ML20134H931

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Technical Specification Bases 3.4
ML20134H931
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 05/12/2020
From: Siva Lingam
NRC/NRR/DORL/LPL4
To:
Lingam S
References
Download: ML20134H931 (73)


Text

Recirculation Loops Operating B 3.4.1 BASES APPLICABLE margins during abnormal operational transients (Ref. 2),

SAFETY ANALYSES which are analyzed in Chapter 15 of the UFSAR.

(continued)

A plant specific LOCA analysis has been performed assuming only one operating recirculation loop. This analysis has demonstrated that, in the event of a LOCA caused by a pipe break in the operating recirculation loop, the Emergency Core Cooling System response will provide adequate core cooling, provided the APLHGR requirements are modified accordingly (Ref. 3).

The transient analyses of Chapter 15 of the UFSAR have also been performed for single recirculation loop operation (Ref. 3) and demonstrate sufficient flow coastdown characteristics to maintain fuel thermal margins during the abnormal operational transients analyzed provided the MCPR requirements are modified. The APLHGR and MCPR limits for single loop operation are specified in the COLR. The Maximum Extended Load Line Limit Analysis Plus (MELLLA+) operating domain is not analyzed for reactor recirculation single loop operation (SLO). Therefore, SLO is prohibited in the MELLLA+ operating domain (Ref. 4).

Recirculation loops operating satisfies Criterion 2 of the NRC Policy Statement.

LCO Two recirculation loops are normally required to be in operation with their flows matched within the limits specified in SR 3.4.1.1 to ensure that during a LOCA caused by a break of the piping of one recirculation loop the assumptions of the LOCA analysis are satisfied. Alternatively, with only one recirculation loop in operation, modifications to the required APLHGR limits (LCO 3.2.1, "AVERAGE PLANAR LINEAR HEAT GENERATION RATE (APLHGR)"), MCPR limits (LCO 3.2.2, "MINIMUM CRITICAL POWER RATIO (MCPR)"), LCO 3.2.3 Linear Heat Generation Rate (LHGR), and LCO 3.3.1.1, RPS Instrumentation, must be applied to allow continued operation consistent with the assumptions of References 3.

The LCO is modified by a Note which allows up to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> before having to put in effect the required modifications to required limits after a change in the reactor operating conditions from two recirculation loops operating to single recirculation loop operation. If the required limits are (continued)

GRAND GULF B 3.4-3 LBDCR 16070

Recirculation Loops Operating B 3.4.1 BASES (continued)

SURVEILLANCE SR 3.4.1.1 REQUIREMENTS This SR ensures the recirculation loop flows are within the allowable limits for mismatch. At low core flow (i.e., < 70% of rated core flow), the MCPR requirements provide larger margins to the fuel cladding integrity Safety Limit such that the potential adverse effect of early boiling transition during a LOCA is reduced. A larger flow mismatch can therefore be allowed when core flow is < 70% of rated core flow. The recirculation loop jet pump flow, as used in this Surveillance, is the summation of the flows from all of the jet pumps associated with a single recirculation loop.

The mismatch is measured in terms of percent of rated core flow. This Surveillance can be met by verifying that the recirculation loop drive flow mismatch, when two loops are in operation, is < 5% of rated recirculation drive flow with core flow t 70% of rated core flow and < 10% of rated recirculation drive flow with core flow < 70% of rated core flow.

This SR is not required when both loops are not in operation since the mismatch limits are meaningless during single loop or natural circulation operation. The Surveillance must be performed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after both loops are in operation. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

(continued)

GRAND GULF B 3.4-7 LBDCR 18127

Recirculation Loops Operating B 3.4.1 BASES (continued)

REFERENCES 1. UFSAR, Section 6.3.3.7.

2. UFSAR, Section 5.4.1.1.
3. UFSAR, Chapter 15, Appendix 15C.
4. NEDC-33006P-A, Maximum Extended Load Line Limit Analysis Plus, Revision 3.
5. Deleted GRAND GULF B 3.4-8 LBDCR 16070

FCVs B 3.4.2 BASES ACTIONS B.1 (continued)

If the FCVs are not deactivated (locked up) and cannot be restored to OPERABLE status within the associated Completion Time, the unit must be brought to a MODE in which the LCO does not apply. To achieve this status, the unit must be brought to at least MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. This brings the unit to a condition where the flow coastdown characteristics of the recirculation loop are not important. The allowed Completion Time of 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> is reasonable, based on operating experience, to reach MODE 3 from full power conditions in an orderly manner and without challenging unit systems.

SURVEILLANCE SR 3.4.2.1 REQUIREMENTS Hydraulic power unit pilot operated isolation valves located between the servo valves and the common "open" and "close" lines are required to close in the event of a loss of hydraulic pressure. When closed, these valves inhibit FCV motion by blocking hydraulic pressure from the servo valve to the common open and close lines as well as to the alternate subloop. This Surveillance verifies FCV lockup on a loss of hydraulic pressure.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

SR 3.4.2.2 This SR ensures the overall average rate of FCV movement at all positions is maintained within the analyzed limits.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

(continued)

GRAND GULF B 3.4-11 LBDCR 18127

FCVs B 3.4.2 BASES REFERENCES 1. UFSAR, Section 15.3.2.

