ML17334B811

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LER 98-030-00:on 980504,noted That Incorrect Installation of Containment Spray Heat Exchanger Could Result in Unanalyzed Condition.Cause Indeterminate.Independent Verification of Heat Exchanger Will Be Performed in mid-Jul.W/980706 Ltr
ML17334B811
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 07/06/1998
From: Pisarsky F, Sampson J
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GL-89-13, LER-98-030, LER-98-30, NUDOCS 9807140083
Download: ML17334B811 (4)


Text

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REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9807140083 DOC.DATE: 98/07/06 NOTARIZED: NO DOCKET 0 FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1,'ndiana M 05000315 AUTH. NAME AUTHOR AFFlLIATION PISARSKY,F. Indiana Michigan Power Co.

SAMPSON,J.R. Indiana Michigan Power Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 98-030-00:on 980504,noted that incorrect installation of containment spray heat exchanger could result in unanalyzed condition. Cause indeterminate. Licensee will perform DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR j independent verification of heat exchanger.W/980706 ltr.

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

ENCL I SIZE:

RECIPIENT ID CODE/NAME COPIES 'ECIPIENT COPIES LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 PD 1 1 STANG, J 1 1 INTERNAL: AEOD SPD B 2, 2 AEOD/SPD/RRAB 1 1 L CEN 1 1 NRR/DE/ECGB 1 1 DE EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOHB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN3 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD D 1 1 LITCO BRYCE, J H 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 0

1 1 NUDOCS FULL TXT 1 1 N

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR 0 UR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 23 ENCL 23

American Electric Po Cook Mrelear Plant One Cook Place Bagman. lbtl49>C6 616465 5901 AAIERIC'AM EI.ECTRIC .

POWER July 6, 1998 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Operating Licenses DPR-58 Docket No. 50-315 Document Control Manager:

In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event i g p 98-030-00 Sincerely,

~24 J. R. Sampson Site Vice President lmbd Attachment C. J. Paperiello (Acting), Region III J. R. Sampson P. A. Barrett S. J. Brewer R. Whale D. Hahn Records Center, INPO

<r=@> i NRC Resident Inspector

'P807i40083 rr80706 PDR ADQCK 05000315 8 PDR

NRC Form 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB NO. 51504104 (4-95) ExpIREs 04150rs 5 ESTIMATED BVRDEN PER RESPONSE TO COMPt.Y WITH THIS MANDATORY LICENSEE EVENT REPORT (LER) INFORMATIONCOLLECTION REQUEST" 50 0 HRS. REPORTED LESSONS LEARN'EO ARE BICORPORATEO 0ITO THE UCENSING PROCESS ANO FEO SACK TO INDUSTRY. FORwARD COMMENTS REGARDING BVRDEN ESTrMATE TO THE (See reverse for required number of digits/characters for each block)

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INFORMATION AND RECORDS MANAGEMENT BRANCH (Te Fssi, V.S. NVCLEAR REGVIATORY COMMISSIN, WASHINGTON. OC 205550001, ANO TO THE REDVCTCN PRCVECT (M5150IIH). CFFICE OF MANAGEMENTANO BVCGET,WASISNGTON. DC 20505 FACILITYNAME (I) OOCKETNUMBER(2) PAGE (5)

Cook Nuclear Plant Unit 1 50-315 1 of1 TITLE (4)

Interim LER - Incorrect Installation of Containment Spray Heat Exchanger Could Result in Unanalyzed Condition EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED(8)

MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR A ILI NAM NUMB NUMBER NUMBER A ILITYNAME 0 CK NUMB 06 04 98 98 030 00 07 06 98 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR (): (Check one or more) (11)

MODE (9) 20.2201 (b) 20.2203(a)(2)(v) 50.73(a)(2)(i) 50.73(a)(2)(viii)

POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x)

LEVEL (10) 00 73.71 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) at Abstract below or 50.36(c)(1) 50.73(a)(2)(v) SI NRC Form 666A 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER (Ioc4de Area Code)

Mr. Frank Pisarsky, Manger - Engineering Component Performance 616/465-5901, x2607 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE NPROS TO NPROS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED M NI AY X YES NO SUBMISSION DATE (15) 09 30 98 (If Yes, complete EXPECTED SUBMISSION DATE).

Abstract (Limit to 1400 spaces, i.e. approximately 15 single-spaced typewritten lines) (16)

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Qn June 4, 1998, with Unit 1 in Mode 5, plant personnel performing Generic Letter 89-13 ("Service Water System Problems Affecting Safety Related Systems" ) inspections made a preliminary determination that the West Containment Spray (CTS) heat exchanger had been installed 180 degrees from the design position. The service water inlet appears to be aligned to the outlet side of the heat exchanger, which results in the impingement plate being located on the service water outlet side. The impingement plate is designed to be located on the inlet side to prevent sand and silt from impinging on the heat exchanger tubes and causing erosion of the tubes. This condition was determined to be a potentially unanalyzed condition, and an ENS notiTication was made at 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br /> EDT under 10CFR50.72(b)(2)(I). This LER is submitted in accordance with 10CFR50.73(a)(2)(ii), for an unanalyzed condition.

Independent verification of the heat exchanger orientation will be performed in mid-July by site Quality Control. If it is confirmed that the impingement plate is located on the outlet side of the heat exchanger instead of the inlet side, visual inspection of the tubes'utside surface and eddy current testing of select tubes in the vicinity of the inlet nozzle will be performed. These inspections will determine the presence and extent of tube degradation.

Review of previous inspection records indicates that the remaining CTS heat exchangers are installed correctly. This will be confirmed by inspection prior to start up of the units.

As the eddy current testing has not yet been scheduled, a tentative date for updating this LER has been set for September 30, 1998. The update may be provided earlier, depending on the testing schedule and the results.

NRC FORM 366 (4-95)