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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
- A,CCELERATED Dl BUTION DEMONS TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RXDS)
ACCESSION NBR:8907280303 DOC.DATE: 89/07/19 NOTARIZED: NO DOCKET g FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION MECREDY,R.C. Rochester Gas & Electric Corp.
BACKUS,W.H. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 89-007-00:on 890619,safety injection pumps inoperability concerns due to flow meter calibration errors.
W/8 ltr.
DISTRIBUTION CODE: IE22T COPXES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event: Report (LER), Incident Rpt, etc.
~
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 RECIPIENT COPIES RECIPXENT COPIES XD CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 JOHNSON,A 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/ADE 8H 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR DREP/RPB 10 2 2 NUDOCS-ABSTRACT 1 1 egREC 02 1 1 RES/DSIR/EIB 1 1 RES/DSR/PRAB 1 1 RGN1 FILE 01 1 1 R EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY,A. 1 1 I L ST LOBBY WARD 1 1 LPDR 1 l.
NRC PDR 1 1 NSIC MAYS,G 1 1 D NSXC MURPHY,G.A 1 1 S
A D
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FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 43 ENCL 42
$ TCR GAS A>VD . I '-CITRIC CORPORATION o 89;=A~;,i,",,:NJ;.,">O',I<;.", ',"
July 19, 1989 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 89-007, Safety In) ection Pumps Inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclear Industry R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, which permits and encourages Licensees to report signi-ficant, events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73, the attached Licensee event report LER 89-007 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Me General Manager Nuclear Production xco U.S. Nuclear Regulatory Commission Region 475 I
Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 3907280303 890719 rDFl ODOCK 0~000244 S PDC
NAC t>>e 200 UX. NVCLCA1 1lOULATOAYCOMMISSION IS021 AttAOVlDOMS NO.2100 OIOV LICENSEE EVENT REPORT ILERI CXtllll 0/SI/05
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tACILITYNAMC Ill DOCS lT NVMStA (2)
- R.E. Ginna Nuclear Power Plant 0 6 oo0244IOF1 0 Safety injection Pumps inoperability Concerns Due To Flow Meter Calibration Errors Could Be Of Generic Concern To Nuclea- Indust tVCNT OATl ISI LtA NUMSCA Ill 1ttOAT OATC Ill OTHtA I'ACILITICS INVOLVCO ISI
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YCS (H tre, CerVNr>> CXttCTCD SVSMISSIOH DATCI X ND AACTAAOT ILervc Io le00 ieec>>, le,. ettroeerN>>lt IHIuo vetreetue ctteorlr>>e xe>>I llsl On June 19, 1989 at 1440 EDST with the reactor at approximately 994 full power- the <<B" and <<C<< Safety In)ection (SI) pumps were declared inoperable due to assessed design flow delivery concerns.
Declaring two (2) SI pumps inoperable placed the plant outside the Technical Specifications requiring a plant shutdown. While in the process of plant shutdown the SI pump flows were returned to the required flow rates by pump minimum flow recirculation line valve throttling.
On June 21, 1989 at 1401 a similar problem occurred with the <<B<<
and <<C<< SI pumps and plant management decided to shut the plant down until the SI pump flow concerns were resolved. The plant was shutdown and subsequently cooled down to less than 350 F.
Original calibration data provided by the plant design was incorrect for the installed application. The underlying cause of the event resulted from incorrect original calibration data, provided by the plant designer for the installed system.
N1C lore 200 (242)
U.L NUCLCAA 004ULAfOAY CCXXXUWISI IIAC tea 000A IM0I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION 4tt+OV lO OQC IIO. 4100&I/8 axxtACS anIICS
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R.E. Ginna Nuclear Power Plant IICIC Axtx ~'ll l17l 0 5 0 0 0 2 4 4 8 9 0 07 00 0 2 of 0 7 PRE-EVENT PLANT CONDITIONS The unit was at approximately 994 steady state full power with no major activities in progress. Results and Test (R&T) personnel were in the Control Room discussing changes to periodic test procedure PT-2.1 (Safety Injection System Pumps) with the Control Room operators. These changes to PT-2.1 were necessary to reflect modifications made to the Safety Injection (SI) pumps minimum flow recirculation lines during the recent annual refueling and maintenance outage. This modification in part increased the size of the SI pumps recirculation lines to increase the recirculation flow for better pump reliability. During the post modification testing of the SZ pumps, the "B" and.
