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=Text=
=Text=
{{#Wiki_filter:May 13, 2019
{{#Wiki_filter:==SUBJECT:==
 
PILGRIM NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000293/2019001
==SUBJECT:==
PILGRIM NUCLEAR POWER STATION
- INTEGRATED INSPECTION REPORT 05000293/2019001


==Dear Mr. Sullivan:==
==Dear Mr. Sullivan:==
On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Pilgrim Nuclear Power Station (Pilgrim).
On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Pilgrim Nuclear Power Station (Pilgrim). On April 18, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
 
On April 18, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.


NRC inspectors documented one self-revealing Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
NRC inspectors documented one self-revealing Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.


If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC resident inspector at Pilgrim. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC resident inspector at Pilgrim. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.


Sincerely,
Sincerely,
/RA/ Anthony Dimitriadis, Chief Reactor Projects Branch 5  
/RA/
 
Anthony Dimitriadis, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Number: 50-293 License Number: DPR-35
Division of Reactor Projects Docket Number: 50-293 License Number: DPR-35  


===Enclosure:===
===Enclosure:===
Inspection Report 05000293/2019001  
Inspection Report 05000293/2019001


==Inspection Report==
==Inspection Report==
 
Docket Number: 50-293 License Number: DPR-35 Report Number: 05000293/2019001 Enterprise Identifier: I-2019-001-0042 Licensee: Entergy Nuclear Operations, Inc. (Entergy)
Docket Number: 50-293  
Facility: Pilgrim Nuclear Power Station (Pilgrim)
 
Location: Plymouth, Massachusetts Inspection Dates: January 1, 2019 to March 31, 2019 Inspectors: E. Burket, Senior Resident Inspector B. Pinson, Resident Inspector P. Boguszewski, Resident Inspector S. Pindale, Senior Reactor Inspector J. Schoppy, Senior Reactor Inspector J. Vazquez, Resident Inspector S. Wilson, Health Physicist A. Ziedonis, Senior Resident Inspector Approved By: Anthony Dimitriadis, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure
License Number: DPR-35  
 
Report Number: 05000293/2019001  
 
Enterprise Identifier: I-2019-001-0042  
 
Licensee: Entergy Nuclear Operations, Inc. (Entergy)  
 
Facility: Pilgrim Nuclear Power Station (Pilgrim)  
 
Location: Plymouth, Massachusetts  
 
Inspection Dates: January 1, 2019 to March 31, 2019  
 
Inspectors: E. Burket, Senior Resident Inspector B. Pinson, Resident Inspector P. Boguszewski, Resident Inspector S. Pindale, Senior Reactor Inspector J. Schoppy, Senior Reactor Inspector J. Vazquez, Resident Inspector S. Wilson, Health Physicist A. Ziedonis, Senior Resident Inspector Approved By: Anthony Dimitriadis, Chief Reactor Projects Branch 5  
 
Division of Reactor Projects  
 
2


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Entergy's performance at Pilgrim by conducting the baseline inspections described in this report in accordance with the  
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Entergys performance at Pilgrim by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process (ROP). The ROP is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.
 
Reactor Oversight Process (ROP). The ROP is the NRC's program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRC's assessment are summarized in the table below.
 
List of Findings and Violations Target Rock Relief Valve Pilot Assembly Fa iled As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone Significance Cross-cutting Aspect Report Section Not Applicable NCV 05000293/2019001-01 Open/Closed Not Applicable 71153 A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendor's test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.


Additional Tracking Items Type Issue number Title Report Section Status LER 05000293/2018-003-00 Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications 71153 Closed LER 05000293/2019-001-00 Reactor Core Isolation Cooling System Declared Inoperable During Surveillance Testing 71153 Closed LER 05000293/2019-002-00 Failure of Main Steam Isolation Valve Limit Switch Results in a Condition Prohibited by Technical Specifications 71153 Closed
List of Findings and Violations Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone          Significance                                  Cross-cutting        Report Aspect              Section Not Applicable      NCV 05000293/2019001-01                      Not Applicable      71153 Open/Closed A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendors test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.


3
Additional Tracking Items Type      Issue number              Title                                      Report      Status Section LER      05000293/2018-003-00      Target Rock Relief Valve Pilot              71153      Closed Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications LER      05000293/2019-001-00      Reactor Core Isolation Cooling              71153      Closed System Declared Inoperable During Surveillance Testing LER      05000293/2019-002-00      Failure of Main Steam Isolation Valve      71153      Closed Limit Switch Results in a Condition Prohibited by Technical Specifications


=PLANT STATUS=
=PLANT STATUS=


===The unit began the inspection period at rated thermal power. On January 3, 2019, the station reduced power to 25 percent to troubleshoot and repair 'A' feedwater regulating valve. On January 6, 2019, operations personnel returned the unit to rated thermal power. On January 16, 2019, the station reduced power to 25 percent to repair a leaking primary containment isolation system valve. On January 17, 2019, operations personnel returned the unit to rated thermal power. On March 20, 2019, the station reduced power to 35 percent to repair a leaking feedwater heater valve in the condenser bay. On March 21, 2019, operations personnel returned the unit to rated thermal power and remained at or near rated thermal power for the remainder of the inspection period.
The unit began the inspection period at rated thermal power. On January 3, 2019, the station reduced power to 25 percent to troubleshoot and repair 'A' feedwater regulating valve. On January 6, 2019, operations personnel returned the unit to rated thermal power. On January 16, 2019, the station reduced power to 25 percent to repair a leaking primary containment isolation system valve. On January 17, 2019, operations personnel returned the unit to rated thermal power. On March 20, 2019, the station reduced power to 35 percent to repair a leaking feedwater heater valve in the condenser bay. On March 21, 2019, operations personnel returned the unit to rated thermal power and remained at or near rated thermal power for the remainder of the inspection period.


==INSPECTION SCOPES==
==INSPECTION SCOPES==
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, "Light-Water Reactor Inspection Program - Operations Phase.The inspectors performed plant status activities described in IMC 2515, Appendix D, "Plant Status," and conducted routine reviews using IP 71152, "Problem Identification and Resolution.The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.


==REACTOR SAFETY==
==REACTOR SAFETY==


==71111.01 - Adverse Weather Protection==
==71111.01 - Adverse Weather Protection     Impending Severe Weather Sample (IP Section 03.03)==
 
===
Impending Severe Weather Sample (IP Section 03.03)===
{{IP sample|IP=IP 71111.01|count=1}}
{{IP sample|IP=IP 71111.01|count=1}}
: (1) The inspectors evaluated readiness for impending adverse weather conditions for   extreme cold temperatures on January 31, 2019.
: (1) The inspectors evaluated readiness for impending adverse weather conditions for extreme cold temperatures on January 31, 2019.


==71111.04 - Equipment Alignment==
==71111.04 - Equipment Alignment     Partial Walkdown (IP Section 03.01)==
 
===
Partial Walkdown (IP Section 03.01)===
{{IP sample|IP=IP 71111.04|count=4}}
{{IP sample|IP=IP 71111.04|count=4}}


Line 102: Line 68:
: (2) High pressure coolant injection system on February 9, 2019
: (2) High pressure coolant injection system on February 9, 2019
: (3) Reactor building closed cooling water on February 25-26, 2019
: (3) Reactor building closed cooling water on February 25-26, 2019
: (4) 'A' and 'B' salt service water before and after 'B' salt service water testing on March 18-20, 2019  
: (4) 'A' and 'B' salt service water before and after 'B' salt service water testing on March 18-20, 2019


4 71111.04S - Equipment Alignment Complete Walkdown (IP Section 03.02) (1 Sample)===
==71111.04S - Equipment Alignment   Complete Walkdown (IP Section 03.02)==
{{IP sample|IP=IP 71111.04S|count=1}}


===The inspectors evaluated system configurations during complete walkdowns of the following system:
The inspectors evaluated system configurations during complete walkdowns of the following system:
: (1) 'A' emergency diesel generator following maintenance and testing on March 27, 2019
: (1) 'A' emergency diesel generator following maintenance and testing on March 27, 2019


==71111.05A - Fire Protection (Annual)==
==71111.05A - Fire Protection (Annual)   Annual Inspection (IP Section 03.02)==
 
===
Annual Inspection (IP Section 03.02)===
{{IP sample|IP=IP 71111.05A|count=1}}
{{IP sample|IP=IP 71111.05A|count=1}}
: (1) The inspectors evaluated fire brigade performance on January 30, 2019.
: (1) The inspectors evaluated fire brigade performance on January 30, 2019.


