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ACCELERATED D.11l!BUTION DEMONS.TION SYS REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION :N'BR:9001080281 DOC.DATE: 89/12/28 NOTARIZED: NO DOCKET #
FACIL:50-281 Surry Power Station, Unit 2, Virginia Electric & Powe 05000281 AUTH.NAME AUTHOR AFFILIATION KANSLER,M.R.
Virginia Power (Virginia Electric & Power Co.)
~CIP.NAME RECIPIENT AFFILIATION SUBJEcrr: LER 8 8-0 O 1-02: on 8 8 O 12 7, improper admin control of containment isolation valves due to personnel error.
W/8 ltr.
I DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR J ENCL j_ SIZE:~
TITLE: 50.73/50.9 Licensee Event Report (LER),-Yncident Rpt, etc. f \\
NOTES:lcy NMSS/FCAF/PM.
5000281 INTERNAL:
EXTERNAL:
NOTES:
REC!PIENT COPIES ID CODE/NAME LTTR ENCL PD2-2 LA 1
1 BUCKLEY,B 1
1 ACRS MICHELSON 1
1 ACRS WYLIE 1
1 AEOD/DSP/TPAB 1
1 DEDRO 1
1 NRR/DET/EMEB9H3 1
1 NRR/DLPQ/LHFBll 1
1 NRR/DOEA/OEABll 1
1 NRR/DST/SELB SD 1
1 NRR/DST/SPLB8D1 1
1 NUDOCS-ABSTRACT 1
1 RES/DSIR/EIB 1
1 EG&G WILLIAMS,S 4
4 LPDR 1
1 NSIC MAYS,G 1
1 NUDOCS FULL TXT 1
1 1
1 NOTE TO ALL "RIDS" RECIPIENfS:
RECIPIENT ID CODE/NAME PD2-2 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP NRR/DET/ECMB 9H NRR/DET/ESGB SD NRR/DLPQ/LPEBlO NRR/DREP /PRPBll NRR/DST/SICB 7E
~ro:oxB ~~
RGN2 FILE 01 L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A COPIES LTTR ENCL 1
2 1
2 1
1 1
2 1
1 1
1 1
1 1
1 2
1 2
1 1
1 2
1 1
1 1
1 1
1 i !.
- 1 PLEASE HELP US TO REDUCE WASTE! CONTACT THE.DOCUMENT CONTROL qESK, ROOM Pl-37 (EXT. 'lJXJ"/9) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR OOCUMENfS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 39 ENCL 39
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December 28, 1989 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555 Gentlemen:
Serial No.:
Docket No.:
License No.:
88-001'8 50-281 DPR-37 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following updated Licensee Event Report for Unit 2.
REPORT NUMBER 88-001-02 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Corporate Nuclear Safety.
Very truly yours, M. R. Kansler Station Manager Enclosure cc:
Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323 9001080281 891228 PDR ADOCK 05000281 S
PDC
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- - ~
Updc.ted Report - Previous ~t Dated 03/04/88 POW 28-06-01
"',IIC Fer111..
,~,
LICENSEE EVENT REPORT (LER)
U.S. W"-LEAII IIEGULATORY ~ISIION
"""ROVED 0MB NO. 311i1M110ol EXl'IIIES: 1/31/a PACILITY NAIii n1 Surry_Power Station, Unit 2 I
DOCKET NUMalll 121 I
PAGE 131 o I s I o I o I o 12 1 8 1 l
, I oFI o, 3 TITLE'" Improper Administrative C.:ontro.L of Containment Isolation Valves Due to Personnel Error IVINT DATI I.II LEA NUMBEII Ill
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OTHER FACILITIES INVOLVED Ill MON'tH DAY YEAR YEAR fl SE~~~:i~AL j{ =t~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(SI 611 2 I 1 8 8 818 -
o I 011 -
012 1 I 2 21 8 819 C,,.IIIATING THII REPORT II IUIMITTED PURIUANT TO THE REQUIIIEMENTI OF 10 CFII §: (ChKil oM or ma.. of rt1* foll"'1(ins} 1111 1----MOO-I*-"..-' --L-N-4---1 20.4021bl 20.4Cllllcl II0.731all2111YI II0.31(cllll II0.731all21M f-73.71(~1 73.711cl
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II0.311cll21 II0.731all21UI II0.731all211ril II0.73(11121MIIIIAI OTHER (Sr,<<:lfy in Ab1tncr Nlow end in Texr. NRC Form 366A}
II0.7:IC.11211111 II0.7311IIZIMIIIIII II0.731all211Hll II0.73(111211*1 LICENSEE COl\\lTACT FOR THII LEA 1121 NAlilE TELEPHONE NUMBER M. R. Kansler, Station Manager AREA CODE 8 IO i4 3 I 51 7 I -1 31 1 18 I 4 CAUSE SYSTEM.
