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| issue date = 08/11/1997
| issue date = 08/11/1997
| title = LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe
| title = LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe
| author name = ST MARTIN J T
| author name = St Martin J
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:NRCRORM366(4-95)U.S.NUCLEARREGULATORY COMMISSIO LICENSEEEVENTREPORT(LER).(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEDBYOMBNO.3150-0104
{{#Wiki_filter:NRC RORM      366                          U.S. NUCLEAR REGULATORY COMMISSIO                                       APPROVED BY OMB NO. 3150-0104 (4-95)                                                                                                                      'XPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
'XPIRES04/30/96ESTIMATED BURDENPERRESPONSEToCOMPLYWITHTHISMANDATORY INFORMATION COLLECTION REQUEST:50.0HRS.REPORTEDLESSONSLEARNEDAREINCORPORATED INTOTHELICENSING PROCESSANDFEDBACKToINDUSTRY.
LICENSEE EVENT REPORT                      (LER)                                  REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK To INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE
FORWARDCOMMENTSREGARDING BURDENESTIMATEToTHEINFORMATION ANDRECORDSMANAGEMENT BRANCHIT-6F33),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, Dc20555-0001, ANDToTHEPAPERWORK REDUCTION PROJECTFACILITYNAME(1)TITLE(4)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2) 05000244PAGE(3)1OF7LeakOutsideContainment, DuetoWeldDefect,ResultsinLeakRateGreaterThanProgramLimitMONTHDAYYEAREVENTDATE(5)LERNUMBER(6)SEQUENT)AL REVISIONNUMBERNUMBERMONTHDAYYEARREPORTDATE(7)FACILITYNAMEOTHERFACILITIES INVOLVED(6)DOCKETNUMBER07239696-009-02081197FACILITYNAMEDOCKETNUMBEROPERATING MODE(9)POWERLEVEL(10)10020.2201(b) 20.2203(a)(1) 20.2203(a)
                      .(See reverse for required number of                                          INFORMATION AND RECORDS MANAGEMENT BRANCH IT-6 F33),
(2)(i)20.2203(a)
digits/characters for each block)                                          U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, Dc 20555-0001, AND To THE PAPERWORK REDUCTION PROJECT FACILITYNAME (1)                                                                                     DOCKET NUMBER(2)                                  PAGE (3)
(2)(v)20.2203(a)
R.E. Ginna Nuclear Power Plant                                                                05000244                            1OF7 TITLE (4)
(3)(i)20.2203(a)(3)(ii) 50.73(a)(2)(i)50.73(a)(2)
Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit EVENT DATE (5)                 LER NUMBER (6)             REPORT DATE (7)                                   OTHER FACILITIES INVOLVED (6)
(ii)50.73(a)(2)(iii)SUANTTOTHEREQUIREMENTS OF10CFRE:(ChackoneorTHISREPORTISSUBMITTED PURmore)(11)50.73(a)(2)(viii) 50.73(a)(2)(x) 73.7120.2203(a)
FACILITYNAME                            DOCKET NUMBER SEQUENT)AL    REVISION MONTH      DAY    YEAR                NUMBER                MONTH          DAY              YEAR NUMBER FACILITY NAME                            DOCKET NUMBER 07        23      96      96  009               02        08            11              97 OPERATING                THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR E: (Chack one or more) (11)
(2)(ii)20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(4) 50.36(c)(1)50.36(c)(2)LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(iv)50.73(a)(2)(v) 50.73(a)(2)(vii)OTHERSpecifyInAbet(ectbeloworinNRCForm365ATELEPHONE NUMBER(lne)udeAfeeCode)JohnT.St.Martin-Technical Assistant (716)771-3641COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE ToNPRDSCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE ToNPRDSBBEPSF0000N:;t~g:~i'~c)NI."i?';.:
MODE (9)                   20.2201(b)                   20.2203(a) (2)(v)                               50.73(a) (2) (i)                     50.73(a)(2)(viii)
SUPPLEMENTAL REPORTEXPECTED(14)YES(Ifyas,completeEXPECTEDSUBMISSION DATE).XNOEXPECTEDSUBMISSION DATE(16)MONTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximately 15single-spaced typewritten lines)(16)OnJuly23,1996,atapproximately 0857EDST,itwasdetermined thattheleakrate(fromaleakonapipingsystemoutsideContainment) wasgreaterthantheanalyzedvalueoftwogallonsperhourforaprimarycoolantsourceoutsideContainment.
POWER                      20.2203(a)(1)                 20.2203(a) (3)(i)                               50.73(a)(2) (ii)                     50.73(a)(2)(x)
Immediate corrective actionwastoconservatively enterTechnical Specification LimitingCondition forOperation 3.0.3andinitiateaplantshutdown, andtoinitiateactionstoisolatetheleakusingafreezeseal.Oncetheleakwasisolated, theplantexitedTechnical Specification 3.0.3andtheshutdownwasstopped.Theleakingpipewascutoutandreplaced.
LEVEL (10)       100        20.2203(a) (2) (i)           20.2203(a)(3)(ii)                               50.73(a) (2)(iii)                   73.71 20.2203(a) (2) (ii)           20.2203(a)(4)                                   50.73(a) (2) (iv)                   OTHER 20.2203(a)(2)(iii)           50.36(c) (1)                                   50.73(a)(2)(v)                 Specify In Abet(ect below or in NRC Form 365A 20.2203(a)(2)(iv)             50.36(c) (2)                                   50.73(a) (2)(vii)
Theunderlying causeoftheleakwasawelddefectwhichdatesbacktooriginalconstruction inthe1960's.ThiseventisNUREG-1022 CauseCode(B).Corrective actiontopreventrecurrence isoutlinedinSectionV.B.Additional corrective actionsareidentified inthissupplement.
LICENSEE CONTACT FOR THIS LER (12)
9708i80050 9708iiPDRADOCK050002448,PDR  
TELEPHONE NUMBER (lne)ude Afee Code)
John T. St. Martin - Technical Assistant                                                                             (716) 771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
SYSTEM      COMPONENT                    REPORTABLE                                                                                      REPORTABLE CAUSE                                  MANUFACTURER                                         CAUSE      SYSTEM      COMPONENT      MANUFACTURER To NPRDS                                                                                        To NPRDS B          BE            PSF            0000            N
:;t~g:~i'~c)NI."i?';.:
SUPPLEMENTAL REPORT EXPECTED (14)                                                                               MONTH        DAY        YEAR EXPECTED YES                                                                                                           SUBMISSION (If yas, complete EXPECTED SUBMISSION DATE).                         X        NO                            DATE (16)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On July 23, 1996, at approximately 0857 EDST, it was determined that the leak rate (from a leak on a piping system outside Containment) was greater than the analyzed value of two gallons per hour for a primary coolant source outside Containment.
Immediate corrective action was to conservatively enter Technical Specification Limiting Condition for Operation 3.0.3 and initiate      a plant shutdown, and to initiate actions to isolate the leak using a freeze seal. Once the leak was isolated, the plant exited Technical Specification 3.0.3 and the shutdown was stopped. The leaking pipe was cut out and replaced.
The underlying cause of the leak was a weld defect which dates back to original construction in the 1960's.
This event is NUREG-1022 Cause Code (B).
Corrective action to prevent recurrence is outlined in Section V.B. Additional corrective actions are identified in this supplement.
9708i80050 9708ii PDR      ADOCK        05000244 8                            ,PDR


