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 Issue dateTitleTopic
ML20084N64631 March 1977Followup AO 50-249/75-44A:on 751125,offgas Activity Increased.Ge Insp Revealed Major Defect in Fuel Assembly DD-418.Assembly Removed from ReactorFuel cladding
ML20084K4985 October 1976Updates AOs 50-265/74-3,50-265/74-13,50-265/74-16 & 50-265/74-19 Re low-low Reactor Water Level Switch LIS-2-263-728 Failure.Surveillance Interval Changed to Monthly.Switch Installation Delayed Pending Analog Trip Sys
ML20084E36329 June 1976Supplemental AO 50-237/75-11A:on 750127,core Spray Injection Line through-wall Cracks Discovered.Stainless Steel Portion of Core Spray Piping from Vessel Nozzle to Second Isolation Valve Replaced w/SA-333 Grade 6 Carbon Steel
ML20084N68329 June 1976Supplemental AO 50-249/1975-42A:motor Operated Valve 3-1501-5D Failed to Open During Testing Due to Thermal Overload Trip.Caused by Undersized Overload Heaters.Overload Heater Will Be Replaced W/Larger Capacity Unit
ML20084D11913 April 1976AO 50-237/75-39A:on 750612,diesel Generator Experienced Starting Failures.Possibly Caused by Two Gouged & Burred Areas on Ring Gear.Ring Gear Repaired
ML20084D15414 January 1976AO 50-237/75-38A Supplementing AO-50-237/75-38 Re Failure of MO-2-1301-2 Valve to Operate.Apparently Caused by Excessive Cycling of Valve.Valve Stem Probably Experienced Metal Fatigue Due to Multiple Actuations
ML20084S22919 December 1975Supplementary Ao:Four Temp Switches Were Found to Trip at Values Exceeding Tech Specs Limits.Caused by Sensors Placed Too Closely to HPCI Turbine & Steam Piping.Different Temp Sensor Will Be Installed
ML20090E45817 December 1975Supplemental AO 50-237/75-44:diesel Generator Failed to Start.Caused by Air Relay Valve Failure Due to Sticking O-rings.O-rings Replaced
ML20084N65411 December 1975AO 50-249/75-44:on 751125,offgas Increase Exhibited Which May Have Represented Abnormal Degradation of Fuel Cladding.Cause Unknown.Investigation UnderwayFuel cladding
ML20090E43220 November 1975AO 50-237/75-52:on 751116,MSIV AO 2-203-1C Closing Time Found Below Tech Spec Section 3.7.D.1.Caused by Out of Adjustment Hydraulic Bleedoff Valve.Bleedoff Valve Readjusted
ML20084S55619 November 1975Preliminary Ao:On 751109,traversing Incore Probe (TIP) Ball Valve 2 Failed to Close.Manual Attempts to Close Valve Failed.No Cause Stated.Addl Info Will Be Submitted in AO 50-265/75-45Squib
ML20084S58517 November 1975AO 50-265/75-44:on 751107,RCIC Turbine Tripped.Caused by Failure of Hydraulic Fluid servo-valve Actuator.Actuator Replaced & Overspeed Trip Mechanism Repaired
ML20084S57310 November 1975Preliminary Ao:On 751107,reactor Core Isolation Cooling (RCIC) Sys Turbine Tripped.Caused by Failure of Hydraulic Fluid servo-valve actuator.Servo-valve Actuator Will Be Replaced.Addl Info Will Be Submitted in AO 50-265/75-44
ML20090E4756 November 1975AO 50-237/75-51:on 751031,torus Water Level Exceeded Tech Spec Limit During HPCI Sys Surveillance.Caused by Operator Failure to Verify Proper Valve Lineup.Water Pumped from Torus Until Level Dropped Below Tech Spec Limits
ML20084S59330 October 1975Ao:On 751029,RHR Sys 2 Supply from Emergency Diesel & Core Spray Sys 2 Bus/Logic Power Failure Alarms Received.Caused by Switch 12 in Off Position.Switch Returned to on Position. Addl Info Will Be Submitted in AO 50-265/75-43
ML20084S60228 October 1975AO 50-265/75-42:on 751018,differential Pressure Across B Train of Standby Gas Treatment Sys Exceeded Tech Spec Limit. Caused by Fouling of High Efficiency Prefilter.Filter Changed & Tested Satisfactorily