COMPONENT X
J1 M I1 S1V I X.
Jt M It SI VI COMPLETE ONE LINE FOR EACH coa.oNENT FAILUIIE DESCRIBED IN THIS REPOIIT 1131 MANUFAC-TURER COMPONENT I
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I MANUFAC TURER I
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I MJ""LEMENTAt. IIEPOIIT !'lll'eCTID il41 MONTH DAY r-, Yl!I (ff IIW. ~
EXl'ECfEIJ SIJIIAlliS:i/fiN DA TEI EXPECTED SUI MISSION DATE.1151 NIIC Form..
fQO'II On January 27, 1988, with Unit 2 at 100% power, it was determined at 1944 hours0.0225 days <br />0.54 hours <br />0.00321 weeks <br />7.39692e-4 months <br /> that leakage through containment isolation valves TV-SS-201A and TV-SS-201B (pressurizer vapor space sample) (EIIS-JM ISV) was greater than the ASME Section XI specification.
The valves were declared inoperable at that time-.- The valves were maintained closed and placed under administr.ative control at 2241 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.527005e-4 months <br /> by lifting a-lead on TV-SS-201A (a solenoid operated valve) and by lifting a lead and isolating instrument air to TV-SS-201B (an air operated valve).
However, on February 2, 1988 at 2225 hours0.0258 days <br />0.618 hours <br />0.00368 weeks <br />8.466125e-4 months <br />, it was discovered-that the wrong leads had been lifted for the trip valves, and that TV-SS-201A, had not ** been properly administratively controlled.
The correct leads were lifted at 2324
- hours, and the trip valves w~re verified to be properly controlled.
Electricians have been instructed as to which are the proper leads to lift to disable these valves.
The leakage* through the valves has been attributed to impurities in the system.
TV-SS-201A was replaced and TV-SS-201B was repaired.
I I 9 I
NRC FORM 368A [6-891 FACILITY NAME (1)
U.S. NUCLEAR REGULATORY COMMISSION l.lCENSE.E EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER C21 APPROVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS ANO REPORTS MANAGEMENT BRANCH [P-5301, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555, ANO TO 1'HE PAPERWORK REDUCTION PROJECT (3150-01041. OFFICE OF MANAGEMENT ANO BUDGET, WASHINGTON, DC 20503.
LER NUMBER (61 PAGE (31 Surry Power Station, Unit 2 o 15 I o I o I o I 2 I 8 I 1 8 I 8 -
ol o I 1 -
o 12 o I 2 oF o I 3 TEXT IN,_. 1/Mt:fl i$ -,ulml, u#... 'idllioMI NRC Fom, 36tl,4~J C17l.
1.0 Description of the Event On January 27, 1988, with Unit 2 at 100% power, it was determined at 1944 hours0.0225 days <br />0.54 hours <br />0.00321 weeks <br />7.39692e-4 months <br /> that leakage through containment isolation valves TV-SS-201A and TV-SS-201B (pressurizer vapor *space sample)
(EIIS-JM ISV) was greater than the ASME Section XI specification.
The valves were declared inoperable at that time.
Technical Specifications require administrative control of inoperable automatic containment isolation valves.
The valves were maintained closed and placed under administrative control at 2241 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.527005e-4 months <br /> by lifting a lead on TV-SS-201A (a solenoid operated valve) and by lifting a lead and isolating instrument air to TV-SS-201B (an air operated valve).
