ML20214V625

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Safety Insp Repts 50-373/86-40 & 50-374/86-40 on 861008- 1117.Major Areas Inspected:Operational Safety,Surveillance, Maint,Training,Lers,Action in Response to IE Bulletin 86-03 & General Site Emergency Plan Drill
ML20214V625
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 11/28/1986
From: Wright G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20214V579 List:
References
50-373-86-40, 50-374-86-40, IEB-86-003, IEIN-86-072, NUDOCS 8612090762
Download: ML20214V625 (16)


See also: IR 05000373/1986040

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No: 50-373/86040(DRP); 50-374/86040(DRP)

Docket Nos: 50-373; 50-374 Licenses No. NPF-11; NPF-18

Licensee: Commonwealth Edison Company

Post Office Box 767

Chicago, IL 60690

Facility Name: LaSalle County Station, Units 1 and 2

Inspection At: LaSalle Site, Marseilles, IL

Inspection Conducted: October 8 through November 17, 1986

Inspectors: M. J. Jordan

R. Kopriva

J. Mueller

D. Bulter /

Approved By: 1

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  1. V8'/4

Reactor Projects Section 2C Date

Inspection Summary

Inspection on October 8 through November 17. 1986 (Reports

No. 50-373/86040(DRP): 50-374/86040(DRP))

Areas Inspected: Routine, unannounced inspection conducted by resident

inspectors of licensee actions on previous inspection findings; operational

safety; surveillance; maintenance; training; Licensee Event Reports; licensee

action on an IE Bulletin; followup of 10 CFR 50.54(f) request for information;

Part 21 followup; general site emergency plan (GSEP) drill; regional request;

and temporary instruction TI 2515/75.

Results: In the area of surveillance, the verification by two individuals

that a valve was open, when in fact it was closed, is considered poor

performance. The corrective action to this event was extensive and considered

good. The performance in remaining areas was considered to be adequate.

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8612090762 861202

PDR ADOCK 05000373

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DETAILS

1. Persons Contacted

  • G. J. Diederich, Manager, LaSalle Station
  • R. D. Bishop, Services Superintendent
  • J. C. Renwick, Production Superintendent

D. Berkman, Assistant Superintendent, Work Planning

W. Huntington, Assistant Superintendent, Operations

  • P. Manning, Assistant Superintendent, Technical Services

T. Hammerich, Assistant Technical Staff Supervisor

W. Sheldon, Assistant Superintendent, Maintenance

J. Atchley, Operating Engineer

R. W. Stobert, Quality Assurance Supervisor

  • M. H. Richter, Assistant Tech Staff Supervisor
  • Denotes personnel attending the exit interview on November 17, 1986.

2. Licensee Action on Previous Inspection Findings (92701)

(Closed) Violation (374/86020-01(DRP)): An operator failed to withdraw a

control rod in accordance with the approved rod sequence provided by the

nuclear engineer. Corrective actions taken were: (1) the control rod

was immediately reinserted to the required position, the nuclear engineer

reviewed the event, and the operator was reprimanded for his lack of

attention to detail; (2) station procedures were revised; and (3) all

shift personnel were trained on the event.

(Closed) Violation (374/86020-02(DRP)): The operator failed to demand

the required process computer printouts and failed to consult the nuclear

engineer prior to returning the mispositioned control rod to its correct

in-sequence position. Corrective actions taken were: (1) the event was

immediately reviewed with a nuclear engineer; (2) the event was reviewed

with the reactor operator involved and the importance of adhering to the  ;

procedures was emphasized; and (3) procedure LOA-RD-03 has been revised. )

(Closed) Open Item (373/83049-08(DRP)): This item concerned isolation

response time of primary containment vent and purge valves. Safety '

EvaluationReport(SER) item 373/81-00-93 and TMI action item II.E.4.2

which also tracked this open item were closed in Inspection Report

373/86035. This item is considered closed.

(Closed) Open Items (373/86018-02;374/86017-01(ORP)): These items '

tracked the inspector's two concerns with the fire door surveillance

system. First, the fire door surveillance was performed by the security

force as part of the security supervision system. However, if a door ,

failed the surveillance, neither the Shift Engineer nor the Fire Marshall

were required to be notified. Without the Fire Marshall or the Shift

Engineer being notified, the action required by the Technical

Specification to be accomplished within one hour may not have been

accomplished.

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The licensee revised the security force's LaSalle Post Order (LPO) 121,

" Fire Door Check,"-to instruct the security personnel who were

performing the fire door surveillance to inform their supervision, who,

L in turn, informs the Shift Engineer. This concern is adequately

!- addressed.

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The inspector's second concern related to the revision process for

i fire-related post orders which appeared not to have the onsite review

! and control system required by Technical Specification section 6.0,

" Administrative Controls."

