Letter Sequence Other |
|---|
|
Results
Other: 05000344/LER-1979-013, Forwards Confirmatory Info to NRC 791229 Question 1 Re LER 79-13 Concerning Stresses in Walls Due to Thermal Gradients. Masonry Walls Subj to Thermal Gradient Across Thickness Will Undergo Deformation.Certificate of Svc Encl, 05000344/LER-1979-015-01, /01T-0:on 791019,discovered That Piping Restraint on Concrete Block Wall Might Result in Localized Overstress Condition & Degradation of Support Function Under Design Loads.Caused by Inadequate Consideration of Piping Design, 05000344/LER-1980-007, Forwards Suppl 1 to LER 80-007/01T-0,providing Description of Engineering Review,Reportable Noncomformances & Related Evaluation Results, 05000344/LER-1980-007-01, /01T-0:on 800516,masonry Wall in Auxiliary Bldg Was Discovered Not Connected to Interfacing Structures at Top.Caused by Misinterpretation of Design Drawings.Positive Connection Being Made W/Grouted Reinforcing Steel, 05000344/LER-1983-001, Forwards LER 83-001/01T-0.Detailed Event Analysis Encl, 05000344/LER-1983-001-01, /01T-0:on 830106,field Insps & Review of Const Records Revealed as-built Conditions of knock-out Panel & wall-to-roof Connection Different than Those Considered in Previous Analyses for Three Masonry Walls.Mods Underway, ML17208A791, ML19207B551, ML19208A864, ML19209B063, ML19210C870, ML19210D585, ML19211A367, ML19211A374, ML19224D636, ML19225C762, ML19248C628, ML19249B712, ML19250C487, ML19253C727, ML19256B483, ML19256E423, ML19257A197, ML19257A200, ML19257A202, ML19257A780, ML19257A782, ML19257B266, ML19260B505, ML19262A945, ML19262A949, ML19268C263, ML19269D190, ML19274F793, ML19290C026, ML19290C028, ML19294B330, ML19296D746, ML19296D752, ML19296D933, ML19305B776, ML19308A352, ML19309C368, ML19309C371, ML19309G033, ML19309G034, ML19309G035, ML19318D060, ML19320B202, ML19320D055... further results
|
MONTHYEARML19268C2631966-10-31031 October 1966 Compressive & Transverse Strength Tests of 8-Inch Brick Walls. Addl Info Re Masonry Walls & Certificate of Svc Encl Project stage: Other ML19269D1901979-02-28028 February 1979 Forwards Addl Info Provided by Bechtel Re Proposed Control Bldg Mod:Suppl Info on Shear Wall Specimen Test Program & Addl Info Re Lateral Stiffnesses & Response Spectra Determination.Plans Submittal of Design Mod Rept in March Project stage: Other ML19308A3521979-06-20020 June 1979 IE Bulletin 79-02,Revision 1,Pipe Support Base Plate Designs Using Concrete Expansion Anchor Bolts Project stage: Other ML19256B4831979-06-21021 June 1979 Forwards IE Bulletin 79-02,Revision 1, Pipe Support Base Plate Designs Using Concrete Expansion Anchor Bolts. Action Required Project stage: Other ML19248C6281979-06-29029 June 1979 Forwards Responses to 14 of 50 Questions Submitted in NRC .Will Submit Remaining Responses by 790706. Certificate of Svc Encl Project stage: Other ML19224D6361979-07-0202 July 1979 Forwards IE Bulletin 79-14, Seismic Analysis for As-Built Safety-Related Piping Sys. Action Required Project stage: Other ML19208A8641979-07-13013 July 1979 Forwards Response to IE Bulletin 79-02,Revision 1,re Seismic Category I Piping Sys Support Base Plates Which Use Concrete Expansion Bolts Project stage: Other ML19274F7931979-07-18018 July 1979 Forwards IE Bulletin 79-14,Revision 1, Seismic Analysis for As-Built Safety-Related Piping Sys Project stage: Other ML19225C7621979-07-19019 July 1979 Forwards Corrected Copy of IE Bulletin 79-14,Revision 1, Seismic Analysis for As-Built Safety-Related