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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20205E2361999-03-31031 March 1999 Mnps,Units 1,2 & 3 Decommissioning Funding Status Rept ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 ML20204K1031999-03-19019 March 1999 Non-proprietary Licensing Rept for Spent Fuel Rack Installation at Mnps,Unit 3 ML20207B2271999-02-22022 February 1999 Rev 0 to SIR-99-021, Evaluation of Stratification Loadings in LBB Analysis for Mnps,Unit 2 Surge Line ML20199D4571999-01-0808 January 1999 Progress Toward Restart Readiness at Millstone Unit 2 - Nu Briefing for Nrc ML20197H5871998-12-31031 December 1998 Independent Corrective Action Verification Program, Final Rept,Vol 1 ML20198G7161998-11-30030 November 1998 Rev 0 to EMF-2145, Millstone Unit 2 Large Break Loca/Eccs Analysis with Replacement SGs & Plant Modifications ML20195H7401998-11-30030 November 1998 Station/Unit 3 Third Quarter Performance Rept ML20195C8091998-11-0909 November 1998 Request for Permission to Apply LBB Methodology to Pressurizer Surge Piping, Plant Specific Info Fo Pressurizer Surge Piping ML20195C7731998-10-13013 October 1998 Rev 0 to SIR-98-096, Pressurizer Surge Line LBB Evaluation Mnps,Unit 2 ML20154P9541998-09-30030 September 1998 Simulator Quadrennial Certification Rept ML20198G7041998-09-30030 September 1998 Rev 0 to EMF-2079, Millstone Unit 2 Large Break Loca/Eccs Analysis with Replacement Sgs ML20237B2801998-07-31031 July 1998 Rev 1 to EMF-98-036, Post-Scram Main Steam Line Break Analysis for Millstone Unit 2 ML20237B4781998-07-31031 July 1998 Station/Unit 3,Second Quarter Performance Rept for Jul 1998 ML20236U6361998-07-0101 July 1998 Rev 0 to Leak-Before-Break Evaluation High Energy Safety Injection Piping,Mnps,Unit 2 ML20236V7541998-07-0101 July 1998 Rev 0 to Little Harbor Consultants,Inc, Evaluation of Millstone Self-Assessment & Independent Oversight Programs ML20236F5221998-06-30030 June 1998 Independent Assessment of Upper Guide Structure (Ugs) Personnel Contamination Event at Millstone Station Unit 2, Final Rept ML20236F5051998-06-25025 June 1998 Rev 1 to Event Review Team Rept Root Cause Investigation Upper Guide Structure (Ugs) Personnel Contamination Event ML20249C3911998-06-22022 June 1998 Simulator Quadrennial Certification Rept ML20248F4071998-06-0101 June 1998 Final Rept SL-5192, Independent Corrective Action Verification Program for Millstone Unit 3 ML20236P4341998-05-22022 May 1998 Progress Toward Restart Readiness at Millstone Station - Northeast Utilities Briefing for Nrc ML20236F6411998-05-11011 May 1998 Rev 0 to Justification of Continued LBB Compliance for Nu MP2 ML20203H3531998-02-24024 February 1998 Transport of Small Air Pocket ML20216E0961998-02-17017 February 1998 Redacted Safety Conscious Work Environment (Assessment of Nuclear Oversight 980121 Statement) ML20199G8031998-01-31031 January 1998 Radiological Survey for Waterford Town Landfill,Waterford, Ct ML20199D9111998-01-23023 January 1998 Independent Corrective Action Verification Program Status Rept, for Period Ending 980123 ML20203H3961997-12-31031 December 1997 Integrated Sys Functional Review for Mnps,Unit 3, Engineering Self Assessment Rept ML20217C2201997-12-16016 December 1997 Exam of Concrete Cores Millstone III Subcontainment Porous Concrete ML20202H2981997-12-0202 December 1997 Independent Corrective Action Verification Program Status Rept ML20203H3661997-11-30030 November 1997 Transient Clearing of Air in Loop Seal ML20199G8091997-11-30030 November 1997 Radiological Survey for Equestrian Ctr Harkness State Park Waterford,Ct ML20211F7171997-09-29029 September 1997 Rev 0 to Critical Design Characteristics Radiological Events for Millstone 2 ML20217F9481997-08-31031 August 1997 Non-proprietary Version of Bases for Millstone Unit 3 ECCS Current & Future Ts ML20217Q7101997-08-29029 August 