2. UFSAR, Section 15.4.5.

GRAND GULF B 3.4-12 LBDCR 18127

Jet Pumps B 3.4.3 BASES (continued)

SURVEILLANCE SR 3.4.3.1 REQUIREMENTS This SR is designed to detect significant degradation in jet pump performance that precedes jet pump failure (Ref. 2). This SR is required to be performed only when the loop has forced recirculation flow since surveillance checks and measurements can only be performed during jet pump operation. The jet pump failure of concern is a complete mixer displacement due to jet pump beam failure. Jet pump plugging is also of concern since it adds flow resistance to the recirculation loop. Significant degradation is indicated if the specified criteria confirm unacceptable deviations from established patterns or relationships. The allowable deviations from the established patterns have been developed based on the variations experienced at plants during normal operation and with jet pump assembly failures (Refs. 2 and 3). Since refueling activities (fuel assembly replacement or shuffle, as well as any modifications to fuel support orifice size or core plate bypass flow) can affect the relationship between core flow, jet pump flow, and recirculation loop flow, these relationships may need to be re-established each cycle. Similarly, initial entry into extended single recirculation loop operation may also require establishment of these relationships. During the initial weeks of operation under such conditions, while baselining new "established patterns,"

engineering judgment of the surveillance results is used to detect significant abnormalities which could indicate a jet pump failure.

The recirculation flow control valve (FCV) operating characteristics (loop flow versus FCV position) are determined by the flow resistance from the loop suction through the jet pump nozzles. A change in the relationship indicates a flow restriction, loss in pump hydraulic performance, leak, or new flow path between the recirculation pump discharge and jet pump nozzle. For this criterion, the loop flow versus FCV position relationship must be verified.

Total core flow can be determined from measurements of the recirculation loop drive flows. Once this relationship has been established, increased or reduced total core flow for the same recirculation loop drive flow may be an indication of failures in one or several jet pumps.

(continued)

GRAND GULF B 3.4-15 LBDCR 18127

Jet Pumps B 3.4.3 BASES SURVEILLANCE SR 3.4.3.1 (continued)

REQUIREMENTS Individual jet pumps in a recirculation loop typically do not have the same flow. The unequal flow is due to the drive flow manifold, which does not distribute flow equally to all risers. The flow (or jet pump diffuser to lower plenum differential pressure) pattern or relationship of one jet pump to the loop average is repeatable. An appreciable change in this relationship is an indication that increased (or reduced) resistance has occurred in one of the jet pumps. This may be indicated by an increase in the relative flow for a jet pump that has experienced beam cracks.

The deviations from normal are considered indicative of a potential problem in the recirculation drive flow or jet pump system (Ref. 2).

Normal flow ranges and established jet pump flow and differential pressure patterns are established by plotting historical data as discussed in Reference 2.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

This SR is modified by two Notes. Note 1 allows this Surveillance not to be performed until 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after the associated recirculation loop is in operation, since these checks can only be performed during jet pump operation. The 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> is an acceptable time to establish conditions appropriate for data collection and evaluation.

Note 2 allows this SR not to be performed when THERMAL POWER is t 21.8% RTP. During low flow conditions, jet pump noise approaches the threshold response of the associated flow instrumentation and precludes the collection of repeatable and meaningful data.

REFERENCES 1. UFSAR, Section 6.3.

2. GE Service Information Letter No. 330, "Jet Pump Beam Cracks,"

June 9, 1990.

3. NUREG/CR-3052, "Closeout of IE Bulletin 80-07: BWR Jet Pump Assembly Failure," November 1984.

GRAND GULF B 3.4-16 LBDCR 18127

S/RVs B 3.4.4 BASES SURVEILLANCE SR 3.4.4.1 (continued)

REQUIREMENTS lift settings must be performed during shutdown, since this is a bench test, and in accordance with the Inservice Testing Program. The lift setting pressure shall correspond to ambient conditions of the valves at nominal operating temperatures and pressures. The safety lift setpoints will still be set within a tolerance of  1 percent, but the setpoints will be tested to within  3 percent to determine acceptance or failure of the as-found valve lift setpoint. If a valve is tested and the lift setpoint is found outside the 3 percent tolerance, two additional valves are to be tested (Reference 4).

The Frequency was selected because this Surveillance must be performed during shutdown conditions and is based on the time between refuelings.

SR 3.4.4.2 The required relief function S/RVs are required to actuate automatically upon receipt of specific initiation signals. A system functional test is performed to verify the mechanical portions of the automatic relief function operate as designed when initiated either by an actual or simulated initiation signal. The LOGIC SYSTEM FUNCTIONAL TEST in SR 3.3.6.5.4 overlaps this SR to provide complete testing of the safety function.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

This SR is modified by a Note that excludes valve actuation. This prevents an RPV pressure blowdown.

SR 3.4.4.3 A manual actuation of each required S/RV (those valves removed and replaced to satisfy SR 3.4.4.1) is performed to (continued)

GRAND GULF B 3.4-20 LBDCR 18127

S/RVs B 3.4.4 BASES SURVEILLANCE SR 3.4.4.3 (continued)

REQUIREMENTS verify that the valve is functioning properly. This SR can be demonstrated by one of two methods. If performed by method 1), plant startup is allowed prior to performing this test because valve OPERABILITY and the setpoints for overpressure protection are verified, per the INSERVICE TESTING PROGRAM requirements, prior to valve installation. Therefore, this SR is modified by a Note that states the Surveillance is not required to be performed until 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after reactor steam pressure and flow are adequate to perform the test. The 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> allowed for manual actuation after the required pressure is reached is sufficient to achieve stable conditions for testing and provides a reasonable time to complete the SR.

If performed by method 2), valve OPERABILITY has been demonstrated for all installed S/RVs based upon the successful operation of a test sample of S/RVs.