ML20084S61927 October 1975AO 50-265/75-41:on 751018,while Performing Monthly Diesel Generator Surveillance Test,Diesel Generator Reactive Power Meter in Control Room Pegged Full Scale.Megawatt Output Load Erratic.Operator Tripped Diesel.Caused by Equipment Failure
ML20084S77724 October 1975AO 50-265/75-38:on 751014,weld Exams Indicated Crack on B Loop of Rx Recirculation Discharge Bypass Line.Caused by Intergranular Stress Assisted Corrosion.Both Bypass Lines Will Be Removed
ML20084S67424 October 1975AO 50-265/75-39:on 751016,one Bergen-Patterson & Two Grinnell Hydraulic Snubbers Found W/Empty Oil Reservoirs. Apparently Caused by Equipment Failure.Snubbers Will Be Repaired or ReplacedEarthquake
ML20084S64724 October 1975AO 50-265/75-40:on 751016,while Performing Routine Surveillance,Three High Drywell Pressure Scram Switches Found to Exceed Tech Spec Limit.Apparently Caused by Instrument Drift.Pressure Switches Recalibr & Tested
ML20084S20720 October 1975Telecopy Ao:On 751020,radwaste Discharge Batch 3709 Discharged at Rate Which Exceeded Tech Spec Limit.Further Info to Be Provided in AO 50-254/75-22
ML20084N68820 October 1975AO 50-249/75-42:on 750920,motor Operated LPCI Suction Valve 3-1501-5D Failed to Open Twice During Testing. Apparently Caused by Defective Valve Motor.Valve Motor Will Be Replaced
ML20084S61220 October 1975Telecopy AO 50-265/75-42:on 751018,differential Pressure Across B Train Particulate Filters of Standby Gas Treatment Sys Exceeded Tech Specs.Caused by Smoke from Small Fire Created by Onsite Welders.Work Request Issued
ML20084S62918 October 1975Telecopy AO 50-265/75-41:on 751017,during Monthly Surveillance Testing of Diesel Generator,Electrical Flash Burned Out Diode Rectifier Array of Generator Exicitation Circuitry.Output Breaker Tripped.Generator Inoperable
ML20084S78217 October 1975AO 50-265/75-37:on 751007,minor Leakage from B Feedwater Flush Line Observed.Caused by Equipment Failure.Flush Line Being Repaired
ML20084S68317 October 1975Telecopy AO 50-265/75-39:on 751016,two Grinnell & One Bergen-Patterson Hydraulic Snubbers Found Defective.Cause Not Stated.Work Request Issued for Repair
ML20084S65617 October 1975Telecopy AO 50-265/75-40:on 751016,during Routine Monthly Surveillance,Three High Drywell Pressure Switches Found to Exceed Tech Spec Limit.Cause Not Stated.Instruments Recalibr & Tested Satisfactorily
ML20090E47817 October 1975AO 50-237/75-49:on 751009,LPCI Loop Selection Logic Circuitry Failed to Select Preferred B Loop.Caused by Out of Calibr Differential Switch 261-34 & Electrically Shorted Switch 261-34D.Mod to Provide Signal Dampening Initiated
ML20090E44717 October 1975AO 50-237/75-48:on 751007,through-wall Crack Discovered in Drywell/Torus Nitrogen Purge Line 1604-18.Caused by Rapid & Uneven Contraction of Line Tee Connection Due to Liquid Nitrogen Impingement Resulting from Boiler Failure
ML20084S21815 October 1975Telecopy Ao:On 751014,two High Drywell Pressure Scram Switches Found in Isolated Condition.Further Info to Be Provided in AO 50-254/75-21
ML20084N83315 October 1975Supplemental AO 50-249/75-22:plant Mod Being Initiated to Eliminate Valve Seat Failures Due to Cryogenic StressPacking leak
ML20084S76814 October 1975Telecopy Ao:On 751014,crack Indication Confirmed on B Loop in heat-affected Zone on Pipe Side of pipe-to-weldolet Weld. Repair Plans Incomplete.Addl Info Will Be Submitted in AO 50-265/75-38
ML20090E4829 October 1975AO 50-237/75-46:on 750929,reactor Scrammed on High Drywell Pressure During Drywell Inerting Process.Caused by Operator Valving Error,Allowing Nitrogen Flow to Bypass Inerting Pressure Control Valve Into Drywell.Operators Cautioned