NRCFORM366A(4.95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERIe)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-009-02PAGEI3)2OF7TEXT(IImorespaceisrequired, useadditional copiesofNRCForm366AJ(17)I.PRE-EVENT PLANTCONDITIONS:
NRC FORM 366A                                                                              U.S. NUCLEAR REGULATORY COMMISSION (4.95)
OnJuly22,1996,theplantwasinMode1atapproximately 100%steadystatereactorpower.Atapproximately 1130EDST,aRadiation Protection (RP)technician, whowasperforming aroutineweeklysurve'yoftheAuxiliary
LICENSEE EVENT REPORT (LER)
: Building, observedwaterdrippinginanareabehindtheRefueling WaterStorageTank(RWST).TheRPtechnician notifiedtheControlRoomoperators.
TEXT CONTINUATION FACILITY NAME I1)                                DOCKET            LER NUMBER Ie)          PAGE I3)
Effortstolocatethesourceofthedrippingwaterandtoquantifytheleakratewereinitiated byOperations andNuclearEngineering Services(NES).Thesourceofwaterwasdetermined tobeasmallleakonatestlinefortheContainment Spray(CS)systemintheAuxiliary
YEAR  SEQUENTIAL REVISION NUMBER    NUMBER 2 OF    7 R.E. Ginna Nuclear Power Plant                                  05000244      96    009           02 TEXT (II more space is required, use additional copies of NRC Form 366AJ (17)
: Building, whichisoutsidetheContainment (CNMT)~Theleakratewasestimated tobeapproximately one(1)gallonperhour(GPH).TheControlRoomoperators didnotidentifyanyrequirement thatwouldlimitplantoperations.
I.     PRE-EVENT PLANT CONDITIONS:
TheShiftSupervisor notifiedOperations management, maintenance management, andplantandNESstaffoftheleak.Allreachedasimilarconclusion.
On July 22, 1996, the plant was in Mode 1 at approximately 100% steady state reactor power. At approximately 1130 EDST, a Radiation Protection (RP) technician, who was performing a routine weekly surve'y of the Auxiliary Building, observed water dripping in an area behind the Refueling Water Storage Tank (RWST). The RP technician notified the Control Room operators. Efforts to locate the source of the dripping water and to quantify the leak rate were initiated by Operations and Nuclear Engineering Services (NES). The source of water was determined to be a small leak on a test line for the Containment Spray (CS) system in the Auxiliary Building, which is outside the Containment (CNMT) The leak rate was
Thestaffworkedondeveloping andimplementing anactionplantoaddresstheproblem.Theissuesoflineintegrity andRWSToperability wereinvestigated byNESandLaboratory Inspection Services(LIS)personnel.
                                                                                                        ~
LISpersonnel measuredtheamountofpipecross-section andweldmetalremaining, andNESpersonnel determined thattherewasamplemetalintheaffectedareatoprovidesystemintegrity.
estimated to be approximately one (1) gallon per hour (GPH).
Thesourceoftheleakwasidentified asasmallpinholeleakonapipe-to-90 degreeforgedsocketelbowweldonatwo(2)inchnominalpipesizeSchedule10stainless steeltestlinefortheCSsystem.TheleakwasinapartoftheCSsystemthatcouldnotbeisolatedfromtheRWSTbyvalvemanipulations withoutmakingbothtrainsoftheemergency corecoolingsystem(ECCS)inoperable.
The Control Room operators did not identify any requirement that would limit plant operations. The Shift Supervisor notified Operations management, maintenance management, and plant and NES staff of the leak. All reached a similar conclusion. The staff worked on developing and implementing an action plan to address the problem. The issues of line integrity and RWST operability were investigated by NES and Laboratory Inspection Services (LIS) personnel. LIS personnel measured the amount of pipe cross-section and weld metal remaining, and NES personnel determined that there was ample metal in the affected area to provide system integrity.
Theleakwasmonitored throughout theremainder ofthedayandnight.Anoperability assessment hadbeenrequested bytheShiftSupervisor onJuly22,whentheexistence oftheleakhadfirstbeenidentified.
The source of the leak was identified as a small pinhole leak on a pipe-to-90 degree forged socket elbow weld on a two (2) inch nominal pipe size Schedule 10 stainless steel test line for the CS system. The leak was in a part of the CS system that could not be isolated from the RWST by valve manipulations without making both trains of the emergency core cooling system (ECCS) inoperable. The leak was monitored throughout the remainder of the day and night.
OnthemorningofJuly23,1996,thisassessment wasreviewedbythePlantOperations ReviewCommittee (PORC)~Thisassessment, whichwasbasedonconservative assumptions, concluded thattheRWSTandECCSwerestilloperablewiththeunisolated leak.Thisconclusion wassupported bythefactthattherewasstillamplemetalareainthecross-section thatcouldprovideintegrity ofthepipeduringaseismiceventandthatthetotalcombinedstresswaslessthantheyieldstrengthofthematerial.
An operability assessment had been requested by the Shift Supervisor on July 22, when the existence of the leak had first been identified. On the morning of July 23, 1996, this assessment was reviewed by the Plant Operations Review Committee (PORC)                 ~ This assessment, which was based on conservative assumptions, concluded that the RWST and ECCS were still operable with the unisolated leak. This conclusion was supported by the fact that there was still ample metal area in the cross-section that could provide integrity of the pipe during a seismic event and that the total combined stress was less than the yield strength of the material.
PORCrequested amoreaccurateestimateoftheleakrate.Theleakratewasmeasuredandestimated tobe2.6GPH.Thisleakrateisinexcessoftwo(2)GPH,whichisspecified inSurveillance TestProcedure PT-39,"LeakageEvaluation ofPrimaryCoolantSourcesOutsideContainment",
PORC requested a more accurate estimate of the leak rate. The leak rate was measured and estimated to be 2.6 GPH. This leak rate is in excess of two (2) GPH, which is specified in Surveillance Test Procedure PT-39, "Leakage Evaluation of Primary Coolant Sources Outside Containment", as the program limit for the maximum integrated leak rate outside CNMT from these sources. Since the leak rate exceeded the requirements of procedure PT-39, it was initially judged to be a violation of the "Primary Coolant Sources Outside Containment Program", as specified in the Ginna Station Improved Technical Specifications (ITS)
astheprogramlimitforthemaximumintegrated leakrateoutsideCNMTfromthesesources.Sincetheleakrateexceededtherequirements ofprocedure PT-39,itwasinitially judgedtobeaviolation ofthe"PrimaryCoolantSourcesOutsideContainment Program",
Section 5.5.2. The PORC chairman directed the Shift Supervisor to enter ITS Limiting Condition for Operation (LCO) 3.0.3, based on the conservative requirements of procedure PT-39 and Administrative Procedure A-52.4, "Control of Limiting Conditions for Operating Equipment", even though the plant was in compliance with all ITS LCOs.
asspecified intheGinnaStationImprovedTechnical Specifications (ITS)Section5.5.2.ThePORCchairmandirectedtheShiftSupervisor toenterITSLimitingCondition forOperation (LCO)3.0.3,basedontheconservative requirements ofprocedure PT-39andAdministrative Procedure A-52.4,"ControlofLimitingConditions forOperating Equipment",
NAC FOAM 356A I4-95)
eventhoughtheplantwasincompliance withallITSLCOs.NACFOAM356AI4-95)
NRCFORM366A(4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)DOCKETLERNUMBER(6)PAGE(3)R.E.GinnaNuclearPowerPlant05000244YEARSEQUENTIAL REVISIONNUMBERNUMBER3OF796-009-02TEXTiifmorespaceisrequired, useaddiu'onal copiesofNRCForm366AJ(17)DESCRIPTION OFEVENT:A.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES:
oJuly22,1996,1130EDST:Aleakisidentified onalineoutsideofContainment.
July23,1996,0857EDST:EventDateandTimeandDiscovery DateandTime.July23,1996,0900EDST:Loadreduction isstarted.July23,1996,1440EDST:Integrated leakageoutsideContainment isdetermined tobelessthantwoGPH.Loadreduction isstopped.B.EVENT:OnJuly23,1996,atapproximately 0857EDST,withtheplantinMode1atapproximately 100%steadystatereactorpower,thePlantOperations ReviewCommittee (PORC)conservatively directedtheShiftSupervisor toenterITSLCO3.0.3.:TheShiftSupervisor directedtheControlRoomoperators toinitiateaplantshutdown.
Atapproximately 0900EDST,theControlRoomoperators initiated aplantshutdownperNormalOperating Procedure 0-2,1,"NormalShutdowntoHotShutdown".
TheMechanical Supportgroupinitiated actionstoprovideafreezesealtoisolatethesourceofleakagefromtheRWST.Afreezesealwasinitiated betweentheleakingsocketandtheCSpumpsuctionlinefromtheRWST.Atapproximately 1440EDSTonJuly23,1996,thefreezesealhadisolatedtheleak.ITSLCO3.0.3wasexitedandtheloadreduction wasstopped.Theaffectedpipeandsocketweldswerecutoutandanewprefabricated spoolpiece wasinstalled.
Theaffectedweldwasretainedforfailuremodeanalysis.
Aloadincreasetoreturntheplanttofullpowerwasinitiated atapproximateiy 1530EDSTonJuly23,1996.C.INOPERABLE STRUCTURES, COMPONENTS, ORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARY FUNCTIONS AFFECTED'ue tothelocationandsizeoftheleak,anoperability assessment determined thatnoemergency safeguards systemfunctionwasmadeinoperable.
However,theleakwasnotisolablefromtheRWSTwithoutvalvemanipulations thatwouldhaveresultedintheinoperability oftheRWSTandbothtrainsoftheECCS.NACFOAM366A(4-95)  


