Semantic search
Jump to navigation
Jump to search
Issue date | Title | Topic | |
---|---|---|---|
ML22307A019 | 1 November 2022 | EN 56196 - NRC 10 CFR Part 21 Notification, Nutherm, Written Notification of Potential Defect Found in Nutherm/Sola Hevi-Duty Uninterruptible Power Supply (Ups), S4K2U1000-NM 191 | Reverse polarity |
ML22301A174 | 28 October 2022 | Global Nuclear Fuel Americas, LLC (GNF) - Part 21 60-Day Interim Report Notification: GNF3 Raised Water Rod (SC-22-04 Rt) | Affidavit GNF3 Water rod |
ML21168A217 | 17 June 2021 | GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors | Operability Determination Fuel cladding |
M210077, GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors | 17 June 2021 | GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors | Operability Determination Fuel cladding |
M200087, GE-Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Non-Conservative BWR/6 Side Entry Orifice (SEO) Loss Coefficients | 24 June 2020 | GE-Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Non-Conservative BWR/6 Side Entry Orifice (SEO) Loss Coefficients | Operability Determination Fuel cladding |
ML20176A432 | 24 June 2020 | GE-Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Non-Conservative BWR/6 Side Entry Orifice (SEO) Loss Coefficients | Operability Determination Fuel cladding |
ML19317D093 | 25 October 2019 | Engine Systems, Inc., 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10 CFR21-0127, Rev. 0, Emd Fuel Injectors - Seized Plunger and Bushing | |
ML19199A034 | 5 July 2019 | Lake Engineering Co., Third Interim Notification Per 10 CFR Part 21 Degraded Snubber SF1154 Hydraulic Fluid Batch No. ZJS1518 | |
ML19190A044 | 7 June 2019 | 10 CFR Part 21 Reporting of Defects for Introl Positioner 890265-010 - Cw SAS Initial Report No. 10CFR21-48 | Overspeed trip Overspeed |
ML19168A012 | 31 May 2019 | Paragon Energy Solution LLC-10 CFR Part 21 Report of Defect GS2 Terry Turbine Introl Positioners | |
ML19071A112 | 1 March 2019 | Lake Engineering Co., Corrected Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch 11KLVS146 Final Report, Per 10 CFR Part 21 | |
ML19002A204 | 21 December 2018 | to Engine Systems, Inc., Part 21 Report Re Emd Fuel and Soakback Pumps - Potentially Undertorqued Cover Bolts | |
ML18354A742 | 4 December 2018 | Engine Systems, Inc., Submittal of 1OCFR21 Reporting of Defects and Non-Compliance - Report No. 1OCFR21-0123, Rev. 0 - Emo Fuel and Soakback Pumps - Potentially Undertorqued Cover Bolts | |
ML18353A428 | 30 November 2018 | Engine Systems, Inc., 10CFR21-0123, Rev. 0, for a 10CFR21 Reportable Condition on Emd Fuel and Soakback Pumps | |
ML18289A455 | 10 October 2018 | Abb, Inc., 10 CFR Part 21 Notification of Deviation, Dry Type Transformer Serial#: 24-26458 | |
ML18295A199 | 24 September 2018 | Lake Engineering - Second Interim Notification Per 10 CFR Part 21: Degraded Snubber SF1154 Hydraulic Fluid Batch No. 11KLVS146 | |
ML17194A825 | 11 July 2017 | Part 21 Report Re Wedge Pin Failure in Anchor Darling Motor Operated Double Disc Gate Valves with Threaded Stem to Upper Wedge Connections | Anchor Darling |
ML17081A453 | 20 March 2017 | Part 21 - Plastic Jar Dedication Sampling | |
ML17026A414 | 20 January 2017 | C&D Technologies, Inc. - Part 21 - Plastic Jar Dedication Sampling | |
ML16294A264 | 18 October 2016 | Part 21 Report - Defective Current to Pressure Transducers | |
ML15288A199 | 9 October 2015 | Part 21 Interim Report - Potential Defect on P/N 535-601 Moore Industries Milliamp Modules | |
ML15187A029 | 29 June 2015 | Part 21 Notification of Deviation Regarding COM-5 Protective Relay Defective Frame Assembly | |
