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Category:Letter
MONTHYEARIR 05000324/20253012024-10-17017 October 2024 Notification of Licensed Operator Initial Examination 05000325/2025301 and 05000324/2025301 IR 05000324/20244012024-10-15015 October 2024 Security Baseline Inspection Report 05000324/2024401 and 05000325/2024401 ML24297A6262024-10-11011 October 2024 PCA Letter to NRC Brunswick Potential Tropical Storm Eight IR 05000324/20240102024-09-10010 September 2024 Focused Engineering Inspection Commercial Grade Dedication Report 05000324-2024010 and 05000325-2024010 ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000324/20240052024-08-23023 August 2024 Updated Inspection Plan for Brunswick Steam Electric Plant, Units 1 and 2 (Report 05000324/2024005 and 05000325/2024005) IR 05000324/20240022024-08-0505 August 2024 Integrated Inspection Report 05000324/2024002 and 05000325/2024002 and 07200006/2024001 ML24206A1062024-07-30030 July 2024 2024 Brunswick Requal Inspection Corporate Notification Letter ML24183A0972024-07-12012 July 2024 ISFSI; Catawba 1, 2 & ISFSI; McGuire 1, 2 & ISFSI; Oconee 1, 2, 3 & ISFSI; Shearon Harris 1; H. B. Robinson 2 & ISFSI; and Radioactive Package Shipping Under 10 CFR 71 (71-266 & 71-345) – Review of QA Program Changes EPID L-2024-LLQ-0002 IR 05000324/20244202024-07-0202 July 2024 – Security Baseline Inspection Report 05000324/2024420 and 05000325/2024420 ML24108A0702024-06-0505 June 2024 – Issuance of License Amendments to Revise the 10 CFR 50.69 Categorization Process to Reflect an Alternative Seismic Approach IR 05000324/20244022024-05-17017 May 2024 Plan Material Control and Accounting Program Inspection Report 05000324/2024402 and 05000325/2024402 - Cover Letter IR 05000324/20240012024-05-0909 May 2024 Integrated Inspection Report 05000324/2024001 and 05000325/2024001 05000325/LER-2024-002, Re Automatic Start of Emergency Diesel Generator Due to Emergency Bus De-energization2024-04-10010 April 2024 Re Automatic Start of Emergency Diesel Generator Due to Emergency Bus De-energization 05000325/LER-2024-001, Primary Containment Penetration Local Leak Rate Testing Failure2024-04-10010 April 2024 Primary Containment Penetration Local Leak Rate Testing Failure ML24066A0132024-03-0505 March 2024 Bru 2024-002 Radiation Safety Baseline Inspection Information Request ML24026A0982024-03-0101 March 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0057 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) IR 05000324/20230062024-02-28028 February 2024 Annual Assessment Letter for Brunswick Steam Electric Plant, Units 1 and 2 – NRC Inspection Reports 05000324/2023006 and 05000325/2023006 IR 05000324/20244032024-02-14014 February 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perm Inspection 05000325/2024403; 05000324/2024403 ML24032A1392024-02-12012 February 2024 Correction of Errors within Authorized Alternative Request RA-22-0308 IR 05000324/20230042024-02-0606 February 2024 Integrated Inspection Report 05000324/2023004 and 05000325/2023004 IR 05000324/20230112023-12-26026 December 2023 NRC Fire Protection Team Inspection - FPTI Report 05000324/2023011 and 05000325/2023011 IR 05000324/20234022023-12-14014 December 2023 Security Baseline Inspection Report 05000324-2023402 and 05000325-2023402 ML23297A0262023-11-27027 November 2023 – Proposed Alternatives to ASME Code Section XI Subsection IWE Requirements for Torus Metallic Liner Inspections ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000324/20230032023-11-0101 November 2023 Integrated Inspection Report 05000324/2023003 and 05000325/2023003 IR 05000324/20230102023-10-17017 October 2023 Biennial Problem Identification and Resolution Inspection Report 05000324/2023010 and 05000325/2023010 IR 05000325/20234012023-10-16016 October 2023 Security Baseline Inspection Report 05000324 