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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E4821989-11-30030 November 1989 LER 89-019-00:on 890927,identified That Closing Torque on Valves May Be Insufficient Against Postulated Worst Case Differential Pressure.Caused by Initial Plant Construction. Mod to Replace Gearing Made to Motor operator.W/891130 Ltr 1998-10-22
[Table view] Category:RO)
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E4821989-11-30030 November 1989 LER 89-019-00:on 890927,identified That Closing Torque on Valves May Be Insufficient Against Postulated Worst Case Differential Pressure.Caused by Initial Plant Construction. Mod to Replace Gearing Made to Motor operator.W/891130 Ltr 1998-10-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8931999-10-31031 October 1999 Rev 1 to BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20212L1141999-10-0101 October 1999 Safety Evaluation Granting Request for Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c 0CAN109902, Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20216J6271999-09-27027 September 1999 Rev 0 to CALC-98-R-1020-04, ANO-1 Cycle 16 Colr ML20212F5261999-09-22022 September 1999 SER Approving Request Reliefs 1-98-001 & 1-98-200,parts 1,2 & 3 for Second 10-year ISI Interval at Arkansas Nuclear One, Unit 1 0CAN099907, Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with ML20211F4281999-08-25025 August 1999 Safety Evaluation Concluding That Licensee Provided Acceptable Alternative to Requirements of ASME Code Section XI & That Authorization of Proposed Alternative Would Provide Acceptable Level of Quality & Safety 0CAN089904, Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with ML20210K8831999-07-29029 July 1999 Non-proprietary Addendum B to BAW-2346P,Rev 0 Re ANO-1 Specific MSLB Leak Rates 0CAN079903, Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with ML20207E7231999-06-0202 June 1999 Safety Evaluation Authorizing Proposed Alternative Exam Methods Proposed in Alternative Exam 99-0-002 to Perform General Visual Exam of Accessible Areas & Detailed Visual Exam of Areas Determined to Be Suspect ML20196A0191999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20196A6251999-05-31031 May 1999 Non-proprietary Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20195D1991999-05-28028 May 1999 Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14 ML20206M7711999-05-11011 May 1999 SER Accepting Relief Request from ASME Code Section XI Requirements for Plant,Units 1 & 2 0CAN059903, Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with ML20206F0691999-04-29029 April 1999 Safety Evaluation Accepting Licensee Re ISI Plan for Third 10-year Interval & Associated Requests for Alternatives for Plant,Unit 1 ML20205M6941999-04-12012 April 1999 Safety Evaluation Granting Relief for Second 10-yr Inservice Inspection Interval for Plant,Unit 1 ML20205D6061999-03-31031 March 1999 Safety Evaluation Supporting Licensee Proposed Approach Acceptable to Perform Future Structural Integrity & Operability Assessments of Carbon Steel ML20205R6351999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ano,Units 1 & 2. with ML20205D4711999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Employ Alternative Welding Matls of Code Cases 2142-1 & 2143-1 for Reactor Coolant System to Facilitate Replacement of Steam Generators at Arkansas Nuclear One,Unit 2 ML20204B1861999-03-15015 March 1999 Safety Evaluation Authorizing Licensee Request for Alternative to Augmented Exam of Certain Reactor Vessel Shell Welds,Per Provisions of 10CFR50.55a(g)(6)(ii)(A)(5) 0CAN039904, Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with ML20212G6381999-02-25025 February 1999 Ano,Unit 2 10CFR50.59 Rept for 980411-990225 ML20203E4891999-02-11011 February 1999 Rev 1 to 97-R-2018-03, ANO-2,COLR for Cycle 14 ML20199F0351998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ano,Units 1 & 2 ML20198M7841998-12-29029 December 1998 SER Accepting Util Proposal to Use ASME Code Case N-578 as Alternative to