/ESB      8D      1    1 NRR/DEST/ICSB 7                        1    1      NRR/DEST/MEB      9H      1     1 NRR/DEST/MTB 9H                        1    1      NRR/DEST/PSB      8D     1    1 NRR/DEST/RSB 8E                        1    1      NRR/DEST/SGB      8D     1    1 NRR/DLPQ/HFB 10                        1    1      NRR/DLPQ/PEB     10     1    1 NRR/DOEA/EAB 11                        1    1      NRR DREP/RPB     10     2    2 NUDOCS-ABSTRACT                        1    1    egREC               02     1    1 RES/DSIR/EIB                            1    1      RES/DSR/PRAB             1    1 RGN1    FILE 01                        1    1                                                    R EXTERNAL: EG&G WILLIAMS,S                            4    4      FORD BLDG HOY,A.         1     1             I L ST LOBBY WARD                        1     1     LPDR                      1     l.
NRC PDR                                1     1     NSIC MAYS,G              1     1             D NSXC MURPHY,G.A                        1     1 S
A D
D NOTE 'IO ALL ''RIC6" R1KIPZE&#xc3;IS'IZASE S
HELP US 'IO RXXQCB HASTE!               CGMI'ACT 'IHE DOCGMERI'ONGEAL DESK, RXH Pl-37 (EXT. 20079)                 K) XXi062QTB RX3R MME PBCH DIPZBIBUTXCN LISTS FOR   DOCUMENTS               KQ DOHiT NEED)
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                           43   ENCL     42
 
      $ TCR GAS A>VD . I '-CITRIC CORPORATION o 89;=A~;,i,",,:NJ;.,">O',I<;.", ',"
July 19,       1989 U.S. Nuclear Regulatory Commission Document     Control Desk Washington,     DC   20555


==Subject:==
==Subject:==
LER 89-007, Safety In)ection Pumps Inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclear Industry R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, which permits and encourages Licensees to report signi-ficant, events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73, the attached Licensee event report LER 89-007 is hereby submitted.
LER       89-007, Safety In) ection Pumps Inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclear Industry R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System,   which permits and encourages Licensees to report signi-ficant, events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73, the attached Licensee event report LER 89-007 is hereby submitted.
This event has in no way affected the public's health and safety.Very truly yours, Robert C.Me General Manager Nuclear Production xco U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 3907280303 890719 rDFl ODOCK 0~000244 S PDC NAC t>>e 200 IS021 LICENSEE EVENT REPORT ILERI UX.NVCLCA1 1lOULATOAY COMMISSION AttAOVlD OMS NO.2100 OIOV CXtllll~0/SI/05 tACILITY NAMC Ill R.E.Ginna Nuclear Power Plant DOCS lT NVMStA (2)*0 6 oo0244IOF1 0 Safety injection Pumps inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclea-Indust tVCNT OATl ISI LtA NUMSCA Ill 1ttOAT OATC Ill OTHtA I'ACILITICS INVOLVCO ISI IeONTH OAY YCAA YCAA~COUINTIAL I)", AlVNIQN NUMetll ctt NUMeell MON'TH OAY YCAA tACIUTV HAULS OOCX CT NVMSCAISI 0 6 0 0 0 06198 9 8 9 007 00 0 7 1 9 8 9 0 6 0 0 0 Ot t A AT INC MOOC Ill~OrrlA LCVSL 0 9 9 (101 20.402(ol 2ILe00(e)Ill(0 20.e00 4)Ill Ill 20.e00 4)ll)IXII 20.e00 4 lll)(II I 20.e00 4)(1 I (el 20.400(el~0DS(el(I)SOW(el(21~0.2 24)(2)10~0.2 541(2)I~I$0024I12IIXO I,ICCNSll CONTACT tOA THIS LCA 1121 50.22(el(2l(lrl 00.254H2)(rl l0.224)(2) lrel 00.2241(2)
This event has in no way affected the public's health and safety.
I>>X)(Al~0.224)(2)(rNIISI 50.224)(2)(el 0 THC AtOVIAtMCNTS Ot 10451)I ICo>>e er>>er>>ere el Me lerrerrert) ill)THIS 1ttOAT IS SUSMITYCD tVASUANT T 222 (IS)12.1141 DTHtA Ite>>IIV M Aereoct e>>e>>errt le TecL HAC t>>IN HAM C Wesley H.Backs Technical Assistant to the Operations Manager TCLttHONl NUMSCA AAtA COOl 31 5524-4 446 COMtLCTC ONC LINC tOA tACH COMtONCNT tAILUAt OCSCAI~CD IN THIS AltOAT (12)CAV52 tYSTCM COMtONCNT MANVtAC TVACA Fek&v~k4kW CAUSC SYSTCM COMtONCNT MANUSAC, TUACA CtOATASL TO NtAOS SUttLCMCNTAL AltOAT CXt CCTCO lie)YCS (H tre, CerVNr>>CXttCTCD SVSMISSIOH DATCI X ND AACTAAOT ILervc Io le00 ieec>>, le,.ettroeerN>>lt IHIuo vetreetue ctteorlr>>e xe>>I llsl tXtCCTCD SVSMI$$ION OATS Ill)MONTH CAY YCAA On June 19, 1989 at 1440 EDST with the reactor at approximately 994 full power-the<<B" and<<C<<Safety In)ection (SI)pumps were declared inoperable due to assessed design flow delivery concerns.Declaring two (2)SI pumps inoperable placed the plant outside the Technical Specifications requiring a plant shutdown.While in the process of plant shutdown the SI pump flows were returned to the required flow rates by pump minimum flow recirculation line valve throttling.
Very truly yours, Robert C. Me General Manager Nuclear Production xco       U.S. Nuclear Regulatory Commission Region 475 I
On June 21, 1989 at 1401 a similar problem occurred with the<<B<<and<<C<<SI pumps and plant management decided to shut the plant down until the SI pump flow concerns were resolved.The plant was shutdown and subsequently cooled down to less than 350 F.Original calibration data provided by the plant design was incorrect for the installed application.
Allendale Road King of Prussia, PA         19406 Ginna USNRC       Senior Resident Inspector 3907280303 890719 rDFl   ODOCK 0~000244 S                   PDC
The underlying cause of the event resulted from incorrect original calibration data, provided by the plant designer for the installed system.N1C lore 200 (242)
 