Piping Sys Project stage: Other ML19207B5511979-08-15015 August 1979 Forwards IE Bulletin 79-14,Suppl 1, Seismic Analysis for As-Built Safety-Related Piping Sys. Action Required Project stage: Other ML19249B7121979-08-20020 August 1979 Forwards IE Bulletin 79-02,Revision 1,Suppl 1,Pipe Support Base Plate Designs Using Concrete Expansion Anchor Bolts. Action Required Project stage: Other ML19209B0631979-09-0505 September 1979 Forwards Responses to NRC 790817 Questions,Transmitted in NRC to Aslb.Includes Info Re Computer Codes for Evaluation of Mods to Control,Auxiliary,Fuel Bldg Complex & Vertical Natural Frequencies Project stage: Other ML19256E4231979-10-22022 October 1979 Confirms NRC 791022 Telcon W/Wj Lindblad Re Facility Steam Generator Tube Defects & Concrete Block wall-pipe Hanger Structural Problems.Discusses Action to Be Taken by Licensee Project stage: Other ML19210C8701979-10-22022 October 1979 Submits Followup to 791019 Rept of Inadequate Pipe Restraint on Spent Fuel Pool Cooling Sys.Plant Presently in Cold Shutdown.Will Complete Corrective Action Before Mode Change Project stage: Other 05000344/LER-1979-015-01, /01T-0:on 791019,discovered That Piping Restraint on Concrete Block Wall Might Result in Localized Overstress Condition & Degradation of Support Function Under Design Loads.Caused by Inadequate Consideration of Piping Design1979-11-0404 November 1979 /01T-0:on 791019,discovered That Piping Restraint on Concrete Block Wall Might Result in Localized Overstress Condition & Degradation of Support Function Under Design Loads.Caused by Inadequate Consideration of Piping Designs Project stage: Other ML19250C4871979-11-0808 November 1979 Forwards IE Bulletin 79-02,Revision 2, Pipe Support Base Plate Designs Using Concrete Expansion Anchor Bolts. Action Required Project stage: Other ML19260B5051979-11-16016 November 1979 Forwards IE Info Notice 79-28, Overloading of Structural Elements Due to Pipe Support Loads. No Response Required Project stage: Other ML19296D9331979-11-21021 November 1979 Forwards Response to IE Bulletin 79-02,Revision 1,Supp 1. Repairs Completed on Five of 11 Pipe Supports W/Anchor Bolt Safety Factors Less than Two, & Eight of 69 Supports W/Factors Less than Five.Revision 2 Response Forthcoming Project stage: Other ML19210D5851979-11-21021 November 1979 Forwards Suppl 1 to RO 79-015 Re Sample Calculations & Tension & Shear Transfer Project stage: Other ML19262A9491979-11-24024 November 1979 Evaluation of Tests of Tensile Bond Strength of Concrete Block-to-Fill in Trojan Nuclear Power Plant Near Portland, Or. Supporting Documentation Encl Project stage: Other ML19253C7271979-11-30030 November 1979 Modifies ASLB Partial Initial Decision Permitting Interim Operation of Facility.Operation Will Not Resume Pending Further Order.Nrc Shall Inform ASLB of Unresolved Items Re Seismic Issues Project stage: Other ML19262A9451979-11-30030 November 1979 Rept on Testing of Composite Masonry Walls Project stage: Other ML19253C7691979-12-0101 December 1979 Notification of 791205-06 Meeting W/Util in Bethesda,Md to Discuss LER 79-15 Re Masonry Block Wall & Support Reaction Problem Project stage: Meeting ML19211C2251979-12-0404 December 1979 Ack Receipt of 791130 Order Re Interim Operation of Plant. Staff Currently Assembling Info Bearing on Seismic & Other Issues in Proceeding & Will Supplement This Info to ASLB on 791207 Project stage: Request ML19211A3741979-12-0707 December 1979 Affidavit by President of Util