ML20040H006

From kanterella
Jump to navigation Jump to search
LER 82-002/03L-0:on 820114,RCS Letdown Isolation Valve CV-1221 Failed to Close Properly During Quarterly Surveillance Test.Caused by Torquing Out of Valve Operator Apparently Due to Low Torque Switch Setting
ML20040H006
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/01/1982
From: Rogers P
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20040G999 List:
References
LER-82-002-03L-01, LER-82-2-3L-1, NUDOCS 8202160725
Download: ML20040H006 (2)


Text

.

.g

= .

NRC FORM 3E4 (7 771 U. S. NUCLE AR REGUL ATOR Y COMMISSION LICENSEE EVENT REPORT EXHtBIT A CONTROL i BLOCK: l l l l i ei ih (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI p8 i AlR 9 l Al Nl 0l 1lg[ 010 l -l0LaCENSE L8CENSEE CODE 44 15 l 0 l Nwo6(H0] 0l 0 l- l 0IS l0 lgfL,(l1L N:,El 1I V,il1 l 1 lgl l lg 26 40 $7 CAT $45 CON *T o '

I S Ou's LLJ@l0 60 ti I s pDOCutT 10101311131@l Nu SER tel oi li l l 418121@l 01 2l 01 11 a l 21@

63 EVENT DATE 34 'S HE,OHT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h o

I On 1-14-82 while at 84% full Dower, the Reactor Coolant System (RCS) i o a i letdown isolation valve CV-1221, failed to close properly during a i o . I quarterly surveillance test which is required per T.S.4.4.1.4. If RCS i in isi 11etdown isolation had been necessary, the letdown cooler inlet valves, i o e i CV-1213 and CV-1215, the letdown cooler outlet valves, CV-1214 and CV- ,

o > (1216. or the letdown block valve and letdown flow control valve, CV-1222 i o ,, i and CV-1223 respectively, could have been closed. In the event of

' ' ' i s :it. C ua C.us. (co,n,,p on aptacnmeny, .o Cool ,

LCCE $UaCool Lo *OktNT Cout sueuout E

' ' I Pl Cl@ LEj@ "

LXJ@

l VI Al L IV 10 I Pl@ LA_j@ Q @

suisLout

~

a -N NT,?. ",9%?! " '" $ ' " h ?'," "' *;""

@ ,a'g..  ; I 8I 21 u

7 KEN ACT N u n L-J n

l 01 012 i

>< 2.,

L_J v

l013I 2 r.

LLJ se L, J d u

,L NT MET 00 MOURS 22 SS 1 0 8 H Sue,t .AN ,aCTu ER LILJ@LX_J@

3J 34 Lzl@

33 LZJO 3t> I 0I 010140i LYJ@ LYj@ LNj@ l L ! 2l0 [ Ol@

33 el 41 aJ 4e op CAUSE DESCRIPTION ANO CORRECflVE ACTIONS h Luo_j l The valve operator had apparently torqued out during operation. Trouble-

[ED I shooting revealed no unusual mechanical hindrance, but did reveal that the EII] I toraue switch settino was in the lower portion of the recomended operat-i i 3 l ina rance. The torque switch setting was increased slightly within the i i 4 Irecommended rance. i 7 8 9 STA  % ,0WER OTM(MSTATUS st v HT De5Cuv E H V i s NA

  • LEJ@ 101814"l@ln I LBj@l Routine SurveillEOCHe,teo ance l

. !T,,,, , Ca ,, ,,,

a a =

.s u asio O,ai u se

.o tur,cNO,,,,a.:,@

LLic]

' ' LZJ

' ,,u.so .'.*< ,,,os

@ l ILJ@e , NA,oOuNTor.CTivif, l

NA

@l =

g

o. . T.,E onc~,,,oN @

i i 10101 Ol@@j@l NA

' ' ' " l

. so NA',, ;uLs =>

Nuo.ca casC..I,oN@

i -

101 010 l l NA

' h,s,o, o,og@,ce' [ o,.Ciui< g

  • a l

8 [JJ@l NA ,

l 2 .L,tsu,'"@l*"hfts'C.,,T,o NA

@ Nac ust mov

> a ,a i [illjir,!,,,;

NAME OF PREPARER - Patrick Rooers _ ,,, oy , _ 5di/964-3100 8202160725 B20201 PDR ADOCK 05000313 S PDR

1

- '* ATTACHMENT LER NO. 50-313/82-002/03L-0

'EVENTDESCRIPTIONANDPROBABLECONSEQUENCES(cont'd) engineered safeguards actuation CV-1214 and CV-1216 would have automatically closed to isolate letdown. This occurrence is reportable per T.S.6.12.3.2.b.

Similar occurrences were reported by LERs 50-313/81-011,81-009, 80-033,80-023, 79-021,78-002 and 75-012.

T

.