ASME Code Section Xi,Table IWX-2500 for Arkansas Nuclear One,Unit 2 0CAN129805, LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With1998-12-11011 December 1998 LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20198D2441998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ano,Units 1 & 2. with ML20199F7401998-11-16016 November 1998 Rev 9 to ANO-1 Simulator Operability Test,Year 9 (First Cycle) ML20195B4801998-11-0707 November 1998 Rev 20 to ANO QA Manual Operations ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 0CAN119808, Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with ML20197H0741998-10-29029 October 1998 Rev 1 to Third Interval ISI Program for ANO-1 ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20154J2471998-10-0909 October 1998 SER Accepting Inservice Testing Program,Third ten-year Interval for License DPR-51,Arkansas Nuclear One,Unit 1 0CAN109806, Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods 0CAN099803, Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with ML20237B7671998-08-19019 August 1998 ANO REX-98 Exercise for 980819 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed 0CAN089804, Monthly Operating Repts for July 1998 for Ano,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ano,Units 1 & 2 ML20196C7831998-07-30030 July 1998 Summary Rept of Results for ASME Class 1 & 2 Pressure Retaining Components & Support for ANO-1 ML20155H7161998-07-15015 July 1998 Rev 1 to 96-R-2030-02, Revised Reactor Vessel Fluence Determination ML20236R0531998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ano,Units 1 & 2 ML20249B7791998-06-22022 June 1998 Part 21 Rept Re Findings,Resolutions & Conclusions Re Failure of Safety Related Siemens 4KV,350 MVA,1200 a Circuit Breakers to Latch Closed ML20249B5091998-06-15015 June 1998 SG ISI Results for Fourteenth Refueling Outage 1999-09-30
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.- Lee HxA AR 722D3 Tel 501377 4000 October 6, 1989 1CAN198954 U. S. Nuclear Regulatory Commission Document Control Desk Mail Station P1-137 Washington, D. C. 20555
SUBJECT:
Arkansas Nuclear One - Unit 1 Docket No. 50-313 License No. OPR-51 Licensee Event Report No. 50-313/89-032-00
(
Gentlemen: I In accordance with 10CFR50.73(a)(2)(1)(B), attached is the subject report concerning inadequate procedural guidance which resulted in the failure to perform the reactor building area radiation monitors monthly surveillance required by Technical Specifications.
! Very truly yours, i E. C. Ewing General Manager, Technical Support and Assessment 1
ECE/0M/sgw attachment cc: Regional Administrator Region IV U. S. Nuclear Regulatory Commission 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 INP0 Records Center 1500 Circle 75 Parkway Atlanta, GA 30339-3064 p >>
0910160264 POR 891016 1 I
S ADOCK 05000313 PDC
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Firm 1062.01 A NRC Fem N6 U.S. Nuclear Regulatory Commission (9-83) Approved OMB No. 3150 0104 Expires: 8/31/85 LICENSEE EV(NT REPORT (L E R)
~ FACILITY NAME (1) Arkansas Nuclear One, Unit One IDOCKET NUMBER (2) IPAGE (3) 10151010101 31 11 !!110Fl013 TITLE (4) Inadequate Procedural Guidance Results in the Failure to Perfom the Reactor Building Ares Radiation Monitors Monthly Surveillance Required by Technical Specifications EVENT DaTE (5) ,ER NuteER (6) i REPORT DATE (7) i l l IJequentiell IRevisioni OTHER FACILITIES INVOLVED (8) ~
I 1 i Month! Day lYear lYear 1 l Number l l Number IMonth Day lYear i Facility Names Docket Number (s)
I 1 I I I i l l l 1 0 3 0 0 0 1 01 91 01 6 81 91 81 91--I 01 31 Pl"I 01 of II 01 01 61 81 91 0 4 0 0 0 t
OPERATING lTHIS REPORT 15 5UgMIIILD PUR5UANT TO THE REQUIREMENT.5 0F 10 CFR 5:
MODE (9) Ni (Check one or more of the follt.winn) (11)
POWERl ,
,,,,,1 20. 402(b) l,,,,,l 20. 405(c) l l 50.73(a)(2)(iv) l LEVEll (10) 10171411,,,,,,l1 20. 405(a)(1)(1) i,,,,1 Sn.36(c)(1) l I 50.73(a)(2)(v) i.,,,1 20.405(a)(1)(ii) 20.405(a)(1)(iii) 50.36(r )
l3l150.73(a)W(2)(1)1.,,,,1 1
l[l50.73(a)(2)(vit)