ML14337A094 | 24 November 2014 | Notification of Potential Part 21 - Lack of Proper Power Supply Indication | |
ML14329A063 | 19 November 2014 | Notification of Potential Part 21 Re Lack of Proper Power Supply Indication | |
ML14274A052 | 22 September 2014 | Final Report 10CFR Part 21 Evaluation Regarding Misaligned Separators in LCR-25 Standby Batteries, Revision 1 - Original Letter Did Not Include the List of Affected Utilities | |
ML14210A010 | 23 July 2014 | Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve | Safe Shutdown Shutdown Margin Scram Discharge Volume Failure to Scram Affidavit |
ML14204A708 | 23 July 2014 | Enclosure 2, Description of Closure Evaluation, Non-Proprietary Information - Class I (Public) | Safe Shutdown Shutdown Margin Scram Discharge Volume Failure to Scram |
ML14204A707 | 23 July 2014 | Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV | Affidavit |
ML14094A445 | 1 April 2014 | Notification of Part 21 Report on Defective Raw Material Used to Manufacture Valve Stems | |
ML14069A468 | 2 March 2014 | Part 21 Report - Defective Raw Material Used to Manufacture Valve Stems | |
ML14055A352 | 10 February 2014 | Part 21 Report - Instruction Leaflet for Subject Relays May Be Deficient | |
ML13165A342 | 12 June 2013 | 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers | |
ML13073A107 | 12 March 2013 | Notification of Potential Part 21 Report - Defective Raw Material Used to Manufacture Valve Stems | |
ML13064A012 | 25 February 2013 | Notification of Potential Part 21 Report Re Wedge Pin Failure of an Anchor/Darling Double-Disc Gate Valve | Anchor Darling |
ML13042A096 | 8 February 2013 | Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Error in Main Steam Line High Flow Calculational Methodology | Power Uprate |
ML13044A075 | 8 February 2013 | Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology | Power Uprate |
ML12352A123 | 13 December 2012 | 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers | |
ML12348A136 | 13 December 2012 | Part 21 60-Day Interim Report Notification: Adequacy of Design Change in Am Magne-Blast Circuit Breakers | |
ML12347A308 | 12 December 2012 | Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology | |
ML12318A041 | 8 November 2012 | Part 21 Report - Commercial Grade Dedication Not Properly Applied to Butterfly Valves | Commercial Grade Dedication Condition Adverse to Quality |
ML12283A244 | 5 October 2012 | Part 21 - Temperature Switch Potentially Shipped Without Set Screw | |
ML12292A197 | 5 October 2012 | Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10CFR21-0106, Rev. 0 | |
ML12319A012 | 27 September 2012 | Error in Main Steam Line High Flow Calculational Methodology | |
ML121910333 | 7 July 2012 | ATC Nuclear, Part 21 Notification Concerning Moore Process Controllers | |
ML121910337 | 2 July 2012 | Update 10 CFR Part 21 Notification of Defective Moore 535 Controllers | |
ML12158A447 | 6 June 2012 | Part 21 60-Day Interim Report Notification - Closufailure of CRD Collet Retainer Tube/Outer Tube Weld | |
ML12163A130 | 6 June 2012 | Part 21 Report - Failure of CRD Collet Retainer Tube/Outer Tube Weld | |
ML12061A268 | 28 February 2012 | Part 21 Report - Potential Minimum Wall Violation on Seismic Plate Valve Bodies | |
ML12040A283 | 7 February 2012 | Notification of Potential Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance | Safe Shutdown Earthquake Operating Basis Earthquake Channel-control blade interference |
ML12038A028 | 2 February 2012 | Failure of CRD Collet Retainer Tube/Outer Tube Weld |