1. Manual actuation of the S/RV, with verification of the response of the turbine control valves or bypass valves, by a change in the measured steam flow, or any other method suitable to verify steam flow (e.g., tailpipe temperature or pressure). Adequate reactor steam pressure must be available to perform this test to avoid damaging the valve. Also, adequate steam flow must be passing through the main turbine or turbine bypass valves to continue to control reactor pressure when the S/RVs divert steam flow upon opening. Sufficient time is therefore allowed after the required pressure and flow are achieved to perform this test. Adequate pressure at which this test is to be performed is consistent with the pressure recommended by the valve manufacturer.
2. The sample population of S/RVs tested each refueling outage to satisfy SR 3.4.4.1 will be stroked in the relief mode during as-found testing to verify proper operation of the S/RV. Just prior to installation of the to be newly-installed S/RVs to satisfy 3.4.4.1 the valve will be stroked in the relief mode during certification testing to verify proper operation of the S/RV. The successful performance of the test sample of S/RVs will perform in a similar fashion. After the S/RVs are replaced, the electrical and pneumatic connections shall be verified either through (continued)

GRAND GULF B 3.4-20a LBDCR 18085

S/RVs B 3.4.4 BASES SURVEILLANCE SR 3.4.4.3 (continued)

REQUIREMENTS mechanical/electrical inspection or test prior to the resumption of electric power generation to ensure that no damage has occurred to the S/RV during transportation and installation.

This verifies that each replaced S/RV will properly perform its intended function.

If the valve fails to actuate due only to the failure of the solenoid but is capable of opening on overpressure, the safety function of the S/RV is considered OPERABLE.

The STAGGERED TEST BASIS Frequency ensures that each solenoid for each S/RV relief-mode actuator is alternately tested. The Frequency of the required relief-mode actuator testing was developed based on the S/RV tests required by INSERVICE TESTING PROGRAM. The testing Frequency required by the Inservice Testing Program is based on operating experience and valve performance. Therefore, the Frequency was concluded to be acceptable from a reliability standpoint. (Reference 5)

REFERENCES 1. Deleted

2. UFSAR, Section 5.2.2.2.3.
3. UFSAR, Section 15.
4. GNRI-96/00134, Amendment 123 to the Operating License.
5. GNRI-96/00229, Amendment 130 to the Operating License.
6. Deleted GRAND GULF B 3.4-21 LBDCR 18085

RCS Operational LEAKAGE B 3.4.5 BASES ACTIONS C.1 and C.2 (continued) 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The allowed Completion Times are reasonable, based on operating experience, to reach the required plant conditions from full power conditions in an orderly manner and without challenging plant systems.

SURVEILLANCE SR 3.4.5.1 REQUIREMENTS The RCS LEAKAGE is monitored by a variety of instruments designed to quantify the various types of LEAKAGE. Leakage detection instrumentation is discussed in more detail in the Bases for LCO 3.4.7, "RCS Leakage Detection Instrumentation." Sump level is typically monitored to determine actual LEAKAGE rates. However, any method may be used to quantify LEAKAGE within the guidelines of Reference 7.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

REFERENCES 1. 10 CFR 50.2.

2. 10 CFR 50.55a(c).
3. 10 CFR 50, Appendix A, GDC 55.
4. GEAP-5620, "Failure Behavior in ASTM A106B Pipes Containing Axial Through - Wall Flaws," April 1968.
5. NUREG-75/067, "Investigation and Evaluation of Cracking in Austenitic Stainless Steel Piping of Boiling Water Reactor Plants,"

October 1975.

6. UFSAR, Section 5.2.5.5.3.
7. Regulatory Guide 1.45, May 1973 with exceptions per UFSAR Appendix 3A.

GRAND GULF B 3.4-26 LBDCR 18127

RCS PIV Leakage B 3.4.6 BASES SURVEILLANCE SR 3.4.6.1 (continued)

REQUIREMENTS The Frequency is every 2 years and is required by the Inservice Testing Program per the ASME Code requirement (Ref. 6).

Therefore, this SR is modified by a Note that states the leakage Surveillance is only required to be performed in MODES 1 and 2. Entry into MODE 3 is permitted for leakage testing at high differential pressures with stable conditions not possible in the lower MODES.

REFERENCES 1. 10 CFR 50.2.

2. 10 CFR 50.55a(c).
3. 10 CFR 50, Appendix A, GDC 55.
4. ASME, Boiler and Pressure Vessel Code,Section XI.
5. NUREG-0677, "The Probability of Intersystem LOCA: Impact Due to Leak Testing and Operational Changes," May 1980.
6. ASME code for Operation and Maintenance of Nuclear Power Plants, 2001 Edition thru 2003 Addendum with portions of 2004 Edition, Subsection IST C-3630.
7. NEDC-31339, "BWR Owners Group Assessment of ECCS Pressurization in BWRs," November 1986.

GRAND GULF B 3.4-31 LBDCR 16269

RCS Leakage Detection Instrumentation B 3.4.7 B 3.4 REACTOR COOLANT SYSTEM (RCS)

B 3.4.7 RCS Leakage Detection Instrumentation BASES BACKGROUND GDC 30 of 10 CFR 50, Appendix A (Ref. 1), requires means for detecting and, to the extent practical, identifying the location of the source of RCS LEAKAGE. Regulatory Guide 1.45, Revision 0, (Ref. 2) describes acceptable methods for selecting leakage detection systems.

Limits on LEAKAGE from the reactor coolant pressure boundary (RCPB) are required so that appropriate action can be taken before the integrity of the RCPB is impaired (Ref. 2).

