ML17334B616

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Responds to NRC 970204 Ltr Re Violations Noted in Insp Rept 50-315/96-13 & 50-316/96-13.Corrective Actions:Instructions Requiring Filter Content Evaluation Were Removed from Charging Pump Recurring Tasks on 970211
ML17334B616
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/12/1997
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1238F, NUDOCS 9703180199
Download: ML17334B616 (32)


Text

CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM DOC.DATE: 97/03/12 NOTARIZED: YES (RIDS)'ACCESSION'NBR:9703180199 DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 UTH.NAME AUTHOR AFFILIATION ITZPATRICK,E.E Indiana Michigan Power Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to NRC 970204 ltr re viol'ations noted in insp rept 50-315/96-13 & 50-316/96-13.Corrective actions: instructions requiring filter content evaluation were removed .from charging pump recurring tasks on 970211.

DISTRIBUTION CODE: IEOID COPIES RECEIVED:LTR 1 ENCL i SIZE: 1 TITLE: C>eneral (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODS/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 PD 1 1 HICKMANPJ 1 1 INTERNAL: AEOD/SPD/RAB 1 1 1 DEDRO 1 1 FILE CENT 1 1 NRR/DISP/PIPB 1 1 RCH/HHFB 1 1 NRR/DRPM/PECB -1 NRR/DRPM/PERB 1 1 NUDOCS-ABSTRACT 1 1 OE DIR 1 1 OGC/HDS2 1 1 RGN3 FILE 01 1 1 RNAL: LITCO BRYCE,J H 1, 1 NOAC 1 1 NRC PDR 1 1 NUDOCS FULLTEXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU"DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL 18

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indiana Michigan Power Company 500 Circle Drive Buchanan, Ml 491071395 INDIANA NICHIGAN POWER

'arch 12, 1997 AEP: NRC: 1238F 10 CFR 2.201 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory'ommission ATTN: Document Control Desk Washington, D.'. 20555 Gentlemen:

Donald C. Cook Nuclear Plant Units 1 and 2, NRC INSPECTION REPORTS NOs. 50-315/96013 (DRS)

AND 50-316/96013 (DRS) REPLY TO NOTICE OF VIOLATIONS This letter is in response to a letter from G, E. Grant, dated February 4, 1997, that forwarded a notice of three violations and one notice of deviation to Indiana Michigan Power Company. The violations and the deviation were identified during a system operational performance inspection (SOPI) of the centrifugal charging system portion of the emergency core cooling systems'and the residual heat removal systems.

Our response was due to you on March 6, 1997; however, we requested a brief extension to recover the time delay from when the report was issued to when Ron Gardner it was of Region received.

III, on FebruaryThe14,extension 1997 was granted by three violations addressed the 1) failure to establish adequate 'he instructions/failure to follow procedures as related to collection of an oil,sample, and adequate minimum thread engagement acceptance criteria; 2) inadequate test control as related to incorporating

, charging pump acceptance limits into the IST program; and 3) failure to perform adequate/timely corrective actions, as .related to determining the correct oil sight-glass related pumps and motors, addressing equipment deficiency tagging fill. marks on 'safety-problems, and locating/reconstituting a centrifugal charging pump net positive sue/ion head calculation.

The deviation was from actions committed to in NUREG-0737.

specifically involving the source term used for a radiological evaluation.

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U. S. Nuclear Regulatory Commission AEP: NRC: 1238F Page 2 Our reply to the violations and deviation are provided in the attachment to this letter. Also included are the results of of technical specification clarifications, which we our'eview committed to perform at the December 13, 1996, exit meeting. The reply does not contain any personal privacy, proprietary, or saf eguards information.