and 05000325 2023401 ML23346A1322023-10-0606 October 2023 Communication from C-10 Research & Education Foundation Regarding NextEra Common Emergency Fleet Plan License Amendment Request and Related Documents Subsequently Published ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000324/20230052023-08-23023 August 2023 Updated Inspection Plan for Brunswick Steam Electric Plant, Units 1 and 2 (Report 05000324/2023005 and 05000325/2023005) IR 05000324/20230022023-08-0404 August 2023 Integrated Inspection Report 05000324/2023002 and 05000325/2023002 ML23201A2042023-07-28028 July 2023 Summary of Regulatory Audit in Support of Alternative Request RA-22-0308 for Inservice Inspection of the Torus Metallic Liner IR 05000324/20243012023-07-25025 July 2023 – Notification of Licensed Operator Initial Examination 05000325/2024301 and 05000324/2024301 05000324/LER-2023-001, Two Main Steam Line Safety Relief Valves Inoperable2023-07-17017 July 2023 Two Main Steam Line Safety Relief Valves Inoperable 05000325/LER-2023-001, Loss of Redundant Power Supply Operation Causes Turbine Trip and Subsequent Reactor Scram2023-06-15015 June 2023 Loss of Redundant Power Supply Operation Causes Turbine Trip and Subsequent Reactor Scram ML23146A0012023-05-24024 May 2023 EN 56538 - Engine Systems Inc and Brunswick ML23212A9502023-05-24024 May 2023 Engine Systems, Inc., Part 21 Report Re Woodward EGB-35P Governor/Actuator with Foreign Material ML23130A3902023-05-12012 May 2023 – Regulatory Audit Plan in Support of Alternative Request RA 22-0308 for Inservice Inspection of the Torus Metallic Liner IR 05000324/20230012023-05-10010 May 2023 – Integrated Inspection Report 05000324 2023001 and 05000325 2023001 ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI IR 05000324/20220042023-04-0404 April 2023 Reissue - Brunswick Steam Electric Plant - Integrated Inspection Report 05000324/2022004 and 05000325/022004 ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility IR 05000324/20220062023-03-0101 March 2023 Annual Assessment Letter for Brunswick Steam Electric Plant, Units 1 and 2 – NRC Inspection Reports 05000324/2022006 and 05000325/2022006 ML23033A5252023-02-0808 February 2023 Integrated Inspection Report 05000324/2022004 and 05000325/2022004 IR 05000324/20223012023-02-0303 February 2023 NRC Operator License Examination Report 05000325/2022301 and 05000324/2022301 IR 05000324/20224022022-11-23023 November 2022 Security Baseline Inspection Report 05000324 2022402 and 05000325 2022402 ML22332A0132022-11-23023 November 2022 Operator Licensing Written Examination Approval 05000325/2022301 and 05000324/2022301 ML22096A0032022-11-18018 November 2022 McGuire Nuclear Station and Shearon Harris Nuclear Power Plant Authorization of RA-19-0352 Regarding Use of Alternative for RPV Head Closure Stud Examinations 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000325/LER-2024-001, Primary Containment Penetration Local Leak Rate Testing Failure2024-04-10010 April 2024 Primary Containment Penetration Local Leak Rate Testing Failure 05000325/LER-2024-002, Re Automatic Start of Emergency Diesel Generator Due to Emergency Bus De-energization2024-04-10010 April 2024 Re Automatic Start of Emergency Diesel Generator Due to Emergency Bus De-energization 05000324/LER-2023-001, Two Main Steam Line Safety Relief Valves Inoperable2023-07-17017 July 2023 Two Main Steam Line Safety Relief Valves Inoperable 05000325/LER-2023-001, Loss of Redundant Power Supply Operation Causes Turbine Trip and Subsequent Reactor Scram2023-06-15015 June 2023 Loss of Redundant Power Supply Operation Causes Turbine Trip and Subsequent Reactor Scram 05000325/LER-2022-001, High Pressure Coolant Injection (HPCI) Inoperable2022-09-12012 September 2022 High Pressure Coolant Injection (HPCI) Inoperable 05000325/LER-2021-001, Automatic Specified System