NRCFORM366A(4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-009-02PAGE(3)4OF7TEXTiifmorespaceisrequired, useedditionalcopiesofNRCForm368A)(17)E.METHODOFDISCOVERY:
NRC FORM 366A                                                                                        U.S. NUCLEAR REGULATORY COMMISSION (4-95)
Theleakwasfirstdiscovered byanRPtechnician duringaroutineweeklysurveyoftheAuxiliary Building.
LICENSEE EVENT REPORT (LER)
'enotifiedtheControlRoomoperators, andthepreciselocationwasconfirmed byOperations andEngineering.
TEXT CONTINUATION FACILITY NAME (1)                                 DOCKET                      LER NUMBER (6)           PAGE (3)
Confirmation thattheleakratewasabove2GPHoccurredaftermeasurements performed atthedirection ofPORC.OPERATORACTION:WhennotifiedbyPORC,theShiftSupervisor directedtheControlRoomoperators toenterITSLCO3.0.3andtoinitiateaplantshutdown.
YEAR    SEQUENTIAL REVISION NUMBER      NUMBER 3 OF    7 R.E. Ginna Nuclear Power Plant                                  05000244                96      009          02 TEXT iifmore spaceis required, use addiu'onal copies of NRC Form 366A J (17)
'heControlRoomoperators initiated aplantshutdownperprocedure 0-2.1.TheShiftSupervisor subsequently notifiedtheNRCper10CFR50.72(b)(1)(i)(A),non-emergency onehournotification, atapproximately 0951EDSTonJuly23,1996.Whentheleakwasisolated, ITSLCO3.0.3wasexited,andtheplantwasreturnedtofullpower.G.SAFETYSYSTEMRESPONSES:
DESCRIPTION OF EVENT:
NoneIII.CAUSEOFEVENT:A.IMMEDIATE CAUSE:Theimmediate causeofthecondition prohibited byTechnical Specifications wastheconservative determination byPORCtoenterITSLCO3.0.3duetotheteak.B.INTERMEDIATE CAUSE:Theintermediate causeoftheleakwasapinholeleakintheweldattaching thepipetothesocketelbow.C.ROOTCAUSE:Theaffectedpipe,socket,andfilletweldwereanalyzedforthefailuremode.Thepinholewasdetermined tobeanoriginalinstallation welddefect(datingfromthe1960's)thatexistedoveranareaofslaginclusion intheweld.Almostalltheslaghadbeenleachedfromthepinholechanneloverthe'ast25years.NACFOAM366A(4.95)  
A.      DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
o        July 22, 1996, 1130 EDST: A leak is identified on                  a line outside of Containment.
July 23, 1996, 0857 EDST: Event Date and Time and Discovery Date and Time.
July 23, 1996, 0900 EDST: Load reduction is started.
July 23, 1996, 1440 EDST: Integrated leakage outside Containment is determined to be less than two GPH. Load reduction is stopped.
B.       EVENT:
On July 23, 1996, at approximately 0857 EDST, with the plant in Mode                      1 at approximately 100%
steady    state  reactor    power,   the  Plant  Operations          Review  Committee    (PORC) conservatively directed the Shift Supervisor to enter ITS LCO 3.0.3.: The Shift Supervisor directed the Control Room operators to initiate a plant shutdown. At approximately 0900 EDST, the Control Room operators initiated a plant shutdown per Normal Operating Procedure 0-2,1, "Normal Shutdown to Hot Shutdown".
The Mechanical Support group initiated actions to provide a freeze seal to isolate the source of leakage from the RWST. A freeze seal was initiated between the leaking socket and the CS pump suction line from the RWST. At approximately 1440 EDST on July 23, 1996, the freeze seal had isolated the leak. ITS LCO 3.0.3 was exited and the load reduction was stopped. The affected pipe and socket welds were cut out and a new prefabricated spoolpiece was installed. The affected weld was retained for failure mode analysis.
A load increase to return the plant to full power was initiated at approximateiy 1530 EDST on July 23, 1996.
C.       INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None D.       OTHER SYSTEMS OR SECONDARY FUNCTIONS                      AFFECTED'ue to the location and size of the leak, an operability assessment determined that no emergency safeguards system function was made inoperable. However, the leak was not isolable from the RWST without valve manipulations that would have resulted in the inoperability of the RWST and both trains of the ECCS.
NAC FOAM 366A (4-95)