Sincerely, E. E. Fit atrick Vice President':

SHORN TO AND SUBSCRIBED BEFORE ME TH s /c2. DAY op 1997 Notary Public My Commission Expires: 2 /Cc'OO/

vlb dANICE h1. 8!CKERS Attachment Notay PuMc, Benien County, Ml My Conurisst'on Expes Feb. 16, 20D1 CC: A. A. Blind A., B. Beach MDEQ - DW & RPD NRC Resident R. Padgett Inspector

1 ATTACHMENT TO AEP:NRC: 1238P REPLY TO 'NOTICE OP UIOLATION:

NRC INSPECTION REPORTS NOs. 50-315/96013 (DRS)

AND 50-316/96013 (DRS)

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Attachment to AEP:NRC:1238F Page 1 During an NRC system operational performance inspection conducted November 18 through December 13, 1996, on the emergency core cooling system portion of the centrifugal charging system and residual heat removal system three violations and one deviation were identified. In accordance with the "General Statement 'of Policy and Procedures for NRC Enforcement Actions," (NUREG-1600) the violations and the responses are provided below. Additionally, we were requested to respond to the deviation, and to provide information related to a commitment regarding technical specification (T/S) clarifications made at the December 13, 1996, exit meeting. Our response to these items is also provided below.

NRC Violation A I

"10 CFR 50, Appendix B, Criterion V, 'Instructions, Procedures, and Drawings,'equires, in part, that activities affecting quality shall be prescribed by instructions,; procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Maintenance procedure 12 MHP 5021.001.009, Revision 8, 'Torque Selection,'ated Maich 21, 1994, requires thread engagement of at least 80 percent of nut height.

Contrary to the ~,bove:

On December 4, 1996, the inspectors identified that a maintenance work package for the 1E centrifugal charging pump, . an activity .affecting quality, failed to include adequate instructions for lube oil sample collection.

2. On November 20, 1996, the inspectors identified that maintenance procedure MDS-600, 'General Erection.Tolerances for Pipe and Tube Supports/Restraints,'as not of a type appropriate to the circumstances since it failed to contain adequate minimum thread engagement acceptance criteria for activities affecting quality.

On November 21, 1996, the inspectors identified t'.'at maintenance personnel failed to perform bolting on safety-related equipment in accordance with maintenance procedure 12MHP5021.001.009, 'Torque Selection.'s a result, nuts associated with emergency core cooling system equipment were, identified with thread engagement less than 80 percent of nut height.

This a Severity Level IV violation."

Res onse to NRC Violation A1 Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits'o the violation as cited in the NRC notice of violation.

2. Reason far the Violation The reason for the violation was failure to remove oil sampling instructions from applicable recurring tasks that were no longer needed after implementation of a formal oil sampling program.

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Attachment to AEP:NRC:1238F Page 2 The instructions found in the job order activity associated with the work on the 1E centrifugal charging pump instructed personnel to:

"Drain oil from filter into a container; A. Deliver oil from CUNO filter to chem lab for analysis. (The results will go to the engineers for evaluation of wear in system)."

The job order activity instructions were developed prior.- to implementation of our formal oil analysis program. At the time it was input as a recurring task, it was intended to provide a rough indication of gross machine problems.

Subsequently, a formal oil. analysis program was implemented, with proceduralized sampling techniques being utilized by chemistry personnel. Under this sampling program, 'done quarterly (as opposed to filter change-,outs that are done yearly), wear particles of considerably less size than those detected via the filter change-out method can be detected, thus giving much earlier indication of machine problems.

The instructions in the re'curring task were inadvertently left in place after the formal program was instituted. The oil collected via these instructions is not analyzed by chemistry personnel; and decisions as to the condition of are not based on these samples. the'quipment

3. Corrective Actions Taken and Results Achieved The instructions requiring filt'er content evaluation were remov'ed from the charging pump recurring tasks on February 11, 1997. The 1E charging pump lube oil was sampled by chemistry personnel on September 12, 1996, prior to the filter change-out observed on December 4, 1996, consistent with the formal oil analysis program.
4. Corrective Actions Taken to Avoid Further Violations A revie'~ of lube oil changes related to'equipment included in the oil analysisprogram was conducted. Similar. wording was found in recurring tasks for the motor-driven and turbine-driven auxiliary,feedwater'umps. This redundant wording will be removed prior to the next required date for filter change-out for this equipment.
5. Date When Full Com liance Will Be 'Achieved Full, compliance was achieved on'February 11, 1997," when the redundant instructions were removed'rom the four charging pump's recurring tasks.