The licensee has revised LAP-900-14 " Fire Protection Program," to

require the concurrence of the Station Manager, Tech Staff Supervisor,

and Fire Marshall prior to revising LPO-105, " Fire Watch," LPO-112,

i' " Roving Fire Watch Patrol," and LPO-121, " Fire Door Check." The licensee

has also' referenced Technical Specification 4.7.6.2.d. in these LPO's.

This adequately addresses the inspector's concern.

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The inspector has confirmed that these revisions have been implemented.

These items are considered closed.

(Closed) Unresolved Item (374/86008-03(DRP)): This unresolved item

tracked the inspector's concern regarding a change to a modification for

Environmental Qualification (EQ) of level and flow instrumentation,

specifically M-1-2-84-136. The change deleted the need for replacement

of four Unit 2 Reactor Vessel High Water Level 8 switches: HPCS level

switches 2B21-N100A and 2B21-N100B, RCIC level switch 2B21-N101A, and

RCIC flow switch 2E51-N002. The station was verbally informed by the i

Station Nuclear Engineering Department (SNED) in March 1985 that these

four switches did not require EQ.

In early March 1986, upon reanalysis after completion of the changed

modification, SNED could not justify why three of the four switches were

not required to have EQ. The licensee subsequently requested their

architect / engineer to reanalyze the switches environment during accident

conditions. The reanalysis confirmed that these switches would be in a

harsh environment and, therefore, required EQ. The unit had been

operating for approximately eighty days (12/22/85 through 3/12/86).

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In late March 1986, the architect / engineer reanalyzed the switches and

determined that the existing HPCS and RCIC level switches were

environmentally qualified for their location and minimum post-accident

operating time; the RCIC flow switch does not require EQ because it does

not have to function while exposed to a harsh environment nor is it

needed for post-accident monitoring.

The inspector was concerned that the licensee had not environmentally

qualified the four switches prior to the 10 CFR 50.49 deadline of

November 30, 1985 as was originally planned'in the modification package.

The licensee was unsure of whether or not the switches were required to

l have EQ since the justification for the March 1985 SNED verbal approval

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of their deletion from the modification package was not sufficiently

documented by SNED nor by the station.

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.The inspector confirmed by review of training records that the licensee

has since trained the technical staff emphasizing that, in all

situations, appropriate documentation is required to change portions of

a modtfication package. The inspector's concerns have been adequately

addressed. This unresolved item is considered closed.

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3. Operational Safety Verification (71707) ,

The inspector observed control room operations, reviewed applicable

, logs and conducted discussions with control room operators during the

inspection period. The inspector verified the operability of selected

emergency systems, reviewed tagout records, and verified proper return

to service of affected components. Tours of Units 1 and 2 reactor

buildings and turbine buildings were conducted to observe plant equipment

l conditions, including potential fire hazards, fluid leaks and excessive

vibrations and to verify that maintenance requests had been initiated

l for equipment in need of maintenance. The inspector by observation and

direct interview verified that the physical security plan was being

l implemented in accordance with the station security plan.

l The inspector observed plant housekeeping / cleanliness conditions and

verified implementation of radiation protection controls.

During the month of October 1986, the inspector walked down the

accessible portions of the following systems to verify operability:

Unit I and 2 Residual Heat Removal (RHR) System

! Unit I and 2 Diesel Fire Pump System

Unit 1 and 2 Diesel Generators

i 4. Monthly Surveillance Observation (61726)

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The inspector observed Technical Specification required surveillance

testing and verified for actual activities observed that testing was

performed in accordance with adequate procedures, that test

instrumentation was calibrated, that limiting conditions for operation

were met, that removal and restoration of the affected components were t

accomplished, that test results conformed with Technical Specification '

l and procedure requirements and were reviewed by personnel other than the

l individual directing the test, and that any deficiencies identified

during the testing were properly reviewed and resolved by appropriate

I management personnel.

! The inspector witnessed portions of the following test activity:

l LIS-MS-403 Unit 2 Main Steam Line High Radiation Scram and MSIV

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Isolation Functional Test

LIS-NB-1-1 Unit 1 Reactor Vessel Low Water Level Scram and Primary

l Containment Isolation Calibration

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On October 17, 1986 the licensee notified the Senior Resident Inspector