NRCFORM366A(4-95)LXCENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)DOCKETLERNUMBER(6)PAGE(3)R.E.GinnaNuclearPowerPlant05000244YEARSEQUENTIAL REVISIONNUMBERNUMBER5OF796-'-009-02TEXTilfmorespeceisrequired, useedditionel copiesofNRCForm366AJ(17)ThiseventisNUREG-1022 CauseCode(B),"Design,Manufacturing, Construction
NRC FORM 366A                                                                              U.S. NUCLEAR REGULATORY COMMISSION (4-95)
/Installation".
LICENSEE EVENT REPORT (LER)
ThesmallpinholeleakdoesnotmeettheNUMARC93-01,"Industry Guideline forMonitoring theEffectiveness ofMaintenance atNuclearPowerPlants",definition ofa"Maintenance Preventable Functional Failure"~IV.ANALYSISOFEVENT:Thiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications".
TEXT CONTINUATION FACILITY NAME (1)                                 DOCKET          LER NUMBER (6)         PAGE (3)
Theintegrated leakrateinexcessof2GPHoutsideCNMTresultedinconservative entryintoITSLCO3.0.3.ITSLCO3.0.3isonlyapplicable torequirements contained inChapter3oftheITS.Therewasnolicenserequirement forentryintoITSLCO3.0.3.Nevertheless, sincetheplantvoluntarily enteredITSLCO3.0.3,thiscondition isreportable.
YEAR  SEQUENTIAL REVISION NUMBER    NUMBER 4 OF    7 R.E. Ginna Nuclear Power Plant                                  05000244      96  009           02 TEXT iifmore space is required, use eddi tional copies of NRC Form 368A) (17)
Anassessment wasperformed considering boththesafetyconsequences andimplications ofthisevent.Thefollowing aretheresultsandconclusions ofthisassessment:
E.       METHOD OF DISCOVERY:
Therewerenooperational orsafetyconsequences orimplications attributed totheleakontheCStestlinebecause:Almostalltheslaghadbeenleachedfromthepinholechannelandtherewasnosignofcorrosion orstress(cracking) attackofthestainless steelmaterialadjacenttothepinhole.Sincethepinholedidnotdegradethecross-sectional areaoftheforgedsocketelbowandpipe,thestressesonthislinedue.totheconcurrent loadsofdeadweight,
Building.  'e The leak was first discovered by an RP technician during a routine weekly survey of the Auxiliary notified the Control Room operators, and the precise location was confirmed by Operations and Engineering. Confirmation that the leak rate was above 2 GPH occurred after measurements performed at the direction of PORC.
: pressure, seismic,andthermaleffectswerestillwithinthecodelimit.Seismicintegrity wasnotthreatened bytheleaknorbytheinstallation ofthefreezeseal.Thenatureofthisleakmechanism wouldnotleadtoanincreaseinholesizeabovethatinitially identified.
OPERATOR ACTION:
Thelinecontaining theaffectedelbowexperiences flowfromtheRefueling WaterStorageTank(RWST)totheContainment Spray(CS)eductorsuctionvalvesduringperiodicsurveillance testingandisnotsubjected toanyappreciable dynamicstressesduringtesting,norwoulditbeexpectedtoduringpost-accident operation oftheCSorsafetyinjection.
When notified by PORC, the Shift Supervisor directed the Control Room operators to enter ITS LCO 3.0.3 and to initiate a plant shutdown.              'he  Control Room operators initiated a plant shutdown per procedure 0-2.1.
Theoffsiteexposureduetoalargebreaklossofcoolantaccident(LOCA)isanalyzedintheGinnaStationUpdatedFinalSafetyAnalysisReport(UFSAR).Thesubjectleaklocationisexposedtoradioactive sumpfluidfollowing 6smallorlargebreakLOCAduringrecirculation.
The Shift Supervisor subsequently notified the NRC per 10 CFR 50.72 (b) (1) (i) (A), non-emergency one hour notification, at approximately 0951 EDST on July 23, 1996. When the leak was isolated, ITS LCO 3.0.3 was exited, and the plant was returned to full power.
NRCFORM366A(4-95)  
G.       SAFETY SYSTEM RESPONSES:
None III. CAUSE OF EVENT:
A.       IMMEDIATECAUSE:
The immediate cause of the condition prohibited by Technical Specifications was the conservative determination by PORC to enter ITS LCO 3.0.3 due to the teak.
B.       INTERMEDIATE CAUSE:
The intermediate cause of the leak was a pinhole leak in the weld attaching the pipe to the socket elbow.
C.       ROOT CAUSE:
The affected pipe, socket, and fillet weld were analyzed for the failure mode. The pinhole was determined to be an original installation weld defect (dating from the 1960's) that existed over an area of slag inclusion in the weld. Almost all the slag had been leached from the pinhole channel over the'ast 25 years.
NAC FOAM 366A (4.95)


