Letter Sequence Other |
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Results
Other: ML20147C490, ML20149E859, ML20151B320, ML20155D675, ML20197B030, ML20199B161, ML20204F596, ML20210R060, ML20211B406, ML20211B442, ML20212H574, ML20212H582, ML20214E205, ML20214L960, ML20215H383, ML20215H397, ML20234F422, ML20235R405, ML20235R426, ML20236D305, ML20236D319, ML20236P920, ML20245E060, ML20245E067
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MONTHYEARML20155D6751985-12-31031 December 1985 Annual Nonradiological Environ Monitoring Rept,1985 Project stage: Other ML20211B4421985-12-31031 December 1985 Annual Radiological Environ Operating Rept for 1985 Project stage: Other ML20210R0601986-02-24024 February 1986 Staff Assessment of Environ Radioactive Contamination in Vicinity of Rancho Seco Nuclear Power Plant Project stage: Other ML20214E2051986-03-0303 March 1986 Forwards Semiannual Radioactive Effluent Release Rept,Jul- Dec 1985. Changes to Offsite Dose Calculation Manual, Process Control Program & Rept Corrections Included. Operational & environmentally-related Events Discussed Project stage: Other ML20214L9801986-04-0101 April 1986 Summary of 860325 Meeting W/Epa Re Offsite Contamination Problems & Requirements of 40CFR190 Project stage: Meeting ML20197B0301986-04-30030 April 1986 Informs That Util Will Submit Completed 1985 Annual Radiological Environ Operating Rept by 860530.Delay Due to Difficulties in Completing Liquid Effluent Pathway Land Use Census Project stage: Other ML20211B4061986-05-27027 May 1986 Forwards 1985 Annual Radiological Environ Operating Rept, Including Parts I & II of Environ Radiological Studies Downstream from Rancho Seco Nuclear Power Generating Station - 1985 Project stage: Other ML20199B1611986-06-0505 June 1986 Special Rept 86-08 Re Max Hypothetically Exposed Individual Surpassing Numerical Guides for Design Objectives of 10CFR50,App I.More Appropriate Modeling Techniques Encl. Offsite Dose Calculation Manual Revised Project stage: Other ML20204F5961986-07-0303 July 1986 Responds to NRC Re Violation Noted in Insp Rept 50-312/86-15.Corrective Actions:Util Will Submit Amend to Tech Spec Table 4.21-1 Re Radioactive Liquid Waste Sampling Prior to Startup Project stage: Other IR 05000312/19860231986-07-18018 July 1986 Enforcement Conference Rept 50-312/86-23 on 860620.Major Areas Discussed:Violation Noted During Insps of Emergency Preparedness Program & Radioactive Effluent Mgt (Insp Repts 50-312/86-14 & 50-312/86-15) Project stage: Request ML20212G1351986-07-22022 July 1986 Advises That Changes to Radiological Effluent Tech Specs Should Be Proposed to Eliminate Possibility of Unacceptable Radiation Levels in Liquid Effluents.Evaluation of 860224 Rept Encl.Meeting Requested Project stage: Meeting ML20214L9601986-08-29029 August 1986 Forwards Documentation Summarizing NRC Actions to Close Out Offsite Contamination Issue,In Response to 860325 Request Project stage: Other ML20055C2251986-09-30030 September 1986 Responds to NRC 860718 Request for Addl Info Re Plant Liquid Effluents.Requested Info Will Be Provided by End of Nov 1986 Due to Magnitude of Effort Required Project stage: Request ML20245E0671986-12-0202 December 1986 Forwards Util Response to 860718 Inquiry Into Operations & Mgt of Plant Liquid Effluent Program.Util Considers That Discharge of Radioactive Matl in Liquid Effluents Allowable by Tech Specs within Limits of 10CFR20,App B Project stage: Other ML20245E0601987-01-0505 January 1987 Forwards Revs to Util 861202 Response to NRC Liquid Effluent Inquiry for Clarification,Per 861222 Discussion W/R Meeks Project stage: Other ML20212H5821987-01-12012 January 1987 Radiological Effluent Release & Radiological Environ Operating Repts for 1984,Rancho Seco Nuclear Generating Station, Technical Evaluation Rept Project stage: Other ML20212H5741987-01-16016 January 1987 Forwards TER-C5506-657, Radiological Effluent Release & Radiological Environ Monitoring Operating Repts for 1984, Rancho Seco Nuclear Generating Station, Technical Evaluation Rept Project stage: Other ML20245E0631987-02-19019 February 1987 Forwards Response to NRC 861224 Request for Addl Info Re Inquiry Into Operations & Mgt of Plant Liquid Effluent Program.Response Completes Util Efforts to Provide Requested Info Project stage: Request ML20205S8181987-02-25025 February 1987 Notification of 870303 Meeting W/Util in Bethesda,Md to Review Discrepancies in Plant Liquid Effluent Program & to Discuss Changes to Tech Specs & Offsite