Also, the manual isolation valve downstream of the penetration, l-SS-113, was closed under. administrative control.
- However, on February 2, 1988 at 2225 hours0.0258 days <br />0.618 hours <br />0.00368 weeks <br />8.466125e-4 months <br />, it was discovered that the wrong leads had been lifted for the trip valves, and that TV-SS-201A had not been properly administratively controlled.
Since air was isolated to TV-SS-201B, it was effectively administratively controlled.* The correct leads were lifted at 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, and the trip valves were verified to be properly controlled.
2.0 Safety.Consequences and Implications The pressurizer vapor space sample system trip valves provide containment isolation in the event of a loss of coolant accident.
Although the leakage through the trip valves exceeded the ASME Section XI allowable leakage for operable containment isolation"""valves, the leakage was well within the total allowable leakage for containment integrity.
Therefore, the health and safety of the public were not affected.
3.0
Cause
Electrical maintenance personnel misinterpreted the electrical sketches and lifted the wrong leads when attempting to disable the trip valves.
Maintenance engineering has determined
.that the
- subject valves are susceptible to leakage due to the entrapment of system impurities in the valve internals.
NRCFORM:.&A 16-691 FACILITY NAIIIIE Ill U.S. NUCLEAR REGULATORY COMMISSION
- LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUM!IER 121 N'l'flOVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BUROEI\\I PER RESPONSE TO COMPLY WTH THIS INFORMATION COU.ECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGAADING BURDEN ESTIMATE TO THE RECORDS AND. REPORTS w..u.AGEMENT BRANCH IP-630), U.S. NUCLEAR REGULATORY a-1SSION, WASHINGTON, DC 20!555, AND TO 11lE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT A.ND BUDGET, WASHINGTON, DC 20503.
LEAN~II (II l'AOE 131 Surry Power Station, Unit 2 o 1s101010121811 818 o lo I 1 TEXT (If men -
u*iedtlltioMI NRC Fann.'111&4'*11171 NRC F-:.A 16,118) and pitting of the internals caused by the impurities.
Pitting of the valve disc was the cause of leakage through TV-SS-201B.
Valve TV-SS-201A could not be disassembled, however, it is suspected that the leakage was due to small system impurities trapped under the valve seat.
4.0 Immediate Corrective Action(s)
When it was discovered that the wrong leads had been lifted, the electricians lifted the proper leads and reconnected the leads.
that had been lifted incorrectly.
Operations then verified that the trip valves could not be opened.
5.0 Additional Corrective Action(s)
TV-SS-201A was and reinstalled satisfactorily.
replaced and TV-SS-201B was repaired and both valves were tested 6.0 Action(s) Taken to Prevent Recurrence Electricians have been instructed as to which are the proper leads to lift to disable these valves.
The present foreign material exclusion controls which.
were enhanced in 1989 and system cleanliness requirements are considered adequate to prevent impurity induced leakage.
7.0
Similar Events
None.
8.0 Manufacturer/Model Number(s)
TV-SS-201A Rock/86V~001 TV-SS-201R Asco/Kx2063803RF 0 I 2 0 I 3 OF O f 3
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| | | Reporting criterion |
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| 05000281/LER-1988-001, :on 880127,discovered That Leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Greater than ASME Section XI Spec.On 880202,wrong Leads Lifted for Trip Valves.Caused by Impurities in Sys |
- on 880127,discovered That Leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Greater than ASME Section XI Spec.On 880202,wrong Leads Lifted for Trip Valves.Caused by Impurities in Sys
| | | 05000281/LER-1988-001-02, :on 880127,leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Discovered Greater than ASME Section XI Spec.Valves Declared Inoperable.Caused by Misinterpretation of Sketches.Leads Lifted |
