ML20003B183

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LER 81-003/03L-0:on 810106,surveillance Frequency for Monthly Diesel Fuel Oil Quality Analysis Was Exceeded.Caused by Personnel Oversight.Analysis Performed W/Satisfactory Results
ML20003B183
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 02/06/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003B179 List:
References
LER-81-003-03L, LER-81-3-3L, NUDOCS 8102100491
Download: ML20003B183 (1)


Text

NEC FORM 366 U. S. NUCLEAR RECULATORY COMMISSION (777 '

LICENSEE EVENT REPORT LER 81-03/3L CoNTROtstOCx: 1 i I 1 1  !

l@ (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 0 l 8t l9 l VI LICENSEE 7

Tl VI CCOE Yl SI 1l@l 0 l 0 l - l 0 LICENSE 14 15 l 0 l 0NUM8ER l 0 l 0 l - l 0l O a5

!@l4 26 lLICENSE 1l 11TYPE 1l 1l@l JG l

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S i LA T be CON'T 10111 s$RC60l L @l 0151010 l 01217 l681 @l 01EVENT Il 0l 6l 8l 1 @l0121016 l 81180l@

? 4 74 61 DOCK ET NUMSER 63 CATE 75 REPORT D ATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h tol2l l During the weekly review of surveillance testing data, it was discovered that the I 10131 I surveillance f requency for the monthly diesel fuel oil quality analysis was exceededL Io!.l l Since the analysis was immediate1v and successfull- done and each delivery of I l o i s t i fuel oil is analyzed prior to storage in the plant tank, it is concluded that there I l o is I l were no consecuences to the health and safety of the nubifc_ Othor occurrences I loI7ll were reported as RO 80-34/3L. R0 80-05/3L and RO 79-12/3L. I lotal! l 7 8 SO DE CODE 5 BC E COMPCNENT CODE S48 O'E SU 0E lal91 7 8 l Z l 7. Ih l A lh l D lh l Z l 7. l Z l 7. l 7, l Z lh Wh W h 9 10 11 20 12 13 18 19

_ SEQUENTI AL OCCURRENCE REPORT REVtSION LER RO EVENTVEAR R EPORT NO. COCE TYPE NO.

O"s3g Ial11 l-l 10 10 13 I l .-l l0 l 3 l lt i L--J LO_J

_ 21 22 2J 24 26 27 28 23 30 31 32 TAK N AC ON ON PL NT METH HOUR $ $8 l FOR 6. $UPPL E MANUFAC RER IHj@lZI@

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42 43 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h liioll The analysis was not performed as scheduled due to personnel oversistht. The l li{ij l analysis was immediately performed with atisfactory results. Applicable personnel I g ;have been reinstructed in the requirements of the surveillance testing program. I t i 131 I l LLidJ l I 7 8 g 80 ST S  % PCwER OTHER $7ATUS 15 C RY I Ol$COVERY C($CRtPTION Ii j s l l Cl@ l 0 l 8 l 7 l@l NA l lB l@lReview of Surveillance Data l

'J1,viTv Co'RTENT '2 " " '

REtEAsEo o, aEttisE ocCAT,0~ o, RELEASE @

AMOUNT e, ACTIVITY @l l1l6l 7 8 9 h 10

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45 NA 80 l

PERSONNEL E APCSURES NUveER TYPE C ;SCRIPTION l i l i l 1 01 01 Ol@lZ_J@l NA  !

PERSONNE'L INJUNIES NUYBER DESCRIPTION @

lilailololol@l 7 8 9 11 12 NA' 80 I

TYPE CESCR PT ON I7 I 9I Lzj@l NA I 7 d 3 10 80

  • UBLICITY NRC USE ONLY issuto OESCRiPrics 45

[_2 l 0 l l N l@l NA l [j;;;;;;[j;;lh 7 8 9 10 68 69 60h N

  • U NAME CF PREPARER 8102100 Yf/