Res onse to NRC Violation A2 & A3

1. Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

Attachment to AEP:NRC:1238F Page 3

2. Reason for the Violation The cause of the violation, as cited in A3, is a combination of the way work was do'cumented and adherence to procedural requirements that were inconsistent.

The reference to MDS-600, cited in A2, as a "maintenance procedure"'equires clarification. MDS-600 is not a procedure, it is a design standard that provides tolerances for installation and evaluation of as-found conditions for ~

piping/tubing supports. tH)S-600 is not. an applicable reference and there is no hierarchial connection between MDS-600 and **12 MHP 5021.001.009.

3. Corrective Actions Taken and 'Results Achieved Eight condition reports were written to..document the inspection team's concerns. Operability reviews were performed based on the identified deficiencies, and the affected equipment was determined to be operable.

Work history for each component was reviewed to assist in determining the potential cause(s). In general, this review identified a general time frame when the deficiency was created, but not a specific work activity.

Action requests were written to correct the deficiency where an action request did not already exist, or the deficiency was evaluated and found to be acceptable as is.

Corrective Actions Taken to Avoid Further Violations

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Maintenance standing. or>er, MS0.009, was issued on February 3, 1997. This document establishes an acceptance criteria of "flush or better" 'for thread engagement.

Further, engagement it provides a policy. for documenting as-found thread deficiencies so they can be evaluated and corrected.

Lastly, the policy provides for in-plant identification of less than flush thread engagement that has been evaluated and found to 4e acceptable. This standing order strengthens management expectations for thread engagement and establishes a mechanism for identification of analyzed, acceptable .

conditions.

I A walkdown was'erformed of a, random sample" of plant components of sufficient size to provide a 99% confidence level that these components are a statistically valid sample of the plant population of components. The as-found configuration of the fasteners associated with these components was evaluated. There were no fastener anomalies identified that af fected component functionality or operability.

Plant management has reinforced procedural adherence to all plant personnel.

    • 12 MHP 5021.001.009 'was enhanced by the addition of acceptance criteria of flush threads or petter.

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Attachment to AEP':NRC:1238F Page 4

5. Date When Full Com liance Will Be Achieved Full compliance was achieved on March 10, 1997. At that time the original 28 NRC-identified thread engagement deficiencies were analyzed as not affecting operability/quality; existing procedures, policies, and standards were upgraded; and the findings of the thread engagement random sample concluded that there were no functionality/operability concerns caused by thread engagement deficiencies associated with any of the sampled components.

NRC Violation B "10 CFR 50', Appendix B, Criterion XZ, 'Test Control,'equires, in part, that a test program be established to assure that all testing required to demonstrate that will perform satisfactorily instructures, systems, and components service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents.

Technical Specification 3.1.1.1, 'Shutdown Margin - Tave greater than 200 'F,'pecifies a boration capability .of 10 gallons per minute (gpm) of 20,000 parts per million (ppm) boron solution or equivalent.

Contrary to the above, on December 11, 1996, the inspectors identified that the correct acceptance limits to assure that the centrifugal charging pumps could perform their boron injection function as specified in Technical Specification been incorporated in the licensee's inservice 3.1 '.1 had not testing (ZST) program.

This is a Severity Level,ZV violation."

Res onse to NRC Violation B Admission or Denial of the Alle ed Violation Zndiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

Reason for the Violation The reason for the violation was that a review to determine applicability to the ZST program was not conducted prior to issuance of a technical specification (T/S) clarification on T/S 3.1.1.1.