ML20090E4819 October 1975AO 50-237/75-45:on 750929,HPCI Turbine Failed to Trip at Designated Reactor Coolant Level.Caused by Open Circuit in Turbine Trip Solenoid Valve Coil Due to Failure of Cold Solder Joint within Coil.Hpci Trip Solenoid Valve Replaced
ML20084S7857 October 1975Telecopy Ao:On 751007,pipe Crack Found on Feedwater Flush Line 2-3206B-4-C at Main Feedwater Line 2-3204B-18-C.Minor Leakage Did Not Affect Reactor Inventory.Repairs Initiated. Addl Info Will Be Submitted in AO 50-265/75-37
ML20084N6717 October 1975AO 50-249/75-43:on 750927,leak Discovered in Drain Line from Feedwater Heater 3D3 to Heater 3C3.Caused by Poor Weld Installation of Drain Line Pipe Support.Crack Ground Out & Pipe Rewelded
ML20090E4642 October 1975AO 50-237/75-44:on 750923,diesel Generator Failed to Start.Caused by Operator Failure to Follow Monthly Insp Procedure & QC Procedure for safety-related Component Replacement.Air Start Sys Inspected & Seal Ring Replaced
ML20090E47019 September 1975AO 50-237/75-43:on 750911,diesel Generator Cooling Water Pump Main Breaker Tripped.Caused by Excessive Heat Buildup within Breaker Housing.Breakers on Buses Replaced & Cover Plates Removed for Ventilation
ML20084N69116 September 1975AO 50-249/75-41:on 750908,intermediate Range Monitors 11, 12,14,16 & 18 Failed to Respond During Plant Startup. Apparently Caused by Personnel Accidentally Loosening Cables.Cables Replaced
ML20090E4918 September 1975AO 50-237/75-42:on 750829,diesel Generator Cooling Water Pump Tripped,Followed by Diesel Generator Trip on High Temp. Cause Not Established.Investigation of Cooling Water Pump & Associated Breakers Continuing
ML20084N8414 September 1975AO 50-249/75-37:on 750826,pressure Switches PS3-263-53A,53B & 53C Had Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods at Zero Pressure. Setpoints Reset
ML20084N7774 September 1975AO 50-249/75-38:on 750826,pressure Switches 3-263-52A1 & 52A2 Found W/Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods of Inactivity. Switches Reset
ML20084N7284 September 1975AO 50-249/75-40:on 750827,during Routine Instrument Surveillance,Pressure Switches PS3-263-51A & 51B Had Setpoints Above Tech Spec Limit.Caused by Drifting Due to Long Periods at Zero Pressure.Switches Reset
ML20084N7483 September 1975AO 50-249/75-39:on 750826,overload Relay Tripped Twice on Motor Operated Isolation Valve 3-220-1.Caused by Defective Overload Relay.Relay Replaced
ML20084N7942 September 1975AO 50-249/75-36:on 750823,reactor High Pressure Sensors 263-55A,55B & 55C Found W/Setpoints Above Tech Spec Limit. Apparently Caused by Extended Periods at Zero Pressure. Switches Reset
ML20084R98731 August 1975Telecopy of AO 50-265/75-36:on 750831,during Shutdown, Instability Was Experienced on Feedwater Control Sys Which Caused 3/4 Inch Drain Lines to Sever from Low Flow Feedwater Regulating Valve.No Radioactive Matl Released
ML20084S03931 August 1975Telecopy Ao:On 750830,while Performing Monthly RCIC Operability Surveillance Test RCIC Would Not Reach Normal Conditions.Possibly Caused by Overspeed Mechanism.Required Testing of HPCI Sys Initiated
ML20084S00431 August 1975Telecopy Ao:On 750830,while Testing Operability of HPCI Sys, Auxiliary Oil Pump Kept Tripping & HPCI Turbine Failed to Start.Orderly Shutdown Was Initiated.Further Info to Be Provided in AO 50-265/75-35
ML20084N86629 August 1975AO 50-249/75-35:on 750821,circuit Breaker 152-3403 Failed to Trip During Breaker Trip Test.Caused by Failure of Trip Coil.Breaker Replaced
ML20084S09925 August 1975Telecopy Ao:On 750824 Grinnel Snubber Had Empty Fluid Reservoir & Bergen-Paterson Snubber Had Leaking Accumulator. Replacement Parts Installed Prior to Reactor Startup on 750825.Further Info to Be Provided in AO 50-265/75-32