ML19350E868

From kanterella
Jump to navigation Jump to search
LER 81-015/03L-0:on 810528,air Circuit Breaker for Pump P-8-1B Tripped Free When Closed,Preventing Performance of LPCI Sys Logic Test.Caused by Worn Bushings on Operating Mechanism.Circuit Breaker Replaced & Tested
ML19350E868
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 06/16/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19350E866 List:
References
LER-81-015-03L, LER-81-15-3L, NUDOCS 8106230603
Download: ML19350E868 (1)


Text

-.

l Nitc pones aos ~ u. s. NUCLEAR REIULATdGY COAAMISSION

- (7.m

-p LICENSEE EVENT REPORT - LER 81-15/3L O co 1 o' 'oc e i, i i i i i p < TEA .Nr o 1, A Eoe fo NPe MA11e >

10 l1l F 8 9 l Vl UCENSEE Tl Vl CODE Yl Sl 1l@l0 14 . tS l0 l- l 0'l0UCENSE 0 l 0 l- l 0 l 0 2h @l26 4 l UCENsE l 0 lNuMeER 1l 1l TYPE 1l 1l@l J0 l

57 CAT 68 l@

CON'T M - *souRy Ql0 l 5 l0 l 0 l0 l 2 l-7 l 1 G)l 0 l 5 l-2 l 8 l 8 l 1 74l@l0 l 6 l 1 l 6 l 8 l 180 l@

-7 8 60 61 DOCX E T NUMgER 68 ' 69 EVENT DATE 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121. l The ACB's for RHRSW Pumps P-8-1B&D must be rocked down in order to conduct the l ITTT'l I 'B' LPCI System Logic Test. Contrary to T.S. 3.5.C.2. the ACB for Pump P-8-1B l 10 l A i l would trip free when closed. All other components of the RHRSW were determined to l 10 i s 1 l be operable. The circuit breaker was replaced and the testing satisfactorily com- l 10teiI pleted'. Based on the above. there were no adverse consecuences to the public healthi l C I 7 I l and safe ty. No nrevious similar occurrences have been reDorted to the Commission. l 10181I l

.7 e, so SOI:E . C0$I sNC0$E COMPONENT CODE sus OC'E SUN E

[ 0, l,9,j lC lF l@ lE l@ l A l@ lC lK lT lB lR lK l@ y@ y @

9 7 8 10 11 12 IJ 18 19 20 sECUENTIAL OCCURRENCE REPORT REVislON LER EVENT YEAR REPORT NO. CODE TYPE NO.

@ ,REPg'Rol8lll 21 22

[-

23 J l0 l1 l5 l 24 26 l/l 27 l 0l 3l 28 29 lL l 30 8

31 W

32 7K AC C 0 P T ME HOURS s8 I POR 8. su L MANUP MER W @lZl@

23 34 (Z,_,j@ (Z,,J@ l0 l01010 l W@ l42Y l@ lAl@ l44G l 0 l 8 l 47 0l@

3a 36 37 40 41 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l This event was caused by worn bushings on the operating mechanism causing the l g l breaker to trip free upon closure. The breaker was manufactured by General Electrici

, l Model AM 4.16 250-8HB. The corrective action was to replace the circuit-breaker l g l and demonstrate satiefactory operation of the RHRSW pump. l I

L'_1.4 ! I 7 . . .0

's'T"2 Ws* sPowtR CTwtR status @ CisEOSOv' oisCQvERv oEsCRiPnON @

lilsl W @ l1l0l0l@l NA l l45B l@l Surveillance Test l

-7 4 Ig 12 11 44 46 80 MEASED OF MEASE LOCAnCN CP RELEASE @

W LzJ

@ W@l '

AMOUNTOF NA ACnVITY l

@I NA l PERsONN[i. E xPCsuE Es NUveER TvPe otsCRiPv0N @

l117ll010l0l@

W @l

NA PERsONNEENJu' dies Nuu8ER oEsCRiPnON@

NA li la 3l l9 01 Ol 0l@l 12 l

7 11 80

?V E DE R PT Or NA U_L.J LZ_l@l l 7 4 9 10 80 NRc USE CNLY

.ssuE o'ESCaiPnON@

[,2do,,J lN hl NA I lt lIIllll11I l*:

7 4 3 to 68 69 80 ;

NAMEC PARER PHONE: (802) 257-7711  ?

8106280 dF

. - -. -. -. - -- - . - - -