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Category:ANNUAL OPERATING REPORT
MONTHYEARSVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With ML20217J1981997-09-30030 September 1997 Summary Rept of Changes,Tests & Experiments Completed, for Period 950101-970930 ML20115D1001992-10-0606 October 1992 Listing of Procedure Changes,Tests & Experiments Completed During Month of Sept 1992 & Summary of Safety Evaluations, Per 10CFR50.59 & 10CFR50.71(e) ML20091F1501992-04-0202 April 1992 Listing of Changes,Tests & Experiments Requiring Safety Evaluations Completed from Jan-Dec 1991 ML20042E4181990-03-31031 March 1990 Listing of Changes,Tests & Experiments Completed During Mar 1990 & Summary of Safety Evaluations,Per 10CFR50.59 & 10CFR50.71(e).W/900402 Ltr ML20206D3351988-10-27027 October 1988 Forwards Listing of Changes,Tests & Experiments Completed During Oct 1988 for Plant ML20207K6591985-12-31031 December 1985 Addendum for Part 3 of 1985 Annual Operating Rept,Indicating Results of Environ Radiological & Meteorological Monitoring ML20094R7901984-07-31031 July 1984 Rept of Changes,Tests & Experiments Completed During Jul 1984 ML20080R1001983-10-0303 October 1983 Forwards Listing of Changes,Tests & Experiments Completed During Sept 1983.Summary of Safety Evaluation Reported Per 10CFR50.59 1999-04-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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Commonwealth Edison 50->54 C Ouad Citiss Nucisar Pawsr Station ;"a5 g? 22710 206 Avenue North Corcova, Illinois 61242 Telephone 309/654-2241 NJK-83-351 ,
October 3, 1983 Mr. I:dson C, Case, Deputy Director Office of Nuclear Reactor Regulation U, S, Nuclear Regulatory Commission Washington, D, C, 20555
Dear Mr. Case:
Enclosed please find a listing of those changes, tests, and experi-ments completed during the month of September,1983, for Quad-Cities Station Units 1 and 2, DPR-29 and DPR-30. A sunanary of the safety evaluation is being reported in compliance with 10 CFR 50.59.
Thirty-nine copies are provided for your use.
Very truly yours, l COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION f
/p/ s / .
N, J, Kallvianakis Station Superintendent bb Enclosu re cc: T, J , Rausch
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10CFR50.59 SAFETY EVALUATION FOR PERFORMING AN ON-LINE CHEMICAL DECONTAMINATION OF THE RECIRCULATION LOOPS OF UNIT 2 USING TEMPORARY EQUIPMENT AND SERVICES SUPPLIED BY LONDON NUCLEAR SERVICES, INC.
- 1. The probability of an occurrence or the consequence of an accident, or malfunction of equipment important to safety as previously evaluated in the Final Safety Analysis Report is not increased as a result of this job. The effect of the decontamination
, solvent on existing plant systems was extensively reviewed and showed the following:
- a. Metallurgy The original materials specifications for the recirculation system and annulus allowed for general corrosion. Results of corrosion testing and analysis by London Nuclear and reviewed by Systems Materials Analysis (SMAD) indicated that the solvent corrosion rates are less than the original allowance by a factor of approximately 30.
Additional corrosion data is being generated by London Nuclear from constant extension rate tests and tests on welded pre-cracked specimens. Although the results of these tests will be useful for expanding the data base, the existing corrosion test data is sufficient to determine that the solvent is acceptable for use. (Reference SMAD letter dated July 28, 1983).
- b. Core Spray The solvent will be contained within the recirculation loops and annulus and will not come in contact with any other systems / equipment necessary to maintain reactor safety.
In the unlikely event that the decontanination solution is transported into the reactor vessel core, the dilution i factor (originally .1 weight percent) is increased at least ten-fold. In their review of corrosion data, SMAD included the possibility of this occurring and, as stated, accepted the solvent for use. In any event, subsequent heating of reactor coolant to 450 F. will decompose the solvent to l oxygen, hydrogen, and carbon dioxide.
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- c. Gaskets / Seals Materials analysis of gaskets, seals, and valve packing materials was included in the SMAD review. Past experience with decontaminations by London Nuclear at other utilities indicates no adverse effects of the decontamination on these materials. Gasket and seal failures are addressed in the FSAR. Their status will not change as a result of this project.
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- d. Corrosion Verification 304 Stainless Steel coupons will be placed in the decontamination flow path and analyzed upon completion of the project for assurance of the actual corrosion rates,
- e. Water Purity The reactor coolant will be returned to technical specification limitations leaving the recirculation system in essentially its original condition.
- 2. The possibility for an accident or malfunction of a different type than any previously evaluated in the Final Safety Analysis Report is not created. Potential accidents or malfunctions of equipment were reviewed and addressed as follows.