(SRI) that on Unit 1, while at approximately 88% power, after performing

surveillance test LIS-RH-312, " Unit 1 Residual Heat Removal (Shutdown

Cooling Mode) High Suction Flow Isolation Functional Test", the Group 6

Division II reactor high pressure (135 psi) isolation instrument

PS-1833-N018B had been left valved out of service with two signatures

verifying the instrament was valved in service. The surveillance was

performed on the high flow isolation instrument, but the procedure also

required the isolation of the high pressure isolation switch for the

Residual Heat Removal (RHR) System. Discussions with the individuals

involved, in the presence of the SRI, revealed that the instrument was

valved out by accident and lockwired by the instrument mechanic (IM)

performing the test. The independent verifier stated he was instructed

to " verify the instrument was back in service". He verified the drain

valve from the instrument closed and also verified the instrument stop

valve closed without concentrating that the instrument stop valve should

be verified open. The lockwire had no detrimental affect on verifying

the valve positions. The instructions in the surveillance required

prepressurizing the 135 lbs. high pressure switch (PS-1833-N0188), then

prepressurizing the high flow switch (DPS-1E31-N012BA), then returning

the high pressure switch to service, and finally returning the high flow

switch to service. The IM performing the surveillance felt that he may

have gotten confused when swapping back and forth between the two

switches and failed to valve the one switch back into service. He

verified the respective relays were energized which was the case because

of the prepressurization. The reason the instruments were prepressurized

was that after the instrument stop was opened, a spike would not be felt

by the instrument and cause an unnecessary actuation. The instrument

checkoff sheet in LIS-RH-312 for PS-1833-N18B required the instrument

stop valve to be open and verified by two people. Technical Specification 6.2.A requires that detailed procedures including checkoff lists shall

be adhered to. Item 7 in the lists of procedures is for surveillance

and testing requirements. Contrary to the above, the check off sheet

for LIS-RH-312 was not adhered to in that two persons did not verify the

instrument valve stop open. This is considered a violation

(373/86040-01(DRP)).

When the prepressurized high pressure instrument eventually bled down

due to slight leakage in the system, the greater than 135 lb isolation

for the RHR system was removed and the Division II indication of this

isolation no longer appeared on the primary containment isolation status

panel in the control room. The control room operator did not recognize

this change in the panel indication. He also did not recognize that the

process computer had printed an alarm, "Rx. vsl. pressure Div II not

high", which indicated that the high pressure isolation was no longer in

affect. Step 43 of the operating surveillance LOS-AA-51, "Shif tly

Surveillance", requires a lamp test on the primary contairment isolation

status panel. The alarm indicating the removal of the high pressure

isolation appeared on the process computer typer at 12:35 a.m. on

October 16, 1986. The midnight shift reactor operator (RO) stated he

thought he had completed the status board light check portion of his

surveillance prior to that time so he would not have seen the abnormal

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_ condition'at that time. However, the dayshift and swing shift

surveillances should have identified the light being out as not normal

and taken action. This was not done. Also, each shift the R0 pushes

the isolation reset pushbuttons. This also extinguished the light on

the back_ panel indicating the Group 6 06 vision II isolation was no longer

enforcing.

Technical Specifications 6.2.A requires 'that detailed procedures shall

be adhered to. Item 7 in the list of procedures was'for surveillance

-and testing requirements. Contrary to the above, procedure LOS-AA-S1

was not followed in that the check that the resulting indications are

normal did not identify' that the Group 6 isolation light were out.

.This is considered a violation (373/86040-02(ORP)).

The RHR isolation function for the Division II inboard valves on high

reactor pressure (135 lbs) was inoperable for approximately 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />

before being discovered. The alarm printer indicated the Division II-

RHR shutdown cooling mode isolation on high reactor pressure did not

have the minimum number of operational channels per trip system. starting

on October 16, 1986 at 12:35 a.m.. The R0 on swing shift noticed the

light out on the Primary Containment. Isolation System (PCIS) panel the

evening of October 16. The required instrument and channel was back

into service on 10:50 p.m. on October 16, 1986. Technical Specification 3.3.2.b. requires that when the number of operable channels per trip

system are less than required by table 3.3.2-1 then either the channel

should be tripped within one hour or, if tripping the channel could cause

the trip function to occur, the inoperable channel shall be restored to

the operable status within two hours or-take the action required by table

3.3.2-1. The table requires for the Group 6 RHR shutdown cooling mode

isolation (RHR cut in permissive pressure - high) to lock the affected

system isolation valves closed within one hour and declare the affected

system inoperable.

The valves listed in Technical Specification 3.6.3 that were controlled

by Group 6 isolation for Division II electrical distribution were not

locked closed within three hours (i.e. 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to restore + 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to

lock closed). These valves were IE12-F009 (inboard RHR shutdown cooling

suction valve) and IE12-F099A and B (RHR shutdown cooling injection

bypass around check valve). The 1E12-F009 valve did have its power

supply turned off, but not " locked" off. The remaining valves had the

power supplies on. The valves all remained closed after the isolation

permissive was removed, but could have beer, manually opened. The failure

to lock the valves closed within the Limiting Condition for Operation

time allowed by Technical Specifications is considered a violation

(373/86040-03(DRP)).

