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Category:Letter type:ULNRC
MONTHYEARULNRC-06853, Submittal of 2023 Fitness for Duty Performance Data Per Per 10 CFR 26.7172024-01-29029 January 2024 Submittal of 2023 Fitness for Duty Performance Data Per Per 10 CFR 26.717 ULNRC-06847, Supplement to Relief Request from Requirements of ASME BPV Code, Section XI, Subsection Iwl Regarding Examination and Testing of the Unbonded Post-Tensioning System (Relief Request C3R-01)2023-12-21021 December 2023 Supplement to Relief Request from Requirements of ASME BPV Code, Section XI, Subsection Iwl Regarding Examination and Testing of the Unbonded Post-Tensioning System (Relief Request C3R-01) ULNRC-06849, License Renewal Resolution for Commitments 34 and 35 Perform Evaluation of Crack Initiation and Propagation in Steam Generator Divider Plate and Tube-To-Tubesheet Welds2023-12-20020 December 2023 License Renewal Resolution for Commitments 34 and 35 Perform Evaluation of Crack Initiation and Propagation in Steam Generator Divider Plate and Tube-To-Tubesheet Welds ULNRC-06844, Request for Exemption from Specific Requirements in 2023 Security Rule, Enhanced Weapons, Firearms Background Checks, and Security Event Notification2023-12-0707 December 2023 Request for Exemption from Specific Requirements in 2023 Security Rule, Enhanced Weapons, Firearms Background Checks, and Security Event Notification ULNRC-06827, Supplement to License Amendment Request Regarding Support System Requirements for Residual Heat Removal and Control Room Air Conditioning Systems Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029)2023-11-20020 November 2023 Supplement to License Amendment Request Regarding Support System Requirements for Residual Heat Removal and Control Room Air Conditioning Systems Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029) ULNRC-06824, Response to Request for Additional Information Regarding Operating Quality Assurance Manual (Oqam) Revision 36A2023-08-17017 August 2023 Response to Request for Additional Information Regarding Operating Quality Assurance Manual (Oqam) Revision 36A ULNRC-06830, Transmittal of Updated Technical Specification Markup and Clean Pages for License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak2023-08-15015 August 2023 Transmittal of Updated Technical Specification Markup and Clean Pages for License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak ULNRC-06223, Minor Correction to License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Test Frequencies (LDCN 2020-0004)2023-07-25025 July 2023 Minor Correction to License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Test Frequencies (LDCN 2020-0004) ULNRC-06799, Submittal of Licensee Event Report 2022-003-01, Class 1E Electrical Air Conditioning System Thermal Expansion Valve Failure Resulted in Condition Prohibited by Technical Specifications2023-07-13013 July 2023 Submittal of Licensee Event Report 2022-003-01, Class 1E Electrical Air Conditioning System Thermal Expansion Valve Failure Resulted in Condition Prohibited by Technical Specifications ULNRC-06821, Post-Audit Follow-Up Information in Support of Callaway'S License Amendment Request and Proposed Exemption to Allow Use of Framatome Gaia Fuel (LDCN 22-0002) (EPID L-2022-LLA-0150 and EPID L-2022-LLE-00301)2023-06-21021 June 2023 Post-Audit Follow-Up Information in Support of Callaway'S License Amendment Request and Proposed Exemption to Allow Use of Framatome Gaia Fuel (LDCN 22-0002) (EPID L-2022-LLA-0150 and EPID L-2022-LLE-00301) ULNRC-06822, Additional Information Regarding Request for NRC Approval of Operating Quality Assurance Manual (Oqam) Revision 36a2023-06-14014 June 2023 Additional Information Regarding Request for NRC Approval of Operating Quality Assurance Manual (Oqam) Revision 36a ULNRC-06815, Request for NRC Approval of Operating Quality Assurance