Explaining Unique Circumstances Facing Region & Affecting Public Need Project stage: Other ML19211A3671979-12-0808 December 1979 Forwards Affidavits of Rh Short & Dj Broehl,President & Vice President of Util,Respectively,In Response to ASLB 791130 Order.Certificate of Svc Encl Project stage: Other ML19294B3301979-12-0808 December 1979 Forwards Response to IE Bulletin 79-02,Revision 2,Items 5, 6 & 7 Project stage: Other ML20125C1751979-12-19019 December 1979 Summary of 791205-06 Meeting W/Util & Bechtel Re Discussion of LER 79-15 Wherein Certain Problems W/Masonry Block Walls & Support Reactions of Equipment/Piping Attached Thereto Were Identified Project stage: Meeting ML19290C0281979-12-20020 December 1979 Supplements Re Concrete Block Wall/Pipe Hanger Structural Problems,Subj of 791220 Discussions.States NRC Understanding That Util Will Resolve re-evaluations Per LER 79-15 Project stage: Other ML19290C0261979-12-21021 December 1979 Joint Affidavit Re Review & Evaluation of as-built Control Bldg Interim Operation.Block Wall Reaction Force Problem Must Be Satisfactorily Resolved Before Resumption of Operation.Problem Chronology Encl Project stage: Other ML19257A1971979-12-27027 December 1979 Forwards Class III Fee Re 791224 License Change Application 56 Project stage: Other ML19257A2021979-12-27027 December 1979 Forwards Util to NRC Region 5 Summarizing All Mods to Pipe Supports & Restraints.W/O Encl.Certificate of Svc Encl Project stage: Other ML19257A2001979-12-27027 December 1979 Submits Followup to RO-79-15.All Analyses & Evaluations Completed.Summary of Corrective Actions on Pipe Supports & Restraints Provided.Power Operation Will Not Resume Until Further ASLB Order Project stage: Other ML19257A7801979-12-31031 December 1979 Advises That Schedule for Implementation & Documentation of Confirmatory Testing Program Will Be Submitted Following NRC Review.Certificate of Svc Encl Project stage: Other ML19257A7821979-12-31031 December 1979 Advises of Resolution of Problems Re Steam Generators & single-wythe,mortared double-wythe & Composite Block/ Concrete Walls,As Described in LER 79-15.NRC Questions & Util Responses Encl Project stage: Other 05000344/LER-1979-015, Responds to NRC Request for Addl Info Re LER 79-15.Forwards Info Re Confirmatory Testing Program on Model double-block Masonry & Composite Walls.Schedule Will Be Established for Completion & Documentation of Results & Conclusio1979-12-31031 December 1979 Responds to NRC Request for Addl Info Re LER 79-15.Forwards Info Re Confirmatory Testing Program on Model double-block Masonry & Composite Walls.Schedule Will Be Established for Completion & Documentation of Results & Conclusions Project stage: Request ML19257B2661980-01-0909 January 1980 Forwards NRC Sample Calculation Comparing Use of Transverse Shear Force Directly from Stardyne Output W/Calculations from Displacement & Rotation Output from Same Analysis. Certificate of Svc Encl Project stage: Other 05000344/LER-1979-013, Forwards Confirmatory Info to NRC 791229 Question 1 Re LER 79-13 Concerning Stresses in Walls Due to Thermal Gradients. Masonry Walls Subj to Thermal Gradient Across Thickness Will Undergo Deformation.Certificate of Svc Encl1980-01-18018 January 1980 Forwards Confirmatory Info to NRC 791229 Question 1 Re LER 79-13 Concerning Stresses in Walls Due to Thermal Gradients. Masonry Walls Subj to Thermal Gradient Across Thickness Will Undergo Deformation.Certificate of Svc Encl Project stage: Other