On November 7, 1986 at 6:00 a.m., while performing LOS-AA-WI,

" Technical Specification Weekly Surveillance" on Unit 2, the licensee

was exercising control rod 42-47 when it started drifting in from the

48 position. The rod continued to drift into the 00 position, fully

. inserted into the reactor core. Subsequent investigation in to this

event determined that the solenoid operated Directional Control Insert

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Valve (123) had some chips of metal which prevented the plunger in the '..

valve from operating. The valve then stuck open which caused the control' W

rod to continuously drift in. The valve was replaced and the control

rod tested and returned to service. All systems functioned as expected.

The licensee is investigating the source of the metal chips which caused

the problem. _This item will remain open (374/86040-01(DRP)).

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5. Monthly Maintenance Observation (62703) w4

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The-inspector observed work on-the leaking Unit 1 B/C Residual Heat

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Removal (RHR) water leg pump 1E12-C003 (Work Request No. 61981). The - A

work involved replacement of a piece of metal tubing and new fittings. }. ,

The inspector observed the removal and replacement of a Traversing Incore - -

Probe (TIP) detector on Unit 1. The inspector attended the pre-job '

meeting, the_ actual job, and a post job critique. .The coordination ..

between the maintenance department and radiation protection department "

was.well planned and executed. The defective TIP detector was removed,

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transported, and placed in the Unit I refuel pool. The new TIP detector

was then installed and tested.

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On November 11, 1986 the licensee had informed the resident inspectors -

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that a section of the station lake make-up piping had ruptured. The lake

make-up system was shut down, isolated, and the piping drained down.

-The locaticn of the rupture was off site by approximately 1-2 miles,"

between the river and station cooling lake. By November 13, 1986 the

ground around the ruptured section of pipe had been removed, the damage ,

evaluated, and a new section of pipe ordered. The make-up line is a 60 ,

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inch diameter, prestressed concrete with metal liner pipe. Repairs to .

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thepipinysystemareexpectedtotakeapproximatelyoneweek. An

operation s concern arises if the cooling lake level through evaporation-

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becomes too low causing the units to be shut down due to insufficient

suction for the circulating water pumps. The repair to the piping system .. ..',

should be completed well before the tire that the lake level becomes a *'fq

concern. +

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6. Training (41400) e

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The inspector, through discussions with personnel and a review of -

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training records, evaluated the licensee's training program for ,

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operations and maintenance personnel and determined that the general ~",,*# o

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knowledge of the individuals was sufficient for their assigned tasks , s

7. Licensee Event Reports (92700) [ ,

Through direct observations, discussions with licensee personnel, and

review of records, the following Licensee Evert Reports (LER's) were

reviewed to determine that reportability requirements were fulfilled,

immediate corrective action was accomplished, and corrective action +to

prevent recurrence had been accomplished in accordance with Technical -

Specifications. ,

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' (Closed) 373/86022-02 - Shutdown cooling isolation due to operator

operating the wrong keylock switch. This revision was issued to correct

the date in the abstract.

(Closed) 373/86029-00 - The (plus or minus) 24 VDC blown fuses for the

SRM'and IRM operability. Fuse failure gave no indication of system

inoperability. Corrective actions were taken and LaSalle has other

safety systems that would mitigate any potential problems concerned

with SRM's or IRM's being inoperable.

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' (Closed)-373/86032-00 - Unit 1 S.0.R. switches 1821-N024A and 1821-N037AB

not actucting at proper level setting and exceeding their respective

Technical Specification LCO's. This event was documented in Inspection

f. Report 374/86023.

Closed) 374/86016-00 - Missed suppression pool high level alarm

% (surveillance.This event was docutented in Inspection Report 374/86036.

[dpen)374/86012-01- Improper terminations of environmentally qualified

/ equirment. This revision was issued to include the Architect Engineer's

,; Mresult'5/vf testing with Raychem overlap less then manufacturer's

recomme ded overlap. Followup on this event was documented in Inspection

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Report 374/86035. This LER was transferred to Region III for final

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closing.

2(Closed)

Dolation374/86006-01

occurred which - On Marchthe

isolated 2, 1986, a Group

Reactor WaterVCleanup

primary System

containment

(RWClt) . This revision presented the apparent cause as failure of a valve

motor. A com'lete p description of the event was presented in Inspection

Report 374/86008.

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(Closed) 373/86025-01 - This revision presented the probable cause of a

w . ppuricus actuation of the 2C hi-radiation monitor as its return to

! . service after a calibration prior to the reinstallation of the detector

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(Closed) 373/86021i01 - This revision presented the probable cause of a

spurious trip of'the 2D hi-radiation monitor as a bad connector from the

, indicator relay at the detector housing. The connector was replaced.