II AC tea 000A IM0I LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.L NUCLCAA 004ULAf OAY CCXXXUWISI 4tt+OV lO OQC IIO.4100&I/8 axxtACS anIICS SACILlf Y HAXIC Ill L0%IIIAX001 ICI XX CU X tt T I k L~t vtxtott It lt 8~A40 I3I R.E.Ginna Nuclear Power Plant TACT Ill awe~4 I+tvlwL~~IICIC Axtx~'ll l17l 0 5 0 0 0 2 4 4 8 9-0 07-00 0 2 of 0 7 PRE-EVENT PLANT CONDITIONS The unit was at approximately 994 steady state full power with no major activities in progress.Results and Test (R&T)personnel were in the Control Room discussing changes to periodic test procedure PT-2.1 (Safety Injection System Pumps)with the Control Room operators.
NAC   t>>e   200                                                                                                                           UX. NVCLCA1 1lOULATOAYCOMMISSION IS021 AttAOVlDOMS NO.2100 OIOV LICENSEE EVENT REPORT ILERI                                                        CXtllll 0/SI/05
These changes to PT-2.1 were necessary to reflect modifications made to the Safety Injection (SI)pumps minimum flow recirculation lines during the recent annual refueling and maintenance outage.This modification in part increased the size of the SI pumps recirculation lines to increase the recirculation flow for better pump reliability.
                                                                                                                                                                  ~
During the post modification testing of the SZ pumps, the"B" and."C" SI pumps exhibited problems meeting the design flow rates to the reactor coolant system as indicated on SI flow indicator FZ-925.Because of the above indicated design flow rate delivery problems, the"B" and"C" SZ pump minimum flow recirculation valves were throttled to 50 gpm to achieve the required design flow rates to the reactor coolant system.As the"A" SX pump did not exhibit problems achieving design flow rates to'he Reactor Coolant System (RCS), its recirculation valve was locked full open.II~DESCRIPTION OP.ER"NT A.DATES AND APPROXIMATE TIMES FOR MAJOR OCCUEKENCES o June 19, 1989, 1440 EDST: Event date and time.o June 19, 1989, 1440 EDST: Discovery date ynd time.o June 19, 1989, 1440 EDST: Started unit load reduction.
tACILITYNAMC Ill                                                                                                                   DOCS lT NVMStA (2)
o June 19, 1989, 1515 EDST: Unusual Event declared.vttC xCAv 0XAA 0 00 I IUIC tone~IMMI H UCENSEE EVENT REPORT HLER)TEXT CONTINUAT!ON US NUCLCAr AIOULATCNY
* R.E. Ginna Nuclear Power Plant                                                                                               0   6   oo0244IOF1                               0 Safety injection Pumps inoperability Concerns Due To Flow Meter Calibration Errors Could                 Be Of Generic Concern To Nuclea- Indust tVCNT OATl ISI                       LtA NUMSCA Ill                       1ttOAT OATC Ill                         OTHtA I'ACILITICS INVOLVCO ISI
~ISI~rovao OUC ro.OIsoaICA cxiIrcl c131es JACILIZY NAAIC III COCKET IIUUCCW Ql vtAA LI1 rlrICIO IQ$44UIIITIAL M r vavIr U r~AOC IS R.E.Ginna Nuclear Power Plant teer (A'~r 1vrvrrL~~WC'IrrI~'11 Im o s o o o 2 4 4 007 00 03 OF 1 0 June 19, 1989, 1615 EDST: "B" and"C" SI pumps declared operable.June 19, 1989, reduction.
                                              ~ COUINTIAL   I)", AlVNIQN MON'TH                                   tACIUTV HAULS                     OOCX CT NVMSCAISI IeONTH        OAY      YCAA    YCAA              NUMetll    ctt  NUMeell              OAY    YCAA 0   6   0   0   0 06198                     9 8 9                 007 Ill(0            00       0 7 1 9 8             9                                                 0   6   0   0   0 Ot t A AT INC THIS 1ttOAT IS      SUSMITYCD tVASUANT T 0 THC AtOVIAtMCNTS Ot      10451 )I ICo>>e er>> er >>ere el Me lerrerrert) ill)
1615 EDST: Stopped unit load 0 June 19, 1989, 1626 EDST: minated.Unusual Event ter-0 0 0 June 21, 1989, 1401 EDST: Started PT-2.1 on the SI pumps.June 21, 1989, 1728 EDST: Declared the"C" SI pump inoperable.
MOOC  Ill                 20.402(ol                              20.400(el                            50.22(el(2l(lrl                            222 (IS)
June 21, 1989, 1915 EDST: Started unit load reduction.
    ~ OrrlA                        2ILe00(e)                              ~ 0DS(el(I)                           00.254H2)(rl                              12.1141 LCVSL        0 9      9 (101                          20.e00 4) IllIll                        SOW(el(21                            l0.224)(2) lrel                          DTHtA Ite>>IIV M Aereoct e>>e>> errt le TecL HAC t>>IN 20.e00  4) ll) IXII                    ~ 0.2 24)(2)10                        00.2241(2) I>>X) (Al 20.e00 4 lll ) (III                    ~ 0.2 541(2) I ~ I                    ~ 0.224)(2)(rNIISI 20.e00 4)(1 I (el                       $ 0024I12IIXO                        50.224) (2)(el I,ICCNSll CONTACT tOA THIS LCA 1121 HAMC                                                                                                                                                  TCLttHONl NUMSCA Wesley H. Backs                                                                                                                 AAtA COOl Technical Assistant to the Operations Manager                                                                                   31         5524-4 446 COMtLCTC ONC LINC tOA tACH COMtONCNT         tAILUAtOCSCAI ~ CD IN THIS AltOAT (12)
0 B.EVENT: June 22, 1989, 0707 EDST: Reactor Coolant System (RCS)cold leg temperatures less than 350 F and RCS pressure less than 1600 psig.On June 19, 1989 at 1440 EDST the reactor was at approximately 994 full power.During discussions in the Control Room between R&T personnel and Control Room operators concerning proposed changes to procedure PT-2.1, it became apparent that the"B and"C" SI pump minimum flow recirculation line valves were locked full open rather than the recpxired throttled position.The Operations Shift Supervisor determined at this time that if the"B" and"C SI pumps were not aligned as per design, then the pumps were inoperable and this placed the plant operations outside of Technical Specification 3.3.1.1.C and 3.3.1.4 which state the following:
MANVtAC                                                                                   MANUSAC,          CtOATASL CAV52 tYSTCM            COMtONCNT                                                              CAUSC  SYSTCM    COMtONCNT              TUACA          TO NtAOS TVACA Fek&v
o 3.3.1.1.C:
                                                                          ~k4kW                                                                                 MONTH      CAY    YCAA SUttLCMCNTAL AltOAT CXt CCTCO       lie)                                               tXtCCTCD SVSMI$ $ ION OATS  Ill)
At or above a reactor coolant system pressure and temperature of 1600 psig and 350oFg except during performance of RCS Hydro Test, three safety injection pumps are operable.
YCS   (H tre, CerVNr>> CXttCTCD SVSMISSIOH DATCI                             X ND AACTAAOT ILervc Io le00 ieec>>, le,. ettroeerN>>lt IHIuo vetreetue ctteorlr>>e xe>>I llsl On        June 19, 1989 at 1440 EDST with the reactor at approximately 994         full power- the <<B" and <<C<< Safety In)ection (SI) pumps were declared inoperable due to assessed design flow delivery concerns.
NAC Fetes~I$4ll UCENSEE EVENT REPORT ILER}TEXT CONTINUATION II.L NUCllAA AIOVLATOAY CAN%ION Atf AOV lO OUO NO.)I94&I04 CXAIACS enII99 AACII.ITY NAMt Ill OOCAIT NUMlN Ql L41 NUU4l1 I9I 1 9 OMAH f I Al U veaoc H U~AOl Iel R.E.Ginna Nuclear Power Plant TTST Id aaae~N NWWC~~A9K'IAAA~'Al IITl o 5 o o o 24 489 00 7-00 040'3.3.1.4: The requirements of 3.3.1.1.C may be modified to allow one.safety injection pump to be inoperable for up to 72 hours.Because more than one SI pump was declared inoperable, this placed the plant-in a condition covered by Technical Specification 3.0.1 which states the following:
Declaring two (2) SI pumps inoperable placed the plant outside the Technical Specifications requiring a plant shutdown.                                                                                                 While in the process of plant shutdown the SI pump flows were returned to the required flow rates by pump minimum flow recirculation line valve throttling.
o In the event a Limiting Condition for operation and/or associated action requirements cannot be satisfied because of circumstances in excess of those addressed in the specification, within 1 hour action shall be initiated to place the unit in at least hot shutdown within the next 6 hours (i;e., a total of seven hours), and in at least cold shutdown within the following 30 hours (i.e., a total of 37 hours)unless corrective measures are completed that permit operation under the permissible action statements for the*specified time interval as measured from initial discovery or until the reactor is placed in a mode in which the specification is not applicable.
On       June 21, 1989 at 1401 a similar problem occurred with the <<B<<
Because of the above specification a unit load reduction to hot shutdown was started June 19, 1989 at 1440 EDST.At approximately 1515 EDST, June 19, 1989, the Operations Shift Supervisor declared an Unusual Event in accordance with SC-100,"Ginna Station Event Evaluation and Classification" EAL: Loss of Engineered Safety Features: exceeding a Limiting Condition for operation on a safety system requiring a plant shutdown;Tech Spec section 3.3 Emergency Core Cooling System.All offsite notifications were made per SC-601,"Unusual Event Notifications".
and <<C<< SI pumps and plant management decided to shut the plant down until the SI pump flow concerns were resolved.                                                                                               The plant was shutdown and subsequently cooled down to less than 350 F.
NIC IOlU)99A 9 QADI LICENSEE EVENT REPORT (LEA)TEXT CONTINUATION 11.4.NUCI,CAN 1!OQLAYOLY COMMI&lOW AttLOVtO OM4 NO.Jl&#xc3;&104 CLiiLee alii eS LAClllYY NAME ill OOCLLY NVIMIL QI L44 NUMClL (41 1%4ML H T I A I N VeaN N M N~A44 1$R.E.Ginna Nuclear Power Plant TKCf III'MWL~N IOOeeC~~NIC IINLI~'ll 117)o s o o o 2 4 4 8 9-0 0 7 0 0 0 5 OF 1 0 At approximately 1615 EDST, June 19, 1989 subsequent to the satisfactory testing and throttling of the"B" and"C" safety injection pumps minimum flow recircula-tion valves to 50 gpm, the"B" and"C" safety in)ection pumps were declared operable and the load reduction stopped.With the"B" and"C" safety in)ection pumps declared operable and the load reduction stopped, the Operations Shift Supervisor," with approval and concurrence from the Plant Manager Ginna Station, and PORC declared the Unusual Event terminated at 1626 EDST, June 19, 1989 in accordance with SC-110,"Ginna Station Event Evaluation For Reducing the Classification".
Original calibration data provided by the plant design was incorrect for the installed application. The underlying cause of the event resulted from incorrect original calibration data, provided by the plant designer for the installed system.
All offsite notifications were made of the Unusual Event termination and the plant was subsequently returned to approximately full power.On June 21, 1989 at 1401 EDST with the reactor at approximately full power, periodic test procedure PT-2.1 (Safety Injection Pumps)was started for the monthly test of the safety injection pumps.The following is a sequence of important events that happened: The"A" SI pump was tested first and tested satisfactorily.
N1C   lore   200 (242)
At approximately 1544 EDST, upon starting the"B" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 70 gpm.This was contrary to the'required 50 gpm maximum flow rate.The recirculation flow rate was reset to 45 gpm per PT-2.1.0 At approximately 1637 EDST, upon starting the"C" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 56 gpm.This was contrary to the required 50 gpm maximum flow rate.The recirculation flow rate was reset to 45 gpm per PT-2.1.%1C iOAM WA Y 4II INC Pens AIA 1044 I LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U,l.ISUCLlAA Cl4ULATOIY C5++%$4SS AppsoYlo oU4 no.$1 90&I4s lX~I'll SIT I ITS PACILITY NASSC Ill OOCIIlT IIU~CW Ql vSAA Llk IIUSSOC1 IN SSOUSNSIAL Q s vis sIn v M s~j4l ISI R.E.Qiana Nuc:lear Powe-Plant neer IS'~~e nWeeC~~P494 Pens~'sI I ITI o s o o o 2 4 4 89-00 7-00 0 6 ov 1 0 o At approximately 1726 EDST, the 99B" and I9C99 SZ pumps were started and stopped to verify recirc flov was less than or.equal to the required 50 gpm.Found the>>B" Sl pump recirc flow at 50 gpm and the"C" SZ pump recirc flov at 55 gpm.o At approximately 1728 EDST the"C" SZ pump was declared inoperable.
 