"C" SI pumps exhibited problems meeting the design flow rates to the reactor coolant system as indicated on SI flow indicator FZ-925. Because of the above indicated design flow rate delivery problems, the "B" and "C" SZ pump minimum flow recirculation valves were throttled to 50 gpm to achieve the required design flow rates to the reactor coolant system. As the "A" SX pump did not exhibit problems achieving design flow rates to'he Reactor Coolant System (RCS), its recirculation valve was locked full open.
II ~ DESCRIPTION OP .ER"NT A. DATES AND APPROXIMATE TIMES FOR MAJOR OCCUEKENCES o June 19, 1989, 1440 EDST: Event date and time.
o June 19, 1989, 1440 EDST: Discovery date ynd time.
o June 19, 1989, 1440 EDST: Started unit load reduction.
o June 19, 1989, 1515 EDST: Unusual Event declared.
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IUIC tone ~ H US NUCLCAr AIOULATCNY ~ISI IMMI UCENSEE EVENT REPORT HLER) TEXT CONTINUAT!ON ~rovao OUC ro. OIsoaICA cxiIrcl c131es JACILIZY NAAIC III COCKET IIUUCCW Ql LI1 rlrICIO IQ ~ AOC IS
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R.E. Ginna Nuclear Power Plant WC'IrrI~'11 Im o s o o o 2 4 4 007 00 03 OF 1 0 June 19, 1989, 1615 EDST: "B" and "C" SI pumps declared operable.
June 19, 1989, 1615 EDST: Stopped unit load reduction.
0 June 19, 1989, 1626 EDST: Unusual Event ter-minated.
0 June 21, 1989, 1401 EDST: Started PT-2.1 on the SI pumps.
0 June 21, 1989, 1728 EDST: Declared the "C" SI pump inoperable.
0 June 21, 1989, 1915 EDST: Started unit load reduction.
0 June 22, 1989, 0707 EDST: Reactor Coolant System (RCS) cold leg temperatures less than 350 F and RCS pressure less than 1600 psig.
B. EVENT:
On June 19, 1989 at 1440 EDST the reactor was at approximately 994 full power. During discussions in the Control Room between R&T personnel and Control Room operators concerning proposed changes to procedure PT-2.1, it became apparent that the "B and "C" SI pump minimum flow recirculation line valves were locked full open rather than the recpxired throttled position.
The Operations Shift Supervisor determined at this time that if the "B" and "C SI pumps were not aligned as per design, then the pumps were inoperable and this placed the plant operations outside of Technical Specification 3.3.1.1.C and 3.3.1.4 which state the following:
o 3.3.1.1.C: At or above a reactor coolant system pressure and temperature of 1600 psig and 350oFg except during performance of RCS Hydro Test, three safety injection pumps are operable.
NAC Fetes I$4ll
~ UCENSEE EVENT REPORT ILER} TEXT CONTINUATION II.L NUCllAA AIOVLATOAYCAN%ION AtfAOV lO OUO NO. )I94&I04 CXAIACS enII99 AACII.ITYNAMt Ill OOCAIT NUMlN Ql L41 NUU4l1 I9I ~ AOl Iel 1 9 OMAH fI Al veaoc U H U TTST Id aaae ~ N NWWC ~ ~
R.E. Ginna Nuclear Power Plant A9K'IAAA~'AlIITl o 5 o o o 24 489 00 7 00 040' 3.3.1.4: The requirements of 3.3.1.1.C may be modified to allow one .safety injection pump to be inoperable for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
Because more than one SI pump was declared inoperable, this placed the plant - in a condition covered by Technical Specification 3.0.1 which states the following:
o In the event a Limiting Condition for operation and/or associated action requirements cannot be satisfied because of circumstances in excess of those addressed in the specification, within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> action shall be initiated to place the unit in at least hot shutdown within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> (i;e., a total of seven hours), and in at least cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> (i.e., a total of 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />) unless corrective measures are completed that permit operation under the permissible action statements for the specified time interval as measured from initial discovery or until the reactor is placed in a mode in which the specification is not applicable.
Because of the above specification a unit load reduction to hot shutdown was started June 19, 1989 at 1440 EDST.
At approximately 1515 EDST, June 19, 1989, the Operations Shift Supervisor declared an Unusual Event in accordance with SC-100, "Ginna Station Event Evaluation and Classification" EAL: Loss of Engineered Safety Features: exceeding a Limiting Condition for QADI operation on a safety system requiring a plant shutdown; Tech Spec section 3.3 Emergency Core Cooling System. All offsite notifications were made per SC-601, "Unusual Event Notifications".