Manual, Revision 36a2023-06-0505 June 2023 Request for NRC Approval of Operating Quality Assurance Manual, Revision 36a ULNRC-06818, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate .2023-06-0505 June 2023 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate . ULNRC-06816, Withdrawal of Previously Submitted Enclosures Regarding License Amendment Request for Adoption of Alternative Source Term and Revision of Technical Specifications (LDCN 21-0015)2023-05-0909 May 2023 Withdrawal of Previously Submitted Enclosures Regarding License Amendment Request for Adoption of Alternative Source Term and Revision of Technical Specifications (LDCN 21-0015) ULNRC-06812, Submittal of 2022 Annual Radiological Environmental Operating Report2023-04-27027 April 2023 Submittal of 2022 Annual Radiological Environmental Operating Report ULNRC-06806, Submittal of Radiological Emergency Response Plan, Revision 552023-04-12012 April 2023 Submittal of Radiological Emergency Response Plan, Revision 55 ULNRC-06807, Submittal of Single Positive Test Forms2023-04-0303 April 2023 Submittal of Single Positive Test Forms ULNRC-06798, Submittal of Status of Plant Decommissioning Funding and ISFSI Decommissioning Funding Plan2023-03-30030 March 2023 Submittal of Status of Plant Decommissioning Funding and ISFSI Decommissioning Funding Plan ULNRC-06801, CFR 50.46 Annual Report Regarding ECCS Evaluation Model Revisions2023-03-30030 March 2023 CFR 50.46 Annual Report Regarding ECCS Evaluation Model Revisions ULNRC-06804, Submittal of Nuclear Property Insurance Reporting2023-03-29029 March 2023 Submittal of Nuclear Property Insurance Reporting ULNRC-06751, Application to Revise Technical Specifications to Adopt TSTF-501-A, Rev. 1, Relocate Stored Oil & Lube Oil Volume Values to Licensee Control2023-03-29029 March 2023 Application to Revise Technical Specifications to Adopt TSTF-501-A, Rev. 1, Relocate Stored Oil & Lube Oil Volume Values to Licensee Control ULNRC-06803, Submittal of Response to Request for Additional Information Regarding Results of Steam Generator Tube In-Service Inspection2023-03-29029 March 2023 Submittal of Response to Request for Additional Information Regarding Results of Steam Generator Tube In-Service Inspection ULNRC-06805, Transmittal of Special Report 2023-02 Non-Functionality of Containment Hydrogen Analyzer Channel for Greater than 30 Days2023-03-21021 March 2023 Transmittal of Special Report 2023-02 Non-Functionality of Containment Hydrogen Analyzer Channel for Greater than 30 Days ULNRC-06802, Special Report 2023-01 (PAM Report); Non-Functionality of a Post-Accident Monitoring Instrument2023-03-0909 March 2023 Special Report 2023-01 (PAM Report); Non-Functionality of a Post-Accident Monitoring Instrument ULNRC-06795, Submittal of Fitness for Duty Reports for 2022, Including Single Positive Test Forms2023-01-24024 January 2023 Submittal of Fitness for Duty Reports for 2022, Including Single Positive Test Forms ULNRC-06794, Submittal of Fitness for Duty Program Data for 20222023-01-24024 January 2023 Submittal of Fitness for Duty Program Data for 2022 ULNRC-06787, Response to Request for Additional Information Regarding License Amendment Request for Adoption of Alternate Source Term and Revision of Technical Specifications (LDCN 21-0015)2022-12-0808 December 2022 Response to Request for Additional Information Regarding License Amendment Request for Adoption of Alternate Source Term and Revision of Technical Specifications (LDCN 21-0015) ULNRC-06781, License Amendment Request to Clarify Support System Requirements for the Residual Heat Removal System and Control Room Air Conditioning System Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029)2022-12-0101 December 2022 License Amendment Request to Clarify Support System Requirements for the Residual Heat Removal System and Control Room Air Conditioning System Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029) ULNRC-06780, Additional Supplement to License Amendment Request to Adopt TSTF-439 and TSTF-505, LDCN 20-0072022-11-30030 November 2022 Additional Supplement to License Amendment Request to Adopt TSTF-439 and TSTF-505, LDCN 20-007 ULNRC-06772, 10 CFR 50.59 and 10 CFR 72.48 Summary Report2022-11-23023 November 2022 10 CFR 50.59 and 10 CFR 72.48 Summary Report ULNRC-06777, Operating Quality Assurance Manual (Oqam) Revision 362022-11-16016 November 2022 Operating Quality Assurance Manual (Oqam) Revision 36 ULNRC-06779, ULNRC-06779: Contesting of Green NCV 05000483/2022010-03, Failure to Perform Required Inservice Testing of Residual Heat Removal Heat Exchanger Pneumatically (Air) Operated Outlet and Bypass Valves2022-11-14014 November 2022 ULNRC-06779: Contesting of Green NCV 05000483/2022010-03, Failure to Perform Required Inservice Testing of Residual Heat Removal Heat Exchanger Pneumatically (Air) Operated Outlet and Bypass Valves ULNRC-06765, License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Testing Frequencies (LDCN 2020-0004)2022-11-0303 November 2022 License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Testing Frequencies (LDCN 2020-0004) ULNRC-06773, Results of Steam Generator Tube In-Service Inspection2022-11-0101 November 2022 Results of Steam Generator Tube In-Service Inspection ULNRC-06775, Submittal of Non-Functionality of Loose-Part Detection System Channel for Greater than 30 Days2022-10-27027 October 2022 Submittal of Non-Functionality of Loose-Part Detection System Channel for Greater than 30 Days ULNRC-06771, Correction to Application to Revise Technical Specifications to Adopt TSTF 577, Revised Frequencies for Steam Generator Tube Inspections (LDCN 21-0013)2022-10-25025 October 2022 Correction to Application to Revise Technical Specifications to Adopt TSTF 577, Revised Frequencies for Steam Generator Tube Inspections (LDCN 21-0013) ULNRC-06770, Cycle 25 Commitment Change Summary Report2022-10-19019 October 2022 Cycle 25 Commitment Change Summary Report ULNRC-06766, Correction of Text Contained in Enclosures Provided with Supplements to Request for License Amendment and Regulatory Exemptions for a Risk-Informed Approach to Address GSI-191 and Respond to GL 2004-02 (LDCN 19-0014)2022-09-0808 September 2022 Correction of Text Contained in Enclosures Provided with Supplements to Request for License Amendment and Regulatory Exemptions for a Risk-Informed Approach to Address GSI-191 and Respond to GL 2004-02 (LDCN 19-0014) ULNRC-06767, Presentation Information for Pre-Application Meeting Regarding New License Amendment Request for Use of Framatome Fuel Assemblies2022-09-0606 September 2022 Presentation Information for Pre-Application Meeting Regarding New License Amendment Request for Use of Framatome Fuel Assemblies ULNRC-06764, Revised Response to Request for Additional Information Regarding License Amendment Request for Adoption Off Alternate Source Term and Revision of Technical Specifications (LDCN 21-0015)2022-09-0101 September 2022 Revised Response to Request for Additional Information Regarding License Amendment Request for Adoption Off Alternate Source Term and Revision of Technical Specifications (LDCN 21-0015) ULNRC-06763, Supplement to Application to Revise Technical Specifications to Adopt TSTF 577, Revised Frequencies for Steam Generator Tube Inspection (LDCN 21-0013)2022-09-0101 September 2022 Supplement to Application to Revise Technical Specifications to Adopt TSTF 577, Revised Frequencies for Steam Generator Tube Inspection (LDCN 21-0013) ULNRC-06762, Submittal of Owner'S Activity Reports (OAR-1 Forms) for Cycle/Refuel 252022-08-25025 August 2022 Submittal of Owner'S Activity Reports (OAR-1 Forms) for Cycle/Refuel 25 ULNRC-06758, Union Electric Co. - Renewed Facility Operating License NPF-30, Withdrawal of License Amendment Request