NRCrORM366A(4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-009-02PAGE(3)6OF7TEXTlifmorespaceisrequired, useadditional copiesofNRCForm386A/(17)Recentanalyseshavebeenperformed byWestinghouse torecalculate siteboundaryandcontrolroomdosesfromalargebreakLOCA,whichisthemostlimitingLOCAsizefordoseevaluations.
NRC FORM 366A                                                                              U.S. NUCLEAR REGULATORY COMMISSION (4-95)
Withanassumedrecirculation leakrateof2.75GPH,itwasdetermined thatthesiteboundaryandlowpopulation zonethyroidandwholebodydosesresulting fromthepostulated largebreakLOCAarewithinthe10CFR100doseguidelines of300REMthyroidand25REMwholebody,respectively.
LXCENSEE EVENT REPORT              (LER)
TheControlRoomdosecalculations resultinaControlRoomthyroid,wholebodyandbetaskindosewithinthedoselimitsdefinedintheNRCStandardReviewPlan(SRP)Section6.4,whichare30REMthyroid,5REIVIwholebodyand30REMbetaskin.Thesecalculated dosesarealsowithinthedosevaluesstatedintheUFSAR.Basedontheabove,it'canbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVE ACTION:A.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:0ThesourceoftheleakagewasisolatedfromtheRWSTbyfreezeseal,permitting exitfromITSLCO3.0.3.0Theaffectedpipeandsocketweldswerecutoutandreplacedwithanewprefabricated spoolpiece, andthefreezesealwasremoved.B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:
TEXT CONTINUATION FACILITY NAME (1)                                DOCKET                LER NUMBER (6)            PAGE (3)
0FailureAnalysisoftheleakinthesocketweldhasbeenperformed.
YEAR    SEQUENTIAL REVISION NUMBER      NUMBER 5  OF    7 R.E. Ginna Nuclear Power Plant                                05000244      96    -'-  009        02 TEXT ilfmore speceis required, use edditionel copies of NRC Form 366AJ (17)
Theadjacentoriginalexistingweldswerecutoutandreplaced, Additional corrective actionsareidentified inthissupplement andarelistedbelow:ThebasesforITSLCO3.6.1,"Containment",
This event is NUREG-1022 Cause Code (B), "Design, Manufacturing, Construction / Installation".
hasbeenrevisedtospecifythenewleakagelimitof2.75GPHforintegrated leakageoutsideCNMTfromtheresidualheatremoval(RHR),safetyinjection (Sl),andCSsystems,andtoconsidertheeffectofthisleakageonCNMToperabiity.
The small pinhole leak does not meet the NUMARC 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a "Maintenance Preventable Functional Failure"    ~
2.TheprogramlimitforleakageoutsideCNMT,asstatedinprocedure PT-39,wasrevisedfrom2.0GPHto2.75GPH,toreflectthesenewleakagelimits.3.Procedure A-52Awasrevisedtoreflectthenewprogramlimit:theintegrated leakagemustbe<I=2.75GPHasdetermined byPT-39.Theconservative requirement toenterITSLCO3.0.3forleakageabovethislimitwaseliminated.
IV. ANALYSIS OF EVENT:
NACFOAM366A(4-95)
This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i)
NRCFORM366AI4.95)LXCENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME<1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-009-02PAGEI3)7OF7TEXTllfmorespaceisrequired, useadditional copiesofNRCForm866AJl17)Vl.ADDITIONAL INFORMATION:
(B), "Any operation or condition prohibited by the plant's Technical Specifications". The integrated leak rate in excess of 2 GPH outside CNMT resulted in conservative entry into ITS LCO 3.0.3. ITS LCO 3.0.3 is only applicable to requirements contained in Chapter 3 of the ITS. There was no license requirement for entry into ITS LCO 3.0.3. Nevertheless, since the plant voluntarily entered ITS LCO 3.0.3, this condition is reportable.
A.FAILEDCOMPONENTS:
An assessment was performed considering both the safety consequences                  and implications of this event.
Thefailedcomponent wasa2inchnominalpipesizeSchedule10pipe-to-90 degreeforgedsocketelbowweld.Thepipeandsocketelbowarestainless steel,ASTMA312Type304andA182F304(forged)respectively.
The following are the results and conclusions of this assessment:
Thesocketweldwasanoriginalinstallation weldmadebefore1970.B.PREVIOUSLERsONSIIVIILAR EVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.
There were no operational or safety consequences          or implications attributed to the leak on the CS test line because:
C.SPECIALCOMMENTS:
Almost all the slag had been leached from the pinhole channel and there was no sign of corrosion or stress (cracking) attack of the stainless steel material adjacent to the pinhole.
NoneNRCFORM366AI4.95)
Since the pinhole did not degrade the cross-sectional area of the forged socket elbow and pipe, the stresses on this line due.to the concurrent loads of deadweight, pressure, seismic, and thermal effects were still within the code limit. Seismic integrity was not threatened by the leak nor by the installation of the freeze seal.
I1}}
The nature of this leak mechanism would not lead to an increase in hole size above that initially identified.
The line containing the affected elbow experiences flow from the Refueling Water Storage Tank (RWST) to the Containment Spray (CS) eductor suction valves during periodic surveillance testing and is not subjected to any appreciable dynamic stresses during testing, nor would it be expected to during post-accident operation of the CS or safety injection.
The offsite exposure due to a large break loss of coolant accident (LOCA) is analyzed in the Ginna Station Updated Final Safety Analysis Report (UFSAR). The subject leak location is exposed to radioactive sump fluid following 6 small or large break LOCA during recirculation.
NRC FORM 366A (4-95)
 