- on 880127,leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Discovered Greater than ASME Section XI Spec.Valves Declared Inoperable.Caused by Misinterpretation of Sketches.Leads Lifted
| | | 05000280/LER-1988-001-01, :on 880131,containment Isolation Valve Not Properly Locked Under Administrative Control.Cause Undetermined.Valve Verified to Be in Closed Position |
- on 880131,containment Isolation Valve Not Properly Locked Under Administrative Control.Cause Undetermined.Valve Verified to Be in Closed Position
| | | 05000281/LER-1988-002, :on 880202,determined That Individual Valve Leakage Through Reactor Coolant Cold Leg Sample Isolation Valves Was Greater than ASME Section XI Spec.Caused by Impurities in Sys.Valves Replaced |
- on 880202,determined That Individual Valve Leakage Through Reactor Coolant Cold Leg Sample Isolation Valves Was Greater than ASME Section XI Spec.Caused by Impurities in Sys.Valves Replaced
| | | 05000281/LER-1988-002-02, :on 880202,containment Isolation Valves Declared Inoperable Due to Leakage in Excess of Spec Value. Cause Not Determined.Valves Will Be Replaced/Repaired Based Upon Failure Analysis Results |
- on 880202,containment Isolation Valves Declared Inoperable Due to Leakage in Excess of Spec Value. Cause Not Determined.Valves Will Be Replaced/Repaired Based Upon Failure Analysis Results
| | | 05000280/LER-1988-002-01, :on 880206,individual Rod Position Indicators Declared Inoperable Following Turbine Stop Valve/Governor Valve Freedom Test.Caused by Instrument Drift.Indicators Recalibr |
- on 880206,individual Rod Position Indicators Declared Inoperable Following Turbine Stop Valve/Governor Valve Freedom Test.Caused by Instrument Drift.Indicators Recalibr
| 10 CFR 50.73(a)(2)(iii) | | 05000281/LER-1988-003-01, :on 880220,individual Rod Position Indicators Differed from Demand Counter by Greater than 12 Steps. Caused by Generic Westinghouse PWR Concern.Indicators Calibr to Give Correct Readings |
- on 880220,individual Rod Position Indicators Differed from Demand Counter by Greater than 12 Steps. Caused by Generic Westinghouse PWR Concern.Indicators Calibr to Give Correct Readings
| | | 05000280/LER-1988-003-02, :on 880216,reactor Trip Occurred Due to Power Range Lo Setpoint Hi Flux & Intermediate Range Hi Flux Trip Signals.Caused by Personnel Error.Peer Group Reviewed Event & Switches Returned to Correct Positions |
- on 880216,reactor Trip Occurred Due to Power Range Lo Setpoint Hi Flux & Intermediate Range Hi Flux Trip Signals.Caused by Personnel Error.Peer Group Reviewed Event & Switches Returned to Correct Positions
| | | 05000281/LER-1988-004, :on 880327,turbine Runback Automatically Initiated Due to Loss of Power to Power Range Nuclear Instrument NI-43.Caused by Internal Conductor Failure Due to Age.Vital Bus Inverters Replaced |
- on 880327,turbine Runback Automatically Initiated Due to Loss of Power to Power Range Nuclear Instrument NI-43.Caused by Internal Conductor Failure Due to Age.Vital Bus Inverters Replaced
| | | 05000280/LER-1988-004, :on 880216,reactor Coolant Dose Exceeded Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core. Level of dose-equivalent I-131 Monitored at Least Every 4 H Until Level Returned to Less than 1 Mci |
- on 880216,reactor Coolant Dose Exceeded Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core. Level of dose-equivalent I-131 Monitored at Least Every 4 H Until Level Returned to Less than 1 Mci
| | | 05000280/LER-1988-005-01, :on 880219,heat Tracing Proper Control Setpoints Could Not Be Verified.Caused by Inadequate Surveillance & Maint Procedures.Verification of Correct Setpoints Initiated |
- on 880219,heat Tracing Proper Control Setpoints Could Not Be Verified.Caused by Inadequate Surveillance & Maint Procedures.Verification of Correct Setpoints Initiated
