LER-1981-041, /03X-1:on 810323,pressurizer Level Channels 1-L-68-339,1-L-68-325C & 1-L-326C Declared Inoperable.Caused by Erroneous Indications Due to Condensate Reservoir Mod Resulting in Increased Static Head in Common Sense Line |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3271981041R03 - NRC Website |
|
text
n.
" U, CONTaOt ato:<: 1 l
l l
1 l
l iPttAss P iNr on tvPe att nsoumEo iNee=AreNi fo lil IT IN ls IN !P'l1 !h!0lO!-l0l0!Ol0l0l-l0l0 l@l4 ! 1 l 1 l 1 l 1 l@l l
l na Cag gij @
P 8 9 LICEN145 CQOg to il LICENSE NuuttM 25 24 LICENSE t yrs Jo CON'T
- ol 1 3[,,$ Lhl015 10 10 10l3l2I7 @l01312 l318l1 @l0I5l1l5l8l1l@
t 4
64 6t DOCatiTNUMOEM 64 49 LVINT DAfg 34 Il PLPORT DATE 80 cvtNT DESCalPTION AND Pn00A8tE CONSEQUENCES @
Ulal lWith Unit I at 97% newer. oressurizer level channels 1-L-68-339, 1-L-68-325C. and o l 31 l l-L-326C declared inoperable when erroneous indications were observed. On 4/2/81, o 14 I l 1-LI-68-339 was again declared inoperable. On 4/17/81, 1-LI-68-325C ahd 1-LT-68-326C
, o I 5 I l were again declared inoperable. On each occasion, the plant entered the applicable
. o is 1 I action statement: LCO 3.3'.1.1 (7) and LCO 3.3.3.5 (a). There was no effect upon 0171 l oublic health or safety. No previous occurrences.
!ola l l v.[v sysitu C4ust
Cause
Cove.
CODE COct*
suecot)t CO8A*CNENT C00E suSCCCE suecoot l t l Alh [B_jh l B lh l Il Nl S l T l R l U lh [_Tjh,[Z_j h oist t
3 9
to 11 12 83 18, 19 20 sEOUf NTI AL OCCURRENCE MEPORT REVistoN Lg nino VENTY(AM R E PonT No.
40oE TYPE No.
@,agg (I8l1I l-l I o 14 l 1 l
{t_]
I 0"I 3 i Lx_]
l--J LtJ
_ 20 22 23 24 26 27 28 29 30 38 32 Actf0f O rLANT MET HOURS 50 IT T FOn [US.
sVPPLit MANU,ACTURER 1A r lF l@l Fl@
l Z l@
lZl@
l 0 l0 l 0l 0l l Y l@
lNl@
lN l@
lB l0l8l0 JJ J4 JS 36 37 40 48 e2 43 44 4
CAUSE DESCntPTION AND CONNECTIVE ACTIONS h i i 1 o 3 lThe ' apparent cause of the error was an' increased static head in a ' common sense line due li1 lto a condensate reservoir modification made under ECN L5392. When corrective actinnn
,;y; ltaken (work plan 9117) failed to correct the conditions, the instrument sense line
,,3 g l configuration was returned to the original configuration (prior to ECN L5392) and the -
l 8 i*I lloons were returned to service.
L i a
sfA
%PontR OTHEn status isc vt Discovt'1Y DisCniPTr04
' I $ I [1.jh l 0l 9 l 7 l@l NA l
lB l@l channel check 40:ive r y Co'0 renf
' In l I Z i @ (LJ@l AoouNT o,ACTivifv @ I toCiToNo,.uAs.@
,u Asto c, neu An NA l
NA
- *,inse~Nci...c a s ocicoi,1,o4 @
~o.,...
1vPc il2]I010l0j@lZlhl NA
,c a s o~ Nil'iN,u'li s o.,C.....oN e
~e...
i in i l oi 01 o l@l NA i,
12 toss or on cauAGE 70 FACILITY tv't DESCntatione l III [Ejhl NA
- 9 to 9
issur OE stnip tion
' I e l l_1 @l i
lIlIllliI1ll m
a 9 iG ss s9 1
l Name of Preparer A.
M. Ullkov AL p. Ib vrl f,,,
Phone (615) 842-8317 RLU0dJLA O b
E---.-
~
Sequoyah Nuciscr Fitnc LER SUPPLEMENTAL INFORMATION SQRO-50-327/81041 REVISION 1 During a channel check performed on March 23, 1981, pressurizer level loop 1-L-68-339 was discovered to be indicating approximately 15% lower than r redundant channels. The loop was declared inoperable and the associated reactor protection bistable was tripped in accordance with action 7 of Since auxiliary control room loops 1-L-68-325C and 1-L-68-326C LCO 3.3.1.1.