Dose Calculation Manual to Correct Identified Discrepancies Project stage: Meeting ML20197D4831987-04-0707 April 1987 Summary of 870303 Meeting W/Util in Bethesda,Md Re Problems Identified W/Facility Liquid Effluent Program & Proposed Corrective Actions.Attendance List Encl Project stage: Meeting ML20215H3831987-04-15015 April 1987 Forwards Rev 1 to Procedure R-0775, Facility Change Safety Analysis. Design Bases of Current Mod to Secondary Waste Water Sys Not Intended to Be Equivalent to Evaporation Ponds Described in Submittal Project stage: Other ML20215H3971987-04-15015 April 1987 Rev 1 to Procedure R-0775, Facility Change Safety Analysis Project stage: Other ML20209C7401987-04-20020 April 1987 Confirms Commitments Made During 870303 Meeting W/Nrc in Bethesda,Md Re Radiological Liquid Effluent Matters.Dose Based Surveillance Std Appropriate for Ensuring Compliance w/10CFR50,App I Regulation.List of Commitments Encl Project stage: Meeting ML20235F7541987-06-30030 June 1987 Application for Amend to License DPR-54,consisting of Amend 155,revising Tech Specs Re Radiological Effluents to Ensure Compliance W/Regulatory Requirements Concerning Effluent Monitoring & Nearby Land Use Identification.Fee Paid Project stage: Request ML20235R4051987-10-0303 October 1987 Rev 1 to Proposed Amend 155,revising Radiological Effluent Tech Specs to Incorporate Clarifications & Correct Editorial Errors Project stage: Other ML20235R4261987-10-0303 October 1987 Proposed Radiological Effluent Tech Specs,Incorporating Clarifications & Correcting Editorial Errors Project stage: Other ML20236D3191987-10-0707 October 1987 Rev 0 to Radiological Environ Monitoring Program Manual Project stage: Other ML20236D3051987-10-20020 October 1987 Forwards Rev 0 to Radiological Environ Monitoring Program Manual, for Review in Support Evaluation of Proposed Amend 155 to License DPR-54 Project stage: Other ML20236P9201987-11-12012 November 1987 Forwards Radioactive Liquid Effluent Sys Description Including P&Id,Design Criteria,Instrumentation & Control Measures to Support Evaluation of Proposed Amend 155 Project stage: Other ML20149E8591987-12-22022 December 1987 Proposed Tech Specs,Establishing New Set Lower Limits of Detection for Prebatch Release & Composite post-release Analyses Project stage: Other ML20149E8521987-12-23023 December 1987 Supplemental Application for Amend to License DPR-54, Consisting of Rev 2 to Proposed Amend 155,establishing New Set of Lower Limits of Detection for Prebatch Release & Composite post-release Analyses Project stage: Supplement ML20234F4221987-12-27027 December 1987 Forwards Rev 5 to AP.310, Offsite Dose Calculation Manual, for Review to Support Evaluation of Proposed Amend 155, Rev 2.Rev Incorporates Results of Verification & Validation as Well as NRC & Internal Reviews Project stage: Other ML20147C4901988-01-0505 January 1988 Forwards Fr Notice of Consideration of Issuance of Amend to License DPR-54 & Proposed NSHC & Opportunity for Hearing on 870630 Request Re Revs to Radiological Effluent Tech Specs Project stage: Other ML20149E2561988-01-0707 January 1988 Forwards Supplemental Info to Radioactive Liquid Effluent Sys Description Provided Via Ltr Gca 87-763 Dtd 871112,to Support Evaluation of Rev 2 to Proposed Amend 155.Concerns Raised Re Radioactive Liquid Effluent Sys Listed Project stage: Supplement ML20148J8111988-03-17017 March 1988 Forwards Amend 98 to License DPR-54 & Safety Evaluation. Amend Revises Tech Specs,Reducing Lower Limits of Detection for Liquid Radioactive Effluents & Changing Requirements to Address Hardware Changes in Effluent Sys Project stage: Approval ML20151B3201988-03-30030 March 1988 Forwards Errata to Amends 97 & 98 to License DPR-54, Correcting Inadvertent Errors in Tech Specs Project stage: Other 1987-10-20
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p hSMUD SACRAMENTO MUNICIPAL UTILITY DISTRICT C 62o1 S Street. P.o. Box 15830, Sacramento CA 95852-1830.(916) 452-3211 RJR 86-087 AN ELECTRIC SYSTEM SERVING THE HEART OF CALIFORNIA March 3, 1986 J B MARTIN ADMINISTRATOR U S NUCLEAR REGULATORY COMMISSION REGION V 0FFICE OF INSPECTION AND ENFORCEMENT 1450 MARIA LANE SUITE 210 WALNUT CREEK CA 94596 DOCKET NO. 50-312 OPERATING LICENSE OPR-54 SEMIANNUAL RADI0 ACTIVE EFFLUENT RELEASE REPORT The Sacramento Municipal Utility District hereby transmits the Semiannual Radioactive Effluent Release Report for the period of July 1, 1985 through December 31, 1985 in compliance with Technical Specification 6.9.2.3.