Leakage detection systems for the RCS are provided to alert the operators when leakage rates above normal background levels are detected and also to supply quantitative measurement of rates. In addition to meeting the OPERABILITY requirements, the monitors are typically set to provide the most sensitive response without causing an excessive number of spurious alarms. The Bases for LCO 3.4.5, "RCS Operational LEAKAGE," discuss the limits on RCS LEAKAGE rates.

Systems for separating the LEAKAGE of an identified source from an unidentified source are necessary to provide prompt and quantitative information to the operators to permit them to take immediate corrective action.

LEAKAGE from the RCPB inside the drywell is detected by at least one of three independently monitored variables, such as sump level changes and drywell gaseous and particulate radioactivity levels. The primary means of quantifying LEAKAGE in the drywell is the drywell floor drain sump monitoring system.

The drywell floor drain sump monitoring system monitors the LEAKAGE collected in the floor drain sump. This unidentified LEAKAGE consists of LEAKAGE from control rod drives, valve flanges or packings, floor drains, the Closed Cooling Water System, and drywell air cooling unit condensate drains, and any LEAKAGE not collected in the drywell equipment drain sump.

(continued)

GRAND GULF B 3.4-32 LBDCR 11068

RCS Leakage Detection Instrumentation B 3.4.7 BASES BACKGROUND The drywell atmospheric monitoring systems continuously (continued) monitor the drywell atmosphere for airborne particulate and gaseous radioactivity. A sudden increase of radioactivity, which may be attributed to RCPB steam or reactor water LEAKAGE, is annunciated in the control room.

Condensate from four of the six drywell coolers is routed to the drywell floor drain sump and is monitored by a flow transmitter that provides indication and alarms in the control room. This drywell air cooler condensate flow rate monitoring system serves as an added indicator, but not quantifier, of RCS unidentified LEAKAGE.

APPLICABLE A threat of significant compromise to the RCPB exists if the SAFETY ANALYSES barrier contains a crack that is large enough to propagate rapidly. LEAKAGE rate limits are set low enough to detect the LEAKAGE emitted from a single crack in the RCPB (Refs. 3 and 4).

Identification of the LEAKAGE allows the operators to evaluate the significance of the indicated LEAKAGE and, if necessary, shut down the reactor for further investigation and corrective action. The allowed LEAKAGE rates are well below the rates predicted for critical crack sizes (Ref. 5).

Therefore, these actions provide adequate response before a significant break in the RCPB can occur.

(continued)

GRAND GULF B 3.4-33 LBDCR 11068

RCS Leakage Detection Instrumentation B 3.4.7 BASES APPLICABLE RCS leakage detection instrumentation satisfies Criterion 1 SAFETY ANALYSES of the NRC Policy Statement.

(continued)

LCO The LCO requires instruments of diverse monitoring principles to be OPERABLE to provide confidence that small amounts of unidentified LEAKAGE are detected in time to allow actions to place the plant in a safe condition, when RCS LEAKAGE indicates possible RCPB degradation.

The LCO requires three instruments to be OPERABLE.

The drywell floor drain sump monitoring system is required to quantify the unidentified LEAKAGE rate from the RCS.

Thus, for the system to be considered OPERABLE, the sump level monitoring portion of the system must be OPERABLE and capable of determining the leakage rate. The identification of an increase in unidentified LEAKAGE will be delayed by the time required for the unidentified LEAKAGE to travel to the drywell floor drain sump and it may take longer than one hour to detect a 1 gpm increase in unidentified LEAKAGE, depending on the origin and magnitude of the LEAKAGE. This sensitivity is acceptable for containment sump monitor OPERABILITY.

The reactor coolant contains radioactivity that, when released to the drywell, can be detected by the gaseous or particulate drywell atmospheric radioactivity monitor. Only one of the two detectors is required to be OPERABLE.

Radioactivity detection systems are included for monitoring both particulate and gaseous activities because of their sensitivities and rapid response to RCS LEAKAGE, but have recognized limitations. Reactor coolant radioactivity levels will be low during initial reactor startup and for a few weeks thereafter, until activated corrosion products have been formed and fission products appear from fuel element cladding contamination or cladding defects. If there are few fuel element cladding defects and low levels of activation products, it may not be possible for the gaseous or particulate drywell atmospheric radioactivity monitors to detect a 1 gpm increase within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> during normal operation. However, the gaseous or particulate drywell atmospheric radioactivity monitor is OPERABLE when it is capable of detecting a 1 gpm increase in unidentified LEAKAGE within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> given an RCS activity equivalent to that assumed in the design calculations for the monitors (Reference 6).

This LCO is satisfied when monitors of diverse measurement means are available. Thus, the drywell floor drain sump monitoring system, in combination with a gaseous or (continued)

GRAND GULF B 3.4-34 LBDCR 11068

RCS Leakage Detection Instrumentation B 3.4.7 BASES LCO particulate drywell atmospheric radioactivity monitor and a (continued) drywell air cooler condensate flow rate monitoring system, provides an acceptable minimum.

APPLICABILITY In MODES 1, 2, and 3, leakage detection systems are required to be OPERABLE to support LCO 3.4.5. This Applicability is consistent with that for LCO 3.4.5.

ACTIONS A.1 With the drywell floor drain sump monitoring system inoperable, no other form of sampling can provide the equivalent information to quantify leakage. However, the drywell atmospheric activity monitor and the drywell air cooler condensate flow rate monitor will provide indications of changes in leakage.