o At approximately 1900 EDST a meeting between shift operations and plant staff was conducted and the following course of action was decided upon: 1)Shutdown the plant to less than 350 F and less than 1600 psig, until the problem with the"C" SI pump minimum flov recirculation line flov repeatability is found and corrected.
U.L NUCLCAA 004ULAfOAY CCXXXUWISI IIAC tea 000A IM0I                         LICENSEE EVENT REPORT ILER) TEXT CONTINUATION                             4tt+OV lO OQC IIO. 4100&I/8 axxtACS anIICS
2)Reset the"C" SI pump minimum flow xecircu-lation flov.3)Test repeatability of the"C" SZ pump minimum flow recirculation flov.4)Correct the cause of pump minimum flow recirculation flow problem.On June 22, 1989 at approximately 0707 EDST the reactor coolant system cold leg temperatures were less than 350 F and RCS pressure was less than 1600 pSige C.D.INOPERABLE STRUCTURES P COMPONENTS P OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None.vsc polU sess 94SI Qec pena 000A I%4SI UCENSEE EVENT REPORT ILER)TEXT CONTINUATION II~NLCLlAN XlOOLATON T CaaaaWON APPNOV lO 440 NO.)ISOMIOS lXtiAIS SnIISS PACILITY NA4l 111 OOCXXT NV40SN ISI vlAA LlN NINS0l1 Ill SSOIISNTIAL U VISION N U a~AOl ISI R.E.Ginna NUclear Power Plant TENET IN rane~0 rsSUSSX~~ASIC Ireaa~'ll I ITI 0 5 0 0 0 2 4 4 8 9-007 00 07 OF 1 0 E.METHOD OF DISCOVERY'he first event was discovered during discussions between RET personnel and the Control Room operators, concerning proposed changes to PT-2.1.The second event was discovered during the monthly test of the safety in)ection pumps.F.OPERATOR ACTION: The ma)or operator action during the events was to reduce plant load and subsequently take the unit off line and cool down to less than 350 F.G.SAFETY SYSTEM RESPONSES:
                                                                                                                            ~ A40 SACILlfY HAXIC Ill                                                                 L0% IIIAX001 ICI                             I3I XXCU X tt T I k L       vtxtott
None.III CAUS OP A.IMMEDIATE CAUSE: The<<B<<and<<C<<SI pumps were thought to be inoperable because they could not meet their design flow rates to the RCS due to their recirc valves being full open rather than throttled as required.B.INTERMEDIATE CAUSE: 0 0 The<<B<<and<<C<<SI pump minimum flow recirculation valves were positioned full open rather than throttled as required.With the pump minimum flow recirculation valves restored to the throttled position, subsequent.
                                                                                            ~ t             It lt 8 TACT Illawe ~   4 I+tvlwL ~ ~
pump testing failed to achieve repeatable pump recirculation flow results.vaC POAU SSSA 9431~~V IIC GYM 500A LICENSEE EVENT REPORT (LER)TEXT CONTINUATION IIA.NJCLCASI 054UWTO4T COINNKIOIS ktf 0OV lO OM0 IIO.5150%104 55NA55 lltt4$SACII.ITV HMI5 Ill OOC&#xc3;5T IIU1%50 Ill YTAA I.I0 IIIAN54 III SSOVSNYIAl M A V%ION M~A45 I5I R.E.Ginna Nuclear Power Plant mCrIS~~e~~~ASSOIISMImauIITI o s o o o~4 4 89 00 7 0 08 oi C.ROOT CAUSE: The underlying cause of the event resulted from incorrect calibration data, provided by the plant designer for the installed system.The calibration data provided for flow transmitters FT-924 and FT-925 did not correlate accurately with the installed flow orifice plates,.FE-924 and FE-925.ALYSIS 0 The event is being reported in accordance with 10 CFR 50.73 Licensee Event Report System, which permits and encourages Licensees to report significant events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73.An assessment was performed considering both the safety consequences and.implications of this event with the following results and conclusions:
R.E. Ginna Nuclear Power Plant IICIC Axtx ~'ll l17l 0 5 0   0 0 2 4 4 8 9 0 07 00                         0   2 of     0 7 PRE-EVENT PLANT CONDITIONS The   unit       was at approximately 994 steady state                         full power with     no major activities in progress.                   Results                 and Test (R&T)       personnel       were   in the Control           Room             discussing changes to periodic test procedure PT-2.1 (Safety Injection System Pumps) with the Control Room operators.                                               These changes to PT-2.1 were necessary to reflect modifications made to the Safety Injection (SI) pumps minimum flow recirculation lines during the recent annual refueling and maintenance outage.               This modification in part increased the size of the SI pumps recirculation lines to increase the recirculation flow for better pump reliability. During the post modification testing of the SZ pumps, the "B" and.
There were no operational or safety consequences or implications attributed to the deemed to be inoperable"B" and"C" SI pumps because: o An analysis was performed using current calibration data, and it was determined that even with the"B" and"Cll SI pumps minimum flow recirculation valves full open, the SI design flow rates to the RCS were still achieved.Thus the'TBTT and"C" SI pumps were never truly inoperable.
                            "C" SI pumps exhibited problems meeting the design flow rates to the reactor coolant system as indicated on SI flow indicator FZ-925.                   Because of the above indicated design flow rate delivery problems, the "B" and "C" SZ pump minimum flow recirculation valves were throttled to 50 gpm to achieve the required design flow rates to the reactor coolant system.               As the "A" SX pump did not exhibit problems achieving design flow rates to'he Reactor Coolant System (RCS), its recirculation valve was locked full open.
Based on the above, it can be concluded that the public's health and safety was assured at all times.VAC+0AM)SSA t ttl LICENSEE EVENT REPORT (LER)TEXT CONTINUATION V.E.NVCLEAA EE4VLAEO4Y OSWE~ON AtMOYEO OME NO.$1%0MIOE~XWAES EnIIEE EACILITY NAME lll OOCEEY NV~EE IEI vEAA LEi NVMEE1 IN EEOVENYIAL H M N VoeN M~A4E 101 R.E.Ginna Nuclem Power Plant TEXr IIY~~4 NeeeC~~AEEC asa~'u Im o s o o o2 44 89 007 00 0 90'0 V.CO CTIVE ACTION A.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
II   ~         DESCRIPTION OP .ER"NT A.     DATES AND APPROXIMATE TIMES FOR MAJOR OCCUEKENCES o         June 19, 1989, 1440 EDST:           Event date and time.
0 The orifice plates installed in SI flow loops F-924 and F-925 were verified to be correct.0 0 o Flow transmitters FT-'924 and FT-925 were correctly calibrated to the installed orifice plates.The three sa f ety in)ection pumps were tested with the pump minimum flow recirculation line throttling valves full open, and the required SI design flow to the RCS was achieved.All installed safety-related flow orifice plates were assessed for correct installation and calibration.
o         June   19,   1989,     1440 EDST:   Discovery date ynd time.
Correct, calibration data was confirmed for each orifice/flow transmitter combination.
o         June   19,   1989,     1440 EDST:   Started unit load reduction.
0 Affected calibration procedures were changed to reflect correct calibration data.0 The nuclear industry will be notified via NUCLEAR NETWORK of the generic concerns of correct calibration data for flow orifice/flow transmitter combinations.
o         June 19, 1989, 1515 EDST: Unusual Event declared.
VAC YOAM EEEA~E 401 AC Sana 500A 10451 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U~lg&l5AA A54UMYOAY CCWWNICSS ASSAOVCO OU0 HO.5150MIOS~5~IA55 5151I55 SACICIYY IIAAI5 lll OOCKSY AU~CA ISI SSAA LCA AUSS051 ISI SSOUSASIAI, Q VAIOA~t U A~Aoa Ia R.E.Ginna Nuclear Power Plant o s o o o 244 8 9 007 001 0 OF 1 0 ADDITIONAL INFORMATION:
vttC xCAv 0XAA 0 00 I
A.B.FAILED COMPONENTS:
 