==71111.05Q - Fire Protection==
==71111.05Q - Fire Protection   Quarterly Inspection (IP Section 03.01)==
 
===
Quarterly Inspection (IP Section 03.01)===
{{IP sample|IP=IP 71111.05Q|count=5}}
{{IP sample|IP=IP 71111.05Q|count=5}}


Line 127: Line 88:
: (3) Radwaste corridor area (fire zone 3.1) on February 26, 2019
: (3) Radwaste corridor area (fire zone 3.1) on February 26, 2019
: (4) 'B' reactor building closed cooling water (fire zone 1.22) on March 9, 2019
: (4) 'B' reactor building closed cooling water (fire zone 1.22) on March 9, 2019
: (5) Machine shop (fire zone 3.8) on March 19, 2019  
: (5) Machine shop (fire zone 3.8) on March 19, 2019


===71111.07T - Heat Sink Performance Triennial Review (IP Section 02.02)===
===71111.07T - Heat Sink Performance   Triennial Review (IP Section 02.02) ===
{{IP sample|IP=IP 71111.07|count=3}}
{{IP sample|IP=IP 71111.07|count=3}}
The inspectors evaluated heat exchanger/sink performance on the following:
The inspectors evaluated heat exchanger/sink performance on the following:
Line 136: Line 97:
: (3) Ultimate heat sink associated with service water system operation and intake structure condition
: (3) Ultimate heat sink associated with service water system operation and intake structure condition


==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance==
==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance   Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)==
 
===
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)  
===
{{IP sample|IP=IP 71111.11Q|count=1}}
{{IP sample|IP=IP 71111.11Q|count=1}}


The inspectors observed and evaluated licensed operator performance in the control room during down power to 25 percent and isolation of 'C' main steam line on January 3, 2019.
The inspectors observed and evaluated licensed operator performance in the control room during down power to 25 percent and isolation of 'C' main steam line on January 3, 2019.


Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)===
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
The inspectors observed and evaluated licensed operator requalification training in the  
The inspectors observed and evaluated licensed operator requalification training in the simulator on March 13, 2019.
 
===simulator on March 13, 2019.
 
==71111.12 - Maintenance Effectiveness==


===
==71111.12 - Maintenance Effectiveness    Routine Maintenance Effectiveness Inspection (IP Section 02.01)==
Routine Maintenance Effectiveness Inspection (IP Section 02.01)===
{{IP sample|IP=IP 71111.12|count=3}}
{{IP sample|IP=IP 71111.12|count=3}}


Line 161: Line 113:
: (3) Neutron monitoring instrumentation following return to (a)(2) status completed March 12, 2019
: (3) Neutron monitoring instrumentation following return to (a)(2) status completed March 12, 2019


==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
==71111.13 - Maintenance Risk Assessments and Emergent Work Control   Risk Assessment and Management Sample (IP Section 03.01)==
 
===
Risk Assessment and Management Sample (IP Section 03.01)===
{{IP sample|IP=IP 71111.13|count=4}}
{{IP sample|IP=IP 71111.13|count=4}}


The inspectors evaluated the risk assessments for the following planned and emergent work  
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
 
activities:
: (1) Emergent work to troubleshoot and replace recirculation motor generator set B1 speed limiter on January 5, 2019
: (1) Emergent work to troubleshoot and replace recirculation motor generator set B1 speed limiter on January 5, 2019
: (2) Elevated risk during reactor core isolation cooling testing and inoperability on January 8, 2019
: (2) Elevated risk during reactor core isolation cooling testing and inoperability on January 8, 2019
Line 175: Line 122:
: (4) Elevated risk during reactor core isolation cooling maintenance and testing on March 27, 2019
: (4) Elevated risk during reactor core isolation cooling maintenance and testing on March 27, 2019


==71111.15 - Operability Determinations and Functionality Assessments==
==71111.15 - Operability Determinations and Functionality Assessments   Sample Selection (IP Section 02.02)==
 
===
Sample Selection (IP Section 02.02)===
{{IP sample|IP=IP 71111.15|count=4}}
{{IP sample|IP=IP 71111.15|count=4}}


Line 185: Line 129:
: (2) Reactor core isolation cooling operability following flow oscillations (CR-2019-0802)on February 6, 2019
: (2) Reactor core isolation cooling operability following flow oscillations (CR-2019-0802)on February 6, 2019
: (3) Main steam isolation valve AO-203-1C input to reactor protection system past operability (CR-2019-0090) on February 20, 2019
: (3) Main steam isolation valve AO-203-1C input to reactor protection system past operability (CR-2019-0090) on February 20, 2019
: (4) Control rod drive operability following scram pilot valve air header alarms (CR-2019-1783) on March 29, 2019  
: (4) Control rod drive operability following scram pilot valve air header alarms (CR-2019-1783) on March 29, 2019


==71111.18 - Plant Modifications==
==71111.18 - Plant Modifications Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)
 
===
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)
The inspectors evaluated the following temporary or permanent modifications:
The inspectors evaluated the following temporary or permanent modifications:
: (1) Feedwater check valve, 6-CK-62B, clamp installation
: (1) Feedwater check valve, 6-CK-62B, clamp installation
: (2) Main steam isolation valve 1C reactor protection system relay K3F
: (2) Main steam isolation valve 1C reactor protection system relay K3F


==71111.19 - Post Maintenance Testing==
==71111.19 - Post Maintenance Testing   Post Maintenance Test Sample (IP Section 03.01)==
 
{{IP sample|IP==
Post Maintenance Test Sample (IP Section 03.01)===
=IP 71111.18|count=3}}
{{IP sample|IP=IP 71111.18|count=3}}


The inspectors evaluated the following post maintenance tests:
The inspectors evaluated the following post maintenance tests:
Line 205: Line 145:
: (3) 'B' fuel pool pump, P210B, post work testing on March 18, 2019
: (3) 'B' fuel pool pump, P210B, post work testing on March 18, 2019


==71111.22 - Surveillance Testing==
==71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests:   In Service Testing (IST) (IP Section 03.01)==
 
===
 
The inspectors evaluated the following surveillance tests:
In Service Testing (IST) (IP Section 03.01)===
{{IP sample|IP=IP 71111.22|count=1}}
{{IP sample|IP=IP 71111.22|count=1}}
: (1) 8.5.4.1 High pressure coolant injection operability and flow rate test on February 5, 2019 Surveillance Testing (IP Section 03.01) (4 Samples)===
: (1) 8.5.4.1 High pressure coolant injection operability and flow rate test on February 5, 2019
: (1) 8.5.5.1 Reactor core isolation cooling operability run on January 10, 2019  


===(2) 8.M.2-1.5.10 High pressure coolant injection vacuum breaker isolation valve testing on February 5, 2019
===Surveillance Testing (IP Section 03.01) (4 Samples)===
: (1) 8.5.5.1 Reactor core isolation cooling operability run on January 10, 2019
: (2) 8.M.2-1.5.10 High pressure coolant injection vacuum breaker isolation valve testing on February 5, 2019
: (3) 8.5.1.1 Core spray operability surveillance on March 5, 2019
: (3) 8.5.1.1 Core spray operability surveillance on March 5, 2019
: (4) 8.3.3 Scram discharge isolation volume vent and drain valve operability surveillance on March 21, 2019
: (4) 8.3.3 Scram discharge isolation volume vent and drain valve operability surveillance on March 21, 2019


==71114.06 - Drill Evaluation==
==71114.06 - Drill Evaluation   Emergency Preparedness (EP) Drill (IP Section 02.01)==
 
===
Emergency Preparedness (EP) Drill (IP Section 02.01)===
{{IP sample|IP=IP 71114.06|count=1}}
{{IP sample|IP=IP 71114.06|count=1}}


The inspectors evaluated the conduct of a routine emergency planning drill on Wednesday, February 13, 2019.
The inspectors evaluated the conduct of a routine emergency planning drill on Wednesday, February 13,


==RADIATION SAFETY==
==RADIATION SAFETY==


==71124.01 - Radiological Hazard Assessment and Exposure Controls==
==71124.01 - Radiological Hazard Assessment and Exposure Controls   Contamination and Radioactive Material Control (IP Section 02.03)==
 
===
Contamination and Radioactive Material Control (IP Section 02.03)===
{{IP sample|IP=IP 71124.01|count=1}}
{{IP sample|IP=IP 71124.01|count=1}}


The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material. The inspectors selected several sealed sources from inventory records and assessed whether the sources were accounted for and were tested for loose surface contamination. The inspectors evaluated whether any recent transactions involving nationally tracked sources were reported in accordance with requirements.
The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material. The inspectors selected several sealed sources from inventory records and assessed whether the sources were accounted for and were tested for loose surface contamination. The inspectors evaluated whether any recent transactions involving nationally tracked sources were reported in accordance with requirements.