| | | 05000281/LER-1988-005-02, :on 880305,control Rod Urgent Failure Alarm Received in Control Room.Caused by Failed Phase Control Card in 1BD Power Cabinet.Control Room Operator Placed Rod in Manual Per Abnormal Procedure for Malfunction |
- on 880305,control Rod Urgent Failure Alarm Received in Control Room.Caused by Failed Phase Control Card in 1BD Power Cabinet.Control Room Operator Placed Rod in Manual Per Abnormal Procedure for Malfunction
| | | 05000280/LER-1988-006-01, :on 880219,individual Rod Position Indicators Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Generic Westinghouse PWR Concern.Rods Calibr to Give Correct Indication & Returned to Svc |
- on 880219,individual Rod Position Indicators Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Generic Westinghouse PWR Concern.Rods Calibr to Give Correct Indication & Returned to Svc
| | | 05000281/LER-1988-006-02, :on 880310,fire Detection Circuit for Facility Containment & Emergency Switchgear Instrument Rack Room Rendered Inoperable.Caused by Failure of Remote Control Module EIIS-IC Imod.Failed Module Replaced |
- on 880310,fire Detection Circuit for Facility Containment & Emergency Switchgear Instrument Rack Room Rendered Inoperable.Caused by Failure of Remote Control Module EIIS-IC Imod.Failed Module Replaced
| | | 05000281/LER-1988-007-02, :on 880405,individual Rod Position Indicators Declared Inoperable Due to Instrument Drift.Setpoint Change Evaluated to Lower Rod Deviation Alarm to Warn Operator Before Deviation Reached |
- on 880405,individual Rod Position Indicators Declared Inoperable Due to Instrument Drift.Setpoint Change Evaluated to Lower Rod Deviation Alarm to Warn Operator Before Deviation Reached
| | | 05000280/LER-1988-007-01, :on 880224,control/relay Room Chiller Tripped. Caused by Insufficient Svc Water Flow.Throttled Svc Water Valves Fully Opened & Correct Outlet Valve Throttled to Obtain Proper Svc Water Flow |
- on 880224,control/relay Room Chiller Tripped. Caused by Insufficient Svc Water Flow.Throttled Svc Water Valves Fully Opened & Correct Outlet Valve Throttled to Obtain Proper Svc Water Flow
| | | 05000280/LER-1988-008-01, :on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested Satisfactorily |
- on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested Satisfactorily
| | | 05000281/LER-1988-008-02, :on 880505,reactor Operator Discovered That No Boric Acid Flowpath Existed from Boric Acid Storage Tanks to Charging Pumps.Caused by Personnel Error & Procedural Inadequacy.Procedures Will Be Revised |
- on 880505,reactor Operator Discovered That No Boric Acid Flowpath Existed from Boric Acid Storage Tanks to Charging Pumps.Caused by Personnel Error & Procedural Inadequacy.Procedures Will Be Revised
| 10 CFR 50.73(o)(2)(ii) | | 05000280/LER-1988-009-01, :on 880311,specific Activity Sample of Reactor Coolant Showed dose-equivalent I-131 Level of 1.5 Uci Which Exceed Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core |
- on 880311,specific Activity Sample of Reactor Coolant Showed dose-equivalent I-131 Level of 1.5 Uci Which Exceed Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core
| | | 05000281/LER-1988-009-02, :on 880420,component Cooling Water HXs Declared Inoperable.Caused by Vacuum Priming Lines Up to Isolation Valves Not Being Seismically Supported.Engineering Work Request to Install Seismic Supports Made |
- on 880420,component Cooling Water HXs Declared Inoperable.Caused by Vacuum Priming Lines Up to Isolation Valves Not Being Seismically Supported.Engineering Work Request to Install Seismic Supports Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000281/LER-1988-010-02, :on 880516,reactor Trip Occurred as Result of Steam Generator lo-lo Level.Caused by Rapid Closure of Turbine Governor Valves.Recorder Will Be Used to Monitor Electrohydraulic Control Sys During Startup |
- on 880516,reactor Trip Occurred as Result of Steam Generator lo-lo Level.Caused by Rapid Closure of Turbine Governor Valves.Recorder Will Be Used to Monitor Electrohydraulic Control Sys During Startup