None.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Station could be identified.
IUIC tone ~                         H US NUCLCAr AIOULATCNY  ~ISI IMMI                         UCENSEE EVENT REPORT       HLER)   TEXT CONTINUAT!ON                   ~rovao OUC ro. OIsoaICA cxiIrcl c131es JACILIZY NAAIC III                                     COCKET IIUUCCW Ql               LI1 rlrICIO IQ                 ~ AOC IS
C.SPECIAL COMMENTS: 'one.wAC sOlQ SSSA 0 SSI}}
                                                                                          $ 44UIIITIAL     vavIr vtAA        M r       U   r teer (A'  ~r      1vrvrrL ~ ~
R.E. Ginna Nuclear Power Plant WC'IrrI~'11 Im o   s   o   o o 2 4   4         007           00 03         OF   1 0 June 19, 1989, 1615 EDST:                   "B" and "C" SI pumps declared operable.
June   19,   1989,         1615   EDST:     Stopped         unit load reduction.
0       June   19,   1989,         1626   EDST:     Unusual Event               ter-minated.
0       June 21, 1989, 1401 EDST:                   Started PT-2.1 on the SI pumps.
0        June 21, 1989,             1728 EDST:       Declared the "C" SI pump   inoperable.
0        June     21,   1989,         1915   EDST:     Started unit load reduction.
0       June 22, 1989, 0707 EDST:                           Reactor Coolant System (RCS) cold leg temperatures                             less than 350 F and RCS pressure less than 1600 psig.
B.          EVENT:
On     June 19, 1989 at 1440 EDST the reactor was at approximately 994 full power. During discussions in the Control Room between R&T personnel and Control Room operators concerning proposed changes to procedure PT-2.1,       it became apparent that the "B and "C" SI pump minimum flow recirculation line valves were locked full open rather than the recpxired throttled position.
The Operations Shift Supervisor determined at this time that       if   the "B" and "C SI pumps were not aligned as per design, then the pumps were inoperable and this placed the plant operations outside of Technical Specification 3.3.1.1.C and 3.3.1.4 which state the following:
o       3.3.1.1.C:       At or above a reactor coolant system pressure and temperature of 1600 psig and 350oFg except during performance of RCS Hydro Test, three safety injection pumps are operable.
 