High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)===
High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)
The inspectors reviewed the procedures and controls for high radiation areas, very high  
The inspectors reviewed the procedures and controls for high radiation areas, very high radiation areas, and radiological transient areas in the plant.
 
===radiation areas, and radiological transient areas in the plant.
 
Instructions to Workers (IP Section 02.02) (1 Sample)===
The inspectors reviewed high radiation area work permit controls and use, reviewed
 
===electronic alarming dosimeter alarms and set points, observed worker briefings on radiological conditions, and observed containers of radioactive materials and assessed whether the containers were labeled and controlled in accordance with requirements.


Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)===
===Instructions to Workers (IP Section 02.02) (1 Sample)===
The inspectors reviewed high radiation area work permit controls and use, reviewed electronic alarming dosimeter alarms and set points, observed worker briefings on radiological conditions, and observed containers of radioactive materials and assessed whether the containers were labeled and controlled in accordance with requirements.


===The inspectors evaluated radiation worker performance with respect to radiation protection work permit requirements. The inspectors evaluated radiation protection technicians in performance of radiation surveys and in providing radiological job coverage.
Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)
The inspectors evaluated radiation worker performance with respect to radiation protection work permit requirements. The inspectors evaluated radiation protection technicians in performance of radiation surveys and in providing radiological job coverage.


Radiological Hazard Assessment (IP Section 02.01) (1 Sample)===
===Radiological Hazard Assessment (IP Section 02.01) (1 Sample)===
 
The inspectors conducted independent radiation measurements during walkdowns of the facility and evaluated:
===The inspectors conducted independent radiation measurements during walkdowns of the facility and evaluated:
: (1) The radiological survey program
: (1) The radiological survey program
: (2) Changes to plant operations since the last inspection
: (2) Changes to plant operations since the last inspection
: (3) Recent plant radiation surveys for radiological work activities
: (3) Recent plant radiation surveys for radiological work activities
: (4) Air sampling and analysis
: (4) Air sampling and analysis
: (5) Continuous air monitor use Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)===
: (5) Continuous air monitor use Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)
 
The inspectors evaluated in-plant radiological conditions and performed independent radiation measurements during facility walkdowns and observation of radiological work activities. The inspectors assessed whether posted surveys; radiation work permits; worker radiological briefings and radiation protection job coverage; the use of continuous air monitoring, air sampling and engineering controls; and dosimetry monitoring were consistent with the present conditions. The inspectors examined the control of highly activated or contaminated materials stored within the spent fuel pool and the posting and physical controls for selected high radiation areas, locked high radiation areas, and very high radiation areas.
===The inspectors evaluated in-plant radiological conditions and performed independent radiation measurements during facility walkdowns and observation of radiological work activities. The inspectors assessed whether posted surveys; radiation work permits; worker radiological briefings and radiation protection job coverage; the use of continuous air monitoring, air sampling and engineering controls; and dosimetry monitoring were consistent 8 with the present conditions. The inspectors examined the control of highly activated or contaminated materials stored within the spent fuel pool and the posting and physical controls for selected high radiation areas, locked high radiation areas, and very high radiation areas.
 
==71124.04 - Occupational Dose Assessment==


===
==71124.04 - Occupational Dose Assessment    External Dosimetry (IP Section 02.02)==
External Dosimetry (IP Section 02.02)===
{{IP sample|IP=IP 71124.04|count=1}}
{{IP sample|IP=IP 71124.04|count=1}}


The inspectors reviewed the current annual collective dose estimate; basis methodology; and measures to track, trend, and reduce occupational doses for ongoing work activities.
The inspectors reviewed the current annual collective dose estimate; basis methodology; and measures to track, trend, and reduce occupational doses for ongoing work activities.


The inspectors evaluated the adjustment of exposure estimates, or re-planning of work. The  
The inspectors evaluated the adjustment of exposure estimates, or re-planning of work. The inspectors reviewed post-job ALARA evaluations.
 
inspectors reviewed post-job ALARA evaluations.
 
Source Term Categorization (IP Section 02.01) (2 Samples)===
: (1) The inspectors evaluated radiological work planning by reviewing significant work activities to verify that ALARA planning was integrated into work procedures and


===radiation work permit documents.
===Source Term Categorization (IP Section 02.01) (2 Samples)===
: (2) The inspectors evaluated the licensee's characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.
: (1) The inspectors evaluated radiological work planning by reviewing significant work activities to verify that ALARA planning was integrated into work procedures and radiation work permit documents.
: (2) The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.


==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==


===71151 - Performance Indicator Verification  
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
 
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) ===
The inspectors verified licensee performance indicators submittals listed below:  
 
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===
{{IP sample|IP=IP 71151|count=1}}
{{IP sample|IP=IP 71151|count=1}}
For the period January 1, 2018 through December 31, 2018 BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)===
For the period January 1, 2018 through December 31, 2018


===For the period January 1, 2018 through December 31, 2018 MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)===
===BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)===
For the period January 1, 2018 through December 31, 2018 MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)
For the period January 1, 2018 through December 31, 2018
For the period January 1, 2018 through December 31, 2018


==71152 - Problem Identification and Resolution==
==71152 - Problem Identification and Resolution   Annual Follow-up of Selected Issues (IP Section 02.03)==
 
===
Annual Follow-up of Selected Issues (IP Section 02.03)===
{{IP sample|IP=IP 71152|count=4}}
{{IP sample|IP=IP 71152|count=4}}


The inspectors reviewed the licensee's implementation of its corrective action program related to the following issues:
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
: (1) Condition reports 2018-9566, 2019-0021, 2019-0078 and 2019-0302, Rod worth minimizer block action outside of design and subsequent inoperability
: (1) Condition reports 2018-9566, 2019-0021, 2019-0078 and 2019-0302, Rod worth minimizer block action outside of design and subsequent inoperability
: (2) Condition report 2016-2205, Boraflex neutron-absorbing panel degradation in the spent fuel pool 9
: (2) Condition report 2016-2205, Boraflex neutron-absorbing panel degradation in the spent fuel pool
: (3) Condition report 2018-0820, Target rock safety relief valve pilot assembly failed as-found lift test
: (3) Condition report 2018-0820, Target rock safety relief valve pilot assembly failed as-found lift test
: (4) Condition report 2007-4079 and 2016-3672, Part 21 automatic voltage regulator for emergency diesel generators  
: (4) Condition report 2007-4079 and 2016-3672, Part 21 automatic voltage regulator for emergency diesel generators


===71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)===
===71153 - Follow-up of Events and Notices of Enforcement Discretion     Event Report (IP Section 03.02) ===
{{IP sample|IP=IP 71153|count=3}}
{{IP sample|IP=IP 71153|count=3}}
The inspectors evaluated the following Licensee Event Reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx
The inspectors evaluated the following Licensee Event Reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
:
: (1) LER 05000293/2018-003-00, Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications (ADAMS Accession No. ML18093A388). The circumstances surrounding this LER are documented in the Inspection Results section of the report.
: (1) LER 05000293/2018-003-00, Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications (ADAMS Accession No. ML18093A388). The circum stances surrounding this LER are documented in the Inspection Results section of the report.
: (2) LER 05000293/2019-001-00, Reactor Core Isolation Cooling System Declared Inoperable During Surveillance Testing on March 5, 2019 (ADAMS Accession No.
: (2) LER 05000293/2019-001-00, Reactor Core Isolation Cooling System Declared Inoperable During Surveillance Testing on March 5, 2019 (ADAMS Accession No.