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AlsoseeLER373{F6030-01.

%. -(Closed) 373/86030-01"- This revision presented the probable cause of a

spurious trip of the 20 hi-radiation monitor as a bad connector from the

indicator relay at the detector housing. The connection was replaced.

Also see LER 373/86021-01.

(Closedi 373/86037-00 - Group II and Group IV containment isolation due

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to inadequate out-of-service. This event was documented in Inspection

Report 373/86035.

(Closed)373/5N38-00-DuringstartupfromColdShutdown, Unit 1

experienced a. Croup I (MSIV) isolation and reactor scram due to an

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erroneous mode switch manipulation. A complete description of the event

and followup is detailed in Inspection Report 373/86035.

j' (Ciosed) 374/86017-00 - Technical' Specification LC0 exceeded. Remote

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. shutdown panel indication inoperable _ due to failure to recognize

Technical Specification related equipment. Residual heat removal heat

exchanger service water outlet temperature indication was not functioning

due to out-of-service to replace thermocouple.,

(Closed) 373/86029-01 - Intermediate Range Monitors (IRM's) potential

inoperability due to blown fuse in (plus or minus) 24 VDC power supply.

LaSalle does not intend to modify the system due to other controlling

systems already established.

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(Closed) 373/85004-00 - Hi Rad Door #396 to the Unit 1 Rx building

  • equipment drain pump room went into alarm without reset. Investigation

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,found this door to be closed but not latched,'thus having no positive

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control over entry which is contrary to Technical Specification 6.1.1.

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The cause of the occurrence was determined to be a faulty door latch.

The latch was repaired. Reviev. of dosimetry records was performed and

no unauthorized exposure occur encas had taken place.

(Closed) 373/85005-00 - The Station Control Room Engineer was informed

that the Unit 1 Standby Gas Treatment (SBGT) train had been declared

inoperable. Since the Unit 2 SBGT train was already inoperable, a

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shutdown of Units 1 and 2 was commenced as specified by Technical

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Specification 3.0.3. The SBGT replacement heaters exceeded the maximum

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power output requirements of Technical Specification 3.6.5. A GSEP alert

was declared. Upon subsequent review and discussions with the licensee's

, corporate' command center, NRC Region III, and NRR, it was determined that

l the SBGT replacement heaters were adequate to allow continued operation

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(Closed) 374/85002-00 - Unit 2 High Pressure Core Spray (HPCS) pump

suction valve to the suppression pool opened while the normal suction

valve to the cycled condensate storage tank closed. The cause of the

, valve transfer was attributed to high suppression pool level. Transfer

on high suppression pool level is a designed function. High suppression

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pool level is due to minor valve leakage. The suppression pool level

was lowered and the normal HPCS suction flow path was reestablished.

(Closed) 374/85003-00 - An air particulate sample from the Unit 2 Standby

Gas Treatment System was collected and analyzed during the period of

December 13 to December 14, 1984. Technical Specification 4.11.2.1.2

requires an off site dose calculation to be performed. This was not done

, 3 due to misplacement of the hard copy computerized analysis information

sheet.

A thorough' search of possible locations for the missing paperwork was

conducted. Off site dose calculations prior to and subsequent to the

incident were reviewed for trends. All fractions resulting from off site

dose calculations are less than 1% for all limits. All other off site

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dose calculations indicate no abnormal releases during this time period.

The continued proper routing of paperwork requiring off site dose

calculation has been re-emphasized to responsible personnel.

(Closed) 374/85021-00 - Cables 2LD054 and 2LD'052 had been mislabeled

and thus were miswired in the control room. This resulted in ambient

temperature sensors being wired to a differential temperature trip

unit and a differential temperature sensor to be wired to an ambient

temperature trip unit. The error appeared to have taken place during

initial construction. The wiring error was corrected and the systems

were checked. Also, on a periodic basis, all detectors are heat checked

to validate proper wiring and functional operation.

The last five LER's were closed in this report to correct an

administrative error in failure to close them in previous reports.

These events had been reviewed at the time they occurred by the resident

inspectors and action was taken at that time.

8. Licensee Action on an IE Bulletin (92703)

(Closed) IE Bulletin 86-03 (373/86-03-BB; 374/86-03-BB): Region III

requested the inspectors to evaluate the licensee's response to IE

Bulletin 86-03 by C. Norelius' memo dated November 5, 1986. The licensee

issued a response on November 14, 1986. This bulletin describes a

single-failure vulnerability in the minimum flow recirculation line of

Emergency Core Cooling System (ECCS) pumps that could cause a failure of

more than one ECCS train. The failure of multiple trains in an ECCS due

to a single failure violates the single failure criterion in General

Design Criterion (GDC) 35 of 10 CFR 50, Appendix A.