_ 1_'t 73.71(c)l**l 50.73(a)(2)(v111)( A)l,,,,,1 Other (Specify in Abstract below and 73.71 l1,,,,l120.405(a)(1)(v)
- 20. 405(a)(1)(i v) l,,,,,1 50. 73(a)(2)(11 ) l_l 50.73(a)(2)(viii)(B)I in Text, NRC Form 1 l 50.73(a)(2)(iii) i i 60.7a(a)(2)(x) i 366A)
LICENSEE CONTACT FOR THIS LER C,2 )
, Name i Telephone humber Dana Millar, Nuclear Safety and Licensing $pecialist l Area l ICode l 510111916141-13111010 COMPL8iTE ONE LINE FOR [ACH COMPONENT FAILURE DISCRIBED IN THIS REPORT ( .3) l l -l lReportablel l l l l lReportablel Causel$ystem ConDonent IManufacturerl to NPRDS I Causel$ystem Component IManufacturerl to NPRD$ 1 i l l l l i i
1 i I i i i i I I l i I I I I I I i 1 l l l l 1 o l I l i I I I I I I i i i i l I i SUPPLEMDr REPORT EXPECTED (14) Day Year EXPECTED l Month H SUBMI$510N l l*l Yes (If ves. complete Expected Submission Date) til No I DATE (15) i I I I I I ABSTRACT -(Limit to 1400 spaces, i.e. , approximately fif teen single-space typewritten lines) (16)
Or September 6, 1989, it was discovered tha* the monthly functional test for the reactor building area radiation oonitors was not performed as required by Technical Specification. A new procedure for the testing of these monitors had been written and the monitors had been deleted from the original test procedure. A Master Test Centrol List (MTCL), maintained to track the testing requirreents associated with Technical Specifications, should be revised whenever a procedure that may affect the MTCL is changed. Currently, there is no procedural guidance given to ensure this is accomplished. A revision
< to the MTCL was submitted with the revisions to the area radiat%n monitor procedures, however, due to an error on the MTCL revision request it wss not approved at the game time the area radiation monitor test procedures were approved and implemented on June 26, 1989. The time lapse associated with the final approval of the MTCL revision resulted in the reactor building area radiation monitors not being tested as required. The subsequent satisfactory completion of the surveillance indicated the monitors were operable. To ensure that a required Technical Specification surveillance is properly identified on the MTCL, a revision to the Procedure Revision Request Form, which accompanies each procedure change, and specific procederal guidance concerning the MTCL has been initiated.
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- NRC F9m M6A F;rm 1062.018 :
,(9*43). . U.S. Nuc1:ar Rogulatiry Commissign !
- Approved OMB ho. 3150 0104
' Expires:. 8/31/85
- LICENSEE EVENT REPORT (LER) TEXT CONTINHA110N l FACILITY NAME (1) f i'
(DOCKET NJWER (2) l LER NUPSER (E) l PAGE (3) ,
Arkansas Nuclear One, Unit One l l l 15equentiall IRevisionl J l l_ Year i Number Number ( !
10151010101 31 11 31 81 9 -l 01 31 2 --
01 OI0lP10Fl013 '
i TUT (If,more space is required, use additional NRC Fem 366A's) (17)
A. Plant Status i
At the time of occurrence of this event Arkansas Nuclear One, Unit One (ANO-1) was operating at i 74 percent of rated thermal power. Reactor Coolant System (RCS) (AB) pressure wat approximately )
2150 psia and RCS teoperature was about 579 degrecs Fahrenheit. ;
- 8. Event Description ,
On September 6,1989, it was discovered that the required monthly functional test of four area radiation monitors (ll) located inside the AND*1 reactor building had not been performed within i the allowable surveil)ance interval specified in the ANQ 1 Technical Specifications. In June 1989, i a procedure which centained the testing requirements for each area radiatier monitor located
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throughout the plant aaas revised into two procedures, a new procedure addressing testing of only the area radiation monitors located in the reactor builoing ano the origine) procedure for the testing requirements of the remaining area radiation monitors (deleting the reactor building l area radiation monitors). On June 26, 1989, these two procedures were approved and authorized for i use by the Plant Safety Committee (PSC).