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==INSPECTION RESULTS==
==INSPECTION RESULTS==
Observation 71152 The inspectors performed a review of Entergy's evaluation and corrective actions associated with LER 05000293/2018-003-00, "Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Techni cal Specifications.This LER, and the associated condition report, CR-PNP-2018-00820, evaluated and documented a main steam safety relief valve as-found lift setpoint test failure. Specifically, one of the four safety relief valves exceeded the technical specification tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendor's test facility. The setpoint drift has been attributed to "corrosion bonding" which involves bridging oxide buildup between the Stellite 21 pilot disc surface and Stellite 6 pilot valve body seating surface.
Observation                                                                                     71152 The inspectors performed a review of Entergy's evaluation and corrective actions associated with LER 05000293/2018-003-00, Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications. This LER, and the associated condition report, CR-PNP-2018-00820, evaluated and documented a main steam safety relief valve as-found lift setpoint test failure. Specifically, one of the four safety relief valves exceeded the technical specification tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendors test facility. The setpoint drift has been attributed to corrosion bonding which involves bridging oxide buildup between the Stellite 21 pilot disc surface and Stellite 6 pilot valve body seating surface.


As documented in NRC Regulatory Issue Summary 2000-12, corrosion bonding is a known phenomenon in the nuclear industry that affects the 2-stage target rock safety relief valves. It characteristically results in the valve lifting at a higher pressure, failing to meet its setpoint criteria during the first lift attempt; but the affected safety relief valve typically lifts satisfactorily at its nominal setpoint during consecutive tests (after the corrosion bond is broken during the initial lift).
As documented in NRC Regulatory Issue Summary 2000-12, corrosion bonding is a known phenomenon in the nuclear industry that affects the 2-stage target rock safety relief valves. It characteristically results in the valve lifting at a higher pressure, failing to meet its setpoint criteria during the first lift attempt; but the affected safety relief valve typically lifts satisfactorily at its nominal setpoint during consecutive tests (after the corrosion bond is broken during the initial lift).


The inspectors evaluated Entergy's prioritization and timeliness of corrective actions to determine whether they were appropriately identifying, characterizing, and correcting problems associated with this issue, and whether the planned or completed corrective actions were commensurate with the safety significance. The inspectors determined Entergy staff 10 implemented corrective actions intended to impr ove safety relief valve performance, which included changing the pilot disc material to Stellite 6B with a platinum coating. This material is expected to reduce the likelihood of corrosion bonding. Previously (circa 2011), Entergy staff replaced the 2-stage safety relief valves with 3-stage target rock safety relief valves, in part, to address the corrosion bonding issue. However, operating experience with the 3-stage target rock safety relief valve at Pilgrim as well as other boiling water reactors, revealed an unrelated problem with the 3-stage safety relief valve design. In response, Entergy staff installed the 2-stage design during the Spring 2015 refueling outage pending a final resolution of the 3-stage safety relief valve design issue.
The inspectors evaluated Entergys prioritization and timeliness of corrective actions to determine whether they were appropriately identifying, characterizing, and correcting problems associated with this issue, and whether the planned or completed corrective actions were commensurate with the safety significance. The inspectors determined Entergy staff implemented corrective actions intended to improve safety relief valve performance, which included changing the pilot disc material to Stellite 6B with a platinum coating. This material is expected to reduce the likelihood of corrosion bonding. Previously (circa 2011), Entergy staff replaced the 2-stage safety relief valves with 3-stage target rock safety relief valves, in part, to address the corrosion bonding issue. However, operating experience with the 3-stage target rock safety relief valve at Pilgrim as well as other boiling water reactors, revealed an unrelated problem with the 3-stage safety relief valve design. In response, Entergy staff installed the 2-stage design during the Spring 2015 refueling outage pending a final resolution of the 3-stage safety relief valve design issue.


Relative to the one safety relief valve that did not meet test acceptance criterion, Entergy staff performed an evaluation of the as-found set pressures for all four safety relief valves and concluded no design or licensing basis limits would have been exceeded had the safety relief valves been required to operate. The inspectors reviewed the evaluation and did not identify deficiencies; the safety impact due to one safety relief valve being slightly out of tolerance was minimal.
Relative to the one safety relief valve that did not meet test acceptance criterion, Entergy staff performed an evaluation of the as-found set pressures for all four safety relief valves and concluded no design or licensing basis limits would have been exceeded had the safety relief valves been required to operate. The inspectors reviewed the evaluation and did not identify deficiencies; the safety impact due to one safety relief valve being slightly out of tolerance was minimal.
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The inspectors concluded Entergy staff implemented corrective actions consistent with industry and vendor initiatives to minimize the corrosion bonding issues. These corrective actions implemented industry and vendor recommendations and were commensurate with the safety significance of the issue. The Enforcement aspect of this issue is dispositioned below.
The inspectors concluded Entergy staff implemented corrective actions consistent with industry and vendor initiatives to minimize the corrosion bonding issues. These corrective actions implemented industry and vendor recommendations and were commensurate with the safety significance of the issue. The Enforcement aspect of this issue is dispositioned below.


Observation 71152 The inspectors conducted inspection activities to follow up on Entergy's continuing corrective actions taken to address degraded Boraflex neutron absorption panels in the Pilgrim spent fuel pool. The NRC previously reviewed this issue and Entergy's prior corrective actions in 2017, as discussed in NRC Inspection Reports 05000293/2017001 (ADAMS Accession No.
Observation                                                                               71152 The inspectors conducted inspection activities to follow up on Entergys continuing corrective actions taken to address degraded Boraflex neutron absorption panels in the Pilgrim spent fuel pool. The NRC previously reviewed this issue and Entergys prior corrective actions in 2017, as discussed in NRC Inspection Reports 05000293/2017001 (ADAMS Accession No.


ML17136A015) and 05000293/2017004 (ADAMS Accession No. ML18045A058).
ML17136A015) and 05000293/2017004 (ADAMS Accession No. ML18045A058).


Inspectors reviewed Entergy's logs for fuel moves taking place in 2018, documentation of the current spent fuel pool configuration, and a revised criticality analysis that was implemented by Entergy. Inspectors also discussed actions taken and the details of the criticality analysis with knowledgeable Entergy staff. Inspectors reviewed Entergy's administrative controls for managing criticality in the spent fuel pool to ensure that fuel moves and the current fuel configuration adhered to the established requirements. Additionally, inspector's reviewed Entergy's current plans for the eventual offload of all fuel in the spent fuel pool to dry cask storage.
Inspectors reviewed Entergys logs for fuel moves taking place in 2018, documentation of the current spent fuel pool configuration, and a revised criticality analysis that was implemented by Entergy. Inspectors also discussed actions taken and the details of the criticality analysis with knowledgeable Entergy staff. Inspectors reviewed Entergys administrative controls for managing criticality in the spent fuel pool to ensure that fuel moves and the current fuel configuration adhered to the established requirements. Additionally, inspectors reviewed Entergys current plans for the eventual offload of all fuel in the spent fuel pool to dry cask storage.


Based on their review, the inspectors concluded that there is reasonable assurance that the reconfigured spent fuel pool provides sufficient margin to ensure that criticality will be maintained within regulatory limits in the spent fuel pool during and following the offload of the fuel currently in the reactor core into the spent fuel pool. Throughout 2018, Entergy took actions to unload a portion of the fuel from the spent fuel pool into dry-cask storage, and these actions introduced sufficient capacity into the spent fuel pool to safely conduct full 11 offload of the fuel currently in the core. This offload is planned to take place following the planned shutdown and permanent cessation of operations.
Based on their review, the inspectors concluded that there is reasonable assurance that the reconfigured spent fuel pool provides sufficient margin to ensure that criticality will be maintained within regulatory limits in the spent fuel pool during and following the offload of the fuel currently in the reactor core into the spent fuel pool. Throughout 2018, Entergy took actions to unload a portion of the fuel from the spent fuel pool into dry-cask storage, and these actions introduced sufficient capacity into the spent fuel pool to safely conduct full offload of the fuel currently in the core. This offload is planned to take place following the planned shutdown and permanent cessation of operations.


Target Rock Relief Valve Pilot Assembly Fa iled As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone Severity Cross-cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000293/2019001-01  
Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone       Severity                                           Cross-cutting Report Aspect           Section Not Applicable Severity Level IV                                     Not              71153 NCV 05000293/2019001-01                           Applicable Open/Closed A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendors test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.


Open/Closed
=====Description:=====
 
On January 26, 2018, Entergy staff received results that an as-found setpoint test for one of the four main steam SRV pilot stage assemblies had exceeded the lift setting tolerance prescribed in TSs. Specifically, one of the four pilot stage assemblies tested experienced drift beyond the +/- 3 percent tolerance permitted by Technical Specification 4.6.D.1. The SRV had been in service the prior operating cycle. Entergy staff concluded that the cause of the setpoint drift was attributed to corrosion bonding between the pilot disc and seating surfaces. This condition was reportable under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition which was prohibited by the plants technical specifications.
Not Applicable 71153 A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendor's test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.


