ML19210D147
| ML19210D147 | |
| Person / Time | |
|---|---|
| Site: | North Anna |
| Issue date: | 11/05/1979 |
| From: | Wil Madison VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | |
| Shared Package | |
| ML19210D121 | List: |
| References | |
| NUDOCS 7911200586 | |
| Download: ML19210D147 (4) | |
Text
..
VIRGIflIA ELECTRIC AND P0'.lER COMPAtlY i;0RTH AtlNA POWER STATI0ft P0llTHLY OPERATIt!G REPORT P.0fiTH June YEAR 1979 (Revised 11-05-79) t SUBMITTED:
- %~'Q, bN csp.,
SUPERINTEll0Elli - OPERATIOilS APPROVED:
/k i4ANAGER J 1367
.324 2911200 5 6 6
OPERATING DATA REPORT 50-338 DOCKET NO.
DATE M.E.*L%.
COMPLETED fly JL.JL !htyson TELEPl!ONE (_W)@g4.-5151 OPERATING STATUS florth Anna, Unit 1 Notes
- 1. Unit N>r.w:
dune 1979 (Revised)
- 2. Reporting Period:
- 3. Licenud Thermal Power (MWr):
2775 947
- 4. Nameptate R2tiag (Gron 51We):
90/
- 5. Design Elearical Rating (Net SIWE):
928
- 6. Maximum Dependab!e Capacity (Gross SIWE):
898
- 7. 51aximura Dependable Capacity (Net MWe):
- 8. If Chanps Occur in Capacity Ra.ings (Items Number 3 Throu th 7) Since Last Report, Give Reasons:
fl/A NE
- 9. Power Lev 4 To Which Restricted,if Any (Net MWe):
h
- 10. Reasons Fue Restrictions,if Any:
This Month
__ Yr.-to-Date Cumulative 20 11, ilours In Reporting Period 4,343 9,360
- 12. Number Of floors Reactor W.n Critical 720-3.103 9 n/.s._
- 13. Reactor Rmrve Shutdown Hours 0
48.7 1/5.5..
L
- 14. Ilours Ger:erator On.Line 720 3,331.3 7,983 0
0 0
- 15. Unit Rexne Shutdown itour,
- 16. Gruu The mal Enegy Genented IMWii) 1,945,847
_8.29]faR95 21.113 490
- 17. Gron Elec:rical Energy Generate 1(MWH) 617 457 2d46,527
_6 7.16d6L__
1 IS. Net Electried Energy Generated (Mhlf) 583 847 2,684.,7/8 6.349.3.2& _
L
- 19. Unit Service Factor 100 76.7 8 5 3._,
2 100 76.7 85.3
- 20. Unit Asailability Factor
- 21. Unit Capacity Factor (U. sing MDC Net) 90.3 68.8 7.5,5_
89.4 68.1 7ML
- 22. Unit Capacity Factor (Using DER Net) 0 7.5 4.1
- 23. Unit ForcM Outage Rate
- 24. Shutdowm Scheduled Over Next 6 Months (Type. Date.and Duration of Eacht Refueling; September, October and flovember; 11 Weeks
- 25. If Shut Down At End Of Report Penod. Estimated Date of Startup:
II/A
- 26. Units In Test Status (Prior to Commercial Operation):
Foreca >r Achieved INITIA L CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 1367 525 mm
DOCKET NO. 50-333 UNIT SliUIDOWNS AND POWER REDUCTIONS North Anna Unit #1 UNrr N AME DA TE ll-5-79 COMPLETED BY
'A r> _ >>,disqn REPORT MONTII June 1979 (Revised)
TELEP!iONE -GP.S)394-5151
~
I
'b 21"i Lkemee Et h
Cause & Correct e.e
~
N.,
Da'e 2.
55
[
$E4 I ert
-i -3 b~i A,t:m to C
g y
]g.
Repe.t -
nC
'+
_E Prewnt Returrence e
6 79-12 THIS P!:RIOD OF SIG'iIFICANT POWER REDUCTION WAS CONC UDED ON C-l-79 AT 2135, WHEN "C" f4AIN FEEDPU 4P WAS RETUR. ;ED TO NCRtGL SERVICi.
g 6
9 4
9 Ei'e)
G 9
2?'P)
M w
W4 hied b
tra i
3 4
F: Ferced Reason:
Methoti:
Exhibit G -Instructions S: Scheau!:d A Equipment Failure (Explain) 1 -Manual for Preparation of Data B-Maintenance ci Test 2-Manual Scram.
Entn Sheets fer Licen ce N
C.Refuelinu 3 Automatie Scram.
Ese:it Report (LI:R) FCe t NU RI.G-C' D Regu!atJry Restriction 4-Other ( Explain)
O!61)
E-Operator Training & License Exainination F-Ad minist ra t i.e 5
G-Operational Error p xp!dn)
Exhibit ! - Same Source N'77)
I!-Ot her ( Esplain)
- See Attached Sheet.
Page 1
of 1
U:!IT SiluTDOWil AtID POUER REDUCTIOlS EXPLAi!ATION S!EET DOCKET li0.
50-338 REPORT !!0Nili June (Revisty[) UNIT FLAME !! orth Anna #1 l979 11-5-79 YEAR DATE COMPLETED BY W. R. IMDIS0tl 79-12 (A) liigh bearing temperature en "C" cain feedpump required a reduction in megawatt load when the feedpump was removed from service.
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