ML19210D132
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| ML19210D132 | |
| Person / Time | |
|---|---|
| Site: | North Anna |
| Issue date: | 11/05/1979 |
| From: | Wil Madison VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | |
| Shared Package | |
| ML19210D121 | List: |
| References | |
| NUDOCS 7911200569 | |
| Download: ML19210D132 (2) | |
Text
,
s VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT MONTH Nov.
YEAR 1978 (Revised 11-05-79)
SUBMITTED:
N D)
Ec,A N
SUPERINTENDENT - OPERATIONS APPROVED:
k V
MANAGd()
1367 502 7911200 66f
OPERATING DATA REPORT DOCKET NO.
DATE 11-6-79 COSIPLETED BY F 4 i D
{,
TELEPHONE 703 8 -
1 OPERATING STATUS fiorth Anna Unit 1 Notes
- 1. Unit h.ame:
el.G l W W 1 %
- 2. Reporting Period:
- 3. Licensed Thermal Power (SIWr):
2,7 75 947
- 4. Nameplate Rating (Grou 51We):
- 5. Desipt Electrical Rating (Net SIWE):
907
- 6. 51aximum Dependable Capacity (Gross 51We):
928
- 7. 51aximu:n Dependable Capacity (Net SIWE):
898
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reucas:
ft/A
- 9. Power Level To Which Restricted,If Any (Net 3:We):
II/8._
- 10. Reasons For Restrictions,if Any:
II/A
~
This blonth
_ ___ Yr.-to Date Cumulative
- 11. Hours In Reporting Per od
- 12. Number Of Hours Reactor Was Critical 716.8 3,958.9 L958.9
- 13. Reactor Reserve Shutdown !!ours 3.2 80.7 80.7
- 14. Hours Generator On Line 714.9 3,926.3 3.925
- 15. Unit Reserve Shutdown I!ours 0
0 0
- 16. Grou Therrnal Ener;y Generated (51WH)
'l,894,450 j 0 274,276 10.274,2.7J5.
2
- 17. Gross E!ectrical Energy Generated (5tWH) 606,775 3,090,113 3,090,113__
3,290,882 3,290.882_
- 18. Net Electrical Ener;;y Generated (SIWH) 572,250
- 19. Unit Service Factor 99.3 91.9 91 3
- 20. Unit Asailability Factor 99.3 91,9_
91 3
- 21. Unit Capacity Factor (Usin3 51DC Net) 88.5 80.5_
80 5.
- 22. Unit Capacity Factor (Using DER Net) 87.6 79.7 73 J
- 23. Unit Forced Outap Rate 0.7 1.4 1,4
- 24. Shutdowns Scheduled Over Next 6 5!onths(Type.Date,and Duration of Each):
Snubber Inspection April 1979, 1 week
- 25. If Saut Down At End Of Report Period. Estimated Date of Startup:
N/A
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY C05151ERCIAL OPERATION I367 303 mn
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