=====Description:=====
Corrective Actions: Entergy staff replaced all four SRVs with those that were refurbished, certified, and tested (to within +/- 1 percent of 1155 psig as per TS 4.6.D.1). Entergy staff implemented additional corrective actions intended to improve SRV performance.
On January 26, 2018, Entergy staff received results that an as-found setpoint test for one of the four main steam SRV pilot stage assemblies had exceeded the lift setting tolerance prescribed in TSs. Specifically, one of the four pilot stage assemblies tested experienced drift beyond the +/- 3 percent tolerance permitted by Technical Specification 4.6.D.1. The SRV had been in service the prior operating cycle. Entergy staff concluded that the cause of the setpoint drift was attributed to corrosion bonding between the pilot disc and seating surfaces. This condition was reportable under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition which was prohibited by the plant's technical specifications.


Corrective Actions:  Entergy staff replaced all four SRVs with those that were refurbished, certified, and tested (to within +/- 1 percent of 1155 psig as per TS 4.6.D.1). Entergy staff implemented additional corrective actions intended to improve SRV performance. Specifically, they changed the pilot disc material (Stellite 6B with a platinum coating), which is expected to be less susceptible to the corrosion bonding phenomenon.
Specifically, they changed the pilot disc material (Stellite 6B with a platinum coating), which is expected to be less susceptible to the corrosion bonding phenomenon.


Corrective Action Reference: CR-PNP-2018-00820
Corrective Action Reference: CR-PNP-2018-00820


=====Performance Assessment:=====
=====Performance Assessment:=====
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=====Enforcement:=====
=====Enforcement:=====
The ROP's significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation, which impedes the NRC's ability to regulate using traditional enforcement. Because there is no performance deficiency, and therefore no finding was identified, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance. The inspectors reviewed the NRC Enforcement Policy, Section 2.2.1, "Factors Affecting Assessment of Violations", issued on May 15, 2018. Section 2.2.1 states, in part, that in determining the appropriate enforcement response to a violation, the NRC considers, whenever possible, risk inform ation in assessing the safety or security significance of violations and assigning severity levels. The inspectors also reviewed IMC 12 0609, Appendix A, "The Significance Determination Process for Findings At-Power," Exhibit 2, "Mitigating Systems Screening Questions," issued on June 19, 2012. The inspectors determined the issue to be of very low safety significance (Green) because it did not represent a loss of system or function because the SRV (pilot valve serial number 1025)remained capable of lifting to protect the reactor coolant system. As a result, the inspectors determined that the issue's significance was Severity Level IV.
The ROPs significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation, which impedes the NRCs ability to regulate using traditional enforcement. Because there is no performance deficiency, and therefore no finding was identified, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance. The inspectors reviewed the NRC Enforcement Policy, Section 2.2.1, Factors Affecting Assessment of Violations, issued on May 15, 2018. Section 2.2.1 states, in part, that in determining the appropriate enforcement response to a violation, the NRC considers, whenever possible, risk information in assessing the safety or security significance of violations and assigning severity levels. The inspectors also reviewed IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, issued on June 19, 2012. The inspectors determined the issue to be of very low safety significance (Green) because it did not represent a loss of system or function because the SRV (pilot valve serial number 1025)remained capable of lifting to protect the reactor coolant system. As a result, the inspectors determined that the issue's significance was Severity Level IV.


Violation: TS 4.6.D.1 requires that all four SRVs shall be operable with a lift setpoint of 1155 psig +/- 34.6.
Violation: TS 4.6.D.1 requires that all four SRVs shall be operable with a lift setpoint of 1155 psig +/- 34.6.


Contrary to the above, on January 26, 2018, Entergy staff identified that the as-found lift setpoint for one SRV (pilot valve serial number 1025) was measured above the TS 4.6.D.1 maximum allowable value. Because this discovery occurred after the valve was removed from service, Entergy determined that it was reasonable to conclude that while the valve had been installed, the lift setpoint was not within the TS required values, resulting in the valve being inoperable for a period of time in excess of the TS 4.6.D.1 allowed outage time for one SRV.
Contrary to the above, on January 26, 2018, Entergy staff identified that the as-found lift setpoint for one SRV (pilot valve serial number 1025) was measured above the TS 4.6.D.1 maximum allowable value. Because this discovery occurred after the valve was removed from service, Entergy determined that it was reasonable to conclude that while the valve had been installed, the lift setpoint was not within the TS required values, resulting in the valve being inoperable for a period of time in excess of the TS 4.6.D.1 allowed outage time for one SRV.


Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. The ROP's significance determination process does not specifically consider violations without findings in its assessment of licensee performance. Therefore, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. The ROPs significance determination process does not specifically consider violations without findings in its assessment of licensee performance.
 
Therefore, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance.


The disposition of this violation closes Licensee Event Report 05000293/2018-003-00.
The disposition of this violation closes Licensee Event Report 05000293/2018-003-00.


Minor Violation 71153 Minor Violation: The failure to take actions in accordance with the time constraints required by Technical Specifications Table 3.1.1.
Minor Violation                                     71153 Minor Violation: The failure to take actions in accordance with the time constraints required by Technical Specifications Table 3.1.1.


As described in Licensee Event Report 05000293/2019-002-00, Entergy identified that on January 3, 2019, operators did not place the associated reactor protection system logic channel in a tripped position within 12 hours as required per technical specifications after the limit switch LS6 failed to open when main steam isolation valve 1C was closed.
As described in Licensee Event Report 05000293/2019-002-00, Entergy identified that on January 3, 2019, operators did not place the associated reactor protection system logic channel in a tripped position within 12 hours as required per technical specifications after the limit switch LS6 failed to open when main steam isolation valve 1C was closed.


Screening: The inspectors determined the performance deficiency was minor, because there was no impact to the main steam isolation valve closure scram function within the reactor protection system.
Screening: The inspectors determined the performance deficiency was minor, because there was no impact to the main steam isolation valve closure scram function within the reactor protection system.


=====Enforcement:=====
=====Enforcement:=====
This failure to comply with Technical Specifications Table 3.1.1 constitutes a minor violation that is not subject to enforcement action in accordance with the NRC's Enforcement Policy.
This failure to comply with Technical Specifications Table 3.1.1 constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.


The disposition of this minor violation closes Licensee Event Report 05000293/2019-002-00.
The disposition of this minor violation closes Licensee Event Report 05000293/2019-002-00.
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On April 18, 2019, the inspector presented the quarterly resident inspector inspection results to Brian Sullivan and other members of the licensee staff.
On April 18, 2019, the inspector presented the quarterly resident inspector inspection results to Brian Sullivan and other members of the licensee staff.
14