and Exemption Request Regarding Transition to Framatome Fuel (LDCN 22-0002)2022-08-0404 August 2022 Union Electric Co. - Renewed Facility Operating License NPF-30, Withdrawal of License Amendment Request and Exemption Request Regarding Transition to Framatome Fuel (LDCN 22-0002) ULNRC-06755, Response to Requests for Additional Information for Proposed Revision to Radiological Emergency Response Plan Regarding Response and Notification Goals2022-07-13013 July 2022 Response to Requests for Additional Information for Proposed Revision to Radiological Emergency Response Plan Regarding Response and Notification Goals ULNRC-06754, Response to Request for Additional Information Regarding Licensee Amendment Request for Adoption of Alternate Source Term and Revision of Technical Specifications2022-07-0505 July 2022 Response to Request for Additional Information Regarding Licensee Amendment Request for Adoption of Alternate Source Term and Revision of Technical Specifications ULNRC-06739, Post-Audit Supplement to License Amendment Request to Adopt TSTF-439 and TSTF-505 (LDCN 20-0007)2022-06-30030 June 2022 Post-Audit Supplement to License Amendment Request to Adopt TSTF-439 and TSTF-505 (LDCN 20-0007) ULNRC-06752, Evacuation Time Estimates Report2022-06-27027 June 2022 Evacuation Time Estimates Report ULNRC-06753, Presentation Information for Pre-Submittal Meeting Regarding Updated Spent Fuel Criticality Safety Analysis2022-06-23023 June 2022 Presentation Information for Pre-Submittal Meeting Regarding Updated Spent Fuel Criticality Safety Analysis ULNRC-06750, Submittal of Cycle 26 Core Operating Limits Report (COLR)2022-06-13013 June 2022 Submittal of Cycle 26 Core Operating Limits Report (COLR) ULNRC-06735, Response to Request for Additional Information Regarding Request for License Amendment and Regulatory Exemptions for Risk-Informed Approach to Address GSI-191 and Respond to Generic Letter 2004-02 (LDCN 19-0014).2022-05-27027 May 2022 Response to Request for Additional Information Regarding Request for License Amendment and Regulatory Exemptions for Risk-Informed Approach to Address GSI-191 and Respond to Generic Letter 2004-02 (LDCN 19-0014). 2024-01-29
[Table view] Category:Licensee Response to Notice of Violation
MONTHYEARULNRC-06779, ULNRC-06779: Contesting of Green NCV 05000483/2022010-03, Failure to Perform Required Inservice Testing of Residual Heat Removal Heat Exchanger Pneumatically (Air) Operated Outlet and Bypass Valves2022-11-14014 November 2022 ULNRC-06779: Contesting of Green NCV 05000483/2022010-03, Failure to Perform Required Inservice Testing of Residual Heat Removal Heat Exchanger Pneumatically (Air) Operated Outlet and Bypass Valves ML22318A1892022-11-14014 November 2022 Enclosure 1 - Ameren Missouri'S Response to Green NCV 05000483/2022010-03 ULNRC-06493, Supplemental Response to Notice of Violation, Inspection Report No. 50-483/20160022019-04-11011 April 2019 Supplemental Response to Notice of Violation, Inspection Report No. 50-483/2016002 IR 05000483/20170072017-11-0101 November 2017 Reply to Notice of Violation 05000483/2017007-01 ULNRC-06394, Reply to Notice of Violation 05000483/2017007-012017-11-0101 November 2017 Reply to Notice of Violation 05000483/2017007-01 ULNRC-06378, Supplemental Response to Notice of Violation Inspection Report No. 50-483/20160022017-06-27027 June 2017 Supplemental Response to Notice of Violation Inspection Report No. 50-483/2016002 ULNRC-06365, Updated Response to Notice of Violation Inspection Report 50-483/20160022017-04-27027 April 2017 Updated Response to Notice of Violation Inspection Report 50-483/2016002 ULNRC-06326, Reply to a Notice of Violation Inspection Report 05000-483/20160022016-09-0909 September 2016 Reply to a Notice of Violation Inspection Report 05000-483/2016002 IR 05000483/20080032008-09-0404 September 2008 Reply to Notice of Violation: EA-08-190, Inspection Report No. 50-483/2008003 ULNRC-05528, Reply to Notice of Violation: EA-08-190, Inspection Report No. 50-483/20080032008-09-0404 September 2008 Reply to Notice of Violation: EA-08-190, Inspection Report No. 50-483/2008003 ML0608304122006-03-14014 March 2006 IR 05000483-05-005, Union Electric Co., Reply to Notice of Violation IR 05000483/20050052006-03-14014 March 2006 IR 05000483-05-005, Union Electric Co., Reply to Notice of Violation ML0535702612005-12-14014 December 2005 Reply to Inspection No 50-483/05-004 IR 05000483/20050042005-12-14014 December 2005 Callaway, Reply to Inspection No 50-483/05-004 ULNRC-04867, Reply to Notice of Violation Inspection Report No. 50-483/2003-0082003-07-21021 July 2003 Reply to Notice of Violation Inspection Report No. 50-483/2003-008 ULNRC-04848, Reply to Preliminary White Finding Regarding Inspection Report No. 50-483/2003-0082003-06-10010 June 2003 Reply to Preliminary White Finding Regarding Inspection Report No. 50-483/2003-008 ULNRC-04653, Reply to Notice of Violation for Inspection Report 50-483/2002-007, Enforcement Action EA-02-0462002-05-0808 May 2002 Reply to Notice of Violation for Inspection Report 50-483/2002-007, Enforcement Action EA-02-046 ML0202903752002-01-22022 January 2002 Response to Enforcement Action (EA-01-005) from Union Electric Co 2022-11-14
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Union Electric PO Box 620 CallawayPlant Fulton, MO 65251 May 8, 2002 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop P1-137 Washington, DC 20555-0001 ULNRC-04653 WAmeren Gentlemen:
UF REPLY TO NOTICE OF VIOLATION INSPECTION REPORT NO. 50-483/2002-007 ENFORCEMENT ACTION EA-02-046 CALLAWAY PLANT UNION ELECTRIC CO.
This responds to Mr. Ellis W. Merschoff's letter dated April 9, 2002, which transmitted a Notice of Violation for events discussed in Inspection Report 50-483/2002-007 and Enforcement Action EA-02-046. Our response to the violation is presented in the attachment.
New commitments are identified in this correspondence.
None of the material in the response is considered proprietary by Union Electric.
If you have any questions regarding this response, or if additional information is required, please let me know.
Very truly yours, Michael S. Evans Manager, Nuclear Engineering MSE/MAR/slk Attachments: 1) Response to Violation
- 2) List of Commitments a subsidiaryof Ameren Corporation
ULNRC-04653 May 8, 2002 Page 2 cc: Mr. Ellis W. Merschoff Regional Administrator U.S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011-8064 Senior Resident Inspector Callaway Resident Office U.S. Nuclear Regulatory Commission 8201 NRC Road Steedman, MO 65077 Mr. Jack N. Donohew (2 copies)
Licensing Project Manager, Callaway Plant Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Mail Stop 7E 1 Washington, DC 20555-2738 Manager, Electric Department Missouri Public Service Commission PO Box 360 Jefferson City, MO 65102 Superintendent, Licensing Wolf Creek Nuclear Operating Corporation PO Box 411 Burlington, KS 66839
ULNRC-04653 May 8, 2002 Page 3 Mr. Scott Bauer Regulatory Affairs Palo Verde Nuclear Generating Station Arizona Public Service Company PO Box 52034-Mail Station 7636 Phoenix, AZ 85072-2034 Mr. Dennis Buschbaum Comanche Peak SES Farm Road 56 P. 0. Box 1002 Glen Rose, TX 76043 Mr. Scott Head Supervisor, Licensing South Texas Project NOC Mail Code N5014 P.O. Box 289 Wadsworth, TX 77483 Mr. Pat Nugent Supervisor, Licensing PG&E Mail Stop 104/5/536 P.O. Box 56 Avila Beach, CA 93424 ULNRC-04653 May 8, 2002 Page 1 Statement of Violation During an NRC inspection conducted between January 28 and February 27, 2002, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the violation is listed below:
10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. For significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective actions taken to preclude recurrence.