1997 Rev 0 to Critical Design Characteristics Reactivity Events ML20217Q7181997-08-29029 August 1997 Rev 0 to Critical Design Characteristics Undercooling Events & Reactor Coolant Flow Reduction Events ML20210H0051997-08-0505 August 1997 Rev 0 to Critical Design Characteristics Reactor Coolant Pressure Boundary Events & Mslb/Loca Containment Analyses ML20149F0971997-07-18018 July 1997 Rev 0 to Critical Design Characteristics Overcooling Events,Millstone 2 ML20148Q2901997-06-24024 June 1997 Simulator Quadrennial Rept for 1993-1997 ML20148K8221997-05-31031 May 1997 Temporary Use of Atlas Copco Diesel Compressor PTMS900 at Millstone Nuclear Power Station Unit 3 Maint of Svc Air Sys ML20148R7151997-05-30030 May 1997 Progress Toward Restart Readiness at Millstone Station ML20210S3711997-04-29029 April 1997 Margin of Immunity Determination for SRV Electric Lift for Neut,Millstone Nucelar Site,Unit 1 ML20138E6391997-04-11011 April 1997 Investigation of Possible Deterioration of Porous Concrete Millstone 3 Nuclear Reactor ML20217C2121997-04-0707 April 1997 Rev 2 to S3-EV-9700574, SE for Containment Structure Porous Concrete Drainage Sys ML20137H3031997-03-31031 March 1997 Rev 2 to Nuclear Training Loit/Lout Audit Reviews ML20137C6281997-03-14014 March 1997 Redacted Version of Rev 1 to Nuclear Training Loit/Lout Audit Reviews ML20138E6471997-03-14014 March 1997 Porous Concrete Investigation Millstone 3 Waterford,Ct ML20141D2881997-02-17017 February 1997 Rev 3 to Maint Rule Unit Basis Document ML20135E3221997-02-13013 February 1997 Independent Review Team Rept 1996 MP -1 Lout NRC Exam Failures ML20133C1451996-12-31031 December 1996 Porous Concrete Mock-Up Testing Phase III W/Containment Mat Concrete 1999-04-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program 05000336/LER-1999-012, :on 990917,unrecoverable CEA Misalignment Entry Into TS 3.0.3 Was Noted.Caused by Grounded Coil Wire for Lower Gripper Assembly.Leads Leading to Lower Gripper Coil Were Insulated1999-10-15015 October 1999
- on 990917,unrecoverable CEA Misalignment Entry Into TS 3.0.3 Was Noted.Caused by Grounded Coil Wire for Lower Gripper Assembly.Leads Leading to Lower Gripper Coil Were Insulated
ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 05000336/LER-1999-011, :on 990823,thermal Reactor Power Limit Was Exceeded.Caused by Lack of Conservatism in Procedures & Alarm Setpoints Used to Limit Reactor Power.Revised Operating Procedures1999-09-20020 September 1999
- on 990823,thermal Reactor Power Limit Was Exceeded.Caused by Lack of Conservatism in Procedures & Alarm Setpoints Used to Limit Reactor Power.Revised Operating Procedures
ML20212A7381999-09-10010 September 1999 Safety Evaluation Supporting Amend 174 to License NPF-49 05000245/LER-1999-001-02, :on 990810,discovered That Stack Flow Monitor Four H LCO Action Statement Had Not Been Met.Caused by Personnel Error.Frequency of LCO Action Was Increased & Personnel Involved Received Coaching.With1999-09-0808 September 1999
- on 990810,discovered That Stack Flow Monitor Four H LCO Action Statement Had Not Been Met.Caused by Personnel Error.Frequency of LCO Action Was Increased & Personnel Involved Received Coaching.With
05000336/LER-1999-010, :on 990804,noted Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve.Caused by Inadequate man-machine Interface. Planning Personnel Will Be Briefed on QC Program Indicators1999-09-0202 September 1999
- on 990804,noted Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve.Caused by Inadequate man-machine Interface. Planning Personnel Will Be Briefed on QC Program Indicators
ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20210U0881999-08-13013 August 1999 Safety Evaluation Supporting Amends 239 & 173 to Licenses DPR-65 & NPF-49,respectively ML20210Q1401999-08-12012 August 1999 Safety Evaluation Supporting Amend 238 to License DPR-65 B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr ML20209G3061999-07-13013 July 1999 Safety Evaluation Supporting Amend 237 to License DPR-65 B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D6581999-07-0202 July 1999 Safety Evaluation Supporting Amend 172 to License NPF-49 ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196H1621999-06-29029 June 1999 Safety Evaluation Supporting Amend 236 to License DPR-65 05000423/LER-1999-007-01, :on 990518,discharge Filter Associated with Crss Cubicle Sump Pump 3DAS-8A,was Determined to Be Contaminated.Caused by Back Leakage from Contaminated Drains Feeding Into ECCS Pump.Lines Modified.With1999-06-17017 June 1999
- on 990518,discharge Filter Associated with Crss Cubicle Sump Pump 3DAS-8A,was Determined to Be Contaminated.Caused by Back Leakage from Contaminated Drains Feeding Into ECCS Pump.Lines Modified.With
05000423/LER-1999-006-01, :on 990516,both Reactor Plant Aerated Drains SR Air Driven Sump Pumps Failed During TRM Surveillance.Caused by Inadequate Preventive Maint Program Design.Surveillance Procedure Sp 3635B.2 Will Be Conducted Monthly1999-06-15015 June 1999
- on 990516,both Reactor Plant Aerated Drains SR Air Driven Sump Pumps Failed During TRM Surveillance.Caused by Inadequate Preventive Maint Program Design.Surveillance Procedure Sp 3635B.2 Will Be Conducted Monthly
05000423/LER-1999-004-01, :on 990516,ESFA of Numerous Plant Components on Restoration of a Train Sequencer Occurred.Caused by Inadequate Procedure Direction.Issued Brief to Operations Describing Inadvertent Sequencer LOP Event.With1999-06-14014 June 1999
- on 990516,ESFA of Numerous Plant Components on Restoration of a Train Sequencer Occurred.Caused by Inadequate Procedure Direction.Issued Brief to Operations Describing Inadvertent Sequencer LOP Event.With
ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR 05000423/LER-1999-005-01, :on 990510,failure to Perform Surveillance on RCS Pressurizer Heater Penetration Breakers Was Noted.Caused by Lack of Mgt Support.Required Surveillance of Identified Ten Breakers Was Completed1999-06-0808 June 1999
- on 990510,failure to Perform Surveillance on RCS Pressurizer Heater Penetration Breakers Was Noted.Caused by Lack of Mgt Support.Required Surveillance of Identified Ten Breakers Was Completed
ML20195E6351999-06-0707 June 1999 Corrected Page Two of Safety Evaluation in Issuance of Amend 232 to FOL DPR-65 for Millstone Nuclear Power Station,Unit 2 05000423/LER-1999-003-01, :on 990505,identified That 18 Month EDG Surveillance Test for LOP with ESF Start Did Not Initiate Test.Caused by Inadequate Understanding of Regulatory Guidance. a & B EDG Returned to Status.With1999-06-0404 June 1999
- on 990505,identified That 18 Month EDG Surveillance Test for LOP with ESF Start Did Not Initiate Test.Caused by Inadequate Understanding of Regulatory Guidance. a & B EDG Returned to Status.With
ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 1999-09-08
[Table view] |
Text
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OVERPRESSURE PROTECTION REPORT
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FOR To MILLSTONE NUCLEAR POWER PLANT A ECEFTAIJCE UNIT 3 ggEQ Q L4ESTIDld 440 2 AS REQUIRED BY
/
ASME BOILER AND PRESSURE VESSEL CODE SECTION III, ARTICLE NB-7300 MARCH 1983 Prepared by:
K.' A. Forcht L
Approved:
%. Little ansient Analysis
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9 WJ) l NM( 7-assmasco U
PROFESSIONAL Certified:
NI AUN Robert A. Wiesemann ENGNEER 7/
Professional Engineer-0 no.snz E s
Commonwealth of Pennsylva 4p9 y
P307060103 830630 PDR ADOCK 05000 J
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' l.0 Purpoco of Report This report documents the overpressure protection provided for the Reactor Coolant System (RCS) in accordance with the ASME Boiler and Pressure Vessel Code,Section III, NB-7300.