=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Inspection
Inspection Type             Designation     Description or Title                               Revision or
Procedure Type Designation Description or Title Revision or
Procedure                                                                                        Date
Date 71111.04 Drawings M212, Sh.1 Service Water System P & ID Revision 97 Miscellaneous 8.5.3.14 SSW Flow Rate Operability Test performed
71111.04   Drawings         M212, Sh.1     Service Water System P & ID                         Revision 97
3/19/19 Procedures 2.2.32 Salt Service Water System (SSW) Revision 97 71111.05Q Procedures 5.5.2 Special Fire Procedure Revision 59 EN-DC-161 Control of Combustibles Revision 19 71111.07A Engineering
Miscellaneous     8.5.3.14       SSW Flow Rate Operability Test                     performed
Evaluations
3/19/19
WT-WTPNP-2017-0140 CA 34 Salt Service Water System Maintenance Rule (a)(1)
Procedures       2.2.32         Salt Service Water System (SSW)                     Revision 97
Evaluation
71111.05Q Procedures         5.5.2           Special Fire Procedure                             Revision 59
dated 8/16/17 Procedures 2.2.32 Salt Service Water System (SSW) Revision 98 5.3.3 Loss of All Service Water Revision 30 5.3.37 Loss of Spent Fuel Pool Cooling Event Revision 6 71111.11Q Procedures EN-OP-115 Conduct of Operations Revision 26 71111.12 Procedures EN-DC-205 Maintenance Rule Monitoring Revision 6 71111.13 Procedures EN-WM-104 On-line Risk Assessment Revision 18 71111.15 Procedures 2.2.92 Main Steam Line Isolation and Turbine Bypass Valves Revision 57 EN-OP-104 Operability Determination Process Revision 16 71111.18 Procedures EN- DC-115 Engineering Change Process Revision 26 EN- DC-136 Temporary Modifications Revision 18 71114.06 Procedures EP-AD-601 Emergency Action Level Technical Basis Document Revision 9 71152 Corrective Action Documents CR-PNP-2016-
EN-DC-161       Control of Combustibles                             Revision 19
205  CR-PNP-2018-
71111.07A Engineering       WT-WTPNP-       Salt Service Water System Maintenance Rule (a)(1)   dated
00565   CR-PNP-2018-
Evaluations      2017-0140 CA 34 Evaluation                                         8/16/17
07519   CR-PNP-2018-
Procedures       2.2.32         Salt Service Water System (SSW)                     Revision 98
09458   CR-PNP-2018-
5.3.3           Loss of All Service Water                           Revision 30
09459   CR-PNP-2018-
5.3.37         Loss of Spent Fuel Pool Cooling Event               Revision 6
71111.11Q Procedures       EN-OP-115       Conduct of Operations                               Revision 26
71111.12   Procedures       EN-DC-205       Maintenance Rule Monitoring                         Revision 6
71111.13   Procedures       EN-WM-104       On-line Risk Assessment                             Revision 18
71111.15   Procedures       2.2.92         Main Steam Line Isolation and Turbine Bypass Valves Revision 57
EN-OP-104       Operability Determination Process                   Revision 16
71111.18   Procedures       EN- DC-115     Engineering Change Process                         Revision 26
EN- DC-136     Temporary Modifications                             Revision 18
71114.06   Procedures       EP-AD-601       Emergency Action Level Technical Basis Document     Revision 9
71152     Corrective Action CR-PNP-2016-
Documents        02205
CR-PNP-2018-
00565
CR-PNP-2018-
07519
CR-PNP-2018-
09458
CR-PNP-2018-
09459
CR-PNP-2018-
09461
09461
Inspection
Inspection Type             Designation     Description or Title                                           Revision or
Procedure Type Designation Description or Title Revision or
Procedure                                                                                                    Date
Date Miscellaneous Engineering
Miscellaneous     Engineering     PNPS Fuel Storage Criticality Safety Analysis of Spent Fuel     Revision 0
Report ECH-NE-
Report ECH-NE-  Storage Racks Utilizing Burnup Credit to Remove Boraflex
19-00018 PNPS Fuel Storage Criticality Safety Analysis of Spent Fuel Storage Racks Utilizing Burnup Credit to Remove Boraflex
19-00018        Credit
Credit Revision 0
ICA 2017- 45   Item Control Area Transfer Forms
ICA 2017- 45
through 2017-49
through 2017-49
Item Control Area Transfer Forms
ICA 2018-03    Item Control Area Transfer Forms
ICA 2018-03
through 2018-17
through 2018-17
Item Control Area Transfer Forms
ICA 2018-27     Item Control Area Transfer Form
ICA 2018-27 Item Control Area Transfer Form
NA             Diagram of current spent fuel pool configuration by criticality generated
NA Diagram of current spent fuel pool configuration by criticality safety analysis fuel type, Cycle 22
safety analysis fuel type, Cycle 22                             on February
generated
28, 2019
on February
Procedures       PNPS 4.3       Fuel Handling                                                   Revision 140
28, 2019 Procedures PNPS 4.3 Fuel Handling Revision 140 71153 Corrective Action Documents
71153     Corrective Action 2019-0090
2019-0090
Documents        2019-0838
2019-0838
15
}}
}}

Latest revision as of 12:50, 18 December 2019

Integrated Inspection Report 05000293/2019001
ML19133A225
Person / Time
Site: Pilgrim
Issue date: 05/13/2019
From: Anthony Dimitriadis
NRC/RGN-I/DRP/PB5
To: Brian Sullivan
Entergy Nuclear Operations
Dimitriadis A
References
IR 2019001
Download: ML19133A225 (18)


Text

{{#Wiki_filter:==SUBJECT:== PILGRIM NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000293/2019001

Dear Mr. Sullivan:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Pilgrim Nuclear Power Station (Pilgrim). On April 18, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one self-revealing Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC resident inspector at Pilgrim. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, /RA/ Anthony Dimitriadis, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Number: 50-293 License Number: DPR-35

Enclosure:

Inspection Report 05000293/2019001

Inspection Report

Docket Number: 50-293 License Number: DPR-35 Report Number: 05000293/2019001 Enterprise Identifier: I-2019-001-0042 Licensee: Entergy Nuclear Operations, Inc. (Entergy) Facility: Pilgrim Nuclear Power Station (Pilgrim) Location: Plymouth, Massachusetts Inspection Dates: January 1, 2019 to March 31, 2019 Inspectors: E. Burket, Senior Resident Inspector B. Pinson, Resident Inspector P. Boguszewski, Resident Inspector S. Pindale, Senior Reactor Inspector J. Schoppy, Senior Reactor Inspector J. Vazquez, Resident Inspector S. Wilson, Health Physicist A. Ziedonis, Senior Resident Inspector Approved By: Anthony Dimitriadis, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Entergys performance at Pilgrim by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process (ROP). The ROP is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone Significance Cross-cutting Report Aspect Section Not Applicable NCV 05000293/2019001-01 Not Applicable 71153 Open/Closed A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendors test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.

Additional Tracking Items Type Issue number Title Report Status Section LER 05000293/2018-003-00 Target Rock Relief Valve Pilot 71153 Closed Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications LER 05000293/2019-001-00 Reactor Core Isolation Cooling 71153 Closed System Declared Inoperable During Surveillance Testing LER 05000293/2019-002-00 Failure of Main Steam Isolation Valve 71153 Closed Limit Switch Results in a Condition Prohibited by Technical Specifications

PLANT STATUS

The unit began the inspection period at rated thermal power. On January 3, 2019, the station reduced power to 25 percent to troubleshoot and repair 'A' feedwater regulating valve. On January 6, 2019, operations personnel returned the unit to rated thermal power. On January 16, 2019, the station reduced power to 25 percent to repair a leaking primary containment isolation system valve. On January 17, 2019, operations personnel returned the unit to rated thermal power. On March 20, 2019, the station reduced power to 35 percent to repair a leaking feedwater heater valve in the condenser bay. On March 21, 2019, operations personnel returned the unit to rated thermal power and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection Impending Severe Weather Sample (IP Section 03.03)

(1) The inspectors evaluated readiness for impending adverse weather conditions for extreme cold temperatures on January 31, 2019.

71111.04 - Equipment Alignment Partial Walkdown (IP Section 03.01)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) 'B' emergency diesel generator on February 5, 2019
(2) High pressure coolant injection system on February 9, 2019
(3) Reactor building closed cooling water on February 25-26, 2019
(4) 'A' and 'B' salt service water before and after 'B' salt service water testing on March 18-20, 2019

71111.04S - Equipment Alignment Complete Walkdown (IP Section 03.02)

The inspectors evaluated system configurations during complete walkdowns of the following system:

(1) 'A' emergency diesel generator following maintenance and testing on March 27, 2019

71111.05A - Fire Protection (Annual) Annual Inspection (IP Section 03.02)

(1) The inspectors evaluated fire brigade performance on January 30, 2019.

71111.05Q - Fire Protection Quarterly Inspection (IP Section 03.01)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) 'B' switchgear (fire zone 2.1) on February 24, 2019
(2) Cable spreading room (fire zone 3.2) on February 24, 2019
(3) Radwaste corridor area (fire zone 3.1) on February 26, 2019
(4) 'B' reactor building closed cooling water (fire zone 1.22) on March 9, 2019
(5) Machine shop (fire zone 3.8) on March 19, 2019

71111.07T - Heat Sink Performance Triennial Review (IP Section 02.02)

The inspectors evaluated heat exchanger/sink performance on the following:

(1) 'B' spent fuel pool cooling heat exchanger
(2) 'B' reactor building closed cooling water heat exchanger
(3) Ultimate heat sink associated with service water system operation and intake structure condition

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

The inspectors observed and evaluated licensed operator performance in the control room during down power to 25 percent and isolation of 'C' main steam line on January 3, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample) The inspectors observed and evaluated licensed operator requalification training in the simulator on March 13, 2019.