The identification of significant conditions adverse to quality shall be documented and reported to appropriate levels of management.
Contrary to the above, between January 1992 and January 31, 2002, the licensee failed to promptly identify and correct a significant condition adverse to quality involving the potential for foreign material to be in the auxiliary feedwater system and condensate storage tank. In addition, between January 25 and 29, 2002, the identification of a significant condition adverse to quality was not reported to the appropriate levels of management. Specifically, there were several missed opportunities to identify and correct the degraded condensate storage tank diaphragm seal, including the following examples:
(1) In 1992, Corrective Action Tracking System Item 31040, which had been initiated to generate an inspection of the condensate storage tank diaphragm seal, was closed without having completed the inspection.
The inspection was to have been completed in response to NRC Information Notice 91-82, "Problems With Diaphragms in Safety Related Tanks."
(2) During the Spring and Summer of 2000, the inspection of the condensate storage tank diaphragm was deferred on two occasions without adequate justification. The deferrals were based on the chemistry specifications of the condensate storage tank water and did not consider the potential for degradation of the diaphragm seal.
ULNRC-04653 May 8, 2002 Page 2 (3) On October 17, 2000, an inadequate inspection of the condensate storage tank diaphragm seal was performed. The inspection did not identify the degraded condition of the diaphragm seal.
(4) On January 15, 2002, foreign material was not considered a credible failure mechanism even though polyurethane foam was discovered in the seal water cooling line for auxiliary feedwater Pump A.
(5) Between January 25 and 30, 2002, a significant condition adverse to quality was not reported to appropriate levels of management in a timely manner. Information regarding the as-found condition of the condensate storage tank diaphragm seal was incorrectly reported.
Consequently, broad corrective actions to assess the extent of condition associated with the failure of the diaphragm seal were delayed.
This violation is associated with a White Significance Determination Process finding.
Reason for the Violation (1) As described, the Callaway Action Tracking System (CATS) Item 31040 status was changed due to a computer error without initiation of the specified inspection work documents. It should be noted that Information Notice 91-82 described concerns with tanks with flexible bladders and was not directly applicable to the Condensate Storage Tank configuration. While all tanks with flexible bladders were inspected and appropriate actions were taken, the incorrect status of the CATS item was not identified until 1999. Detection of the improper closure of the action item was not likely to occur, since the CATS action monitoring was passive.
(2) & (3) A more thorough inspection of the floating cover seal was not conducted for two primary reasons. First, the vendor stated that even if degradation of the seal occurred, the foam would float. Second, no industry Operating Experience relative to this type of seal had been identified. Therefore, the inspection was limited in its scope.
(4) Based on the rapid recovery of the pump and the subsequent successful pump surveillance (after venting) verifying normal vibration and flow parameters, the Root Cause Analysis focused on causes other than foreign material. An obstruction of the pump suction was recognized as a potential cause for the failure experienced.
However, this was considered to be unlikely due to industry operating experience, which suggested system voids were more likely to be the cause. Additionally, industry ULNRC-04653 May 8, 2002 Page 3 experience with foreign material manifested itself in ways that typically did not allow rapid pump recovery. Failure of the pump caused by a suction obstruction was not pursued until all other potential causes were eliminated. Therefore, the significance of the polyurethane foam found in the seal water cooling line for the 'A' auxiliary feedwater pump was not initially challenged.
