ML20203J060

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Recommends That Directorate of Licensing Take Lead Responsibility in Reviewing Safety Aspects of Vibrations in Torus & torus-ring Header During Relief Valve Operation. Licensee Stated Concern Re long-term Effects on Torus Walls
ML20203J060
Person / Time
Site: 05000000, Browns Ferry
Issue date: 12/28/1973
From: Grier B
US ATOMIC ENERGY COMMISSION (AEC)
To: Moore V
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML082390329 List: ... further results
References
FOIA-85-782 RO-C&O-73-21, NUDOCS 8604300093
Download: ML20203J060 (2)


Text

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IRANSFER OF LEAD RESPONSIBILITK' DEC 2 8 1973 Date:

Serial No.:

R0-C&O-73-21 R:

Voss A. Moore, Assistant Director for Boiling Water Reactors, L Subj ect:

Vibrations in the Torus and Torus-Ring Header During Relief Valve Operation Facility: Tennessee Valley Authority, Browns Ferry Nuclear Plant Units 1, 2 and 3 Responsible R0 Assistant Director:

B.'H. Grier Description of Item Requiring Resolution:

During testing of relief valves at the Browns Ferry 1 facility, vibrations were noted in the vicinity of the torus. As a result, special instrumentation was installed to measure the acceleration and deflection of the torus walls and torus-ring header. The licensee characterized the measured data as "more than desirable, but within the range predicted by General Electric Company." TVA has calculated critical stress points on the torus and concluded that the stresses occurring during relief valve operation are within the allowable range.

However, the licensee has stated a concern for the long-term fatigue effects on the torus wall.

TVA and other licensees have recently made modifications to their Target Rock relief valves to increase the opening response time. This is of possible significance, in that Cen.iral Electric has shown during studies made on Quad Cities 1 torus (Reference 3) that more rapid opening times for these valves result in higher transient pressures at their point of discharge into the torus.

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References:

1.

TVA - Browns Ferry 1, Abnormal Occurrence Reports,BFAO 7343W dated November 28, 1973 and Interim Report dated Deccnoer 16, 1973.

2.

Transfer of Lead Responsibility No. R0-C&O-8, dated October 18, 1973, Target Rock Safety Relief Valves.

3.

NEDO 10859, Steam Vent Clearing Phenomena and Structural Responce of the BWR Torus.

8604300093 860317 hRO

-782 PDR i

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TRANSFER OF LEAD RESPONSIBILITY DEC 2 8 1973 30 Recommendations and Proposed Course of Action:

It is recommended that the Directorate of Licensing take the lead responsibility in reviewing the safety aspects of this matter.

Concurrences:

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