71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness Inspection (IP Section 02.01)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Rod worth minimizer troubleshooting and repairs on February 20, 2019
(2) Main stack high range effluent monitors following return to (a)(2) status on February 20, 2019
(3) Neutron monitoring instrumentation following return to (a)(2) status completed March 12, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control Risk Assessment and Management Sample (IP Section 03.01)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Emergent work to troubleshoot and replace recirculation motor generator set B1 speed limiter on January 5, 2019
(2) Elevated risk during reactor core isolation cooling testing and inoperability on January 8, 2019
(3) Elevated risk during emergency diesel generator maintenance on February 4, 2019
(4) Elevated risk during reactor core isolation cooling maintenance and testing on March 27, 2019

71111.15 - Operability Determinations and Functionality Assessments Sample Selection (IP Section 02.02)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Reactor core isolation cooling operability evaluation after quarterly surveillance and replacement of flow controller (CR-2019-0145) on January 8, 2019
(2) Reactor core isolation cooling operability following flow oscillations (CR-2019-0802)on February 6, 2019
(3) Main steam isolation valve AO-203-1C input to reactor protection system past operability (CR-2019-0090) on February 20, 2019
(4) Control rod drive operability following scram pilot valve air header alarms (CR-2019-1783) on March 29, 2019

==71111.18 - Plant Modifications Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples) The inspectors evaluated the following temporary or permanent modifications:

(1) Feedwater check valve, 6-CK-62B, clamp installation
(2) Main steam isolation valve 1C reactor protection system relay K3F

71111.19 - Post Maintenance Testing Post Maintenance Test Sample (IP Section 03.01)

[[IP sample::=

=IP 71111.18|count=3}}

The inspectors evaluated the following post maintenance tests:

(1) 'B' emergency diesel generator turbo air assist relay replacement post work testing on February 4, 2019
(2) Drywell to torus vacuum breaker AO-5045D relay replacement post work testing on March 14, 2019
(3) 'B' fuel pool pump, P210B, post work testing on March 18, 2019

71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: In Service Testing (IST) (IP Section 03.01)

(1) 8.5.4.1 High pressure coolant injection operability and flow rate test on February 5, 2019

Surveillance Testing (IP Section 03.01) (4 Samples)

(1) 8.5.5.1 Reactor core isolation cooling operability run on January 10, 2019
(2) 8.M.2-1.5.10 High pressure coolant injection vacuum breaker isolation valve testing on February 5, 2019
(3) 8.5.1.1 Core spray operability surveillance on March 5, 2019
(4) 8.3.3 Scram discharge isolation volume vent and drain valve operability surveillance on March 21, 2019

71114.06 - Drill Evaluation Emergency Preparedness (EP) Drill (IP Section 02.01)

The inspectors evaluated the conduct of a routine emergency planning drill on Wednesday, February 13,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls Contamination and Radioactive Material Control (IP Section 02.03)

The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material. The inspectors selected several sealed sources from inventory records and assessed whether the sources were accounted for and were tested for loose surface contamination. The inspectors evaluated whether any recent transactions involving nationally tracked sources were reported in accordance with requirements.

High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample) The inspectors reviewed the procedures and controls for high radiation areas, very high radiation areas, and radiological transient areas in the plant.

Instructions to Workers (IP Section 02.02) (1 Sample)

The inspectors reviewed high radiation area work permit controls and use, reviewed electronic alarming dosimeter alarms and set points, observed worker briefings on radiological conditions, and observed containers of radioactive materials and assessed whether the containers were labeled and controlled in accordance with requirements.

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample) The inspectors evaluated radiation worker performance with respect to radiation protection work permit requirements. The inspectors evaluated radiation protection technicians in performance of radiation surveys and in providing radiological job coverage.

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)

The inspectors conducted independent radiation measurements during walkdowns of the facility and evaluated:

(1) The radiological survey program
(2) Changes to plant operations since the last inspection
(3) Recent plant radiation surveys for radiological work activities
(4) Air sampling and analysis
(5) Continuous air monitor use Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions and performed independent radiation measurements during facility walkdowns and observation of radiological work activities. The inspectors assessed whether posted surveys; radiation work permits; worker radiological briefings and radiation protection job coverage; the use of continuous air monitoring, air sampling and engineering controls; and dosimetry monitoring were consistent with the present conditions. The inspectors examined the control of highly activated or contaminated materials stored within the spent fuel pool and the posting and physical controls for selected high radiation areas, locked high radiation areas, and very high radiation areas.

71124.04 - Occupational Dose Assessment External Dosimetry (IP Section 02.02)

The inspectors reviewed the current annual collective dose estimate; basis methodology; and measures to track, trend, and reduce occupational doses for ongoing work activities.

The inspectors evaluated the adjustment of exposure estimates, or re-planning of work. The inspectors reviewed post-job ALARA evaluations.

Source Term Categorization (IP Section 02.01) (2 Samples)

(1) The inspectors evaluated radiological work planning by reviewing significant work activities to verify that ALARA planning was integrated into work procedures and radiation work permit documents.
(2) The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below: BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) ===

For the period January 1, 2018 through December 31, 2018

BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)

For the period January 1, 2018 through December 31, 2018 MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample) For the period January 1, 2018 through December 31, 2018

71152 - Problem Identification and Resolution Annual Follow-up of Selected Issues (IP Section 02.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Condition reports 2018-9566, 2019-0021, 2019-0078 and 2019-0302, Rod worth minimizer block action outside of design and subsequent inoperability
(2) Condition report 2016-2205, Boraflex neutron-absorbing panel degradation in the spent fuel pool
(3) Condition report 2018-0820, Target rock safety relief valve pilot assembly failed as-found lift test
(4) Condition report 2007-4079 and 2016-3672, Part 21 automatic voltage regulator for emergency diesel generators

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following Licensee Event Reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000293/2018-003-00, Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications (ADAMS Accession No. ML18093A388). The circumstances surrounding this LER are documented in the Inspection Results section of the report.
(2) LER 05000293/2019-001-00, Reactor Core Isolation Cooling System Declared Inoperable During Surveillance Testing on March 5, 2019 (ADAMS Accession No.

ML19064A593). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.

(3) LER 05000293/2019-002-00, Failure of Main Steam Isolation Valve Limit Switch Results in a Condition Prohibited by Technical Specifications (ADAMS Accession No. ML19065A050). The circumstances surrounding this LER are documented in the Inspection Results section of the report.

INSPECTION RESULTS

Observation 71152 The inspectors performed a review of Entergy's evaluation and corrective actions associated with LER 05000293/2018-003-00, Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications. This LER, and the associated condition report, CR-PNP-2018-00820, evaluated and documented a main steam safety relief valve as-found lift setpoint test failure. Specifically, one of the four safety relief valves exceeded the technical specification tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendors test facility. The setpoint drift has been attributed to corrosion bonding which involves bridging oxide buildup between the Stellite 21 pilot disc surface and Stellite 6 pilot valve body seating surface.

As documented in NRC Regulatory Issue Summary 2000-12, corrosion bonding is a known phenomenon in the nuclear industry that affects the 2-stage target rock safety relief valves. It characteristically results in the valve lifting at a higher pressure, failing to meet its setpoint criteria during the first lift attempt; but the affected safety relief valve typically lifts satisfactorily at its nominal setpoint during consecutive tests (after the corrosion bond is broken during the initial lift).

The inspectors evaluated Entergys prioritization and timeliness of corrective actions to determine whether they were appropriately identifying, characterizing, and correcting problems associated with this issue, and whether the planned or completed corrective actions were commensurate with the safety significance. The inspectors determined Entergy staff implemented corrective actions intended to improve safety relief valve performance, which included changing the pilot disc material to Stellite 6B with a platinum coating. This material is expected to reduce the likelihood of corrosion bonding. Previously (circa 2011), Entergy staff replaced the 2-stage safety relief valves with 3-stage target rock safety relief valves, in part, to address the corrosion bonding issue. However, operating experience with the 3-stage target rock safety relief valve at Pilgrim as well as other boiling water reactors, revealed an unrelated problem with the 3-stage safety relief valve design. In response, Entergy staff installed the 2-stage design during the Spring 2015 refueling outage pending a final resolution of the 3-stage safety relief valve design issue.

Relative to the one safety relief valve that did not meet test acceptance criterion, Entergy staff performed an evaluation of the as-found set pressures for all four safety relief valves and concluded no design or licensing basis limits would have been exceeded had the safety relief valves been required to operate. The inspectors reviewed the evaluation and did not identify deficiencies; the safety impact due to one safety relief valve being slightly out of tolerance was minimal.