This report documents the overpressure protection provided in the Westinghouse NSSS scope.
2.0 Description of Overpressure Protection 2.1 Overpressure protection is provided for the RCS and its compo-nents to prevent a rise in pressure of more than 10% above the system design pressure of 2485 psig, in accordance with NB-7400.
This protection is afforded for the following events which envelope those credible events which could lead to over-pressure of the RCS if adequate over pressure protection were not provided.
1.
Loss of Electrical Load and/or Turbine Trip 2.
Uncontrolled Rod Withdrawal at Power 3.
Loss of Reactor Coolant Flow 4.
Ioss of Normal Feedwater 5
Loss of Offsite Power to the Station Auxiliaries 22 The extent of the RCS is as defined in 10CFR50 and includes:
1.
The reactor vessel including control rod drive mechanism housings.
2.
The reactor coolant side of the steam generators.
3.
Reactor coolant pumps.
4.
A pressurizer attached to one of the reactor coolant loops.
5.
Safety and relief valves.
6 The interconnecting piping, valves and fittings between the principal components listed above.
e i
7.
The piping, fittings and valves leading to connecting auxiliary or support systems up to and including the second isolation valve (from the high pressure side) on each line.
2.3 The pressurizer provides volume surge capacity and is designed to mitigate pressure increases (as well as decreases) caused by load transients.
A pressurizer spray system condenses steam at a rate sufficient to prevent the pressurizer pressure from reaching the setpoint of the power-operated relief valves during a step reduction in power level equivalent to ten per-cent of full rated load.
1673Q:1 (1)
Tha sprcy n3zzio is 1centcd in the tap herd of the pracsur-izar.
Sprcy 10 initicted when tha proscuro contro11sd spray d:Ccnd signal is abovo a giv:n satpoint.
The sprcy rato increases proportionally with increasing compensated error signal until it reaches a maximum value.
The compensated error signal is the output of a proportional plus integral controller, the input to which is an error signal based on the difference between actual pressure and a reference pressure..
The pressurizer is equipped with 2 power-operated relief valves which limit system pressure for a large power mismatch to avoid actuation of the fixed high pressure reactor trip.
1 The relief valves are operated automatically or by remote i
manual control.
The operation of these valves also limits the frequency of opening of the spring-loaded safety valves.
Remotely operated stop valves are provided to isolate the power-operated relief valves if excessive leakage occurs.
The relief valves are designed to limit the pressurizer pressure to a value below the high pressure trip setpoint for all design transients up to and including the design percentage step load decrease with steam dump but without reactor trip.
Isolated output signals from the pressurizer pressure protec-tion channels are used for pressure control.
These are used to control pressurizer spray and power-operated relief valves in the event of increase in RCS pressure.
In the event of unavailability of the pressurizer spray or power operated relief valves, and a complete loss of steam flow to the turbine, protection of the RCS against overpres-sure is afforded by the pressurizac safety valves in conjunc-tion with the steam generator safety valves and a reactor trip initiated by the Reactor Protection System.