The ECCS at LaSalle County Station is not vulnerable to the multiple

train failure due to a single failure in a minimum flow recirculation

line since each ECCS pump has an individual minimum flow valve which is

fed from an individual Motor Control Center (MCC) 480V breaker. Failure

of any minimum flow valve and/or breaker will potentially cause the loss

of only one ECCS pump. Therefore, multiple ECCS failures will not occur

due to loss of one minimum flow valve or MCC breaker.

This problem was addressed specifically for the Residual Heat Removal

(RHR) system in IE Bulletin 86-01 which was summarized and closed in

Inspection Report 373/86025.

The inspector reviewed the licensee's response and found the content to

satisfy inspection procedure 92703. This item is considered closed.

9. Followup of 10 CFR 50.54(f) Request for Information (71707, 30702)

On October 16, 1986 a management meeting between the NRC and the licensee

was held at the U.S. Nuclear Regulatory Commission's Regional Office to

discuss the licensee's progress in resolving the NRC's concerns related

to the overall operation of the LaSalle County Station. These concerns

were expressed to the licensee by letter, dated November 22, 1985. The

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meeting was attended by Mr. J. G. Keppler, NRC Region III Administrator

and members of his staff, and Mr. J. J. O' Conner of Commonwealth Edison

and members of his staff.

The discussion included a progress report of the licensee's commitments

for improved performance and a followup on the error free start up and

operation of LaSalle Unit 2. It was noted and agreed that significant

progress was being made toward improved performance in all areas of

concern. Also included in the meeting was an update of activities on

the Static-0-Ring switches, a review of recent personnel errors and

Engineered Safety Feature (ESF) actuations, and a review of the Unit 1

startup and power ascension.

10. Part 21 Followup (92701)

The inspectors received a 10 CFR 21 notification concerning a potentially

significant safety problem resulting from the failure of springs in

solenoid globe valves manufactured by Valcor Engineering Corporation.

This problem was also addressed in IE Information Notice 86-72. The Part

21 was sent to the inspectors by memorandum from C. E. Norelius dated

October 28, 1986. The residents forwarded a copy of the Part 21 to the

Assistant Superintendent of Technical Services.

The licensee has completed their review of the extent of implementation

of this type of Valcor valve at LaSalle County Station. This review by

the licensee indicates that no valves of this specific type are currently

in use on safety-related systems which contain borated water or reactor

chemistry water. The inspector reviewed the licensee's documentation and

finds the review and documentation acceptable. This item is closed.

(373/86040-05; 374/86040-02)

11. General Site Emergency Plan (GSEP) Orill (82205)

On November 5, 1986 the site held an unannounced GSEP assembly drill.

The drill went well with a few exceptions. There were twenty people who

were not logged in on the computer as assembling. Of the twenty people

not logged in, twelve had logged in at the assigned card reader in the

control room. Due to a computer software problem, the card reader used

did not record those persons as having used a designated assembly card

reader. Six of the twenty people not logged in were interviewed and

found to have logged in correctly, but due to card reader errors, had

not been recorded by the computer. Two of the twenty people, contractors,

did not acknowledge the assembly alarms and did not assemble, The

remainder of the drill was executed well and no other problems were

encountered.

12. Regional Request (92703)

The Region III office received a memorandum from R. L. Baer, Office of

Inspection and Enforcement, dated September 30, 1986 requesting the

resident inspectors to followup on the licensee's actions taken with

respect to the Ir.termediate Range Monitor (IRM) fuse failure event which

occurred at Monticello.

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The IRM system is required for startup per the Technical Specifications

for adequate neutron monitoring capability. It was shown that a

Monticello type single failure event occurring at LaSalle will not

unexpectedly and unknowingly result in an IRM trip system being left

inoperable. The General Electric analysis of LaSalle's IRM circuitry

concluded that for a single failure event that would cause the (plus or

minus) 24 VDC IRM chassis fuses on one RPS bus to blow, the operator

would detect the failure of the +24 VDC fuses. In order to make sure

that the -24 VDC fuses are checked, a placard has been placed above the

IRM and SRM chassis drawers stating that if any of the (plus or minus)

24 VDC chassis fuses are found defective or blown, check all the fuses

on the same bus and perform the weekly IRM/SRM functional tests (these

functional tests, performed weekly when in startup or shutdown, cannot be

performed successfully if any of the (plus or minus) 24 VDC chassis fuses

are defective) upon completion of troubleshooting. The reason the note

applies also to the SRM's is that at LaSalle the SRM and IRM electronics

are powered by the same power supply. There are also 6 AMP panel fuses

linking both systems. If any of these fuses should blow, as a minimum,

an RMCS rod block will occur preventing further rod pulls. Thus, LaSalle

is now protected against a single failure like the one that occurred at

Monticello. General Electric is not aware of any other single failure

event that would cause multiple undetected IRM channel failures, i.e.,

anything that would cause just the 4 -24 VDC IRM chassis fuses on one bus

to blow.