Actuation Due to Loss of Power to Emergency Bus E32022-01-20020 January 2022 Automatic Specified System Actuation Due to Loss of Power to Emergency Bus E3 05000324/LER-2017-0032017-08-0303 August 2017 1 OF 4, LER 17-003-00 for Brunswick, Unit 2, Regarding Setpoint Drift in Main Steam Line Safety/Relief Valves Results in Three Valves Inoperable, 05000325/LER-2017-0032017-08-0202 August 2017 Control Room Air Conditioning and Emergency Ventilation Systems Rendered Inoperable, LER 17-003-00 for Brunswick, Unit 1, Regarding Control Room Air Conditioning and Emergency Ventilation Systems Rendered Inoperable 05000324/LER-2017-0022017-06-12012 June 2017 Plant Mode Change with Primary Containment Inoperable, LER 17-002-00 for Brunswick, Unit 1, Regarding Foreign Material in Switch Results in Unplanned Automatic Start of Emergency Diesel Generators 05000324/LER-2017-0012017-05-18018 May 2017 Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, LER 17-001-00 for Brunswick, Unit 2, Regarding Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 05000324/LER-2016-0012016-08-0808 August 2016 Mispositioned Valves Result in Residual Heat Removal Service Water System Inoperability, LER 16-001-00 for Brunswick Steam Electric Plant, Unit 2, Regarding Mispositioned Valves Result in Residual Heat Removal Service Water System lnoperability 05000325/LER-2016-0032016-05-0202 May 2016 Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, LER 16-003-00 for Brunswick Steam Electric Plant, Unit 1 Regarding Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 05000324/LER-2016-0022016-05-0202 May 2016 High Pressure Coolant Injection System Inoperable due to Failed Relay Coil, LER 16-002-00 for Brunswick Steam Electric Plant (BSEP), Units 1 and 2, Regarding Emergency Diesel Generator 3 Inoperable Due to Failure to Auto-Start 05000325/LER-2016-0012016-04-0606 April 2016 Electriqal Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power, LER 16-001-00 for Brunswick, Unit 1, Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power BSEP 15-0088, Special Report, Technical Specification 5.6.6, Post Accident Monitoring (PAM) Instrumentation Report2015-10-22022 October 2015 Special Report, Technical Specification 5.6.6, Post Accident Monitoring (PAM) Instrumentation Report ML1019404522008-06-0303 June 2008 10CFR50.75g File: AR00237296 Overflowed CST ML1019404542008-05-13013 May 2008 10CFR50.75g File: AR00272173 Thru Wall Leak in Cw Intake Pipe Was Found to Contain Tritium in the Groundwater Leaking Into the Pipe ML1019404562008-04-28028 April 2008 10CFR50.75g File: AR00242461 Routine Environmental Soil/Water Sampling Has Identified Low Levels of Tritium . BSEP 03-0023, LER 2002-02-00 from Brunswick, Unit 2 Regarding Remote Shutdown Panel Power Supply Inventer Design Deficiency2003-02-14014 February 2003 LER 2002-02-00 from Brunswick, Unit 2 Regarding Remote Shutdown Panel Power Supply Inventer Design Deficiency 2024-04-10
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U.S. Nuclear Regulatory Commission Page 2 of 2
cc (with enclosure):
Ms. Laura Dudes, NRC Regional Administrator, Region II Mr. Luke Haeg, NRC Project Manager Mr. Gale Smith, NRC Senior Resident Inspector
Abstract
At 01:48 Eastern Daylight Time (EDT) on April 20, 2023, with Unit 1 in Mode 1 at approximately 100% power, an automatic reactor scram occurred due to a turbine trip. All control rods inserted as expected. Turbine bypass valves did not open on the scram; Safety Relief Valves (SRVs) opened automatically to control reactor pressure. Reactor Pressure reached approximately 1100 psig on the scram, exceeding the Reactor Protection System (RPS) setpoint. Reactor water level reached low level 1 following the scram resulting in automatic actuation of Primary Containment Isolation System (PCIS) Group 2, 6, and 8 isolation valves, by design.