| | | 05000280/LER-1988-010-01, :on 880409,individual Rod Position Indicators (Irpis) Inoperable.Caused by Incorrect Rod Position Indication Due to Primary Coolant Temp Changes.Work Request to Calibr Irpis Submitted |
- on 880409,individual Rod Position Indicators (Irpis) Inoperable.Caused by Incorrect Rod Position Indication Due to Primary Coolant Temp Changes.Work Request to Calibr Irpis Submitted
| 10 CFR 50.73(a)(2) | | 05000281/LER-1988-010-03, :on 880516,reactor Trip Occurred Due to lo-lo Steam Generator Level.Caused by Rapid Closure of Turbine Governor Valves.Turbine Impulse Pressure Transmitter Calibr. Further Monitoring Performed During Startup |
- on 880516,reactor Trip Occurred Due to lo-lo Steam Generator Level.Caused by Rapid Closure of Turbine Governor Valves.Turbine Impulse Pressure Transmitter Calibr. Further Monitoring Performed During Startup
| | | 05000280/LER-1988-011, :on 880415,PORVs PCV-1455C & PCV-1456 Failed to Manually Open When Selector Switches Placed in Open Position from Auto Position.Caused by Procedural Inadequacy. Valve Actuator Bolts & Screws Torqued |
- on 880415,PORVs PCV-1455C & PCV-1456 Failed to Manually Open When Selector Switches Placed in Open Position from Auto Position.Caused by Procedural Inadequacy. Valve Actuator Bolts & Screws Torqued
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000280/LER-1988-011-01, :on 880415,power-operated Relief Valves Failed to Manually Open When Selector Switches Placed in Open Position.Cause Under Investigation.Selector Switches,Air Supply & Valves Examined for Malfunctions |
- on 880415,power-operated Relief Valves Failed to Manually Open When Selector Switches Placed in Open Position.Cause Under Investigation.Selector Switches,Air Supply & Valves Examined for Malfunctions
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(v) 10 CFR 50.73(o)(2)(i) | | 05000281/LER-1988-011-02, :on 880423,control Room/Relay Room Chiller Removed from Svc After Second Chiller Removed from Svc. Caused by Fouled Chiller Refrigerant filter-dryer Elements. Filter-dryer Elements Replaced |
- on 880423,control Room/Relay Room Chiller Removed from Svc After Second Chiller Removed from Svc. Caused by Fouled Chiller Refrigerant filter-dryer Elements. Filter-dryer Elements Replaced
| | | 05000280/LER-1988-012-01, :on 880418,Tech Spec 1.0.H.5 Violated.Caused by Discovery of Valve 1-RS-11 Held in Open Position by Counter Weight Due to Personnel Error.Valves Inspected & Verified to Be in Closed Position & 1-RS-11 Disassembled |
- on 880418,Tech Spec 1.0.H.5 Violated.Caused by Discovery of Valve 1-RS-11 Held in Open Position by Counter Weight Due to Personnel Error.Valves Inspected & Verified to Be in Closed Position & 1-RS-11 Disassembled
| | | 05000281/LER-1988-012-02, :on 880517,individual Rod Position Indicators for Four Rods in Shutdown Bank B Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Incorrect Rod Position Indication Due to RCS Changes |
- on 880517,individual Rod Position Indicators for Four Rods in Shutdown Bank B Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Incorrect Rod Position Indication Due to RCS Changes
| 10 CFR 50.73(o)(2)(iv) | | 05000281/LER-1988-013-01, :on 880523,reactor Trip Breakers Automatically Opened in Response to Reactor Trip Signal Generated on Low Steam Generator Water Level.Caused by Inadequate Procedure. Personnel Reinstructed on Deviating Procedures |
- on 880523,reactor Trip Breakers Automatically Opened in Response to Reactor Trip Signal Generated on Low Steam Generator Water Level.Caused by Inadequate Procedure. Personnel Reinstructed on Deviating Procedures
| | | 05000280/LER-1988-013-02, :on 880523,emergency Diesel Generator 3 Automatically Started.Caused by Performing Multiple Procedures W/O Adequate Review of Individual Procedures. Testing Suspended & Diesel Shutdown |
- on 880523,emergency Diesel Generator 3 Automatically Started.Caused by Performing Multiple Procedures W/O Adequate Review of Individual Procedures. Testing Suspended & Diesel Shutdown
