ML19210D155
| ML19210D155 | |
| Person / Time | |
|---|---|
| Site: | North Anna |
| Issue date: | 11/05/1979 |
| From: | Wil Madison VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | |
| Shared Package | |
| ML19210D121 | List: |
| References | |
| NUDOCS 7911200590 | |
| Download: ML19210D155 (4) | |
Text
.
VIRGINIA. ELECTRIC Af;D P0',lER COMPANY t' ORTH ANNA POWER STATION M0flTHLY OPERATIfG REPORT MONTH Sept.
YEAR 1979 (Revised 11-05-79)
SUBMITTED:
N. .')
- (.
- L 1
SUPERINTENDENT - OPERATIONS APPROVED:
8 AM MAilAGER(/
1367 334 7.911200 WD
D'3~ Y mq m
oa v
- 3 OPERATING DATA REF ORT DOCKE r NO. b'I-333 dan. ll !L-79_
COMPl.E1E:) ny W. P. f'nfison 1 ELEPilON E (2fa).EM-5151 OPE R[rlNG STATUS
!! orth Anna Unit 1 Notes h.. Reportm ', Pen. d-
- D.
SepTenber 1979 (ETsLT7~
o
- 3. Li:enwd Therntd Power (11Wt):
277_5 947
- 4. Namenlite Ratics (Grow SIWE).
90/
- 5. Design E!ectrical Ratin3 (Net SlWe):
928
- 6. $1aximura Dep. ndable Capacity (Gros. SlWe):
098
- 7. Maxhntun Dependabic Capacity (Net 31Wr):
- 8. If Chanys Occur in Cap.uity Ratiny (Items Number 1 Through 7) Since La t Repmt, Give Rea>oo,:
N/A
"!^
- 9. Power Level To Which Restricted,if Any (Net 31We)-
- 10. Renons For !!estrictions. If Any-I'/A This Month Yr..to.D ite Crmutatiu II. iloins la R portin3 P. riod 720 6,551 _,
'l l_,5508 1
68ET~
!GUIL4 o,b25.2 1,.. S. umber O f Ilours,,.netor N.s Critical 2.8 bl.S 148.3
- 13. Reietor nevrs e ShotJown lioun 5,401.5 10,053.2
- 14. Ilours Gen-rator On 1.ine 582.2 G
0 0
- 15. Unit Revr. Shutdown flourt
- 16. Grow Thennal Ener::y Genented (51bif) 1,134,3' 21 083,118 26,279,913 1
- 17. Grou Electrie:d Ener3y Generate!(MWil) 34b,793 4,445,776 8,34 6,3 ?_)
- 18. N-t I:lectrical Ener3y Generated (MWil) 320,744 4,188,866_ _
7,853 / 46 T 0.7 82.4 86.9
- 19. tl nit Service Factor 80./
6F4-86 9
- 20. Unit Ano.tability Factor 49.6 7I.2 75.6
- 21. Unit Capeit-Factor (Usin; MDC Net)
- 22. Unit Capae. ~ Factor (Usin,; DER Net)
~4FT 7DT
~~T1. 8
- tf
- 23. Unit Forced Out.3e Rate 0.5 4.8 3m3
- 24. Shutdowns Schahhl Over Next 6 Moaths (Type. Date,and Duration of Each):
H/h
- 25. If Shut Down At End Of Report Periott. Estimated Date of Startup:
2ti. IJnit, I. Test Sr.tus (Prior to Conunercial Operationl:
Torec.ht At.hin ed INITI A L CRITICA LI FY INITIAL El.CC IR!Ci rY COMM ERCI \\ L Ot'E R A IION 1367 335 en
50-338 U f,
,,; ToFYIi7snna Unit 1 UNIT SHUTDOWNS AND POWER REDUCTIONS DAIE T-5-B Sectember 1979 (Revised) COMPLrr1DIY 3
_Jgl R EPOR r '.t oN TH EL
}
h k
I.iecmce hr.,
rause & rorrectne w.
Date s
==
I E=3 Evem I-Amon to
[@
d Report.
nC Present Recurrence 6
79-15 790912 S
0 F*
4*
N/A N/A N/A Ramped down to 355 reactor pr :er in preparation for extended period of operation beyond 9/15/79 pending amendment of NPF-4.
79-16 790921 F
0 B*
4*
N/A N/A N/A Ramped down to 28% reactor power to perform turbine valve freedcm test.
Testing was perforced & the reactor was escalated to 80%.
4 9
Automatic R Turbine Generator trip 6
9 79-17 790925 F
2.8 A*
3*
LER/R0 79-128 SF VALVEX x
due to high level in the extraction, ;E?pg) steam side cf the 5B feedwater heated The plant is presently shutdown &
f-- 9 the cooler will be repaired.
Commenced scheduled refueling cutage< g 79-18 790925 S
135 C*
4*
N/A N/A N/A u
it"] cd o~
N M
BED i
~
1 4
h s
F: Forced Reason :
Methed:
Exhibit G -Instructions S: ScheJu!cd A-Equipment Failure (Exp!ain)
- 1. Man a 2!
for P:cparation of D na B Maintenance of Test 2-Manual Scram.
E:nry Sheets Ier L:.nsee
- c. Refueling I-Automatic Scram.
E.ent Report (Ll'R1 Fue (NL:RI G D-Regulatory Restriction 4-Ot her ( E xplain )
0161)
F-Operator Training & l.icense Examination F. AJ minist rat n e G-Operational 1 rror (Explam)
Exhibn 1 - Same Sourt.
(9/77)
!!-Other ( E xplain )
- See Attached Sheet Shutdcwn 79-18 continued into October.
page 1, of 1
UllIT SliUT00WM AtlD p0WER REDUCTIONS EXPl.Al:ATIGli SiiEET DOCKET liO.
50-338 REPORT l'0:lTH Sepcember (Reviut!ED i:AME ilorth Anna YEAR 1979 DATE 11-5-79 _
COMPLETED BY 11. R. T'ADIS0N 79-15 (F) (4)
The reactor was operating in the end 6f cycle 1 coastdcv:n:
Reactor power was decreased to extend the cycle to October 5,1979 pending itRC approval.
Amendment 15 to fiPF-4 was approved.
Subsequent analysis indicated that reactor power could be increased back to maxiinum attainable.
Reac;.or power was increased to approximately 00%.
79-16 (B) (4)
Reactor power was decreased to establish the required conditions for turbine valve testing.
The required testing was completed and reactor power was escalated to 80%.
The reactor was not shutdorm.
79-17 t.
(3)
The 5th point heater drain cooler dump valve LCV.iD-1280 began to cycle due to a tube rupture inside the cooler The leakage was nore than the capability of the drain valves causing extraction steam condensate to back up into the Lth point heater to the turbine trip setpoint.
This resulted in an automatic Reactor Turbine Generator trip.
The heat 7r drain cooler tubes will be replaced during the current cutage.
79-18 (C) (4)
Comenced the scheduled refueling outage at 0900 Septeirbar 25, 1979.
The reactor was already shutdown from event 79-16.
i 1367 337