- A Master Test Control List P CL) procedure, which lists the surveillknces that are required by Technical Specification, is used by Plannir.g and $cheduling personnel to ensure surveillances are scheduled and performed within the required time intervals as established by Technical Specifications. Any time procedures are changed which are reflected on the MTCL, an appropriate change to the MTCL procedure may be necessary. Personnel responsible for writing or changing procedures are responsible for ensuring that the MTCL procedure is revised, if necessary. When the new procedure was written for the testing of the rest
- tor building area radiation monitors and the ceiginal procedure was revised to delete these monitors, a MTCL revision form was prepared and submitted to the PSC, at the same time the new procedures for testing were submitted for approval.
Upon review of the procedures and NTCL revisions by the PSC, the MTCL revision was found to be unacceptable and the procedure writer was notified of the need to correct the MTCL revision prior to apprcval by the PSC. However, the testing procedures were approved and issbed. On September 6, 1989, the MTCL revision request was approved by the PSC. As a result, between June 26 and September 6 the reacter building area radiation monitors were not functionally tested, since the MTCL did not reference the new testing procedure. This error was not detected because the original procedure which had contained the testing requirements for the area radiation monitors located inside the reactor building was listed on the MTCL and had been properly scheduled and performed.
Therefore, it appeared List the reactor building area radiation monitors were being tested as required by Technical Specifications. On September 6,1989, when it was discovered that the reactor building area radiation monitots had not been functionally tested, the monitors were declared inoperable until the testing requirements were completed. The monitors were tested satisfactorily and returned to service on September 6, 1989.
C. Safety $1gnificance Upon completion of the functional testing of the reactor building area radiation monitors, the monitors were declared operable and returned to service. Although the surveillance requirements were not perfomed within the required time interval, the satisfactory completion of the testing indicated the monitors were operable, therefore, no significant safety concerns exist.
Si Root Cause Currently, the station administrativw procedure which provides guidance to personnel concerning the procedure review, approval, and revision process does not address the need to update the MTCL if necessary when a prccedure which may affect the MTCL is changed. Without procedural v ;ance, if a change to the MTCL vvre necessary, the personnel responsible for writing, review %, or changing a procedere could only rely upon thtir memory to ensure the MTCL procedure was appropriately changed. Therefore, the lack of procedural guidance resulted in an unreliable means of ensuring the MTCL was properly updated.
E. Basis for Repottability The failure to perform a surveillance within the allowable interval specified in Technical Specifications is considered to be a condition prohibited by Technical Specifications and is therefore reportable under 10CFR50.73(a)(2)(1)(B).
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F rm 1062.01B
- . NRC F. ors 366A . ,
U.S. Nuclear Regulatory Commisstn
,(F8h) Approved OMI, No. 3150-0104-l'[T
, . Expires: 8/31/85
' LICEldF.E EVENT REPORT (LER) TEXT CONTINUATION i.
~ q~ ' FACILITY NAME (1) lDDCKET NUfW[R (2) l LIR NLNWER (6) l PAGE (3)~
l l i , Sequential i Revisioni Arkansas Nuclear Ot.e, tinit One l l Year Humber Number !-
1015l010101 31 11 3i l l 9 --
O! 31 2 " 01 Ol01310Fl013
, ILKT (If more space is reqsired, use 40ditional NRC Fore 366A's) (17)
F. ' Corrective Actions-When it was identified that the surveillance asscciated with the testing requirements for the reactor building area radiation monitors had not oeen perfonned within the required time interval the tonitors were declared 1.1 operable. Lipon satisfactory completion of the surveillance on September 6, 1989, the monitors were declared operable and returned to service. Additionally, a change to the Procedure Revision Request Form, which is required to accompany each procedure that is subtitted to the PSC for approvais h6s beest initiated. Procedural guidance will be given and a specific entry on the Procedure Revision Request Form required for each procedure as to whether a change to
the MTCL is necessary or not, in the future, if a change to the MTCL in required for a given procedure the required effective date for the procedure to be implemented will be assigned when theMTCLIsupdated. This improved process provides relative assurance that the cause of missing a surveillance as a result of the NTCL not being update should not occu;' again.
G. Additional Information
. There are no ptvviously identified similar events which resulted in a Technical Specification surveillance not being performed within the required testin0 interval.because the MICL was not properly updated.
Energy Indutry Identification System (E!!$) codes are identified in the text as (dX).
i