ML19296D7521980-02-13013 February 1980 Rept on Design Criteria for Masonry Walls Project stage: Other ML19296D7461980-02-13013 February 1980 Forwards Rept on Design Criteria for Masonry Walls Project stage: Other ML19296D7381980-02-22022 February 1980 Forwards Safety Evaluation Re Concrete Masonry Wall Design Criteria for Transverse Loadings & Rept on Design Criteria for Masonry Walls. Discussion Will Take Place During Wk of 800225 Project stage: Approval ML19296D7431980-02-22022 February 1980 Safety Evaluation Re Concrete Masonry Wall Design Criteria for Transverse Loadings Project stage: Approval ML19344D2271980-03-0505 March 1980 Informs That Testing & Grouting Program Completed 800213. Estimates 86% Fill in Collar Joint.No Wall Areas Contain Continuous Collar Joint Voids Project stage: Other ML19344D2681980-03-0606 March 1980 Forwards Info Re Values for Ultimate Compressive Strength of Masonry Assemblies.No Violation of Tech Specs Occurred as Result of Values Used in Accordance W/Uniform Bldg Code Project stage: Other ML19305B7761980-03-15015 March 1980 Forwards Comments Re App B of J Colville 800213 Rept Concerning Design Criteria of Plant Masonry Walls.Analysis Indicates That Wall 46 Has Capacity to Resist Out of Plane Loads During SSE Event.Certificate of Svc Encl Project stage: Other ML19305C3161980-03-17017 March 1980 Forwards Response to NRC Questions Presented at 800307 Meeting Re Structural Considerations for Proposed Mods to Control Bldg.Overall Modified Complex Has Available Capacity to Satisfy 1.4 Load Factor OBE Criteria Project stage: Meeting ML19309C3711980-04-0101 April 1980 Addendum 1 to Rept on Testing of Composite Masonry Walls Project stage: Other ML19309C3681980-04-0101 April 1980 Forwards Mar 1980 Addendum 1 to Rept on Testing of Composite Masonry Walls,Nov 1979. Test Results Described in Addendum Indicate That 40 Psi Is Appropriate Principle Tensile Stress Value at block-core Interface of Wall Project stage: Other ML19309G0341980-04-0808 April 1980 Response to Comments on App B of Coleville Rept of 800213 on Trojan Masonry Walls Project stage: Other ML19309G0351980-04-0808 April 1980 Comments on Review by Professor B Bresler of Evaluation of Tensile Bond & Shear Bond of Masonry by Means of Centrifugal Force,By M Hatzinikolas,J Longworth & J Warwaruk,Alberta Masonry Institute,Undated (1978-1979) Project stage: Other 1979-06-20
[Table View] |
Text
.. '.
- . s ATTACHMENT 3 TROJAN NTCLEAR PU37 REPORT ON TESTING OF CCMPOSITE MASONRY WALLS Novenber 1979 Portland General Electric Co.
Northwest Testing Laboratories Wiss, Janney, Elstner & Assoc., Inc.
1528 157 79 /2 //03Y4
f, s
TABLE OF CONTENTS Section Page 1
Test Objectives 1
2 Methodology 3
3 Results 10 4
Evaluation of Test Results 12 a
6 1528
- 53
Section 1 Test Objectives 1.1 The testing was performed in order to confirm the accuracy of our judgment with respect to the tension capacity at the interface between masonry block and concrete core of composite walls located in the Trojan Nuclear Plant.
The testing was performed "in-situ" on walls repr.3sentative of the various types of composite walls at the plant.
Figure 1.1 shows a cross-section of the type of composite wall utili:ed in the facility.
1528 159
CONCRETE MASONRY REINFORCING STEEL CELL GROUT 1
CONCRETE CORE
'e NNNNN'N' s' A ' " ' S NN N N '<
1
.A N. '. s n ' '
s)X"'p'k.,.'N}'.2.'.,s'i'.ra'isTd'
$ x ').., r a
^
- j.
!57, N
x
\\s. i e :i.
c.E N -l *
i-f -l
. y. _.
.. q.'3..,. e -
s
.s
.< x.<.N*
,c3
..e
.e..