T/S 3.1.1.1, Shutdown Margin - T,~ greater than 2004F provides shutdown margin requirements while in modes 1, 2, 3, or 4. The .action statement for T/S 3.1.1.1 requiies immediate and continuous boration at'reater than or equal to 10 gpm of a solution containing greater than or equal to 20,000 ppm boron or "equivalent" Westinghouse performed an analysis'o clarify the meaning of this statement if the

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refueling water storage tank (RWST) was used as a source of borated water. Westinghouse defined "equivalence" as "xenon burnout equivalence", which is the capability to inject sufficient boron to adjust boron concentration to compensate for xenon burnout from its peak value. Their analysis assumed a plant trip followed by a step return to 100% power

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Attachment to AEP:NRC:1238F Page 5 at peak xenon concentration. In addition, they assumed that the reactor would be maintained at full power during the transient. The results of this analysis showed that a centrifugal charging pump (CCP) flow of 120 gpm from the RWST could compensate for xenon throughout the transient if certain restrictions were observed.

On November 5, 1990, a revision to T/S clarification no. 7 was issued, which defined the 120 gpm of RWST water containing 2400 ppm boron as an acceptable source of water to satisfy boration flow . requirements for T/S 3.1.1.1.

Development and issuance of this T/S clarification was not coupled with a review of the test program to ensure the test program confirmed the ability of the CCPs to perform this function. This deficiency was identified by our engineers during efforts to respond to an inspector's question on the design functions of the CCPs during the inspection.

Corrective Actions Taken and Results Achieved Following identification of this deficiency, a calculation was performed to'etermine the maximum degradation the CCPs could tolerate while still being'able to deliver 120 gpm of RWST water to the reactor coolant system. This calculation revealed that the CCPs could tolerate a degradation of 9.5%.

for Unit 1 and 3.5% for Unit 2. A review of IST data as far back as 1990 determined that the pumps were capable of performing this function. The IST program has been revised to include limitations for allowable degradation of the CCPs to ensure that 120 gpm of 2400 ppm boron could be supplied from the RWST.

Additionally, as a point of information, since the original analysis by Westinghouse, which defined the 120 gpm value of 2400 ppm boron included a very conservative assumption that a step increase in power to 100% occurred while at'eak xenon,, a'reanalysis was performed using a more realistic ramp rate of 10%/hr, which is a limitation contained in plant procedures. This reanalysis indicated that the boration flow requirements of T/S 3.1.1.1 could be satisfied by as little as 60.1 gpm of 2400 ppm boron. We may relax the allowable degradation for the CCPs based on this revised 60.1 gpm flow.

4, Corrective Actions Taken to Avoid Further Violations Failure to ensure the test program for the CCPs included provisions to ensure the CCPs could deliver 120 gpm of 2400 ppm boron occurred as a result of failure to'ouple the development and issuance of a T/S clarification with

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appropriate reviews of the test program. As noted in the SOPI report, several examples were identified where T/S clarifications could, not be justified.'uring the exit meeting, we committed to perform a review of all of our T/S clarifications. The results of this review are contained in the "Commitment" section'f this attachment. Additionally, as noted, improvements will be made in the T/S clarification review process to ensure an adequate technical review of future clarifications.

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Attachment to AEP:NRC:1238F Page 6

5. Date When Full Com liance Will Be Achieved Full compliance was achieved on December 18, 1996, when the IST program was revi s'ed to include appropriate limits to ensure the" each units'CPs can supply .120 gpm of 2400 ppm boron from the RWST.

l NRC Violation C "10 CFR 50, Appendix B, Criterion XVI, 'Corrective Actions,'

requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected.

Contrary to the above:

1. Corrective actions to address potentially inaccurate sight'-

glass f ill marks for saf ety-related pumps and motors, a condition adverse to quality, were not initiated until November 27, 1996, although in" 1995 job orders were written to address potentially inaccurate sight-glass fill safety-related pumps and motors, and on March 6, 1996, marks on request was written to determine correct sight-glass fill an'ction marks on safety-related pumps and motors.

On December 5, 1996, the inspectors identified that the licensee failed to take corrective actions to either locate or re-constitute a centrifugal charging pump net positive suction head (NPSH) calculation although the calculation had been identified as missing about 18 months earlier.

3. On December 4, 1996, the inspectors determined that the licensee failed to take timely corrective actions to address equipment deficiency tagging problems. Although the licensee had identified that about 30 percent of plant components in the work control system reviewed in a three week period were not properly tagged in the field, corrective actions to address this concern had not been initiated.