NRC rORM 366A                                                                              U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)                                 DOCKET          LER NUMBER (6)           PAGE (3)
YEAR  SEQUENTIAL REVISION NUMBER    NUMBER 6  OF    7 R.E. Ginna Nuclear Power Plant                                    05000244    96    009          02 TEXT lifmore space  is required, use additional copies of NRC Form 386A/ (17)
Recent analyses have been performed by Westinghouse to recalculate site boundary and control room doses from a large break LOCA, which is the most limiting LOCA size for dose evaluations. With an assumed recirculation leak rate of 2.75 GPH, it was determined that the site boundary and low population zone thyroid and whole body doses resulting from the postulated large break LOCA are within the 10 CFR 100 dose guidelines of 300 REM thyroid and 25 REM whole body, respectively. The Control Room dose calculations result in a Control Room thyroid, whole body and beta skin dose within the dose limits defined in the NRC Standard Review Plan (SRP) Section 6.4, which are 30 REM thyroid, 5 REIVI whole body and 30 REM beta skin. These calculated doses are also within the dose values stated in the UFSAR.
Based on the above, it'can be concluded that the public's health and safety was assured at all times.
V. CORRECTIVE ACTION:
A.         ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
0        The source of the leakage was isolated from the RWST by freeze seal, permitting exit from ITS LCO 3.0.3.
0        The affected pipe and socket welds were cut out and replaced with a new prefabricated spoolpiece, and the freeze seal was removed.
B.         ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
Failure Analysis of the leak in the socket weld has been performed.
The adjacent original existing welds were cut out and replaced, 0        Additional corrective actions are identified in this supplement and are listed below:
The bases for ITS LCO 3.6.1, "Containment", has been revised to specify the new leakage limit of 2.75 GPH for integrated leakage outside CNMT from the residual heat removal (RHR), safety injection (Sl), and CS systems, and to consider the effect of this leakage on CNMT operabiity.
: 2.       The program limit for leakage outside CNMT, as stated in procedure PT-39, was revised from 2.0 GPH to 2.75 GPH, to reflect these new leakage limits.
: 3.       Procedure A-52A was revised to reflect the new program limit: the integrated leakage must be <I= 2.75 GPH as determined by PT-39. The conservative requirement to enter ITS LCO 3.0.3 for leakage above this limit was eliminated.
NAC FOAM 366A (4-95)
 
NRC FORM 366A                                                                            U.S. NUCLEAR REGULATORY COMMISSION I4.95)
LXCENSEE EVENT REPORT              (LER)
TEXT CONTINUATION FACILITY NAME <1)                                 DOCKET          LER NUMBER I6)          PAGE I3)
YEAR  SEQUENTIAL REVISION NUMBER    NUMBER 7 OF    7 R.E. Ginna Nuclear Power Plant                                  05000244    96    009           02 TEXT llfmore spaceis required, use additional copies of NRC Form 866AJ l17)
Vl. ADDITIONALINFORMATION:
A.       FAILED COMPONENTS:
The failed component was a 2 inch nominal pipe size Schedule 10 pipe-to-90 degree forged socket elbow weld. The pipe and socket elbow are stainless steel, ASTM A312 Type 304 and A182 F304 (forged) respectively. The socket weld was an original installation weld made before 1970.
B.       PREVIOUS LERs ON SIIVIILAR EVENTS:
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.
C.       SPECIAL COMMENTS:
None NRC FORM 366A I4.95)
 
I 1}}

Latest revision as of 17:56, 29 October 2019

LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe
ML17264A991
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/11/1997
From: St Martin J
ROCHESTER GAS & ELECTRIC CORP.
To:
Shared Package
ML17264A990 List:
References
LER-96-009, LER-96-9, NUDOCS 9708180050
Download: ML17264A991 (12)


Text

NRC RORM 366 U.S. NUCLEAR REGULATORY COMMISSIO APPROVED BY OMB NO. 3150-0104 (4-95) 'XPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.

LICENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK To INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE

.(See reverse for required number of INFORMATION AND RECORDS MANAGEMENT BRANCH IT-6 F33),

digits/characters for each block) U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, Dc 20555-0001, AND To THE PAPERWORK REDUCTION PROJECT FACILITYNAME (1) DOCKET NUMBER(2) PAGE (3)

R.E. Ginna Nuclear Power Plant 05000244 1OF7 TITLE (4)

Leak Outside Containment, Due to Weld Defect, Results in Leak Rate Greater Than Program Limit EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (6)

FACILITYNAME DOCKET NUMBER SEQUENT)AL REVISION MONTH DAY YEAR NUMBER MONTH DAY YEAR NUMBER FACILITY NAME DOCKET NUMBER 07 23 96 96 009 02 08 11 97 OPERATING THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR E: (Chack one or more) (11)

MODE (9) 20.2201(b) 20.2203(a) (2)(v) 50.73(a) (2) (i) 50.73(a)(2)(viii)

POWER 20.2203(a)(1) 20.2203(a) (3)(i) 50.73(a)(2) (ii) 50.73(a)(2)(x)

LEVEL (10) 100 20.2203(a) (2) (i) 20.2203(a)(3)(ii) 50.73(a) (2)(iii) 73.71 20.2203(a) (2) (ii) 20.2203(a)(4) 50.73(a) (2) (iv) OTHER 20.2203(a)(2)(iii) 50.36(c) (1) 50.73(a)(2)(v) Specify In Abet(ect below or in NRC Form 365A 20.2203(a)(2)(iv) 50.36(c) (2) 50.73(a) (2)(vii)

LICENSEE CONTACT FOR THIS LER (12)

TELEPHONE NUMBER (lne)ude Afee Code)

John T. St. Martin - Technical Assistant (716) 771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

SYSTEM COMPONENT REPORTABLE REPORTABLE CAUSE MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER To NPRDS To NPRDS B BE PSF 0000 N

t~g
~i'~c)NI."i?';.:

SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED YES SUBMISSION (If yas, complete EXPECTED SUBMISSION DATE). X NO DATE (16)

ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)

On July 23, 1996, at approximately 0857 EDST, it was determined that the leak rate (from a leak on a piping system outside Containment) was greater than the analyzed value of two gallons per hour for a primary coolant source outside Containment.