^
__...+. ' O i N L 6,0,6
, i.# A i e,.a '
. c' ;,.,,
4 w
T
's ' \\ N ' s N 's N
\\ \\ \\ N s N'N
\\NN N s s. 's N N N \\ \\ N\\ ' \\ \\
. y ~ ~., c I,
. ::, %.'.f *:'.A.~
, :.' ' 1 j*,i. :
C
, J.., p-t
,I.g
.^,#
,. '- = * <
- f...-:.. ;
- a..,.s. ;
. p;x
~.
M I
~
4B" gsg
4E
p.,.
- s..
.,.. c.8
'a...
h / '*?.t>.:)
2,,'.' / :.'l'e-a sy N N N N 'xNNNN NNN N sN,N N N N N o..'
\\\\NN
.,z'ss\\NNN'sy.,.,,,.
s,.w c' y4 m.j., t,j
...s.
\\;
. 4-N,d
N N
,,,gf N s
N N'. * <* c... N
,f N
d j#.4 d T' 4,' a - \\.'- D i* I*- \\s 4s. ' ~
hNNNNxx 'x x s u NN' N N N N x ' \\ x x x x xN\\\\\\N Y
x PL AN SECTION REPRESENTATIVE COMPOSITE WALL F16 l. l 1528 160
Section 2 Methodology 2.1 Location of test sites.
By inspection of Plant drawings, test sites which are representative of the cenposite walls at the Plant and which are readily accessible in the present plant operating mode were chosen.
Those chosen were located at the 25' and 5' elevations in the Auxiliary Building and are shown in Figure 2.1.
Preliminary ava-4 nation was conducted to assure that no wall attach =ents were present on either side of the test region and to atte=pt to identify rebar that might interfere with the test.
2.2 Test preparation.
The testing program was conducted in two stages.
In the first stage the bond strength between the front facing block and the central core concrete was tested and the second stage the bond strength between the central core concrete and the remaining bicek at the same sites tested in the first stage.
This procedure was followed with the exception of test No. 3A where the second stage test could not be performed validly due to wall geometry.
2.2.1 First stage preparation.
A 12" dia, diamond drill type core borer was utilized to core through the front facing block and into the concrete core, providing an "in-situ" sample 1528 161
~
I f
I SITE 4 & 4A r l
9 i
223 s
l g
s W
l sa v.M _. _
. I._.
=
551 i
r#'4 SITE 2 & 2A-SITE 5 & SA l'
DI SITE 3 \\
I
. i SITE 8 & 8A-k#' '
s 5
E; : ',7
.M I:
>2
?^h Og F,
u.
E s
I
- ga i
es!
f*
b OH s!l t'-
SITE 7 & 7A g
9 t'
f I
l
+
5' PAP,TI AL FLOOR PLAN 6 25' p) j_.,
),ySITE9&9A
~
r
,u! -
i ('
h gyn.
gw mn.-
s V
f g =2-l t
D FIG. 2.1 PARTIAL FLOOR PLAN 8 5' 1528 162
_4_
m e
s a
of 11-1/2" dia, with a 1/4" annulus between it and toe surrounding material.
3-Block dimensions are 7-5/8" thick. To assure adequate penetration of the block the core bore was extendad beyond that depth by about 1".
Initial placing of vedge anchors utilized one of two recommended patterns as depicted in Figure 2.2.
Anchor bolts utilized were 3/4" phillips wedge anchors set to the =anufacturers recoc=endations and torqued prior to the coring operation. The 11-1/2" dia. core was drilled concentric round the 6" dia. anchor tolt pitch circle.
This method (utilizing three wedge anchors) was discontinued following the first three tests due to the concern of possible bolt interaction and was replaced by a method utilizing one central 1" phillips wedge anchor.
2.2.2 First stage testing.
The testing equipment utilized consisted of the following:
1.
Fabricated compression beam and bearing plate, hydraulic jack support bracket with 4 "C" clamps.
Figure 2.3 2.