During the refueling outage in which the four safety relief valves were removed for testing, Entergy staff replaced all four safety relief valves with those that were refurbished, certified, and tested (to within +/- 1 percent of 1155 psig as per TS 4.6.D.1). As stated above, Entergy provided a less susceptible material with platinum coating in an effort to prevent continued setpoint drift due to corrosion bonding.

The inspectors concluded Entergy staff implemented corrective actions consistent with industry and vendor initiatives to minimize the corrosion bonding issues. These corrective actions implemented industry and vendor recommendations and were commensurate with the safety significance of the issue. The Enforcement aspect of this issue is dispositioned below.

Observation 71152 The inspectors conducted inspection activities to follow up on Entergys continuing corrective actions taken to address degraded Boraflex neutron absorption panels in the Pilgrim spent fuel pool. The NRC previously reviewed this issue and Entergys prior corrective actions in 2017, as discussed in NRC Inspection Reports 05000293/2017001 (ADAMS Accession No.

ML17136A015) and 05000293/2017004 (ADAMS Accession No. ML18045A058).

Inspectors reviewed Entergys logs for fuel moves taking place in 2018, documentation of the current spent fuel pool configuration, and a revised criticality analysis that was implemented by Entergy. Inspectors also discussed actions taken and the details of the criticality analysis with knowledgeable Entergy staff. Inspectors reviewed Entergys administrative controls for managing criticality in the spent fuel pool to ensure that fuel moves and the current fuel configuration adhered to the established requirements. Additionally, inspectors reviewed Entergys current plans for the eventual offload of all fuel in the spent fuel pool to dry cask storage.

Based on their review, the inspectors concluded that there is reasonable assurance that the reconfigured spent fuel pool provides sufficient margin to ensure that criticality will be maintained within regulatory limits in the spent fuel pool during and following the offload of the fuel currently in the reactor core into the spent fuel pool. Throughout 2018, Entergy took actions to unload a portion of the fuel from the spent fuel pool into dry-cask storage, and these actions introduced sufficient capacity into the spent fuel pool to safely conduct full offload of the fuel currently in the core. This offload is planned to take place following the planned shutdown and permanent cessation of operations.

Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone Severity Cross-cutting Report Aspect Section Not Applicable Severity Level IV Not 71153 NCV 05000293/2019001-01 Applicable Open/Closed A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendors test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.

Description:

On January 26, 2018, Entergy staff received results that an as-found setpoint test for one of the four main steam SRV pilot stage assemblies had exceeded the lift setting tolerance prescribed in TSs. Specifically, one of the four pilot stage assemblies tested experienced drift beyond the +/- 3 percent tolerance permitted by Technical Specification 4.6.D.1. The SRV had been in service the prior operating cycle. Entergy staff concluded that the cause of the setpoint drift was attributed to corrosion bonding between the pilot disc and seating surfaces. This condition was reportable under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition which was prohibited by the plants technical specifications.

Corrective Actions: Entergy staff replaced all four SRVs with those that were refurbished, certified, and tested (to within +/- 1 percent of 1155 psig as per TS 4.6.D.1). Entergy staff implemented additional corrective actions intended to improve SRV performance.

Specifically, they changed the pilot disc material (Stellite 6B with a platinum coating), which is expected to be less susceptible to the corrosion bonding phenomenon.

Corrective Action Reference: CR-PNP-2018-00820

Performance Assessment:

The NRC determined this violation was not reasonably foreseeable and preventable by the licensee and therefore is not a performance deficiency.

The inspectors concluded Entergy staff implemented corrective actions consistent with industry and vendor initiatives to minimize the corrosion bonding issues. These corrective actions implemented industry and vendor recommendations and were commensurate with the safety significance of the issue.

Enforcement:

The ROPs significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation, which impedes the NRCs ability to regulate using traditional enforcement. Because there is no performance deficiency, and therefore no finding was identified, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance. The inspectors reviewed the NRC Enforcement Policy, Section 2.2.1, Factors Affecting Assessment of Violations, issued on May 15, 2018. Section 2.2.1 states, in part, that in determining the appropriate enforcement response to a violation, the NRC considers, whenever possible, risk information in assessing the safety or security significance of violations and assigning severity levels. The inspectors also reviewed IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, issued on June 19, 2012. The inspectors determined the issue to be of very low safety significance (Green) because it did not represent a loss of system or function because the SRV (pilot valve serial number 1025)remained capable of lifting to protect the reactor coolant system. As a result, the inspectors determined that the issue's significance was Severity Level IV.

Violation: TS 4.6.D.1 requires that all four SRVs shall be operable with a lift setpoint of 1155 psig +/- 34.6.

Contrary to the above, on January 26, 2018, Entergy staff identified that the as-found lift setpoint for one SRV (pilot valve serial number 1025) was measured above the TS 4.6.D.1 maximum allowable value. Because this discovery occurred after the valve was removed from service, Entergy determined that it was reasonable to conclude that while the valve had been installed, the lift setpoint was not within the TS required values, resulting in the valve being inoperable for a period of time in excess of the TS 4.6.D.1 allowed outage time for one SRV.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. The ROPs significance determination process does not specifically consider violations without findings in its assessment of licensee performance.

Therefore, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance.

The disposition of this violation closes Licensee Event Report 05000293/2018-003-00.

Minor Violation 71153 Minor Violation: The failure to take actions in accordance with the time constraints required by Technical Specifications Table 3.1.1.

As described in Licensee Event Report 05000293/2019-002-00, Entergy identified that on January 3, 2019, operators did not place the associated reactor protection system logic channel in a tripped position within 12 hours as required per technical specifications after the limit switch LS6 failed to open when main steam isolation valve 1C was closed.

Screening: The inspectors determined the performance deficiency was minor, because there was no impact to the main steam isolation valve closure scram function within the reactor protection system.

Enforcement:

This failure to comply with Technical Specifications Table 3.1.1 constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

The disposition of this minor violation closes Licensee Event Report 05000293/2019-002-00.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 18, 2019, the inspector presented the quarterly resident inspector inspection results to Brian Sullivan and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or Procedure Date 71111.04 Drawings M212, Sh.1 Service Water System P & ID Revision 97 Miscellaneous 8.5.3.14 SSW Flow Rate Operability Test performed 3/19/19 Procedures 2.2.32 Salt Service Water System (SSW) Revision 97 71111.05Q Procedures 5.5.2 Special Fire Procedure Revision 59 EN-DC-161 Control of Combustibles Revision 19 71111.07A Engineering WT-WTPNP- Salt Service Water System Maintenance Rule (a)(1) dated Evaluations 2017-0140 CA 34 Evaluation 8/16/17 Procedures 2.2.32 Salt Service Water System (SSW) Revision 98 5.3.3 Loss of All Service Water Revision 30 5.3.37 Loss of Spent Fuel Pool Cooling Event Revision 6 71111.11Q Procedures EN-OP-115 Conduct of Operations Revision 26 71111.12 Procedures EN-DC-205 Maintenance Rule Monitoring Revision 6 71111.13 Procedures EN-WM-104 On-line Risk Assessment Revision 18 71111.15 Procedures 2.2.92 Main Steam Line Isolation and Turbine Bypass Valves Revision 57 EN-OP-104 Operability Determination Process Revision 16 71111.18 Procedures EN- DC-115 Engineering Change Process Revision 26 EN- DC-136 Temporary Modifications Revision 18 71114.06 Procedures EP-AD-601 Emergency Action Level Technical Basis Document Revision 9 71152 Corrective Action CR-PNP-2016- Documents 02205 CR-PNP-2018- 00565 CR-PNP-2018- 07519 CR-PNP-2018- 09458 CR-PNP-2018- 09459 CR-PNP-2018- 09461 Inspection Type Designation Description or Title Revision or Procedure Date Miscellaneous Engineering PNPS Fuel Storage Criticality Safety Analysis of Spent Fuel Revision 0 Report ECH-NE- Storage Racks Utilizing Burnup Credit to Remove Boraflex 19-00018 Credit ICA 2017- 45 Item Control Area Transfer Forms through 2017-49 ICA 2018-03 Item Control Area Transfer Forms through 2018-17 ICA 2018-27 Item Control Area Transfer Form NA Diagram of current spent fuel pool configuration by criticality generated safety analysis fuel type, Cycle 22 on February 28, 2019 Procedures PNPS 4.3 Fuel Handling Revision 140 71153 Corrective Action 2019-0090 Documents 2019-0838 15| ]]