NIC IOlU )99A 9
11.4. NUCI,CAN 1!OQLAYOLYCOMMI&lOW AttLOVtO OM4 NO. JlÃ&104 LICENSEE EVENT REPORT (LEA) TEXT CONTINUATION CLiiLee alii eS OOCLLY NVIMILQI ~ A44 1$
LAClllYYNAME ill L44 NUMClL (41 1% 4MLH T I A I VeaN N N M N TKCf III'MWL~ N IOOeeC ~ ~
R.E. Ginna Nuclear Power Plant NIC IINLI~'ll117) o s o o o 2 4 4 8 9 0 0 7 0 0 0 5 OF 1 0 At approximately 1615 EDST, June 19, 1989 subsequent to the satisfactory testing and throttling of the "B" and "C" safety injection pumps minimum flow recircula-tion valves to 50 gpm, the "B" and "C" safety in)ection pumps were declared operable and the load reduction stopped.
With the "B" and "C" safety in)ection pumps declared operable and the load reduction stopped, the Operations Shift Supervisor," with approval and concurrence from the Plant Manager Ginna Station, and PORC declared the Unusual Event terminated at 1626 EDST, June 19, 1989 in accordance with SC-110, "Ginna Station Event Evaluation For Reducing the Classification". All offsite notifications were made of the Unusual Event termination and the plant was subsequently returned to approximately full power.
On June 21, 1989 at 1401 EDST with the reactor at approximately full power, periodic test procedure PT-2.1 (Safety Injection Pumps) was started for the monthly test of the safety injection pumps. The following is a sequence of important events that happened:
The "A" SI pump was tested satisfactorily.
first and tested At approximately 1544 EDST, upon starting the "B" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 70 gpm.
This was contrary to the'required 50 gpm maximum flow rate. The recirculation flow rate was reset to 45 gpm per PT-2.1.
0 At approximately 1637 EDST, upon starting the "C" SI pump for the test, the pump minimum flow recirculation flow rate was found to be 56 gpm.
This was contrary to the required 50 gpm maximum flow rate. The recirculation flow rate was reset to 45 gpm per PT-2.1.
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U,l. ISUCLlAA Cl4ULATOIYC5++%$ 4SS INC Pens AIA 1044 I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION AppsoYlo oU4 no. $ 1 90& I4s lX~ I'll SIT I ITS PACILITY NASSC Ill OOCIIlT IIU~CW Ql Llk IIUSSOC1 IN ~ j4l ISI vSAA SSOUSNSIAL vis sIn Q s v M s R.E. Qiana Nuc:lear Powe neer IS'~ ~ e nWeeC ~ ~ - Plant P494 Pens ~'sI I ITI o s o o o 2 4 4 89 00 7 00 0 6 ov 1 0 o At approximately 1726 EDST, the 99B" and I9C99 SZ pumps were started and stopped to verify recirc flov was less than or .equal to the required 50 gpm. Found the >>B" Sl pump recirc flow at 50 gpm and the "C" SZ pump recirc flov at 55 gpm.
o At approximately 1728 EDST the "C" SZ pump was declared inoperable.
o At approximately 1900 EDST a meeting between shift operations and plant staff was conducted and the following course of action was decided upon:
- 1) Shutdown the plant to less than 350 F and less than 1600 psig, until the problem with the "C" SI pump minimum flov recirculation line flov repeatability is found and corrected.
- 2) Reset the "C" SI pump minimum flow xecircu-lation flov.
- 3) Test repeatability of the "C" SZ pump minimum flow recirculation flov.
- 4) Correct the cause of pump minimum flow recirculation flow problem.
On June 22, 1989 at approximately 0707 EDST the reactor coolant system cold leg temperatures were less than 350 F and RCS pressure was less than 1600 pSige C. INOPERABLE STRUCTURES P COMPONENTS P OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
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Qec pena 000A II~ NLCLlAN XlOOLATONT CaaaaWON I%4SI UCENSEE EVENT REPORT ILER) TEXT CONTINUATION APPNOV lO 440 lXtiAIS SnIISS NO. )ISOMIOS PACILITY NA4l 111 OOCXXT NV40SN ISI LlN NINS0l1 Ill ~ AOl ISI vlAA SSOIISNTIAL VISION U N U a TENET IN rane ~ 0 rsSUSSX ~ ~
R.E. Ginna NUclear Power Plant ASIC Ireaa ~'ll I ITI 0 5 0 0 0 2 4 4 8 9007 00 07 OF 1 0 E. METHOD OF DISCOVERY'he first event was discovered during discussions between RET personnel and the Control Room operators, concerning proposed changes to PT-2.1.
