ML19260D680

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LER 80-001/03L-0:on 800107,during Mode 1 Operation, Containment Isolation Valve 25V-5876-2 Failed to Close After Taking Samples from Safety Injection Tanks for Boron Analysis.Caused by Faulty Valve Position Indication
ML19260D680
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/05/1980
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19260D677 List:
References
LER-80-001-03L, LER-80-1-3L, NUDOCS 8002110576
Download: ML19260D680 (1)


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