There are no safety consequences at LaSalle due to the fact that LaSalle

has hardware systems that Monticello does not (RSCS,' RWM, and 15% APRM

setdown upscale trip). The two events of concern, rod drop accident, and

the continuous rod withdrawal transient, are bounded by the 15% APRM

setdown upscale trip.

In addition, Sargent and Lundy performed a review of the possible design

problem. They concluded, based on a review of the FSAR and Regulatory

Guide 1.47, that no circuit modification is required.

In Inspection Report 373/86025; 374/86026, it was stated that actions

taken by the licensee were:

A. A warning label was to be placed on each SRM/IRM chassis to help the

operator in diagnosing a problem.

A plaque has been placed on the IRM/SRM drawers to check all the

(plus or minus) 24 VDC chassis fuses if any are found blown or

defective, and perform weekly surveillance upon completion of

troubleshooting. To date the licensee has completed item 1.

B. A long term hardware modification is to take place. Two SRM/IRM

modifications are being evaluated and will be submitted to the

licensee for review after a safety analysis has been performed.

Concerning item 2, the licensee has elected to not pursue the

modifications. Due to the reviews performed by General Electric

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and Sargent & Lundy, coupled with the hardware systems already in

place at LaSalle, the licensee is electing not to pursue the issue

any further.

In a memorandum from G. C. Wright to C. E. Norelius dated August 23,

1986, the resident inspectors were requested to perform an inspection on

items of concern pertaining to the Brookhaven National Laboratory (BNL)

Report on LaSalle's modification program.

Commonwealth Edison listed responses to the eight concerns identified in

section 2 of the BNL report. Followup on seven of the eight items was

necessary.

Item 1 - Closed (0 pen Item 373/86040-04A(DRP)).

The training of personnel, especially licensed operators, on the system

changes resulting from a modification, should be accomplished prior to

declaring the modification operable.

A. Procedures LAP-1300-2, " Modifications," and LAP-200-3 pertaining

to shift change, and the Administration and Course Management

Information (ACMI) for license requalification have been revised

to reflect new or changed requirements due to modifications.

B. Training on modifications completed after issuance of the BNL report

has been thorough and effective.

Item 2 - Closed (0 pen Item 373/86040-04B(DRP)).

Modification 83-018 regarding the upgrade of the de system instrumentation

and annunciation should specify that procedures be changed and operator

training be conducted prior to returning the modified system to service.

Commonwealth Edison's response was adequate. No further action is

necessary.

Item 3 - Open (0 pen Item 373/86040-04C(DRP)).

Conflicting setpoint information provided in the CRD Auto Scram

modification package (82-305) should be resolved by approved documentation

within the package.

The concern was to determine if the Control Rod Drive (CRD) charging

water header pressure instrument calibration setpoint was adequate to

meet the design setpoint when the inaccuracies of the calibration method

and plant instruments were taken into consideration. The Technical

Specification instrument setpoint for this reactor trip was greater than

or equal to 1157 psig (TS Table 2.2.1-1, Functional Unit 13.a). The

allowable value was greater than or equal to 1134 psig. The engineering

calculations determined the 1157 setpoint by considering all of the

system, calibration, and environmental inaccuracies. Setting the CRD

low charging header pressure at greater than or equal to 1157 will

ensure the analyzed inaccuracies will keep the trip setpoint range of

uncertainty from reaching the Limiting Safety System Setting (1134).

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Engineering Change Notice (ECN) No. PFL-67-LS-A, pages 11 and 12, changed

the range of the pressure transmitter (500 to 1500 psig), and the trip.

unit setpoint to 1170 psig. The licensee was setting the trip setpoint

at 1170. This was performed in surveillance procedure, " Control Rod

Drive Water Header Low Pressure Scram Calibration," LIS-RD-104 (Unit 1)

-and LIS-RD-204 (Unit 2).

Further review of the two procedures determined the static head

correction (2.25 psig) in Section E.8 was not considered in the

calibration. Both procedures stated the head correction was less than

0.1% of full calibrated range. The 0.1% was based on'the previous design

, (range of 0 to 2500 psig). The present design uses a range of 500 to

1500 psig (span of 1000). This makes the head correction 0.225% of

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- calibrated range.