Threaded 1" dia. rod with nuts and coupling.
3.
Calibrate; hydraulic jacking system
a.
Enerpac Eand Pump (SN 11754) b.
Enerpac 30 Ton Ram (SN 11752)
Ashcrof t 3000 PSIG Hydraulic Gauge (SN 11755) c.
- This equipment provided and operated by Northwest Testing 'aboratories. See Appendix 1. __
l 3
TYPE 5.2 CENTER OF 6" BOLT CIRCLE I
I y-l BLOCK JOINT (TYP.)
! _ h _ _.2 _
~
3/4" HOLE (TYP.)
O' 12" 0.0.
M 5.3 11 " I.D.
I l
'=
BLOCK JOINT (TYP.)
I i
CENTER OF BLOCK
- \\
))l O
3/4" HOLE (TYP.)
_ g _ - _ _ 7 _= _
CENTRAL ANCHOR 1" HOLE (TYP.)
l n
I
!=
BLOCK JOINT (TYP.)
i I
l l
y i
=
CENTER OF BLOCK
l N
C l
l
__L_
______._s__
U o
FIG. 2.2 1528 164 ma w.m
O s'
e i
l l
!l l
i i
l PLAN VIEW _
i
_ _ _ _ _.J j
_c ELEVATION VIEW FI G, 2.3 1528 165
d.
Ashcrof t 6000 PSIG Hydraulic Gauge (SN 11757)
Multi-port Hydraulic Couplings and Hydraulic Hose.
e.
4.
Two dial micrometer.
The assembled test rig is shown in Figure 2.4 The testing was perforned in accordance with SPT-51 (Special Plant Test - 51) Rev. O included here as Appendix 2.
Results were recorded in accordance with SPT-51 and also independently by the Northwest Testing Laboratory Representative. These results are reproduced in Section 3 of this report.
2.2.3 Second stage preparation Following completion of the first stage test for each rest site and subsequent napping and photography of the broken section a 1" dia, phillips wedge anchor was set into the central core concrete, concentric with the exist-ing geometry, and further coring utilizing the 11-1/2" dia. core borer proceeded.
The depth of the coring was determined such that the inside surface of the re-
=aining block was just penetrated (no more than 1/8").
2.2.4 Second stage testing The testing was performed as described in Section 2.2.2.
Subsequent to the testing the broken sections were mapped and photographed.
. 1SJ28 166
'tI Il ll il
////kH//EV//n E
?'
I y
t i
i l
I 7
4
\\
_=
Il
-s l
i
!! M
.1,,p
.5 i
PLAN VIEW "C" CLAMP LOCATION TYP. ALL CORNERS I
I f_ _ __ _ i _
I i
s, i
--7
, - ".(--
i j
ELEVATION FIG. 2 A g
1528 167
Section 3 Results The test results were recorded by PGE personnel utilizing the dr.ta sheet from $PT-51, Rev. O and were also recorded by Northwest Testing Laboratory Representative using standard laboratory workaheets. Appendix 1 provides a su==ary from Northwest Testing Laboratories of tha failure loads and cali-bration data for the test equipment. Appendix 2 provides a copy of SPT-51 (Special Plant Test Procedure).
(The deflection data from the microne 2rs was disregarded due to the difficulty of obtaining representative readings).
In addition, all test sites were mapped and the broken spec 1=ents photographed.
The results are presented 's tabular form Table 3.1.