The second event was discovered during the monthly test of the safety in)ection pumps.
F. OPERATOR ACTION:
The ma)or operator action during the events was to reduce plant load and subsequently take the unit off line and cool down to less than 350 F.
G. SAFETY SYSTEM RESPONSES:
None.
III CAUS OP A. IMMEDIATE CAUSE:
The <<B<< and <<C<< SI pumps were thought to be inoperable because they could not meet their design flow rates to the RCS due to their recirc valves being rather than throttled as required.
full open B. INTERMEDIATE CAUSE:
0 The <<B<< and <<C<< SI pump minimum flow recirculation valves were positioned full open rather than throttled as required.
0 With the pump minimum flow recirculation valves restored to the throttled position, subsequent.
pump testing failed to achieve repeatable pump recirculation flow results.
vaC POAU SSSA 9431
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IIA. NJCLCASI 054UWTO4T COINNKIOIS IIC GYM 500A LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ktf0OV lO OM0 IIO. 5150%104 55NA55 lltt4$
SACII.ITV HMI5 Ill OOCÃ5T IIU1%50 Ill I.I0 IIIAN54 III ~ A45 I5I SSOVSNYIAl V%ION YTAA M A M R.E. Ginna Nuclear Power Plant o s o o o ~4 4 89 00 7 0 08 oi mCrIS ~~e~ ~~ASSOIISMImauIITI C. ROOT CAUSE:
The underlying cause of the event resulted from incorrect calibration data, provided by the plant designer for the installed system. The calibration data provided for flow transmitters FT-924 and FT-925 did not correlate accurately with the installed flow orifice plates, .FE-924 and FE-925.
ALYSIS 0 The event is being reported in accordance with 10 CFR 50.73 Licensee Event Report System, which permits and encourages Licensees to report significant events that may be of generic interest or concern even though they may not meet the criteria contained in 10 CFR 50.73.
An assessment was performed considering both the safety consequences and . implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the deemed to be inoperable "B" and "C" SI pumps because:
o An analysis was performed using current calibration data, and it was determined that even with the "B" and "Cll SI pumps minimum flow recirculation valves full open, the SI design flow rates to the RCS were still achieved. Thus the 'TBTT and "C" SI pumps were never truly inoperable.
Based on the above, it can be concluded that the public's health and safety was assured at all times.
VAC +0AM )SSA t ttl
V.E. NVCLEAA EE4VLAEO4Y OSWE~ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AtMOYEO OME NO. $ 1%0MIOE
~ XWAES EnIIEE EACILITYNAME lll OOCEEY NV~EE IEI LEi NVMEE1 IN ~ A4E 101 vEAA EEOVENYIAL VoeN H M N M R.E. Ginna Nuclem Power Plant o s o o o2 44 89 007 00 0 90' 0 TEXr IIY~ ~ 4 NeeeC ~ ~AEEC asa ~'u Im V. CO CTIVE ACTION A. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
0 The orifice plates installed in SI flow loops F-924 and F-925 were verified to be correct.
0 Flow transmitters FT-'924 and FT-925 were correctly calibrated to the installed orifice plates.
0 The three sa fety in) ection pumps were tested with the pump minimum flow recirculation line throttling valves full open, and the required SI design flow to the RCS was achieved.
o All installed safety-related flow orifice plates were assessed for correct installation and calibration. Correct, calibration data was confirmed for each orifice/flow transmitter combination.
0 Affected calibration procedures were changed to reflect correct calibration data.
0 The nuclear industry will be notified via NUCLEAR NETWORK of the generic concerns of correct calibration data for flow orifice/flow transmitter combinations.
VAC YOAM EEEA
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U~ lg&l5AAA54UMYOAYCCWWNICSS AC Sana 500A 10451 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ASSAOVCO OU0 HO. 5150MIOS
~ 5 ~ IA55 5151I55 SACICIYY IIAAI5 lll OOCKSY AU~CA ISI LCA AUSS051 ISI ~ Aoa Ia SSAA SSOUSASIAI, VAIOA Q ~ t U A R.E. Ginna Nuclear Power Plant o s o o o 244 8 9 007 001 0 OF 1 0 ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
None.
B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Station could be identified.
C. SPECIAL COMMENTS:
'one.
wAC sOlQ SSSA 0 SSI