Immediate corrective action was to conservatively enter Technical Specification Limiting Condition for Operation 3.0.3 and initiate a plant shutdown, and to initiate actions to isolate the leak using a freeze seal. Once the leak was isolated, the plant exited Technical Specification 3.0.3 and the shutdown was stopped. The leaking pipe was cut out and replaced.

The underlying cause of the leak was a weld defect which dates back to original construction in the 1960's.

This event is NUREG-1022 Cause Code (B).

Corrective action to prevent recurrence is outlined in Section V.B. Additional corrective actions are identified in this supplement.

9708i80050 9708ii PDR ADOCK 05000244 8 ,PDR

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4.95)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME I1) DOCKET LER NUMBER Ie) PAGE I3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 2 OF 7 R.E. Ginna Nuclear Power Plant 05000244 96 009 02 TEXT (II more space is required, use additional copies of NRC Form 366AJ (17)

I. PRE-EVENT PLANT CONDITIONS:

On July 22, 1996, the plant was in Mode 1 at approximately 100% steady state reactor power. At approximately 1130 EDST, a Radiation Protection (RP) technician, who was performing a routine weekly surve'y of the Auxiliary Building, observed water dripping in an area behind the Refueling Water Storage Tank (RWST). The RP technician notified the Control Room operators. Efforts to locate the source of the dripping water and to quantify the leak rate were initiated by Operations and Nuclear Engineering Services (NES). The source of water was determined to be a small leak on a test line for the Containment Spray (CS) system in the Auxiliary Building, which is outside the Containment (CNMT) The leak rate was

~

estimated to be approximately one (1) gallon per hour (GPH).

The Control Room operators did not identify any requirement that would limit plant operations. The Shift Supervisor notified Operations management, maintenance management, and plant and NES staff of the leak. All reached a similar conclusion. The staff worked on developing and implementing an action plan to address the problem. The issues of line integrity and RWST operability were investigated by NES and Laboratory Inspection Services (LIS) personnel. LIS personnel measured the amount of pipe cross-section and weld metal remaining, and NES personnel determined that there was ample metal in the affected area to provide system integrity.

The source of the leak was identified as a small pinhole leak on a pipe-to-90 degree forged socket elbow weld on a two (2) inch nominal pipe size Schedule 10 stainless steel test line for the CS system. The leak was in a part of the CS system that could not be isolated from the RWST by valve manipulations without making both trains of the emergency core cooling system (ECCS) inoperable. The leak was monitored throughout the remainder of the day and night.

An operability assessment had been requested by the Shift Supervisor on July 22, when the existence of the leak had first been identified. On the morning of July 23, 1996, this assessment was reviewed by the Plant Operations Review Committee (PORC) ~ This assessment, which was based on conservative assumptions, concluded that the RWST and ECCS were still operable with the unisolated leak. This conclusion was supported by the fact that there was still ample metal area in the cross-section that could provide integrity of the pipe during a seismic event and that the total combined stress was less than the yield strength of the material.

PORC requested a more accurate estimate of the leak rate. The leak rate was measured and estimated to be 2.6 GPH. This leak rate is in excess of two (2) GPH, which is specified in Surveillance Test Procedure PT-39, "Leakage Evaluation of Primary Coolant Sources Outside Containment", as the program limit for the maximum integrated leak rate outside CNMT from these sources. Since the leak rate exceeded the requirements of procedure PT-39, it was initially judged to be a violation of the "Primary Coolant Sources Outside Containment Program", as specified in the Ginna Station Improved Technical Specifications (ITS)

Section 5.5.2. The PORC chairman directed the Shift Supervisor to enter ITS Limiting Condition for Operation (LCO) 3.0.3, based on the conservative requirements of procedure PT-39 and Administrative Procedure A-52.4, "Control of Limiting Conditions for Operating Equipment", even though the plant was in compliance with all ITS LCOs.

NAC FOAM 356A I4-95)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 3 OF 7 R.E. Ginna Nuclear Power Plant 05000244 96 009 02 TEXT iifmore spaceis required, use addiu'onal copies of NRC Form 366A J (17)

DESCRIPTION OF EVENT:

A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:

o July 22, 1996, 1130 EDST: A leak is identified on a line outside of Containment.

July 23, 1996, 0857 EDST: Event Date and Time and Discovery Date and Time.

July 23, 1996, 0900 EDST: Load reduction is started.

July 23, 1996, 1440 EDST: Integrated leakage outside Containment is determined to be less than two GPH. Load reduction is stopped.

B. EVENT:

On July 23, 1996, at approximately 0857 EDST, with the plant in Mode 1 at approximately 100%

steady state reactor power, the Plant Operations Review Committee (PORC) conservatively directed the Shift Supervisor to enter ITS LCO 3.0.3.: The Shift Supervisor directed the Control Room operators to initiate a plant shutdown. At approximately 0900 EDST, the Control Room operators initiated a plant shutdown per Normal Operating Procedure 0-2,1, "Normal Shutdown to Hot Shutdown".

The Mechanical Support group initiated actions to provide a freeze seal to isolate the source of leakage from the RWST. A freeze seal was initiated between the leaking socket and the CS pump suction line from the RWST. At approximately 1440 EDST on July 23, 1996, the freeze seal had isolated the leak. ITS LCO 3.0.3 was exited and the load reduction was stopped. The affected pipe and socket welds were cut out and a new prefabricated spoolpiece was installed. The affected weld was retained for failure mode analysis.

A load increase to return the plant to full power was initiated at approximateiy 1530 EDST on July 23, 1996.

C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED'ue to the location and size of the leak, an operability assessment determined that no emergency safeguards system function was made inoperable. However, the leak was not isolable from the RWST without valve manipulations that would have resulted in the inoperability of the RWST and both trains of the ECCS.

NAC FOAM 366A (4-95)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 4 OF 7 R.E. Ginna Nuclear Power Plant 05000244 96 009 02 TEXT iifmore space is required, use eddi tional copies of NRC Form 368A) (17)

E. METHOD OF DISCOVERY:

Building. 'e The leak was first discovered by an RP technician during a routine weekly survey of the Auxiliary notified the Control Room operators, and the precise location was confirmed by Operations and Engineering. Confirmation that the leak rate was above 2 GPH occurred after measurements performed at the direction of PORC.