3
}h _
j
~
TABl.E 3.1 TAllUI.ATIOt10F TEST RESUI.TS l
1 110. OF CYCLES TE.ST D1 A Al i I.I I.0AD LOCATIOli APPLIED l
SITE PATTER!l 0F COHE AT FAILURE 5,000#
7,500#
10,000#
15,000#
20,000f 4
2 Elev. 25' 5.3 8 1/16" 5
0 1
0 0
9,820f f
i 2A Eic e. 25' Central Anctior 20 1/2" 5
3 3
0 0
17,670f 3
Elev. 25' 5.2 9 1/4" 1
0 0
0 0
4,5007 4
Elev. 25' 5.3 9"
5 2
0 0
0 7,120f 4A Elev. 25' Central Anctior 19 1/2" 5
3 3
0 0
24,5007
),
5 Elev. 25' 5.3 9"
5 0
0 0
0 4,730f r
i SA Elev. 25' Central Anctior 19 7/16" 5
3 3
0 0
14,460#
7 Elev. 25' Central Anctior 9 1/8" 5
3 3
3 0
15,G90f I
7A Elev. 25' Central Anciaor 19 3/4" 5
5 5
5 3
21,790#
8 Elev. 25' Central Anctior 9"
1 0
0 0
0 3,7907 8A Elev. 25' Central Anctior 22" 5
5 5
5 0
14,8507 9
Elev. S' Central Anctior 9"
5 5
5 3
0 l 'i,000f 9A Elev. 5' central Anctior 12 1/8" 5
5 5
5 1
21,7907 s
N CO i
Section 4 Evaluation of Test Results The testing results were evaluated by a representative of Wiss, Janney, Eistner & Associates Incorporated of Chicago.
The report is attached as Appendix 3.
e 9 1528 170
- 13V1111177 M 1 11.A.J 1 A.L 1 % JI
.2 a AJ / %# Au n. a. v s swv f,
's.
4115 N. MISSISSIPPtAVENuE P. O. 5OX 17126 mon.ossinuenya vasnno constavenom insesenose wasoswo cannricanon
" Avan ass insesano" P Q R T t. A N D. OREGCN 97217 so66 vasnno enameca6 ana6vs s
.ss n.o vs.cai vasn o November 19, 1979 Portland General Electric Company 121 S.W. Salmon Portland, Oregon 07204 Re: Trojon Nuclear Power Plant Report Of: Composit Wall Masonry Block - Concrete Core interface Bond Testing Load App!ication Equipment Test Loads were applied by e calibrated hydraulic jacking system consisting of the following: Enerpac hand pump (SN11754), Enerpac 30 Ton Ram (SN11752), Ashcraft 3000 Psig hydraulic gage (SN 11755), Ashcraft 6000 psig hydraulic gage (SN11757), Multi-Port hydraulic coupling and 25 feet of hydraulic hose.
Test Site No.
Ulimate Failure Loads (Pounds)*
Cage Used.{ PSI 6) 1 Not Applicable / Hit Rebar in Block 2
9820 6000 2A 17670 60JO 3
4500 6000 4
7120 6000 4A 24500 6000 5
4730 3000 SA 14460 6000 6
Not Applicable /Not Composit Wall 7
15890 6000 7A 21790 6000 8
3790 3000 8A 14850 3000 9
15000 3000 9A 21790 6000
Failure Loads determined by Mathmatical Interpolation between adjacent calibration points.
e 1528 171
.o......
Re: Trojan Nucelar Power Plant i
The test loading system, including hydraulic ram, couplings and pressure gages were calibrated on a Tinius Olson Testing Machine.
Certified accuracy of this machine was established December 7,197f by Cal-Cert Co.
8 f u nluih By hand pumping, a wide range of loads were applied to the test machine.
These loads along with the associated gage pressures were recorded. This was done for both the 3000 Psig PCE gage and the 6000 Psig Northwest Testing laboratory gage. Results of this calibaration follows:
Actual Load (pounds) from Tinius Olson 3000 PSIC Gage 6000 PSIG Cage 320 100 200 950 200 30 0 1,690 300 375 2,390 400 475 2,500 430 500 5,000 800 875 7,500 1150 1225 10,000 1500 1575 12,500 1860 1925 15,000 2200 2275 17,500 2540 2625 22,000 2900 3000 22,500 beyond range 3350 25,000 beyond range 3725 27,500 beyond range 4075 30,000 beyond range 4425 Respectfully, NORTHWEST TESTING LABORATORIES, INC.
9 Charles R. Lane, P.E.
CRL/lz Report No. 211094 1523 172
--.