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | | 05000280/LER-1988-014-01, :on 870630,determined That Unique Scenario Could Exist Whereby Auxiliary Feedwater Could Be Lost to Operating Unit.Administrative Controls Established & Safety Analysis Reviewed for high-energy Line Break |
- on 870630,determined That Unique Scenario Could Exist Whereby Auxiliary Feedwater Could Be Lost to Operating Unit.Administrative Controls Established & Safety Analysis Reviewed for high-energy Line Break
| | | 05000281/LER-1988-014-02, :on 880528,RCS PORV PCV-2455C Cycled Open & Closed,Simultaneous W/Rcs Venting & Filling.Caused by Failure to Revise RCS Venting Procedure.Operating Procedures Revised |
- on 880528,RCS PORV PCV-2455C Cycled Open & Closed,Simultaneous W/Rcs Venting & Filling.Caused by Failure to Revise RCS Venting Procedure.Operating Procedures Revised
| 10 CFR 50.73(o)(2)(vii) | | 05000281/LER-1988-015-02, :on 880626,rod Urgent Failure Annunciator Activated in Control Room.Caused by Failed Circuit Card & Blown Fuse.Failed Circuit Card & Blown Fuse Replaced & Rod Control Sys Tested Satisfactorily |
- on 880626,rod Urgent Failure Annunciator Activated in Control Room.Caused by Failed Circuit Card & Blown Fuse.Failed Circuit Card & Blown Fuse Replaced & Rod Control Sys Tested Satisfactorily
| 10 CFR 50.73(a)(2)(i) | | 05000280/LER-1988-015-01, :on 880523,emergency Bus Transformer Cooling Fans Powered from nonsafety-related Power Supply.Caused by Design Deficiency.Power Sources Relocated to Diesel Generator Backed Supplies |
- on 880523,emergency Bus Transformer Cooling Fans Powered from nonsafety-related Power Supply.Caused by Design Deficiency.Power Sources Relocated to Diesel Generator Backed Supplies
| | | 05000281/LER-1988-016-02, :on 880731,discovered That Individual Rod Position Indicators (Irpis) Differed from Group Step Demand Counter by Greater than 12 Steps.Caused by Drift in Irpi Indication.Irpis Adjusted |
- on 880731,discovered That Individual Rod Position Indicators (Irpis) Differed from Group Step Demand Counter by Greater than 12 Steps.Caused by Drift in Irpi Indication.Irpis Adjusted
| | | 05000280/LER-1988-016-01, :on 880510,pressurizer Safety Valve Setpoints Found Outside of Allowable Limits During Refueling Surveillance Testing.Possibly Caused by Setpoint Drift. Valves Refurbished & Lift Setpoints Adjusted |
- on 880510,pressurizer Safety Valve Setpoints Found Outside of Allowable Limits During Refueling Surveillance Testing.Possibly Caused by Setpoint Drift. Valves Refurbished & Lift Setpoints Adjusted
| 10 CFR 50.73(a)(2)(i) | | 05000281/LER-1988-017-02, :on 880730,failure of Recirculation Spray Svc Water MOVs Due to Premature Actuation of Torque Switch. Both Valves Declared Inoperable & Tech Spec 3.0.1 Entered on Basis That Both Subsystems Were Inoperable |
- on 880730,failure of Recirculation Spray Svc Water MOVs Due to Premature Actuation of Torque Switch. Both Valves Declared Inoperable & Tech Spec 3.0.1 Entered on Basis That Both Subsystems Were Inoperable
| | | 05000280/LER-1988-017-01, :on 880606,discovered Debris in Temporary Discharge Cone Strainer & Recirculation Spray Sump Pumps. Caused by Inadequate Insp Program.Containment Sump & Pump Screen Surveillance Will Be Implemented |
- on 880606,discovered Debris in Temporary Discharge Cone Strainer & Recirculation Spray Sump Pumps. Caused by Inadequate Insp Program.Containment Sump & Pump Screen Surveillance Will Be Implemented
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000280/LER-1988-017, :on 880606,foreign Matl Found in Temporary Discharge Cone Strainer & Deficiencies Found in Sump Screens.Caused by Inadequate Insp Program During Const Activities.Foreign Objects Removed |
- on 880606,foreign Matl Found in Temporary Discharge Cone Strainer & Deficiencies Found in Sump Screens.Caused by Inadequate Insp Program During Const Activities.Foreign Objects Removed