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          ~              UCENSEE EVENT REPORT ILER} TEXT CONTINUATION II.L NUCllAA AIOVLATOAYCAN%ION AtfAOV lO OUO NO. )I94&I04 CXAIACS enII99 AACII.ITYNAMt Ill                               OOCAIT NUMlN Ql       L41 NUU4l1 I9I                     ~ AOl Iel 1 9 OMAH fI Al       veaoc U             H U TTST Id aaae ~  N NWWC ~ ~
R.E. Ginna Nuclear Power Plant A9K'IAAA~'AlIITl o 5   o o   o 24 489     00         7 00 040' 3.3.1.4: The requirements of 3.3.1.1.C may be modified to allow one .safety injection pump to be inoperable for up to 72 hours.
Because more than one SI pump was declared inoperable, this placed the plant - in a condition covered by Technical Specification 3.0.1 which states the following:
o       In the event     a Limiting Condition for operation and/or associated action requirements cannot be satisfied because of circumstances in excess of those addressed in the specification, within 1 hour action shall be initiated to place the unit in at least hot shutdown within the next 6 hours (i;e., a total of seven hours), and in at least cold shutdown within the following 30 hours (i.e., a total of 37 hours) unless corrective measures   are completed that permit operation under the permissible action statements for the specified time interval as measured from initial discovery or until the reactor is placed in a mode in which the specification is not applicable.
Because       of the above specification a unit load reduction to hot shutdown was started June 19, 1989 at     1440 EDST.
At approximately 1515 EDST, June 19, 1989, the Operations Shift Supervisor declared an Unusual Event in accordance with SC-100, "Ginna Station Event Evaluation and Classification" EAL: Loss of Engineered Safety Features:           exceeding a Limiting Condition for QADI operation on a safety system requiring a plant shutdown; Tech Spec section 3.3 Emergency Core Cooling System. All offsite notifications were made per SC-601, "Unusual Event Notifications".
NIC IOlU )99A 9
 
11.4. NUCI,CAN 1!OQLAYOLYCOMMI&lOW AttLOVtO OM4 NO. Jl&#xc3;&104 LICENSEE EVENT REPORT (LEA) TEXT CONTINUATION                        CLiiLee alii eS OOCLLY NVIMILQI                                              ~ A44 1$
LAClllYYNAME ill                                                           L44 NUMClL (41 1% 4MLH T I A I       VeaN N               N M N TKCf III'MWL~ N IOOeeC ~ ~
R.E. Ginna Nuclear Power Plant NIC IINLI~'ll117) o s   o o o 2 4 4 8 9 0     0 7             0 0 0 5       OF 1 0 At approximately 1615 EDST, June 19, 1989 subsequent to the satisfactory testing and throttling of the "B" and "C" safety injection pumps minimum flow recircula-tion valves to 50 gpm, the "B" and "C" safety in)ection pumps were declared operable and the load reduction stopped.
With the "B" and "C" safety in)ection pumps declared operable and the load reduction stopped, the Operations Shift Supervisor," with approval and concurrence from the Plant Manager Ginna Station, and PORC declared the Unusual Event terminated at 1626 EDST, June 19, 1989 in accordance with SC-110, "Ginna Station Event Evaluation For Reducing the Classification".                                     All offsite notifications were made of the Unusual Event termination and the plant was subsequently returned to approximately full power.
On     June 21, 1989 at 1401 EDST with the reactor at approximately full power, periodic test procedure PT-2.1 (Safety Injection Pumps) was started for the monthly test of the safety injection pumps.                                       The following is a sequence of important events that happened:
The   "A" SI pump was tested satisfactorily.
first           and       tested At approximately 1544 EDST, upon starting the "B" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 70 gpm.
This was contrary to the'required 50 gpm maximum flow rate.         The recirculation flow rate was reset to 45 gpm per PT-2.1.
0         At approximately 1637 EDST, upon starting the "C" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 56 gpm.
This was contrary to the required 50 gpm maximum flow rate.         The recirculation flow rate was reset to 45 gpm per PT-2.1.
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U,l. ISUCLlAA Cl4ULATOIYC5++%$ 4SS INC Pens AIA 1044 I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION                               AppsoYlo oU4 no. $ 1 90& I4s lX~ I'll   SIT I ITS PACILITY NASSC Ill                                     OOCIIlT IIU~CW Ql             Llk IIUSSOC1 IN                         ~ j4l ISI vSAA  SSOUSNSIAL           vis sIn Q   s         v M s R.E. Qiana Nuc:lear Powe neer IS'~ ~   e nWeeC ~ ~             - Plant P494 Pens ~'sI I ITI o s     o   o o 2 4   4 89 00             7 00                 0 6 ov 1 0 o         At approximately 1726 EDST, the 99B" and I9C99 SZ pumps were started and stopped to verify recirc flov was less than or .equal to the required 50 gpm.     Found the >>B" Sl pump recirc flow at 50 gpm and the "C" SZ pump recirc flov at 55 gpm.
o         At approximately 1728 EDST the "C" SZ pump was declared inoperable.
o         At approximately 1900 EDST a meeting between shift operations and plant staff was conducted and the following course of action was decided upon:
: 1)     Shutdown the plant to less than 350 F and less than 1600 psig, until the problem with the "C" SI pump minimum flov recirculation line flov repeatability is found and corrected.
: 2)     Reset the "C" SI           pump minimum           flow xecircu-lation flov.
: 3)     Test repeatability of the "C"                                   SZ         pump minimum flow recirculation flov.
: 4)     Correct the cause of pump minimum                                         flow recirculation flow problem.
On June 22, 1989 at approximately 0707 EDST                                                   the reactor coolant system cold leg temperatures                                                 were less than 350 F and RCS pressure was less than                                               1600 pSige C. INOPERABLE STRUCTURES P COMPONENTS                     P     OR     SYSTEMS                 THAT CONTRIBUTED TO THE EVENT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
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Qec pena 000A II~ NLCLlAN XlOOLATONT CaaaaWON I%4SI UCENSEE EVENT REPORT ILER) TEXT CONTINUATION                                           APPNOV lO 440 lXtiAIS SnIISS NO. )ISOMIOS PACILITY NA4l 111                                                       OOCXXT NV40SN ISI             LlN NINS0l1 Ill                   ~ AOl ISI vlAA    SSOIISNTIAL       VISION U           N U a TENET IN rane ~ 0 rsSUSSX ~ ~
R.E. Ginna NUclear Power Plant ASIC Ireaa ~'ll I ITI 0 5   0   0 0 2 4 4 8   9007                00 07             OF     1 0 E.     METHOD OF         DISCOVERY'he first               event was discovered               during discussions between RET personnel and the Control Room operators, concerning proposed changes to PT-2.1.
The second                       event was discovered             during the monthly test of the safety in)ection                               pumps.
F.     OPERATOR ACTION:
The ma)or                 operator action during the events was to reduce plant load and subsequently take the unit off line       and cool down                     to less than       350 F.
G.     SAFETY SYSTEM RESPONSES:
None.
III           CAUS       OP A.     IMMEDIATE CAUSE:
The <<B<< and <<C<< SI pumps were thought to be inoperable because they could not meet their design flow rates to the RCS due to their recirc valves being rather than throttled as required.
full      open B.     INTERMEDIATE CAUSE:
0         The <<B<< and <<C<< SI pump minimum flow recirculation valves were positioned full open rather than throttled as required.
0          With the pump minimum flow recirculation valves restored to the throttled position, subsequent.
pump testing failed to achieve repeatable pump recirculation flow results.
vaC POAU     SSSA 9431
                                                                              ~     ~
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IIA. NJCLCASI 054UWTO4T COINNKIOIS IIC GYM 500A LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                         ktf0OV lO OM0 IIO. 5150%104 55NA55   lltt4$
SACII.ITV HMI5 Ill                             OOC&#xc3;5T IIU1%50 Ill           I.I0 IIIAN54 III                   ~ A45 I5I SSOVSNYIAl         V%ION YTAA          M  A          M R.E. Ginna Nuclear Power Plant             o   s   o   o   o ~4 4 89       00       7           0   08     oi mCrIS  ~~e~      ~~ASSOIISMImauIITI C. ROOT CAUSE:
The   underlying cause of the event resulted from incorrect calibration data, provided by the plant designer for the installed system.                       The calibration data provided for flow transmitters FT-924 and FT-925 did not correlate accurately with the installed flow orifice plates, .FE-924 and FE-925.
ALYSIS 0 The   event is being reported in accordance with 10 CFR 50.73 Licensee Event Report System, which permits and encourages Licensees to report significant events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73.
An assessment     was     performed considering both the safety consequences     and . implications of this event with the following results       and conclusions:
There were no operational or safety consequences                                               or implications attributed to the deemed to be inoperable "B" and "C" SI pumps because:
o     An   analysis was performed using current calibration data, and   it was determined that even with the "B" and "Cll SI pumps minimum flow recirculation valves full open, the SI design flow rates to the RCS were still achieved.     Thus the 'TBTT and "C" SI pumps were never truly inoperable.
Based on the above,         it   can be concluded that the public's health and safety was assured at all times.
VAC +0AM )SSA t ttl
 