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The head correction acts in the non-conservative direction. The present

calibration method in both procedures sets the desired trip setpoint to

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open at-1170 psig with an allowable tolerance of.1157 to 1183. The ,

actual trip setpoint will be (1170-2.25) 1167.75 psig with a tolerance

of 1154.75 to 1180.75. The actual trip setpoint will be different from

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what was stated in design documents (1170) and the lower setpoint limit -

(1154.75) will exceed the Technical Specification trip setpoint value

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(1157).

Static head corrections are not included in the setpoint design

calculations. They are determined after field installation of the
transmitter and may have a measurable affect on the instrument loop

calibration.

This item will remain open pending the licensee's resolution of section

E.8 and inclusion of the head correction in the instrument loop

calibration for procedures LIS-RD-104 and LIS-RD-104 and LIS-RD-204.

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Item 4 - Closed (0 pen Item 373/86040-04D(DRP)).

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Completed engineering and design of the modification, including a

physical walkdown of the proposed installation, should be conducted

prior to submittal of the package to the plant.

Although Commonwealth Edison's response appeared to have only addressed

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actions for the upcoming Unit 2 refueling outage, they do in fact have a

i program in place for reviewing all modifications with respect to design

problems, conflicts with current station equipment configuration, review

for potential reduction of Field Change Requests (FCR's) and verification

, walkdowns.

- Item 5 - Closed (0 pen Item 373/86040-04E(DRP)).

An excessive turnaround time for drawing changes resulting from

modifications exists which could increase the potential for operating

errors.

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A. The Proactive Management Plan.has established a goal'of six months

for a turnaround time for processing of drawing changes. fTo date

this appears adequate. The LaSalle site is monitoring the progress

of drawing. change turnaround time and may try to decrease this time

. frame even further.

B. There is a program in place to monitor the status of the drawing

changes prior to the six month time limit established. Periodic

printouts of the outstanding drawing changes are reviewed and

tracked for completion within the established time limit.

Item 6 - Closed (0 pen Item 373/86040-04F(DRP)).

Quality Assurance (QA) involvement in the_ station modification program-

sh'ould address the operationally significant aspects of the program.

The QA department, in compliance with.their program, has: (1) established

requirements necessary to perform audits on modifications, and (2) has

physically performed the. audits prior to signing _the Modification ,

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Approval Sheet. The inspector reviewed the program requirements and

reviewed an audit performed on a recent modification,

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Item 7 - Closed (0 pen Item 373/86040-04G(DRP)).

Licensed operators should be made aware of precedure and Technical

Specification changes resulting from certain safety related modifications

activities prior to system operability.

This item is similar to Item 1. All the applicable revisions to

. procedures LAP-1300-2, LAP-200-3 and the ACMI for License

Requalification have been made. These actions to date have been

effective in notifying on shift personnel of Technical Specification

and procedural changes relating to critical modifications.

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Item 8 - Closed (0 pen Item 373/86040-04H(DRP)).

An inventory of " critical control room drawing" status is performed on

a quarterly basis. The results of the inventory should be reviewed by

technical staff management to insure appropriate action is taken to

correct discovered * discrepancies.

The licensee's response appeared to meet the recommendations of

Brookhaven. A consideration for the licensee was to possibly increase

the frequency of the audits on inventory check of critical control room

drawings. The inspector held a discussion with the licensee on reviewing

their present audit schedule and to give some consideration to increasing

the frequency of their audits.

-13. Temporary Instruction (TI) (92701)

TI 2515/75 requested a followup inspection of the limitorque motor valve

operator wiring to determine if wiring is environmentally qualified.

This licensee was one of the first sites in 1985 to identify this

problem. Inspec, tion Report 373/85039; 374/85040, paragraph 2.a.,

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documents the inspection conducted in November and December 1985 on

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miswiring and unqualified wiring of limitorque operators. The

inspection documents the licensee's action taken to resolve the problem.

The inspection was conducted prior to issuance of this TI; however, a

review of the inspection report indicates the action required by the TI

had been completed. A followup inspection in July 1986 (IR 373/86030;

374/86031) addressed the notices of violation identified in the previous

inspection and closed all items concerned. Based on these two

inspections, this TI is considered closed.

14. Open Items

Open items are matters which have been discussed with the licensee, which

will be reviewed further by the inspector, and which involve some action

on the part of the NRC or licensee or both. Open items evaluated and

closed during the inspection are discussed in Paragraphs 10 and 12.

Open items disclosed during the inspection are discussed in Paragraph 4.

15. Exit Interview (30703)

The inspectors met with licensee representatives (denoted in Paragraph 1)

throughout the month and at the conclusion of the inspection period and

summarized the scope and findings of the inspection activities. The

licensee acknowledged these findings. The inspector also discussed the

likely informational content of the inspection report with regard to

documents or processes reviewed by the inspector during the inspection.

The licensee did not identify any such documents or processes as

proprietary.

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