OPERATOR ACTION:

When notified by PORC, the Shift Supervisor directed the Control Room operators to enter ITS LCO 3.0.3 and to initiate a plant shutdown. 'he Control Room operators initiated a plant shutdown per procedure 0-2.1.

The Shift Supervisor subsequently notified the NRC per 10 CFR 50.72 (b) (1) (i) (A), non-emergency one hour notification, at approximately 0951 EDST on July 23, 1996. When the leak was isolated, ITS LCO 3.0.3 was exited, and the plant was returned to full power.

G. SAFETY SYSTEM RESPONSES:

None III. CAUSE OF EVENT:

A. IMMEDIATECAUSE:

The immediate cause of the condition prohibited by Technical Specifications was the conservative determination by PORC to enter ITS LCO 3.0.3 due to the teak.

B. INTERMEDIATE CAUSE:

The intermediate cause of the leak was a pinhole leak in the weld attaching the pipe to the socket elbow.

C. ROOT CAUSE:

The affected pipe, socket, and fillet weld were analyzed for the failure mode. The pinhole was determined to be an original installation weld defect (dating from the 1960's) that existed over an area of slag inclusion in the weld. Almost all the slag had been leached from the pinhole channel over the'ast 25 years.

NAC FOAM 366A (4.95)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)

LXCENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 5 OF 7 R.E. Ginna Nuclear Power Plant 05000244 96 -'- 009 02 TEXT ilfmore speceis required, use edditionel copies of NRC Form 366AJ (17)

This event is NUREG-1022 Cause Code (B), "Design, Manufacturing, Construction / Installation".

The small pinhole leak does not meet the NUMARC 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a "Maintenance Preventable Functional Failure" ~

IV. ANALYSIS OF EVENT:

This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i)

(B), "Any operation or condition prohibited by the plant's Technical Specifications". The integrated leak rate in excess of 2 GPH outside CNMT resulted in conservative entry into ITS LCO 3.0.3. ITS LCO 3.0.3 is only applicable to requirements contained in Chapter 3 of the ITS. There was no license requirement for entry into ITS LCO 3.0.3. Nevertheless, since the plant voluntarily entered ITS LCO 3.0.3, this condition is reportable.

An assessment was performed considering both the safety consequences and implications of this event.

The following are the results and conclusions of this assessment:

There were no operational or safety consequences or implications attributed to the leak on the CS test line because:

Almost all the slag had been leached from the pinhole channel and there was no sign of corrosion or stress (cracking) attack of the stainless steel material adjacent to the pinhole.

Since the pinhole did not degrade the cross-sectional area of the forged socket elbow and pipe, the stresses on this line due.to the concurrent loads of deadweight, pressure, seismic, and thermal effects were still within the code limit. Seismic integrity was not threatened by the leak nor by the installation of the freeze seal.

The nature of this leak mechanism would not lead to an increase in hole size above that initially identified.

The line containing the affected elbow experiences flow from the Refueling Water Storage Tank (RWST) to the Containment Spray (CS) eductor suction valves during periodic surveillance testing and is not subjected to any appreciable dynamic stresses during testing, nor would it be expected to during post-accident operation of the CS or safety injection.

The offsite exposure due to a large break loss of coolant accident (LOCA) is analyzed in the Ginna Station Updated Final Safety Analysis Report (UFSAR). The subject leak location is exposed to radioactive sump fluid following 6 small or large break LOCA during recirculation.

NRC FORM 366A (4-95)

NRC rORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 6 OF 7 R.E. Ginna Nuclear Power Plant 05000244 96 009 02 TEXT lifmore space is required, use additional copies of NRC Form 386A/ (17)

Recent analyses have been performed by Westinghouse to recalculate site boundary and control room doses from a large break LOCA, which is the most limiting LOCA size for dose evaluations. With an assumed recirculation leak rate of 2.75 GPH, it was determined that the site boundary and low population zone thyroid and whole body doses resulting from the postulated large break LOCA are within the 10 CFR 100 dose guidelines of 300 REM thyroid and 25 REM whole body, respectively. The Control Room dose calculations result in a Control Room thyroid, whole body and beta skin dose within the dose limits defined in the NRC Standard Review Plan (SRP) Section 6.4, which are 30 REM thyroid, 5 REIVI whole body and 30 REM beta skin. These calculated doses are also within the dose values stated in the UFSAR.

Based on the above, it'can be concluded that the public's health and safety was assured at all times.

V. CORRECTIVE ACTION:

A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:

0 The source of the leakage was isolated from the RWST by freeze seal, permitting exit from ITS LCO 3.0.3.

0 The affected pipe and socket welds were cut out and replaced with a new prefabricated spoolpiece, and the freeze seal was removed.

B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

Failure Analysis of the leak in the socket weld has been performed.

The adjacent original existing welds were cut out and replaced, 0 Additional corrective actions are identified in this supplement and are listed below:

The bases for ITS LCO 3.6.1, "Containment", has been revised to specify the new leakage limit of 2.75 GPH for integrated leakage outside CNMT from the residual heat removal (RHR), safety injection (Sl), and CS systems, and to consider the effect of this leakage on CNMT operabiity.

2. The program limit for leakage outside CNMT, as stated in procedure PT-39, was revised from 2.0 GPH to 2.75 GPH, to reflect these new leakage limits.
3. Procedure A-52A was revised to reflect the new program limit: the integrated leakage must be <I= 2.75 GPH as determined by PT-39. The conservative requirement to enter ITS LCO 3.0.3 for leakage above this limit was eliminated.

NAC FOAM 366A (4-95)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I4.95)

LXCENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME <1) DOCKET LER NUMBER I6) PAGE I3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER 7 OF 7 R.E. Ginna Nuclear Power Plant 05000244 96 009 02 TEXT llfmore spaceis required, use additional copies of NRC Form 866AJ l17)

Vl. ADDITIONALINFORMATION:

A. FAILED COMPONENTS:

The failed component was a 2 inch nominal pipe size Schedule 10 pipe-to-90 degree forged socket elbow weld. The pipe and socket elbow are stainless steel, ASTM A312 Type 304 and A182 F304 (forged) respectively. The socket weld was an original installation weld made before 1970.

B. PREVIOUS LERs ON SIIVIILAR EVENTS:

A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.

C. SPECIAL COMMENTS:

None NRC FORM 366A I4.95)

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