V.E. NVCLEAA EE4VLAEO4Y OSWE~ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                    AtMOYEO OME NO. $ 1%0MIOE
                                                                                            ~ XWAES EnIIEE EACILITYNAME lll                               OOCEEY NV~EE IEI           LEi NVMEE1 IN                 ~ A4E 101 vEAA  EEOVENYIAL       VoeN H M N           M R.E. Ginna Nuclem Power Plant               o  s  o  o  o2 44 89          007            00      0  90'        0 TEXr IIY~ ~  4 NeeeC ~ ~AEEC asa ~'u Im V.           CO     CTIVE ACTION A. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
0       The orifice plates installed in SI flow loops F-924 and F-925 were         verified to be correct.
0       Flow transmitters FT-'924 and FT-925 were correctly calibrated to the installed orifice plates.
0      The three sa fety in) ection pumps were tested with the pump minimum flow recirculation line throttling valves full open, and the required SI design flow to the RCS was achieved.
o      All installed safety-related flow orifice plates were assessed           for correct installation and calibration.             Correct, calibration data was confirmed for each orifice/flow transmitter combination.
0     Affected calibration procedures were changed to reflect correct calibration data.
0     The nuclear         industry will be notified via NUCLEAR NETWORK of the generic                       concerns of correct calibration data for flow orifice/flow transmitter combinations.
VAC YOAM EEEA
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U~ lg&l5AAA54UMYOAYCCWWNICSS AC Sana 500A 10451 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                   ASSAOVCO OU0 HO. 5150MIOS
                                                                                        ~ 5 ~ IA55 5151I55 SACICIYY IIAAI5 lll                         OOCKSY AU~CA ISI           LCA AUSS051 ISI                     ~ Aoa Ia SSAA    SSOUSASIAI,             VAIOA Q             ~ t U   A R.E. Ginna Nuclear Power Plant           o   s   o o   o 244 8 9       007                 001       0   OF   1 0 ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
None.
B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results:               No documentation                         of similar LER events with the same root cause at Ginna Station could be identified.
C. SPECIAL COMMENTS:
                          'one.
wAC   sOlQ SSSA 0 SSI}}

Latest revision as of 11:30, 4 February 2020

LER 89-007-00:on 890619 & 21 Safety Injection Pumps B & C Inoperable Due to Assessed Design Flow Delivery Concerns. Caused by Recirculation Valves Being Full Open.Orifice Plates in Flow Loops Verified to Be correct.W/890719 Ltr
ML17250A891
Person / Time
Site: Ginna Constellation icon.png
Issue date: 07/19/1989
From: Backus W, Mecredy R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-007, LER-89-7, NUDOCS 8907280303
Download: ML17250A891 (12)


Text

A,CCELERATED Dl BUTION DEMONS TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RXDS)

ACCESSION NBR:8907280303 DOC.DATE: 89/07/19 NOTARIZED: NO DOCKET g FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION MECREDY,R.C. Rochester Gas & Electric Corp.

BACKUS,W.H. Rochester Gas & Electric Corp.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 89-007-00:on 890619,safety injection pumps inoperability concerns due to flow meter calibration errors.

W/8 ltr.

DISTRIBUTION CODE: IE22T COPXES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event: Report (LER), Incident Rpt, etc.

~

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 RECIPIENT COPIES RECIPXENT COPIES XD CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 JOHNSON,A 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/ADE 8H 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR DREP/RPB 10 2 2 NUDOCS-ABSTRACT 1 1 egREC 02 1 1 RES/DSIR/EIB 1 1 RES/DSR/PRAB 1 1 RGN1 FILE 01 1 1 R EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY,A. 1 1 I L ST LOBBY WARD 1 1 LPDR 1 l.

NRC PDR 1 1 NSIC MAYS,G 1 1 D NSXC MURPHY,G.A 1 1 S

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FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 43 ENCL 42

$ TCR GAS A>VD . I '-CITRIC CORPORATION o 89;=A~;,i,",,:NJ;.,">O',I<;.", ',"

July 19, 1989 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

LER 89-007, Safety In) ection Pumps Inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclear Industry R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, which permits and encourages Licensees to report signi-ficant, events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73, the attached Licensee event report LER 89-007 is hereby submitted.

This event has in no way affected the public's health and safety.

Very truly yours, Robert C. Me General Manager Nuclear Production xco U.S. Nuclear Regulatory Commission Region 475 I

Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 3907280303 890719 rDFl ODOCK 0~000244 S PDC

NAC t>>e 200 UX. NVCLCA1 1lOULATOAYCOMMISSION IS021 AttAOVlDOMS NO.2100 OIOV LICENSEE EVENT REPORT ILERI CXtllll 0/SI/05

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  • R.E. Ginna Nuclear Power Plant 0 6 oo0244IOF1 0 Safety injection Pumps inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclea- Indust tVCNT OATl ISI LtA NUMSCA Ill 1ttOAT OATC Ill OTHtA I'ACILITICS INVOLVCO ISI

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YCS (H tre, CerVNr>> CXttCTCD SVSMISSIOH DATCI X ND AACTAAOT ILervc Io le00 ieec>>, le,. ettroeerN>>lt IHIuo vetreetue ctteorlr>>e xe>>I llsl On June 19, 1989 at 1440 EDST with the reactor at approximately 994 full power- the <<B" and <<C<< Safety In)ection (SI) pumps were declared inoperable due to assessed design flow delivery concerns.

Declaring two (2) SI pumps inoperable placed the plant outside the Technical Specifications requiring a plant shutdown. While in the process of plant shutdown the SI pump flows were returned to the required flow rates by pump minimum flow recirculation line valve throttling.