- a. Hydro / Pre-Op Prior to performing the decentamination, a hydrostatic pressure test is performed on the decontamination skid and hoses to the recirculation system taps. Pre-operational tests are performed on the skid to verify instrumentation, controls, and equipment operability and to determine the adequacy of shutdown safeguards. Process hoses are rated at 400 pais operating pressure is 35-40 psi and hydrostatic test pressure is 100 psi.
- b. Residual Chemicals The effects of residual solvent in the system was determined negligible. Reactor coolant is cleaned and returned to technical specification limits. Residual solvent will be highly diluted and at high temperatures will decompose.
At the conclusion of the decontamination, the recirculation pump seals and instrument lines will be backflushed.
- c. Leaks / Spills Potential leak points outside the drywell will be under visual surveillance during the process. Leaks within the drywell will be contained by isolating the drywell sump pumps until the decontamination is complete. Secondary containment will be maintained throughout the process.
Caseous releases from the evaporation of spills will be monitored via the standby gas system.
Liquid spills will be processed through normal radwaste lines. The diluted solvent is compatible with the station radwaste system.
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- d. Radiation Protection Station radiation protection procedures will be followed throughout the decontamination. During resin transfer to the solidification truck, the affected areas of the reactor building will be evacuated. Access into the drywell during the process will be strictly controlled by station health physicists.
- e. Level Monitoring The level of the solvent in the recirculation system risers will be continuously monitored. Since SMAD has reviewed the material / solvent interface for materials within the core and has accepted the solvent for use, the consequences of a failure in the level controls causing a spill into the core are negligible. At the conclusion of the decon-tamination, the reactor coolant in the core will be analyzed for assurance that significant solvent did not enter this area.
- f. Equipment Failure Major components of the decontamination skid are isolable for repair or replacement. The length of time required for equipment repairs is not constrained by the expected corrosion rates of the solvent left stagnant in the system.
These rates are temperature and flow dependent and will decrease rapidly when process circulation is interrupted.
- 3. The margin of safety as defined in the basis for any Technical l Specification is not reduced. The decontamination project will be performed in accordance with the existing technical specification.
The reactor will be maintained in the shutdown mode with all interlocks in the shutdown position.
- a. Chemistry Coolant chemistry will be monitored continuously as part of the project, and upon completion of the decontamination, coolant will be returned to the technical specification limits,
- b. Release Monitoring o
Liquid and/or gaseous releases will be monitored as normal and will adhere to technical specification limitations.
- c. Temperature / Pressure Limitations The decontamination will be performed at 250 F. and 25-30 psig; both ranges fall within technical specification limits for maintaining primary system integrity.
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- d. Head Replacement To obtain the 250 F. operating temperature, the reactor vessel head will be replaced and tensioned to 0-Ring Seating pass requirements. The temperature limitation of 100 F.
f flange temperature specified in the technical specifications does not apply to an 0-Ring seating pass tension. General Electric determined that the studs could be tensioned to 10% of the designed flange loading without temperature dependency.
The 0-Ring seating pass will induce approximately a 7% flange .
load.
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10 CFR 50.59 SAFETY EVALUATION TO DOCUMENT THE REVIEW PERFORMED CN SEPTEMBER 21, 1983, TO CERTIFY / QUALIFY MATERI AL RECEIVED FROM BRAND INDUSTRIAL SERVICES CORPORATION FOR USE AS A PlPE PENETRATION BARRIER ON THE "D" STEAM LINE
- l. Is the probability of an occurrence or the consequence of an accident, or malfunction of equipment i...portant to safety as previously evaluated in the Final Safety Analysis Report increased?
No. The use of SGR600 Silicone Rubber Fabric in lieu of Keene Corporation PE2141 Flame Retardant Fabric will not degrade the integrity of Secondary Containment. Visual inspection and tests indicate the material will perform the function of a pipe penetration barrier sufficiently adequate to mitigate the consequences of the dropped fuel bundle, failed fuel or the postulated rod droo accident.
- 2. Is the possibility of an accident or malfunction of a different type than any previously evaluated in the Final Safety Analysis Report created?
No. This pipe penetration barrier is a passive component which will not cause the failure of any other safety equipnent to perform its function to nitigate the consequences of an accident. Based on the Certificate of Compilance issued by Brand Industrial Services Corporation, this material is viewed as an acceptable replacement for the original Purchase Order material Keene Corporation PE2141.
Therefore, upon installation of this material the Reactor Building is considered intact and Secondary Containment integrity is maintained. Post-maintenance inspections verified the integrity of the penetration barrier.
3 Is the margin of safety, as defined in the basis for any Technical Specification, reduced?
No. The ability to maintain sufficient negative pressure on the Reactor Building will be enhanced by the installation of this material as a pipe penetration barrier. The Secondary Containment Capability Test recently successfully performed indicates the failure of the penetration wlil not degrade the safety margin.
Flame tests performed on material and the supplier Certificate of Compliance adequately assures this penetration is sealed as a fire barrier.