(5) Limited inspection criteria for the Condensate Storage Tank (CST) coupled with Callaway's philosophy for degraded component evaluations resulted in less than adequate communication. Specifically, insufficient communication occurred between inspection personnel and plant management to ensure the as found condition of the CST was understood and responded to appropriately. Written reports, which were characterized as "Operability Evaluations", did not identify the required technical elements/functions, nor the extent of the observed Degraded or Non-Conforming Condition, consistent with Generic Letter 91-18 guidance.
Corrective Steps Taken and Results Achieved:
(1) The CATS was re-opened and a Work document was initiated to accomplish the inspection. The computer error that caused the incorrect CATS status could not be reproduced.
(2) (3) & (4) The inspection was completed and the floating cover was removed.
(5) An interim guidance document for Operability Determinations was developed.
Training was provided to selected Engineers, Emergency Duty Officers (EDOs) and Engineering Duty Supervisors (EDS) from February 27 through March 1, 2002.
Additionally, this guidance was discussed at the Shift Supervisor (SS) meeting on February 25, 2002. An Operations Night Order was also issued providing further discussion of how to conduct these Operability Determinations until procedure APA-ZZ-00500, 'Corrective Action Program' was revised to include the guidance.
In addition, all Significance Level 1 Callaway Action Requests (CARs) were reviewed by the Vice President, Nuclear and Nuclear Division Managers. Review criteria included adequacy of the root cause determination as well as specified corrective actions.
Corrective Steps to Avoid Further Violations:
(1) The CATS application has been replaced with the Callaway Action Request System (CARS). The CARS application has active monitoring capabilities versus the passive ULNRC-04653 May 8, 2002 Page 4 monitoring capabilities of the CATS application, and will prevent undetected closure of action items. The CARS application went into production in February 2001.
(2) & (3) The old seal has been removed. A new seal will be installed during the Refuel 12 outage. Specific inspection frequency and inspection criteria for the new seal will be established prior to startup from Refuel 12.
(4) & (5) Procedure APA-ZZ-00500, 'Corrective Action Program', Revision 32, was issued March 22, 2002. Key elements of the revision included:
" Requirement to complete Operability Determinations within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
" Requirement for the Manager, Callaway Plant, or his designee, to identify the Root Cause Team composition, scope and due date within two working days of designation of a Significance Level 1 CARs.
"* Requirement for completion of Significance Level 1 & 2 CARs evaluations within 45 days or sooner commensurate with significance and plant needs.
Performance Indicators have been enhanced to assure effective monitoring of the Corrective Action Program.
In addition, the APA-ZZ-00500 revision also incorporated significant changes to embrace the Generic Letter 91-18 philosophy. Follow up training for the corrective action program changes is being provided using an outside consultant. This will assist in providing the "cultural shift" necessary to address the concerns identified. A series of two-day sessions is being conducted from April 11 through June 14, 2002.
Additional training will be provided to Operations personnel during Continued Operations Training.
Date when Full Compliance will be Achieved:
Training on the changes to the Corrective Action Program will be complete prior to startup for Refuel 12. Installation of the condensate storage tank seal will be completed during Refuel 12. Condition monitoring, including scope, acceptance criteria, and frequency for the replacement seal will be established prior to startup from Refuel 12.
All other actions are complete.
ULNRC-04653 May 8, 2002 Page 1 LIST OF COMMITMENTS The following table identifies those actions committed to by Callaway Plant in this document. Any other statements in this submittal are provided for information purposes and are not considered to be commitments. Please direct questions regarding these commitments to Mr. Mark A. Reidmeyer, Regional Regulatory Affairs Supervisor (573) 676-4306.
COMMITMENT Due Date/Event Training on the changes to the Corrective Action Program. Prior to Refuel 12.
Replacement of the condensate storage tank seal. Refuel 12 Condition monitoring, including scope, acceptance criteria Prior to restart from Refuel 12.
and frequency, for the replacement seal will be established.
Note: Refuel 12 is currently scheduled to start October 23, 2002.