On June 21, 1989 at 1401 a similar problem occurred with the <<B<<

and <<C<< SI pumps and plant management decided to shut the plant down until the SI pump flow concerns were resolved. The plant was shutdown and subsequently cooled down to less than 350 F.

Original calibration data provided by the plant design was incorrect for the installed application. The underlying cause of the event resulted from incorrect original calibration data, provided by the plant designer for the installed system.

N1C lore 200 (242)

U.L NUCLCAA 004ULAfOAY CCXXXUWISI IIAC tea 000A IM0I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION 4tt+OV lO OQC IIO. 4100&I/8 axxtACS anIICS

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R.E. Ginna Nuclear Power Plant IICIC Axtx ~'ll l17l 0 5 0 0 0 2 4 4 8 9 0 07 00 0 2 of 0 7 PRE-EVENT PLANT CONDITIONS The unit was at approximately 994 steady state full power with no major activities in progress. Results and Test (R&T) personnel were in the Control Room discussing changes to periodic test procedure PT-2.1 (Safety Injection System Pumps) with the Control Room operators. These changes to PT-2.1 were necessary to reflect modifications made to the Safety Injection (SI) pumps minimum flow recirculation lines during the recent annual refueling and maintenance outage. This modification in part increased the size of the SI pumps recirculation lines to increase the recirculation flow for better pump reliability. During the post modification testing of the SZ pumps, the "B" and.

"C" SI pumps exhibited problems meeting the design flow rates to the reactor coolant system as indicated on SI flow indicator FZ-925. Because of the above indicated design flow rate delivery problems, the "B" and "C" SZ pump minimum flow recirculation valves were throttled to 50 gpm to achieve the required design flow rates to the reactor coolant system. As the "A" SX pump did not exhibit problems achieving design flow rates to'he Reactor Coolant System (RCS), its recirculation valve was locked full open.

II ~ DESCRIPTION OP .ER"NT A. DATES AND APPROXIMATE TIMES FOR MAJOR OCCUEKENCES o June 19, 1989, 1440 EDST: Event date and time.

o June 19, 1989, 1440 EDST: Discovery date ynd time.

o June 19, 1989, 1440 EDST: Started unit load reduction.

o June 19, 1989, 1515 EDST: Unusual Event declared.

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IUIC tone ~ H US NUCLCAr AIOULATCNY ~ISI IMMI UCENSEE EVENT REPORT HLER) TEXT CONTINUAT!ON ~rovao OUC ro. OIsoaICA cxiIrcl c131es JACILIZY NAAIC III COCKET IIUUCCW Ql LI1 rlrICIO IQ ~ AOC IS

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R.E. Ginna Nuclear Power Plant WC'IrrI~'11 Im o s o o o 2 4 4 007 00 03 OF 1 0 June 19, 1989, 1615 EDST: "B" and "C" SI pumps declared operable.

June 19, 1989, 1615 EDST: Stopped unit load reduction.

0 June 19, 1989, 1626 EDST: Unusual Event ter-minated.

0 June 21, 1989, 1401 EDST: Started PT-2.1 on the SI pumps.

0 June 21, 1989, 1728 EDST: Declared the "C" SI pump inoperable.

0 June 21, 1989, 1915 EDST: Started unit load reduction.

0 June 22, 1989, 0707 EDST: Reactor Coolant System (RCS) cold leg temperatures less than 350 F and RCS pressure less than 1600 psig.

B. EVENT:

On June 19, 1989 at 1440 EDST the reactor was at approximately 994 full power. During discussions in the Control Room between R&T personnel and Control Room operators concerning proposed changes to procedure PT-2.1, it became apparent that the "B and "C" SI pump minimum flow recirculation line valves were locked full open rather than the recpxired throttled position.

The Operations Shift Supervisor determined at this time that if the "B" and "C SI pumps were not aligned as per design, then the pumps were inoperable and this placed the plant operations outside of Technical Specification 3.3.1.1.C and 3.3.1.4 which state the following:

o 3.3.1.1.C: At or above a reactor coolant system pressure and temperature of 1600 psig and 350oFg except during performance of RCS Hydro Test, three safety injection pumps are operable.

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~ UCENSEE EVENT REPORT ILER} TEXT CONTINUATION II.L NUCllAA AIOVLATOAYCAN%ION AtfAOV lO OUO NO. )I94&I04 CXAIACS enII99 AACII.ITYNAMt Ill OOCAIT NUMlN Ql L41 NUU4l1 I9I ~ AOl Iel 1 9 OMAH fI Al veaoc U H U TTST Id aaae ~ N NWWC ~ ~

R.E. Ginna Nuclear Power Plant A9K'IAAA~'AlIITl o 5 o o o 24 489 00 7 00 040' 3.3.1.4: The requirements of 3.3.1.1.C may be modified to allow one .safety injection pump to be inoperable for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

Because more than one SI pump was declared inoperable, this placed the plant - in a condition covered by Technical Specification 3.0.1 which states the following:

o In the event a Limiting Condition for operation and/or associated action requirements cannot be satisfied because of circumstances in excess of those addressed in the specification, within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> action shall be initiated to place the unit in at least hot shutdown within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> (i;e., a total of seven hours), and in at least cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> (i.e., a total of 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />) unless corrective measures are completed that permit operation under the permissible action statements for the specified time interval as measured from initial discovery or until the reactor is placed in a mode in which the specification is not applicable.

Because of the above specification a unit load reduction to hot shutdown was started June 19, 1989 at 1440 EDST.

At approximately 1515 EDST, June 19, 1989, the Operations Shift Supervisor declared an Unusual Event in accordance with SC-100, "Ginna Station Event Evaluation and Classification" EAL: Loss of Engineered Safety Features: exceeding a Limiting Condition for QADI operation on a safety system requiring a plant shutdown; Tech Spec section 3.3 Emergency Core Cooling System. All offsite notifications were made per SC-601, "Unusual Event Notifications".

NIC IOlU )99A 9

11.4. NUCI,CAN 1!OQLAYOLYCOMMI&lOW AttLOVtO OM4 NO. JlÃ&104 LICENSEE EVENT REPORT (LEA) TEXT CONTINUATION CLiiLee alii eS OOCLLY NVIMILQI ~ A44 1$

LAClllYYNAME ill L44 NUMClL (41 1% 4MLH T I A I VeaN N N M N TKCf III'MWL~ N IOOeeC ~ ~

R.E. Ginna Nuclear Power Plant NIC IINLI~'ll117) o s o o o 2 4 4 8 9 0 0 7 0 0 0 5 OF 1 0 At approximately 1615 EDST, June 19, 1989 subsequent to the satisfactory testing and throttling of the "B" and "C" safety injection pumps minimum flow recircula-tion valves to 50 gpm, the "B" and "C" safety in)ection pumps were declared operable and the load reduction stopped.

With the "B" and "C" safety in)ection pumps declared operable and the load reduction stopped, the Operations Shift Supervisor," with approval and concurrence from the Plant Manager Ginna Station, and PORC declared the Unusual Event terminated at 1626 EDST, June 19, 1989 in accordance with SC-110, "Ginna Station Event Evaluation For Reducing the Classification". All offsite notifications were made of the Unusual Event termination and the plant was subsequently returned to approximately full power.

On June 21, 1989 at 1401 EDST with the reactor at approximately full power, periodic test procedure PT-2.1 (Safety Injection Pumps) was started for the monthly test of the safety injection pumps. The following is a sequence of important events that happened:

The "A" SI pump was tested satisfactorily.

first and tested At approximately 1544 EDST, upon starting the "B" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 70 gpm.