With the drywell floor drain sump monitoring system inoperable, but with RCS unidentified and total LEAKAGE being determined every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> (SR 3.4.5.1), operation may continue for 30 days. Manual methods, using approved M&TE, can be used to monitor sump fill times and leakage and change in leakage during the 30 day allowed outage time for the drywell floor drain sump monitoring system to ensure compliance with SR 3.4.5.1. The 30 day Completion Time of Required Action A.1 is acceptable, based on operating experience, considering the multiple forms of leakage detection that are still available.

(continued)

GRAND GULF B 3.4-34a LBDCR 11068

RCS Leakage Detection Instrumentation B 3.4.7 BASES ACTIONS B.1 (continued)

With both gaseous and particulate drywell atmospheric monitoring channels inoperable, grab samples of the drywell atmosphere shall be taken and analyzed to provide periodic leakage information. Provided a sample is obtained and analyzed every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, the plant may continue operation since at least one other form of drywell leakage detection (i.e., air cooler condensate flow rate monitor) is available. The 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> interval provides periodic information that is adequate to detect LEAKAGE.

C.1 With the required drywell air cooler condensate flow rate monitoring system inoperable, SR 3.4.7.1 is performed every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to provide periodic information of activity in the drywell at a more frequent interval than the routine Frequency of SR 3.4.7.1. The 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> interval provides periodic information that is adequate to detect LEAKAGE and recognizes that other forms of leakage detection are available. However, this Required Action is modified by a Note that allows this action to be not applicable if the required drywell atmospheric monitoring system is inoperable. Consistent with SR 3.0.1, Surveillances are not required to be performed on inoperable equipment.

D.1, D.2, D.3.1 and D.3.2 With the drywell floor drain sump monitoring system and the drywell air cooler condensate flow rate monitoring system inoperable, the only means of detecting LEAKAGE is the drywell atmospheric gaseous radiation monitor. A Note clarifies this applicability of the Condition. The drywell atmospheric gaseous radiation monitor typically cannot detect a 1 gpm leak within one hour when RCS activity is low. In addition, this configuration does not provide the required diverse means of leakage detection. Indirect methods of monitoring RCS leakage must be implemented. Grab samples of the drywell atmosphere must be performed every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> to provide alternate periodic information.

Administrative means of monitoring RCS leakage include monitoring and trending parameters that may indicate an increase in RCS leakage. There are diverse alternative mechanisms from which appropriate indicators may be selected based on plant conditions. It is not necessary to utilize all of these methods, but a method or methods should be selected considering the current plant conditions and historical or expected sources of unidentified leakage. The administrative methods are drywell pressure and temperature, Component Cooling Water System outlet temperatures and makeup, Reactor Recirculation System pump seal motor cooler temperature indication, Drywell cooling fan outlet temperatures, Control Rod Drive System flange temperatures, and Safety Relief Valves tailpipe temperature. These indications, coupled with the atmospheric grab (continued)

GRAND GULF B 3.4-35 LBDCR 11068

RCS Leakage Detection Instrumentation B 3.4.7 BASES ACTIONS (continued) samples, are sufficient to alert the operating staff to an unexpected increase in unidentified LEAKAGE.

The 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> interval is sufficient to detect increasing RCS leakage. The Required Action provides 7 days to restore another RCS leakage monitor to OPERABLE status to regain the intended leakage detection diversity.

The 7 day Completion Time ensures that the plant will not be operated in a degraded configuration for a lengthy time period.

E.1 and E.2 With both the gaseous and particulate drywell atmospheric monitor channels and the drywell air cooler condensate flow rate monitor inoperable, the only means of detecting LEAKAGE is the drywell floor drain sump monitoring system. This Condition does not provide the required diverse means of leakage detection. The Required Action is to restore either of the inoperable monitoring systems to OPERABLE status within 30 days to regain the intended leakage detection diversity. The 30 day Completion Time ensures that the plant will not be operated in a degraded configuration for a lengthy time period.

F.1 and F.2 If any Required Action of Condition A, B, C, D, or E cannot be met within the associated Completion Time, the plant must be brought to a MODE in which the LCO does not apply. To achieve this status, the plant must be brought to at least MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and to MODE 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The allowed Completion Times are reasonable, based on operating experience, to reach the required plant conditions in an orderly manner and without challenging plant systems.

G.1 With all required monitors inoperable, no required automatic means of monitoring LEAKAGE are available, and immediate plant shutdown in accordance with LCO 3.0.3 is required.

SURVEILLANCE SR 3.4.7.1 REQUIREMENTS This SR requires the performance of a CHANNEL CHECK of the required drywell atmospheric monitoring system. The check gives reasonable confidence that the channel is operating properly. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

(continued)

GRAND GULF B 3.4-36 LBDCR 18127

RCS Leakage Detection Instrumentation B 3.4.7 BASES SURVEILLANCE REQUIREMENTS (continued)

SR 3.4.7.2 This SR requires the performance of a CHANNEL FUNCTIONAL TEST of the required RCS leakage detection instrumentation. The test ensures that the monitors can perform their function in the desired manner. The test also verifies the relative accuracy of the instrumentation. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

(continued)

GRAND GULF B 3.4-36a LBDCR 18127

THIS PAGE INTENTIONALLY LEFT BLANK RCS Leakage Detection Instrumentation B 3.4.7 BASES SURVEILLANCE SR 3.4.7.3 REQUIREMENTS (continued) This SR requires the performance of a CHANNEL CALIBRATION of the required RCS leakage detection instrumentation channels. The calibration verifies the accuracy of the instrumentation, including the instruments located inside the drywell. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program..