This is a Severity Level IV violation."

Res onse to NRC Violation C1

1. Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

Reason for the Violation The cause of the untimely response for guidance on plant pump/motor oil fill levels was the lack of a communication protocol resulting in an unrecognized request to engineering personnel from operations personnel for technical assistance.

The request for assistance was made by means of an action

,request. Requests for engineering direction are made within the nuclear plant maintenance (NPM) computer system by means of an evaluation request. Different searches are required to action requests and .evaluation requests. 'Engineering 'ocate personnel did not search action requests because they were not an expected means for requesting assistance.

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Attachment to AEP:NRC:1238F Page 7 The was request for guidance on plant pump/motor oil brought to engineering management's fill levels attention approximately five months af ter the action request was initiated. At that time engineering personnel began work to provide the- requested guidance. The background research was completed and the guidance issued on December 5, 1996.

3. Corrective Actions Taken and Results Achieved The requested information on pump/motor oil fill levels was provided on December 5, 1996. A search of action requests assigned to engineering personnel has been performed to ensure the responsible groups are aware of assignments.

Additionally, as an interim action, plant personnel have been instructed to make daily searches to ensure no new action requests for engineering assistance go unrecognized.

4 ~ Corrective Actions Taken to Avoid Further Violations An acceptable method for requesting engineering. assistance will be developed by March 21, 1997.

Date When Full Co liance Will Be Achieved Full compliance was achieved on December 5, 1996, when the requested technical guidance was provided.

Res onse to NRC Violation C2 Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

2. Reason for the Violation,.

In June 1995, as part of the design basis documentation.(DBD) program, it was identified that the NPSH calculation for the CCPs could not be located. A DBD action item was i itiated in accordance with DBD program procedures. This item was classified as an instance of a "missing reference document",

a categorization with a normal resolution time of 60 days.

Engineering personnel involved in the classification o'f this item were aware that an NPSH calculation for the CCPs had been performed at one time, even though it could not be located. Operability was not considered to be a concern because it was known that the calculation had been performed but could not be found. Therefore, a high priority was not placed on reconstituting the calculation or resolving the DBD action item.

Corrective Actions Taken and Results Achieved As noted in the SOPI report, a new calculation was completed prior to and approved during the SOPI inspection, which confirmed adequate NPSH to the CCPs.

4, Corrective Actions Taken to Avoid Further Violations Following the SOPI inspection, a review of all open DBD action items was performed, by January 15, 1997, to assesd

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Attachment to AEP:NRC:3.238F Page 8 the appropriateness of their classification. A series of additional DBD action items were formally entered .into the corrective action system (via condition reports) as a result of this review. The corrective action system includes requirements for determining operability in a timely manner.

Entry into the corrective action system ensures a review of these issues by our condition assessment group (CAG). In its oversight function, the CAG assesses the need and makes assignments for confirmatory operability determinations or supplemental analysis. '

Beginning in January 1997, additional resources were added to the DBD project to enable prompt closure of DBD action items.

Specifically, the DBD project manager position, which had been vacant since. September 1996, was filled and two additional utility personnel and two contract personnel were assigned to the project. These personnel are aggressively pursuing resolution of open DBD action items. , This augmentation of personnel will continue through late 1997, by which time we expect to have made significant progress in the closure df DBD action items.

Additionally, we are training members of our staff, who have ownership of the DBDs, to ensure they understand the importance of promptly resolving.DBD action items and also to ensure they clearly understand the process for effecting closure of these items. This training commenced in early February 1997 and will be completed by March 15, 1997.

Finally, the DBD action item review process is being strengthened to limit the number of available classifications for DBD.action items and also to ensure a morecomprehensive review of action items by appropriate personnel. Project instructions related to action item processing are being revised. These revisions will be completed by March 28, 1997.

5. Date When Full Com liance Will Be Achieved Full compliance was achieved o.s December 2, 1996, 'when a new calculation was approved which confirmed adequate NPSH to the CCPs.