| | | 05000281/LER-1988-018-02, :on 880811,steam Generator B Channel III Steam Flow Failed to High Flow Indication.Failed Multiplier/ Divider Replaced.Affected Channels Placed in Trip Mode |
- on 880811,steam Generator B Channel III Steam Flow Failed to High Flow Indication.Failed Multiplier/ Divider Replaced.Affected Channels Placed in Trip Mode
| | | 05000280/LER-1988-019-01, :on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing Jumpers |
- on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing Jumpers
| | | 05000281/LER-1988-019-03, :on 880901,steam Generator a Inside Containment Steam Valve Closed for No Apparent Reason Due to Actuation of High Flow Trip Solenoid.Solenoid Reset,Blowdown Flow Established & Trip Valve & Solenoid Verified |
- on 880901,steam Generator a Inside Containment Steam Valve Closed for No Apparent Reason Due to Actuation of High Flow Trip Solenoid.Solenoid Reset,Blowdown Flow Established & Trip Valve & Solenoid Verified
| | | 05000280/LER-1988-020, :on 880628,control/relay Room Chiller Condenser Svc Water (SW) Pumps & Unit 2 Charging Pump SW Pumps Lost Suction.Caused by Inadequate Procedure.Filling of SW Supply Line Secured & Supply Header Vented |
- on 880628,control/relay Room Chiller Condenser Svc Water (SW) Pumps & Unit 2 Charging Pump SW Pumps Lost Suction.Caused by Inadequate Procedure.Filling of SW Supply Line Secured & Supply Header Vented
| | | 05000281/LER-1988-020-01, :on 880909,individual Rod Position Indicators for Four Control Rods of Control Bank D Differed from Demand Counter by More than 12 Steps.Caused by Indicator Indication Drift.Indicators Adjusted |
- on 880909,individual Rod Position Indicators for Four Control Rods of Control Bank D Differed from Demand Counter by More than 12 Steps.Caused by Indicator Indication Drift.Indicators Adjusted
| | | 05000281/LER-1988-021-01, :on 880908,required Test Frequency for B Low Head Safety Injection Pump Exceeded.Caused by Inability of Operator to Obtain Required Vibration Test W/Test Equipment Used.Formal Training of Equipment Administered |
- on 880908,required Test Frequency for B Low Head Safety Injection Pump Exceeded.Caused by Inability of Operator to Obtain Required Vibration Test W/Test Equipment Used.Formal Training of Equipment Administered
| | | 05000280/LER-1988-021, :on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed |
- on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed
| | | 05000280/LER-1988-022, :on 880710,unit Ramped Down to Shutdown.Caused by MOV-CS-101B Leakage Due to Lost Motion in Shaft & Linkage Between Motor Operator & Shaft.Valve Disassembled & Valve Seat & O-rings Replaced |
- on 880710,unit Ramped Down to Shutdown.Caused by MOV-CS-101B Leakage Due to Lost Motion in Shaft & Linkage Between Motor Operator & Shaft.Valve Disassembled & Valve Seat & O-rings Replaced
| | | 05000281/LER-1988-022-01, :on 880910,reactor Trip by Turbine Trip Occurred While Attempting to Maintain Turbine at Synchronous Speed.Caused by Inadequate Procedure & Faulty Valve Position Indication.Testing to Be Performed |
- on 880910,reactor Trip by Turbine Trip Occurred While Attempting to Maintain Turbine at Synchronous Speed.Caused by Inadequate Procedure & Faulty Valve Position Indication.Testing to Be Performed
| | | 05000280/LER-1988-023, :on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip Mode |
- on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip Mode
| | | 05000281/LER-1988-023-02, :on 881006,three Containment Trip Valves Found Closed & Radiation Monitor Sample Pump & Particulate Monitor Discovered Stopped Due to Trip Valve Interlock.Caused by Personnel Error.Trip Valves Opened |
- on 881006,three Containment Trip Valves Found Closed & Radiation Monitor Sample Pump & Particulate Monitor Discovered Stopped Due to Trip Valve Interlock.Caused by Personnel Error.Trip Valves Opened
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