The format of this report follows that found in Appendix 8 of Regulatory Guide 1.21.
In addition, changes to the Offsite Dose Calculation Manual and to the Process Control Program are included as required by Technical Specification 6.9.2.3.
Corrections, if any, to previous reports are also included.
Doerational Events Rancho Seco was not operating during the period of July 1, 1985 to September 28, 1985 for plant modifications.
On September 28, 1985, the reactor achieved criticality and was brought to 40%
power on September 30, 1985 for physics testing.
The power level was reduced to 15% on October 1, 1985 to perform the turbine overspeed trip test. The reactor tripped on high coolant pressure following the turbine trip.
The plant was brought to hot shutdown, where it remained until November 2, 1985.
Criticality was achieved on November 2, 1985. The 220 KV breakers were closed on November 3, 1985 and power was leveled at 42%.
Power was reduced to 15%
and the turbine overspeed trip test performed on November 7, 1985. The breakers were reclosed on November 8, 1985 and the reactor power was brought to 42%.
The power level was increased to 75% on November 17,1985 and to 91%
on November 19, 1985. Power level remained at approximately 91% to December 5, 1985.
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B603070196 060303 PDR ADOCK 05000312 M
R PDR I
RJR 86-087 J B Martin March 3, 1986 The reactor tripped on reactor coolant system high pressure on December 5, 1985.
The reactor was brought to hot shutdown for control system maintenance until December 12, 1985.
The reactor was brought back on line on December 12, 1985.
Power was gradually increased to near 100% on December 15, 1985 and remained at 100% until December 22, 1985. On December 22, 1985, the plant was brought to hot shutdown to repair a leaking pressurizer sampling isolation valve. The reactor was brought back on line on December 24, 1985.
The plant tripped on December 26, 1986 due to loss of power to the Integrated Control System.
The plant was brought to cold shutdown for the remainder of December.
Environmentally Related Events An abnormal release occurred on July 24, 1985 associated with recirculating the "A" steam generator. Approximately 1.6 uC) of Cs-134 and 3.5 pCi of Cs-137 were released to a plant drain which discharges directly to the plant efEluent. Samples of the plant effluent indicated no detectable activity.
The carbon adsorber trays in the reactor building's exhaust air system were replaced in August 1985. The replacement became necessary due to spray painting in the reactor building.
A sample for the regenerate hold-up tank release 85-137 was taken for composite but was not included in the August composite A separate area in the hot laboratory has been set aside for storing composites to reduce confusion.
A release of noble gases occurred through the secondary steam relief valves on the December 26, 1985 plant trip. A description of the event was transmitted to your office by District letter RJR 86-075 dated February 19, 1986.
Approximately 30 gallons of tritiated water were released to the ground on the south side of the protected area on December 28, 1985.
No radiological impact is expected due to dispersion and evaporation in the soil. Samples taken at the fenceline indicated no detectable activity.
Water samples were collected in October 1985 from the regenerate hold-up tanks and the retention basins onsite at Rancho Seco for purposes of the ongoing Lawrence Livermore National Laboratory (LLNL) Rancho Seco Environmental Studies program.
The results of the analysis of these samples are included in LLNL report UCID-20641 Part I, February 6,1986 and Part II, January 23, 1986 which have been already transmitted to you.
Radionuclides were detected in these samples but at concentrations less than the Technical Specifications
RJR 86-087 J B Martin March 3, 1986' 4.21 Lower Limits of Octection requirements. However, the District will prepare a special report which will reevaluate the 1985 radiological liquid
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effluent source term and submit this report to you by August 31, 1986.
This report was prepared by R. G. Oesterling and R. L. Gardner of United Energy Services Corporation under the review and direction of E. W. Bradley, Supervising Health Physicist in the Nuclear Engineering Department.
1 If there are any questions concerning this report, please contact Mr. Bradley j
a(the,0istrictoffice.
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R. J. RODRIGUEZ ASSISTANT GENERAL MANAGER, NUCLEAR Attachment I
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