Res onse to NRC Violation C3 Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

2. Reason for the Violation The primary reason for the violation is that plant personnel were not sufficiently aware of the guidance regarding when to hang deficiency tags for corrective maintenance. This was further compounded by the lack of clarity prov-'ded by the administrative requirements that def ine def iciency tag hanging requirements.

Further, condition reports were not generated when missing

~ deficiency tag's were identified to prompt appropriate actions via the plant's corrective'ction program. While written

Attachment to AEP:NRC:1238F Page 9 memoranda identifying the missing deficiency tags were generated, condition reports were not written and therefore appropriate attention and follow-through were not instituted.

En all cases evaluated, the wor): control process had captured the identified degraded component, ensuring that the deficient condition would be corrected in a timely manner.

Corrective Actions Taken and Results Achieved Recent plant management actions have been taken to improve focus on promptly identifying problems and corrective actions dealing with conditions adverse to plant requirements. A condition report was promptly written when the NRC noted the lack of timely corrective action to address the identified deficiency tagging 'issue. The condition report 1) proposes that the material condition group replace missing tags when discovered, 2) recommends changes to the governing document .

NPM-02CM, and 3) requests assistance from computer personnel to modify existing NPM software to better support the rehanging of tags.

The personnel responsible for identifying missing deficiency tags were coached on the expectation to generate additional condition reports in the future.

4, Corrective Actions Taken to Avoid Further Violations By April 1, 1997, the governing document detailing when and how to tag deficiencies will be revised and appropriate personnel will be made aware of, the revised requirements.

Also, as of April 1, 1997: action requests generated that have not met the revised deficiency tagging requirements will be returned to the originating personnel for resolution before the action request will be processed further.

By September 1, 1997, system walkdowns will have been performed to verify that deficiency tags associated with existing corrective maintenance action requests (those generated before. April 1, 1997), comply with the revised requirements.

II Date When Full Com liance Will Be Achieved Full compliance will be achieved by April 1, 1997, when th' deficiency tagging requirements have been revised 'and appropriate personnel. have been made aware ,of 'hose requirements.

Further, condition reports will be written as of April 1, 1997, for any deficiency tag not in compliance with the revised requirement (regardless of when the action request and associated deficiency tags were generated).

Attachment to AEP:NRC:1238F Page 10 Deviation In addition to the above three violations, the;.notice <.f violation contained the following notice of deviation, which is addressed below.

DEV 50-315 96013-09 DRS and DEV 50-316 96013-09 DRS "During an NRC inspection conducted November 18 through December 13, 1996, a deviation of your actions committed to in NUREG-,0737,Section II.B.2 was identified. In accordance with the

'General Statement of Policy and Procedures for NRC Enforcement Actions,'UREG-1600, the deviation is listed below:

NUREG-0737,Section II.B.2, 'Design Review of Plant'hielding and Environmental Qualif ication of Equipment Spaces/Systems Which May Be Used in Postaccident for that 50 percent of the total iodine and 100 percent Operations,'equires of the noble gases 'are assumed to be released from the fuel in the design basis accident radiological analysis.

Contrary to the above, on December 4, 1996, the inspectors identified that the licensee failed to correctly translate Section II.B.2 of NUREG-0737 into the centrifugal charging pump emergency leakoff valve failure design basis accident radiological analysis. As a result, only one percent fuel damage was assumed in the analysis and resulted in dose estimates lower than revised calculated values."

Res onse to NRC Deviation Reason for the Deviation In August 1991,, a small break loss of coolant accident scenario run on the plant simulator identified a flowpath that had the potential to divert water away from the emergency 'core cooling system and containment building,. The flowpath was from the safety injection system (SIS) centrifugal charging pump discharge through an emergency leakoff valve, through the reactor coolant pump (RCP) seal.

return line safety valve to the volume control tank (VCT) and through the VCT safety valve to the chemical and volume control system holdup tanks. This condition was documented in LER 91-007-00. A review was conducted to asse'ss the safety consequence and implications of the postulated event.