REFERENCES 1. 10 CFR 50, Appendix A, GDC 30.

2. Regulatory Guide 1.45, Revision 0, Reactor Coolant Pressure Boundary Leakage Detection System. May 1973.
3. GEAP-5620, "Failure Behavior in ASTM A106B Pipes Containing Axial Through C Wall Flaws," April 1968.
4. NUREG-75/067, "Investigation and Evaluation of Cracking in Austenitic Stainless Steel Piping of Boiling Water Reactor Plants,"

October 1975.

5. UFSAR, Section 5.2.5.5.3.
6. UFSAR, Section 5.2.5.2.

GRAND GULF B 3.4-37 LBDCR 18127

RCS Specific Activity B 3.4.8 BASES (continued)

SURVEILLANCE SR 3.4.8.1 REQUIREMENTS This Surveillance is performed to ensure iodine remains within limit during normal operation. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

This SR is modified by a Note that requires this Surveillance to be performed only in MODE 1 because the level of fission products generated in other MODES is much less.

REFERENCES  10 CFR 50.67, Accident Source Term.

 UFSAR, Section 15.6.4.

GRAND GULF B 3.4-41 LBDCR 18127

RHR Shutdown Cooling System C Hot Shutdown B 3.4.9 BASES LCO OPERABLE RHR pump, two heat exchangers in series, and the (continued) associated piping and valves. Each shutdown cooling subsystem is considered OPERABLE if it can be manually aligned (remote or local) in the shutdown cooling mode for removal of decay heat. In MODE 3, one RHR shutdown cooling subsystem can provide the required cooling, but two subsystems are required to be OPERABLE to provide redundancy.

Operation of one subsystem can maintain or reduce the reactor coolant temperature as required. However, to ensure adequate core flow to allow for accurate average reactor coolant temperature monitoring, nearly continuous operation is required. Management of gas voids is important to RHR Shutdown Cooling System Operability.

Note 1 permits both RHR shutdown cooling subsystems and recirculation pumps to not be in operation for a period of 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> in an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> period.

Note 2 allows one RHR shutdown cooling subsystem to be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for performance of surveillance tests. These tests may be on the affected RHR System or on some other plant system or component that necessitates placing the RHR System in an inoperable status during the performance. This is permitted because the core heat generation can be low enough and the heatup rate slow enough to allow some changes to the RHR subsystems or other operations requiring RHR flow interruption and loss of redundancy.

APPLICABILITY In MODES 1 and 2, and in MODE 3 with reactor steam dome pressure greater than or equal to the RHR cut in permissive pressure, this LCO is not applicable. Operation of the RHR System in the shutdown cooling mode is not allowed above this pressure because the RCS pressure may exceed the design pressure of the shutdown cooling piping. Decay heat removal at reactor pressures greater than or equal to the RHR cut in permissive pressure is typically accomplished by condensing the steam in the main condenser. Additionally, in MODE 2 below this pressure, the OPERABILITY requirements for the Emergency Core Cooling Systems (ECCS) (LCO 3.5.1, "ECCS C Operating") do not allow placing the RHR shutdown cooling subsystem into operation.

In MODE 3 with reactor steam dome pressure below the RHR cut in permissive pressure (i.e., the actual pressure at which the interlock resets) the RHR System may be operated in the (continued)

GRAND GULF B 3.4-43 LBDCR 14044

RHR Shutdown Cooling System - Hot Shutdown B 3.4.9 BASES ACTIONS B.1, B.2, and B.3 (continued) separately for each occurrence involving a loss of coolant circulation.

Furthermore, verification of the functioning of the alternate method must be reconfirmed every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> thereafter. This will provide assurance of continued temperature monitoring capability.

During the period when the reactor coolant is being circulated by an alternate method (other than by the required RHR shutdown cooling system or recirculation pump), the reactor coolant temperature and pressure must be periodically monitored to ensure proper function of the alternate method. The once per hour Completion Time is deemed appropriate.

SURVEILLANCE SR 3.4.9.1 REQUIREMENTS This Surveillance verifies that one RHR shutdown cooling subsystem or recirculation pump is in operation and circulating reactor coolant. The required flow rate is determined by the flow rate necessary to provide sufficient decay heat removal capability. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

This Surveillance is modified by a Note allowing sufficient time to align the RHR System for shutdown cooling operation after clearing the pressure interlock that isolates the system, or for placing a recirculation pump in operation. The Note takes exception to the requirements of the Surveillance being met (i.e., forced coolant circulation is not required for this initial 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> period), which also allows entry into the Applicability of this Specification in accordance with SR 3.0.4 since the Surveillance will not be "not met" at the time of entry into the Applicability.

SR 3.4.9.2 RHR Shutdown Cooling System piping and components have the potential to develop voids and pockets of entrained gases. Preventing and managing gas intrusion and accumulation is necessary for proper operation of the RHR shutdown cooling system subsystems and may also prevent water hammer, pump cavitation, and pumping of noncondensible gas into the reactor vessel.

Selection of RHR Shutdown Cooling System locations susceptible to gas accumulation is based on a review of system design information, including piping and instrumentation drawings, isometric drawings, plan and elevation drawings, and calculations. The design review is supplemented by system walk downs to validate the system high points and to confirm the location and orientation of (continued)

GRAND GULF B 3.4-46 LBDCR 18127

RHR Shutdown Cooling System - Hot Shutdown B 3.4.9 BASES important components that can become sources of gas or could otherwise cause gas to be trapped or difficult to remove during system maintenance or restoration. Susceptible locations depend on plant and system configuration, such as stand-by versus operating conditions.