There are 3 safety valves with a minimum required capacity of 422,410 lb/ hour for each valve at system design pressure plus 3% allowance for accumulation.
The pressurizer safety valves are totally enclosed pop-type, spring loaded, self-setivated x
valves with back pressure compensation.
The set pressure of the safety valves will be no greater than system design pres-sure of 2485 psig in accordance with section NB7511.
The pressurizer safety valves and power operated relief valves discharge to the pressurizer relief tank (PRT).
Ruptura disks are installed on the pressurizer relief tank to prevent PRT overpressurizat' ion.
The safety valve flow rates quoted are based on a design maximum PRT back pressure of 100 psig.
Figure 1 shows a schematic arrangement of the pressure reliev-ing devices.
3.0 Sizing of Pressurizer Safety Valves 3.1 The sizing of the pressurizer safety valves is based on analy-sis of a complete loss of steam flow to the turbine with the reactor operating at 102% of Engineered Safeguards Design 1673Q:1 (2)
Powar.
In this cnclysis, fesdwatcr ficw 10 cocumsd to ba maintain d, cud no credit is tcken for operation of pras-surizar power operated roliof velvac, procourizar level con-trol system, pressurizer spray system, rod control system, steandump system or steam line power operated relief valves.
The reactor is maintained at full power (no credit for reactor trip), and steam relief through the steam generator safety valves is considered.
The total pressurizer safety valve capacity is required to be at least as large as the maximum surge rate into the pressurizer during this transient.
)
l This sizing procedure results in a safety valve capacity well in excess of the capacity required to prevent exceeding 110%
of system design pressure for the events listed in Section 2.1.
The conservative nature of this sizing procedure is demonstrated in the following section.
3.2 Each of the overpressure transients listed in Section 2.1 has been analyzed and reported in the Final Safety Analysis Report.
The analysis methods, computer codes, plant initial conditions and relevant assumptions are discussed in the FSAR for each transient.
Review of these transients shows that the Turbine Trip results in the maximum system pressure and the maximum safety valve I
relief requirements. This transient is presented in detail below.
For a turbine trip event, the reactor would be tripped directly (unless below approximately 50 percent power) from a signal derived from the turbine stop emergency trip fluid pressure and turbine stop. valves. The turbine stop valves close rapidly (typically 0.1 seconds) on loss of trip fluid pressure actuated by one of a number of possible turbine trip signals. This will cause a sudden reduction in steam flow, resulting in an increase in pressure and temperature in the steam generator shell. As a result, heat transfer rate in the steam generator is reduced, causing the reactor coolant tem-perature to rise, which in turn causes coolant expansion, pressurizer insurge, and RCS pressure rise.
The automatic steam dump system would normally accommodace ;r -
I excess steam generation.
Reactor coolant temperature and pressure do not significantly increase if the steam dump sys-tem and pressurizer pressure control system are functioning properly.
If the turbine condenser were not available, the i
excess steam generation would be dumped to the atmosphere and main feedwater flow would be lost.
For this situation feed-water flow would be maintained by the Auxiliary Feedwater System to ensure adequate' residual and decay heat removal capability.
Should the steam dump system fail to operate, the steam generator safety valves may lift to provide pressure control.
~
1673Q:1 (3)
- ~
In this annlysis, the behavior of the unit is evaluated for e completa loco of steca lond froa 102 parcent of full power with:ut dirset racetor trip; that is, ths turbino is assumed to trip without actuating all the sensors for reactor trip on l
the turbine stop valves.
The assumption delays reactor trip until conditions in the RCS result in a trip due to other signals.
Thus, the analysis assumes a worst trans ien t.
In i
addition, no credit is taken for steam dump.
Main feedwater flow is terminated at the time of turbine trip, with no credit taken for auxiliary feedwater to mitigate the consequences of the transient.
The turbine trip transients are analyzed by employing the detailed digital computer program IDFTRAN.