After shared a common sensing line with 1-L-68-139, they were also checked.
verifying that the two auxiliary control loops were also indicating approx-imately 15% low, the plant entered action statement "a" of LCO 3.3.3.5.
The error was diagnosed as an increased static head in the common reference A modification to this leg had been performed leg for the loop transmitters.
(ECN L5392) to improve the performance of the condensate pot in the reference The 15% error was leg to ensure that the reference leg was maintained'.
attributed to an accumulation of water in the tubing added by ECN L5392.
To compensate for the increased static head, the pressurizer high level In addition, temporary trip bistable setpoint was shifted from 92% to 76%.
scales were installed on main control room indicators to enable operators to obtain direct readings. The auxiliary control room loops were retubed to the sensing line for 1-L-68-335, which did not have the sense line modification (ECN L5392).
On April 2, 1981, a channel check of 1-L-68-339 revealed that loop to be indicating approximately 8% high. Since this indicated that previous corrective action was not adequate, the loop was declared inoperable and the associated bistable tripped in accordance with action statement 7 of A return to the premodification configuration was planned LCO 3.3.1.1.
for the next unit outage.
On April 17, 1981, auxiliary control room loops 1-L-68-325C and 1-L-326C were observed to be reading approximately 15% high. The plant again 4
l entered action statement "a" of LCO 3.3.3.5.
i During the subsequent unit outage, the sense lines for 1-L-68-339, 1-L-68-325C,
(
Since_this 1-L-68-326C were returned to their premodification configuration.
configuration is susceptible to variations in the reference leg static head, Since losses I
the loops will be monitored closely and refilled as necessary.
of condensate in the reference leg result in higher (than actual) pressurizer level signals, the limiting safety system setting of 693% will not be compromised..
A design change request has been initiated for a permanent solution to the condensate pot deficiencies for the pressurizer loops.
l 1
l l
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000327/LER-1981-001-03, /03L-0:on 810102,condensate Storage Tank Level Channel 0-L-2-230 Declared Inoperable When Control Room Indicator Failed Low.Caused by Disconnected Instrument Sense Line Due to Improperly Tightened Compression Fitting | /03L-0:on 810102,condensate Storage Tank Level Channel 0-L-2-230 Declared Inoperable When Control Room Indicator Failed Low.Caused by Disconnected Instrument Sense Line Due to Improperly Tightened Compression Fitting | | | 05000327/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000327/LER-1981-002-03, /03L-0:on 810109,two Intermediate Deck Doors in Ice Condenser Found Frozen Closed.Caused by Water Leaking from AHU-3A Defrost Drain Line Flange Due to Loose Flange Bolts.Bolts Retightened | /03L-0:on 810109,two Intermediate Deck Doors in Ice Condenser Found Frozen Closed.Caused by Water Leaking from AHU-3A Defrost Drain Line Flange Due to Loose Flange Bolts.Bolts Retightened | | | 05000327/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000327/LER-1981-003-03, /03L-0:on 810105,main Feedwater Flow Channel F-3-35B Failed Low.On 810112 Feedwater Channel F-3-35B & F-3-90B Failed.Caused by Freezing of Inadequately Protected Instrument Sense Lines.Lines Thawed | /03L-0:on 810105,main Feedwater Flow Channel F-3-35B Failed Low.On 810112 Feedwater Channel F-3-35B & F-3-90B Failed.Caused by Freezing of Inadequately Protected Instrument Sense Lines.Lines Thawed | | | 05000327/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000327/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000327/LER-1981-004-03, /03L-0:on 810112,RWST Instrument Channel L-63-54 Failed.Caused by Sense Lines Freezing Due to Insufficient Insulation Around Lines & on Sides of Cabinet Housing Level Transmitter.Heaters in Use Until Insulation Can Be Added | /03L-0:on 810112,RWST Instrument Channel L-63-54 Failed.Caused by Sense Lines Freezing Due to Insufficient Insulation Around Lines & on Sides of Cabinet Housing Level Transmitter.Heaters in Use Until Insulation Can Be Added | | | 05000327/LER-1981-005-03, /03L-0:on 810114,capacitor C1A in A10 Power Supply & Control Card RB-8 Failed While in Svc.Caused by Failure of Vital Inverter 2-II.Components Replaced & Inverter Returned to Svc on 810114 | /03L-0:on 810114,capacitor C1A in A10 Power Supply & Control Card RB-8 Failed While in Svc.Caused by Failure of Vital Inverter 2-II.Components Replaced & Inverter Returned to Svc on 810114 | | | 05000327/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000327/LER-1981-006-03, /03L-0:on 810114,stroke Test Not Performed Following 800929 Repair of Leaking Valve 1-FCV-63-38.Caused by Inadequate Procedure.Procedure Being Revised | /03L-0:on 810114,stroke Test Not Performed Following 800929 Repair of Leaking Valve 1-FCV-63-38.Caused by Inadequate Procedure.Procedure Being Revised | | | 05000327/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000327/LER-1981-007-03, /03L-0:on 810116,level Channel for Steam Generator 3 (L-3-97) Declared Inoperable.Caused by Failure of Trip Bistable 1-LS-3-97F to de-energize.Module Replaced,Calibr & Returned to Svc | /03L-0:on 810116,level Channel for Steam Generator 3 (L-3-97) Declared Inoperable.Caused by Failure of Trip Bistable 1-LS-3-97F to de-energize.Module Replaced,Calibr & Returned to Svc | | | 05000327/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000327/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000327/LER-1981-008-03, /03L-0:on 810116,three Intermediate Deck Doors to Ice Condenser,Under Air Handling Units 6A,8A & 8B,found Frozen Closed.Caused by Frozen Water in Drain Lines Due to Fuse Failure in Heat Tape Controller.Ice Removed | /03L-0:on 810116,three Intermediate Deck Doors to Ice Condenser,Under Air Handling Units 6A,8A & 8B,found Frozen Closed.Caused by Frozen Water in Drain Lines Due to Fuse Failure in Heat Tape Controller.Ice Removed | | | 05000327/LER-1981-009-03, /03L-0:on 810127,containment Sump Level Loop L-63-177 Declared Inoperable.Caused by Calibr Drift Due to Problem W/Level Transmitter.Transmitter Replaced | /03L-0:on 810127,containment Sump Level Loop L-63-177 Declared Inoperable.Caused by Calibr Drift Due to Problem W/Level Transmitter.Transmitter Replaced | | | 05000327/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000327/LER-1981-010-03, /03L-0:on 810128,notification Received That During Ieb 79-14 review,180-1b (Light) Weight Discrepancy Discovered,Altering Support Design Requirements.Caused by Incorrect Weights Being Used in Computer Analysis | /03L-0:on 810128,notification Received That During Ieb 79-14 review,180-1b (Light) Weight Discrepancy Discovered,Altering Support Design Requirements.Caused by Incorrect Weights Being Used in Computer Analysis | | | 05000327/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000327/LER-1981-011-03, /03L-0:on 810130,vital Inverter & Vital Instrument Power Board 1-I Declared Inoperative.Caused by Severance of Conduit & Cable B30I Supplying Power to Inverter.Cable & Conduit Replaced | /03L-0:on 810130,vital Inverter & Vital Instrument Power Board 1-I Declared Inoperative.Caused by Severance of Conduit & Cable B30I Supplying Power to Inverter.Cable & Conduit Replaced | | | 05000327/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000327/LER-1981-012-03, /03L-0:on 810126,RCS Tave Decreased Below Limits. Caused by Operator Failure to Coordinate Turbine Loading Rate.Turbine Load Reduced & RCS Tave Increased | /03L-0:on 810126,RCS Tave Decreased Below Limits. Caused by Operator Failure to Coordinate Turbine Loading Rate.Turbine Load Reduced & RCS Tave Increased | | | 05000327/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000327/LER-1981-013-03, /03L-0:on 810203,liquid Radwaste Monitor, 0-RE-90-122,declared Inoperable.Caused by High Background Count Reading Due to Leak in Brooks Rotameter.Rotameter Seals Replaced,Sample Chamber Cleaned & Monitor Flushed Out | /03L-0:on 810203,liquid Radwaste Monitor, 0-RE-90-122,declared Inoperable.Caused by High Background Count Reading Due to Leak in Brooks Rotameter.Rotameter Seals Replaced,Sample Chamber Cleaned & Monitor Flushed Out | | | 05000327/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000327/LER-1981-014-03, /03L-0:on 810123,testing Procedure SI-158 for Containment Isolation Valves 1-FCV-62-72,73 & 74 Was Determined to Be Inadequate.Caused by Failure to Take Into Account back-pressure in Line.Procedure Changed | /03L-0:on 810123,testing Procedure SI-158 for Containment Isolation Valves 1-FCV-62-72,73 & 74 Was Determined to Be Inadequate.Caused by Failure to Take Into Account back-pressure in Line.Procedure Changed | | | 