The RHR Shutdown Cooling System is OPERABLE when it is sufficiently filled with water. Acceptance criteria are established for the volume of accumulated gas at susceptible locations. If accumulated gas is discovered that exceeds the acceptance criteria for the susceptible location (or the volume of accumulated gas at one or more susceptible locations exceeds an acceptance criteria for gas volume at the suction or discharge of a pump), the Surveillance is not met. If it is determined by subsequent evaluation that the RHR Shutdown Cooling System is not rendered inoperable by the accumulated gas (i.e., the system is sufficiently filled with water), the Surveillance may be declared met.

Accumulated gas should be eliminated or brought within the acceptance criteria limits.

RHR Shutdown Cooling System locations susceptible to gas accumulation are monitored and, if gas is found, the gas volume is compared to the acceptance criteria for the location. Susceptible locations in the same system flow path which are subject to the same gas intrusion mechanisms may be verified by monitoring a representative subset of susceptible locations. Monitoring may not be practical for locations that are inaccessible due to radiological or environmental conditions, the plant configuration, or personnel safety. For these locations alternative methods (e.g., operating parameters, remote monitoring) may be used to monitor the susceptible location. Monitoring is not required for susceptible locations where the maximum potential accumulated gas void volume has been evaluated and determined to not challenge system OPERABILITY.

The accuracy of the method used for monitoring the susceptible locations and trending of the results should be sufficient to assure system OPERABILITY during the Surveillance interval.

This SR is modified by a Note that states the SR is not required to be performed until 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after reactor steam dome pressure is < the RHR cut in permissive pressure. In a rapid shutdown, there may be insufficient time to verify all susceptible locations prior to entering the Applicability.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program. The Surveillance Frequency may vary by location susceptible to gas accumulation.

REFERENCES None.

GRAND GULF B 3.4-46a LBDCR 18127

PAGE INTENTIONALLY LEFT BLANK

RHR Shutdown Cooling System C Cold Shutdown B 3.4.10 BASES LCO aligned (remote or local) in the shutdown cooling mode for (continued) removal of decay heat. In MODE 4, one RHR shutdown cooling subsystem can provide the required cooling, but two subsystems are required to be OPERABLE to provide redundancy. Operation of one subsystem can maintain and reduce the reactor coolant temperature as required. However, to ensure adequate core flow to allow for accurate average reactor coolant temperature monitoring, nearly continuous operation is required. Management of gas voids is important to RHR Shutdown Cooling System OPERABILITY.

Note 1 permits both RHR shutdown cooling subsystems and recirculation pumps to not be in operation for a period of 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> in an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> period.

Note 2 allows one RHR shutdown cooling subsystem to be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for performance of surveillance tests. These tests may be on the affected RHR System or on some other plant system or component that necessitates placing the RHR System in an inoperable status during the performance. This is permitted because the core heat generation can be low enough and the heatup rate slow enough to allow some changes to the RHR subsystems or other operations requiring RHR flow interruption and loss of redundancy.

Note 3 permits both RHR shutdown cooling subsystems and recirculation pumps to not be in operation during performance of inservice leak testing and during hydrostatic testing. This is permitted because RCS pressures and temperatures are being closely monitored as required by LCO 3.4.11.

APPLICABILITY In MODES 1 and 2, and in MODE 3 with reactor steam dome pressure greater than or equal to the RHR cut in permissive pressure, this LCO is not applicable. Operation of the RHR System in the shutdown cooling mode is not allowed above this pressure because the RCS pressure may exceed the design pressure of the shutdown cooling piping. Decay heat removal at reactor pressures greater than or equal to the RHR cut in permissive pressure is typically accomplished by condensing the steam in the main condenser. Additionally, in MODE 2 below this pressure, the OPERABILITY requirements for the Emergency Core Cooling Systems (ECCS) (LCO 3.5.1, "ECCS C Operating") do not allow placing the RHR shutdown cooling subsystem into operation.

(continued)

GRAND GULF B 3.4-48 LBDCR 14044

RHR Shutdown Cooling System - Cold Shutdown B 3.4.10 BASES SURVEILLANCE SR 3.4.10.1 (continued)

REQUIREMENTS determined by the flow rate necessary to provide sufficient decay heat removal capability. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

SR 3.4.10.2 RHR Shutdown Cooling System piping and components have the potential to develop voids and pockets of entrained gases. Preventing and managing gas intrusion and accumulation is necessary for proper operation of the RHR shutdown cooling subsystems and may also prevent water hammer, pump cavitation, and pumping of noncondensible gas into the reactor vessel.

Selection of RHR Shutdown Cooling System locations susceptible to gas accumulation is based on a review of system design information, including piping and instrumentation drawings, isometric drawings, plan and elevation drawings, and calculations. The design review is supplemented by system walk downs to validate the system highpoints and to confirm the location and orientation of important components that can become sources of gas or could otherwise cause gas to be trapped or difficult to remove during system maintenance or restoration.

Susceptible locations depend on plant and system configuration, such as stand-by versus operating conditions.

The RHR Shutdown Cooling System is OPERABLE when it is sufficiently filled with water. Acceptance criteria are established for the volume of accumulated gas at susceptible locations. If accumulated gas is discovered that exceeds the acceptance criteria for the susceptible location (or the volume of accumulated gas at one or more susceptible locations exceeds an acceptance criteria for gas volume at the suction or discharge of a pump), the Surveillance is not met. If it is determined by subsequent evaluation that the RHR Shutdown Cooling System is not rendered inoperable by the accumulated gas (i.e., the system is sufficiently filled with water), the Surveillance may be declared met.