The program simu-
"lates the neutron kinetics, RCS, pressurizer, pressuriser relief and safety valves, pressurizer spray, steam generator, and steam generator safety valves.
The program computes per-tinent plant variables including temperatures, pressures, and power level.
Major assumptions are summarized below:
a.
Initial operating conditions The initial reactor power and RCS temperatures are assumed at their maximum values consistent with the steady state
~~
full power operation including allowances for calibration and instrument errors.
The initial RCS pressure is assumed at a minimum value consistent with the steady state full power operation including allowances for cali-bration and instrument errors.
This results in the maxi-
'aum power difference for the load loss, and the minimum
~?: Psargin to core protection limits at the initiation of the.
- -accident.
7,y..-,-
b.
Moderator and Doppler coefficients of reactivity
- Rm - J '-- The analysis assumes both a least negative moderator coef-
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thie results in maximum pressure relieving requirements.
c.
Reactor control Tilr2C...From the standpoir.t of the maxinum pressures attained it is conservative to assume that the reactor is in manual control.
If the reactor were in automatic control, the control rod banks would move prior to trip and reduce the severity of the transient.
1673Q:1 (4) s
\\
=
d.
Steem release No credit is taken for the operation of the steam dump system or steam senerator power operated relief valves.
The steam generator pressure rises to the safety valve setpoint where steam release through safety valves limits secondary steam press' re at the setpoint value.
u e.
Pressurizer spray and power operated relief valves No credit is taken for the effect of pressurizer spray and power operated relief valves in reducing or limiting the coolant pressure.
Safety valves are operable.
f.
reedwater flow 4
Main feedwater flow to the steam generatore is assumed to be lost at the time of turbine trip.
No credit is taken j
for auxiliary feedwater flow since a stabilized plant condition will be reached before auxiliary feedwater initiation is nornelly assumed to occur; however, the auxiliary feedwater pumps would be expected to start' on a trip of the main feedwater pumps.
The auxiliary feedwater flow would remove core decay heat following plant stabilization.
g.
Reactor trip Reactor trip is actuated by the first Reactor Protection System trip setpoint reached with no credit taken for the direct reactor trip on the turbine trip.
Trip signals are expected due to high pressurizer pressure, Overtemperature dy, high pressurizer water level, and low-low steam generator water level.
The results of the Turbine Trip transient are shown in Figures 2 and 3.
Figure 2 shows the pressurizer pressure, the reactor coolant pump discharge pressure, which is the point of highest pressure, in the,RCS, and the pressurizer safety valve relief rate.
Figure 3 shows steam generator shall side pressure, reactor coolant loop hot leg and cold leg temperature, and nuclear power.
The reactor is tripped on a high pressurizer pressure signal for this transient.
l The results of this analysis show that the overpressure pro-taction provided is sufficient to maintain peak RCS pressure below the code limit of 110% of system design pressure.
The plot of pressurizar safety valve relief rate also shows that adequate overprsseure protection for this limiting event could be provided by two of the three installed safety valves.
1 16734:1 (5)
4.0 Refernnc.ns 1.
ASME Boiler and Pressure Vessel Code,Section III, Article NB 7000, l
1971 Edition Winter 1972 Addenda.
2.
Topical Report - Overpressure Protection for Westinghouse 1
Pressurizer Water Reactors, WCAP 7769, Rev.1, June 1972.
3.
Certified Safety Valve capacity, Calculation No. CSDA-83-21; SAT 0/POE-lli, February 28, 1983.
4.
NEU Loss of Load Analysis, Calculation No. CN-PP-81-220, November, 1981.
5.
NEU Rod Withdrawal at Power Analysis, Calculation No. CN-PP-82-08, January, 1982.
6.
NEU Loss of Flow / Locked Rotor Analysis, Calculation No.
CN-PP-8,2-46, March, 1982.
7.
NEU Loss of Normal Feedwater/ Station Blackout Analysis, Calculation No. CN-PP-81-222, January, 1982.
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