05000327/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000327/LER-1981-015-03, /03L-0:on 810216,during Surveillance Testing,Ice Condenser Basket Bays 1,18 & 24 Were Found Below Limits for Average Basket Weight.Caused by Sublimation.Ice Added Throughout Ice Condenser | /03L-0:on 810216,during Surveillance Testing,Ice Condenser Basket Bays 1,18 & 24 Were Found Below Limits for Average Basket Weight.Caused by Sublimation.Ice Added Throughout Ice Condenser | | | 05000327/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000327/LER-1981-016-03, /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated | /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated | | | 05000327/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000327/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000327/LER-1981-017-03, /03L-0:on 810212,welder Accidentally Blew Pin Hole in Pipe Sleeve,Releasing Low Level Activity Xe-133.Caused by Thin Wall Pipe & Restricted Access.Pin Hole Repaired | /03L-0:on 810212,welder Accidentally Blew Pin Hole in Pipe Sleeve,Releasing Low Level Activity Xe-133.Caused by Thin Wall Pipe & Restricted Access.Pin Hole Repaired | | | 05000327/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000327/LER-1981-018-03, /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip | /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip | | | 05000327/LER-1981-019-03, /03L-0:on 810211,inside Containment Isolation Valve 1-33-704 on Svc Air Header Discovered Omitted from Drawing.Valve Added | /03L-0:on 810211,inside Containment Isolation Valve 1-33-704 on Svc Air Header Discovered Omitted from Drawing.Valve Added | | | 05000327/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000327/LER-1981-020, Forwards LER 81-020/03X-1 | Forwards LER 81-020/03X-1 | | | 05000327/LER-1981-020-03, /03X-1:on 810207,w/unit in Mode 5 & Auxiliary Bldg Gas Treatment Sys Train B Fan Discharging Through Shield Bldg Exhaust Vent,Radiation Monitor for Exhaust Path 2-RM-90-100 Discovered Inoperable.Cause Not Stated | /03X-1:on 810207,w/unit in Mode 5 & Auxiliary Bldg Gas Treatment Sys Train B Fan Discharging Through Shield Bldg Exhaust Vent,Radiation Monitor for Exhaust Path 2-RM-90-100 Discovered Inoperable.Cause Not Stated | | | 05000327/LER-1981-021-03, /03L-0:on 810211,reactor Coolant Pumps 1 & 2 Were Stopped.Caused by RCS Pressure Going to Zero After RHR Containment Spray Isolation Valve Inadvertently Opened.Pumps Returned to Operable Status in Approx 1-h | /03L-0:on 810211,reactor Coolant Pumps 1 & 2 Were Stopped.Caused by RCS Pressure Going to Zero After RHR Containment Spray Isolation Valve Inadvertently Opened.Pumps Returned to Operable Status in Approx 1-h | | | 05000327/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000327/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000327/LER-1981-022-03, /03L-0:on 810219,w/unit in Mode 5,chlorine Detector O-CLAN-43-205A Declared Inoperable.Caused by Electrolyte Used to Drip Onto Sensor Becoming Stopped Up in Felt Filter.Filter Replaced & Detector Returned to Svc | /03L-0:on 810219,w/unit in Mode 5,chlorine Detector O-CLAN-43-205A Declared Inoperable.Caused by Electrolyte Used to Drip Onto Sensor Becoming Stopped Up in Felt Filter.Filter Replaced & Detector Returned to Svc | | | 05000327/LER-1981-023-03, /03L-1:on 810303,four Undersized Pipe Sleeves Associated W/Seal Injection Water Lines to Reactor Coolant Pumps Identified.Caused by Incorrect Installation.Workplan 9073 Issued to Reshape Subj Piping Sleeves | /03L-1:on 810303,four Undersized Pipe Sleeves Associated W/Seal Injection Water Lines to Reactor Coolant Pumps Identified.Caused by Incorrect Installation.Workplan 9073 Issued to Reshape Subj Piping Sleeves | | | 05000327/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000327/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000327/LER-1981-024-03, /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolatio | /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolation | | | 05000327/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000327/LER-1981-025-03, /03L-0:on 810217,during Surveillance Instruction SI-7,diesel Generator 1B-B Failed to Load Properly.Caused by Blown Fuse in Governor Potentiometer Circuit.Fuse Replaced | /03L-0:on 810217,during Surveillance Instruction SI-7,diesel Generator 1B-B Failed to Load Properly.Caused by Blown Fuse in Governor Potentiometer Circuit.Fuse Replaced | |
|