Operations responded and stabilized the plant. Operations transitioned pressure control from SRVs to main steam line drains to the condenser. Following the scram, reactor water level was maintained via the condensate and feedwater systems.
The turbine trip and subsequent inoperative turbine bypass valves resulted from a complete loss of 24 Vdc power to the Turbine Protection system. The power supplies were replaced prior to restart.
There was no impact on the health and safety of the public or plant personnel. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) due to valid actuation of the RPS and PCIS.
Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
Background
Initial Conditions
At the time of the event, Unit 1 was in Mode 1 (i.e., Power Operation), at approximately 100 percent rated thermal power.
Reportability Criteria
This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) because it involved actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B). Specifically, the Reactor Protection System [JC] and Primary Containment Isolation System [JM] actuated during this event.
The NRC was notified of this event per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50. 72(b)(3)(iv)(A) via Event Notification 56478 at 05:24 Eastern Daylight Time (EDT) on April 20, 2023.
Event Description
At 01:48 Eastern Daylight Time (EDT) on April 20, 2023, with Unit 1 in Mode 1 at approximately 100% power, an automatic reactor scram occurred due to a turbine trip. All control rods inserted as expected.
The turbine bypass valves [JI] did not open on the scram; main steam [SB] Safety Relief Valves (SRVs) 1C, 1F, 1G, 1K, and 1L cycled open automatically to control reactor pressure. Reactor pressure reached approximately 1100 psig on the scram; exceeding the 1060 psig Reactor Protection System (RPS) setpoint.
Reactor water level reached the low level 1 (LL1) setpoint following the scram. Per design, the LL1 signal resulted in Primary Containment Isolation System Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations.
Operations responded and stabilized the plant. Operations manually cycled open SRV 1B then transitioned pressure control from SRVs to the main steam line drains [SB] to the condenser [SG]. Following the scram, reactor water level was maintained via the condensate [SD] and feedwater [SJ] systems.
Event Cause
The direct cause of the turbine trip and subsequent inoperative turbine bypass valves was a complete loss of 24 Vdc power to the Turbine Protection system [JJ]. When 24 Vdc power was lost, Turbine Protection system data inputs for required pressure and flow transmitters were lost. With the loss of monitoring capability, the Turbine Protection system responded as designed by initiating a turbine trip to protect the turbine and inhibiting the opening of the turbine bypass valves to protect the condenser.
24 Vdc power is supplied to the Turbine Protection system via redundant power supplies [RJX]. Due to inadequacies in the vendor design, a unique combination of internal component failures on one power supply impacted the operation of the redundant power supply. As a result, both power supplies failed/shutdown within a short timeframe of one another resulting in a total loss of 24 Vdc power.
Prior to this event the power supplies had operated successfully with no indication of deficiencies for approximately five years.
Safety Assessment
There was no adverse impact on the health and safety of the public or plant personnel. The safety significance of this event is minimal. The condenser remained available for pressure control. The condensate and feedwater systems remained available for level control.
Corrective Actions
Prior to restart from this event, the 24 Vdc Turbine Protection system power supplies were replaced.
The site is planning to implement changes to the current 24Vdc power supply functionality that will prevent a power supply internal failure from impacting the redundant power supply.
Any changes to corrective actions or completion schedules w ill be made in accordance with the sites corrective action program.
Previous Similar Events
No previous similar events have occurred within the past three years in which inadequate vendor design resulted in a turbine trip and reactor scram.
Commitments
No regulatory commitments are contained in this report.