Accumulated gas should be eliminated or brought within the acceptance criteria limits.

RHR Shutdown Cooling System locations susceptible to gas accumulation are monitored and, if gas is found, the gas volume is compared to the acceptance criteria for the location. Susceptible locations in the same system flow path which are subject to the same gas inrusion mechanisms may be verified by monitoring a representative subset of susceptible locations. Monitoring may not be practical for locations that are inaccessible due to radiological or environmental conditions, the plant configuration, or personnel safety. For these locations alternative methods (e.g., operating parameters, remote monitoring) may be used (continued)

GRAND GULF B 3.4-51 LBDCR 18127

RHR Shutdown Cooling System - Cold Shutdown B 3.4.10 BASES to monitor the susceptible location. Monitoring is not required for susceptible locations where the maximum potential accumulated gas void volume has been evaluated and determined to not challenge system OPERABILITY. The accuracy of the method used for monitoring the susceptible locations and trending of the results should be sufficient to assure system OPERABILITY during the Surveillance interval.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program. The Surveillance Frequency may vary by location susceptible to gas accumulation.

REFERENCES None.

GRAND GULF B 3.4-51a LBDCR 18127

RCS P/T Limits B 3.4.11 BASES ACTIONS C.1 and C.2 (continued)

Operation outside the P/T limits in other than MODES 1, 2, and 3 (including defueled conditions) must be corrected so that the RCPB is returned to a condition that has been verified by stress analyses. The Required Action must be initiated without delay and continued until the limits are restored.

Besides restoring the P/T limit parameters to within limits, an evaluation is required to determine if RCS operation is allowed. This evaluation must verify that the RCPB integrity is acceptable and must be completed before approaching criticality or heating up to > 200°F. Several methods may be used, including comparison with pre-analyzed transients, new analyses, or inspection of the components. ASME Section XI, Appendix E (Ref. 6), may be used to support the evaluation; however, its use is restricted to evaluation of the beltline.

SURVEILLANCE SR 3.4.11.1 REQUIREMENTS Verification that operation is within limits is required when RCS pressure and temperature conditions are undergoing planned changes. The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

Surveillance for heatup and cooldown, or inservice leakage and hydrostatic testing may be discontinued when the criteria given in the relevant plant procedure for ending the activity are satisfied.

This SR has been modified by a Note that requires this Surveillance to be performed only during system heatup and cooldown operations and inservice leakage and hydrostatic testing.

(continued)

GRAND GULF B 3.4-57 LBDCR 18127

RCS P/T Limits B 3.4.11 BASES SURVEILLANCE SR 3.4.11.5, SR 3.4.11.6, and SR 3.4.11.7 REQUIREMENTS (continued) Limits on the reactor vessel flange and head flange temperatures are generally bounded by the other P/T limits during system heatup and cooldown. However, operations approaching MODE 4 from MODE 5 and in MODE 4 with RCS temperature less than or equal to certain specified values require assurance that these temperatures meet the LCO limits.

The flange temperatures must be verified to be above the limits before and while tensioning the vessel head bolting studs to ensure that once the head is tensioned the limits are satisfied. When in MODE 4 with RCS temperature 80°F, checks of the flange temperatures are required because of the reduced margin to the limits. When in MODE 4 with RCS temperature 100°F, monitoring of the flange temperature is required to ensure the temperatures are within the limits.

The Surveillance Frequency is controlled under the Surveillance Frequency Control Program.

SR 3.4.11.8 and SR 3.4.11.9 Differential temperatures within the applicable limits ensure that thermal stresses resulting from increases in THERMAL POWER or recirculation loop flow during single recirculation loop operation will not exceed design allowances. Performing the Surveillance within 15 minutes before beginning such an increase in power or flow rate provides adequate assurance that the limits will not be exceeded between the time of the Surveillance and the time of the change in operation.

An acceptable means of demonstrating compliance with the temperature differential requirement in SR 3.4.11.9 is to compare the temperatures of the operating recirculation loop and the idle loop.

(continued)

GRAND GULF B 3.4-59 LBDCR 18127

Reactor Steam Dome Pressure B 3.4.12 BASES APPLICABILITY In MODES 3, 4, and 5, the limit is not applicable because (continued) the reactor is shut down. In these MODES, the reactor pressure is well below the required limit, and no anticipated events will challenge the overpressure limits.

ACTIONS A.1 With the reactor steam dome pressure greater than the limit, prompt action should be taken to reduce pressure to below the limit and return the reactor to operation within the bounds of the analyses. The 15 minute Completion Time is reasonable considering the importance of maintaining the pressure within limits. This Completion Time also ensures that the probability of an accident while pressure is greater than the limit is minimal.

B.1 If the reactor steam dome pressure cannot be restored to within the limit within the associated Completion Time, the plant must be brought to a MODE in which the LCO does not apply. To achieve this status, the plant must be brought to at least MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The allowed Completion Time of 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> is reasonable, based on operating experience, to reach MODE 3 from full power conditions in an orderly manner and without challenging plant systems.

SURVEILLANCE SR 3.4.12.1 REQUIREMENTS Verification that reactor steam dome pressure is 1045 psig ensures that the initial conditions of the vessel overpressure protection analysis are met. The Surveillance Frequency is controlled under the Surveillance Frequency Control PClean rogram.

REFERENCES 1. UFSAR, Section 5.2.

2. UFSAR, Section 15.

GRAND GULF B 3.4-62 LBDCR 18127