This was contrary to the'required 50 gpm maximum flow rate. The recirculation flow rate was reset to 45 gpm per PT-2.1.

0 At approximately 1637 EDST, upon starting the "C" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 56 gpm.

This was contrary to the required 50 gpm maximum flow rate. The recirculation flow rate was reset to 45 gpm per PT-2.1.

%1C iOAM WA Y 4II

U,l. ISUCLlAA Cl4ULATOIYC5++%$ 4SS INC Pens AIA 1044 I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION AppsoYlo oU4 no. $ 1 90& I4s lX~ I'll SIT I ITS PACILITY NASSC Ill OOCIIlT IIU~CW Ql Llk IIUSSOC1 IN ~ j4l ISI vSAA SSOUSNSIAL vis sIn Q s v M s R.E. Qiana Nuc:lear Powe neer IS'~ ~ e nWeeC ~ ~ - Plant P494 Pens ~'sI I ITI o s o o o 2 4 4 89 00 7 00 0 6 ov 1 0 o At approximately 1726 EDST, the 99B" and I9C99 SZ pumps were started and stopped to verify recirc flov was less than or .equal to the required 50 gpm. Found the >>B" Sl pump recirc flow at 50 gpm and the "C" SZ pump recirc flov at 55 gpm.

o At approximately 1728 EDST the "C" SZ pump was declared inoperable.

o At approximately 1900 EDST a meeting between shift operations and plant staff was conducted and the following course of action was decided upon:

1) Shutdown the plant to less than 350 F and less than 1600 psig, until the problem with the "C" SI pump minimum flov recirculation line flov repeatability is found and corrected.
2) Reset the "C" SI pump minimum flow xecircu-lation flov.
3) Test repeatability of the "C" SZ pump minimum flow recirculation flov.
4) Correct the cause of pump minimum flow recirculation flow problem.

On June 22, 1989 at approximately 0707 EDST the reactor coolant system cold leg temperatures were less than 350 F and RCS pressure was less than 1600 pSige C. INOPERABLE STRUCTURES P COMPONENTS P OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None.

D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

None.

vsc polU sess 94SI

Qec pena 000A II~ NLCLlAN XlOOLATONT CaaaaWON I%4SI UCENSEE EVENT REPORT ILER) TEXT CONTINUATION APPNOV lO 440 lXtiAIS SnIISS NO. )ISOMIOS PACILITY NA4l 111 OOCXXT NV40SN ISI LlN NINS0l1 Ill ~ AOl ISI vlAA SSOIISNTIAL VISION U N U a TENET IN rane ~ 0 rsSUSSX ~ ~

R.E. Ginna NUclear Power Plant ASIC Ireaa ~'ll I ITI 0 5 0 0 0 2 4 4 8 9007 00 07 OF 1 0 E. METHOD OF DISCOVERY'he first event was discovered during discussions between RET personnel and the Control Room operators, concerning proposed changes to PT-2.1.

The second event was discovered during the monthly test of the safety in)ection pumps.

F. OPERATOR ACTION:

The ma)or operator action during the events was to reduce plant load and subsequently take the unit off line and cool down to less than 350 F.

G. SAFETY SYSTEM RESPONSES:

None.

III CAUS OP A. IMMEDIATE CAUSE:

The <<B<< and <<C<< SI pumps were thought to be inoperable because they could not meet their design flow rates to the RCS due to their recirc valves being rather than throttled as required.

full open B. INTERMEDIATE CAUSE:

0 The <<B<< and <<C<< SI pump minimum flow recirculation valves were positioned full open rather than throttled as required.

0 With the pump minimum flow recirculation valves restored to the throttled position, subsequent.

pump testing failed to achieve repeatable pump recirculation flow results.

vaC POAU SSSA 9431

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IIA. NJCLCASI 054UWTO4T COINNKIOIS IIC GYM 500A LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ktf0OV lO OM0 IIO. 5150%104 55NA55 lltt4$

SACII.ITV HMI5 Ill OOCÃ5T IIU1%50 Ill I.I0 IIIAN54 III ~ A45 I5I SSOVSNYIAl V%ION YTAA M A M R.E. Ginna Nuclear Power Plant o s o o o ~4 4 89 00 7 0 08 oi mCrIS ~~e~ ~~ASSOIISMImauIITI C. ROOT CAUSE:

The underlying cause of the event resulted from incorrect calibration data, provided by the plant designer for the installed system. The calibration data provided for flow transmitters FT-924 and FT-925 did not correlate accurately with the installed flow orifice plates, .FE-924 and FE-925.

ALYSIS 0 The event is being reported in accordance with 10 CFR 50.73 Licensee Event Report System, which permits and encourages Licensees to report significant events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73.

An assessment was performed considering both the safety consequences and . implications of this event with the following results and conclusions:

There were no operational or safety consequences or implications attributed to the deemed to be inoperable "B" and "C" SI pumps because:

o An analysis was performed using current calibration data, and it was determined that even with the "B" and "Cll SI pumps minimum flow recirculation valves full open, the SI design flow rates to the RCS were still achieved. Thus the 'TBTT and "C" SI pumps were never truly inoperable.

Based on the above, it can be concluded that the public's health and safety was assured at all times.

VAC +0AM )SSA t ttl

V.E. NVCLEAA EE4VLAEO4Y OSWE~ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AtMOYEO OME NO. $ 1%0MIOE

~ XWAES EnIIEE EACILITYNAME lll OOCEEY NV~EE IEI LEi NVMEE1 IN ~ A4E 101 vEAA EEOVENYIAL VoeN H M N M R.E. Ginna Nuclem Power Plant o s o o o2 44 89 007 00 0 90' 0 TEXr IIY~ ~ 4 NeeeC ~ ~AEEC asa ~'u Im V. CO CTIVE ACTION A. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

0 The orifice plates installed in SI flow loops F-924 and F-925 were verified to be correct.

0 Flow transmitters FT-'924 and FT-925 were correctly calibrated to the installed orifice plates.

0 The three sa fety in) ection pumps were tested with the pump minimum flow recirculation line throttling valves full open, and the required SI design flow to the RCS was achieved.

o All installed safety-related flow orifice plates were assessed for correct installation and calibration. Correct, calibration data was confirmed for each orifice/flow transmitter combination.

0 Affected calibration procedures were changed to reflect correct calibration data.

0 The nuclear industry will be notified via NUCLEAR NETWORK of the generic concerns of correct calibration data for flow orifice/flow transmitter combinations.

VAC YOAM EEEA

~E 401

U~ lg&l5AAA54UMYOAYCCWWNICSS AC Sana 500A 10451 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ASSAOVCO OU0 HO. 5150MIOS

~ 5 ~ IA55 5151I55 SACICIYY IIAAI5 lll OOCKSY AU~CA ISI LCA AUSS051 ISI ~ Aoa Ia SSAA SSOUSASIAI, VAIOA Q ~ t U A R.E. Ginna Nuclear Power Plant o s o o o 244 8 9 007 001 0 OF 1 0 ADDITIONAL INFORMATION:

A. FAILED COMPONENTS:

None.

B. PREVIOUS LERs ON SIMILAR EVENTS:

A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Station could be identified.

C. SPECIAL COMMENTS:

'one.

wAC sOlQ SSSA 0 SSI