Analysis of the potential dose rate from the'iverted water to the whole body at the site boundary was calculated to be.

insignificant compared to the 10 CFR 100 accident dose limit and even with the 10 CFR 20.105 dose limits- for unrestricted areas during s.ormal operations, based on the assumption of 1%.

failed fuel.

LER 91-007-01 provided original corrective action'for this scenario. The scenario of concern occurs following the switchover of the CCP suction from the refueling water

. storage tank to the recirculation sump via the residual heat removal. (RHR) pumps. With the RHR pumps supplying suction to the CCPs, the pressure in 'the CCP emergency leakoff (ELO) lines could be in excess of the downstream safety valve set pressure, and then approximately 60 gpm flow would be diverted from the ECCS to the VCT. Corrective actions for this scenario included emergency operating procedure (EOP)

Attachment to AEP:NRC:1238F Page ll modifications to close the charging pump ELO valves as part of the switchover from injection to recirculation ph se where the ECCS pumps take suction from the recirculation sump.

In June 1995, as part of our DBD program, it was identified that the EOPs noted above can be implemented, but were not single failure proof. The DBD program includes a process to identify, classify (with respect to safety significance), and resolve action items identified ..during the development of DBDs., A DBD action item was created to document that in the event the single failure is an ELO valve that cannot be isolated, the leakage path to the VCT would still persist.

Within the DBD program, this issue was classified as a discrepancy that was not safety significant, based on the analysis described above and documented in LER 91-007.

The reliance on the prior analysis in LER 91-007, which provided a practical assessment of safety significance per 10 CFR 50.73, to classify the DBD action item as a non-significant discrepancy was incorrect because consider design basis it did not assumptions for source term per NUREG-0737. The misclassification of the DBD action item was made by engineering personnel who incorrectly assumed that the analysis presented in LER 91-007 was also an adequate basis for classification of the DBD action item.

2. Corrective Actions Taken and Results Achieved The EOPs have been modified to instruct the operator to turn off a CCP for which the ELO valve cannot be closed. Flow through the idle pump of up to 5. 2 gpm may still exist; therefore, instructions have been added to isolate the valve manually. (The 5.2 gpm i." within the 10 gpm value for outside containment leakage previously evaluated and determined acceptable regar'ding offsite and control room doses.) The maximum dose to personnel expected to isolate the valve is 0.28 rem 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after the accident occurs.
3. Cor ective Actions Taken to Avoid Further Deviations Following'he SOPI inspection, a review of all open DBD action items was completed on January 15, 1997, to'assess the appropriateness of theix previous classification. A,series of additional DBD action items were formally entered into the corrective action system as a result of this review. Entry into the corrective action system ensures a thorough screening of these issues by the CAG for assignment to the appropriate organization for resolution. The corrective action system includes requirements for determining operability in a timely manner. In its oversight function,

. the CAG assesses the need and makes assignments for

.confirmatory operability determinations or supplemental analysis.

The DBD action item review process is being strengthened to limit the number of available classifications for DBD action items and also to ensure a more comprehensive review of action items by appropriate personnel. Project instructions related to action item'processing are being revised: These revisions will be completed by March 28, 1997,

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Attachment to AEP:NRC:1238F Page 12 II Date When Full Com liance Will Be Achieved Corrective action was completed on December 13, 1996, when changes were made to the EOPs to instruct the operator to turn off a CCP for which the ELO valve cannot be closed.

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Attachment to AEP:NRC:1238F Page 13 Commitment The inspection report requested we respond in writing regarding of T/S clarifications. The notice of violation contained our,'eview the following discussion.

"The licensee had 37 technical specification clarifications in effect. The inspectors reviewed the TSCs listed below(TSCs) and questioned whether the licensee could provide technical justification to support the TSCs. Subsequently, the licensee determined that ,the following clarifications could not be technically justified and should be canceled:

TSC ¹14 Airborne Radioactivity Monitor Operability TSC ¹15 Diesel Generator Surveillance Runs - Paralleled Grid TSC ¹48  :, Technical specification (TS) 4.8.1.1.2.F.2 Leak Testing of AD and CD Fuel Oil Tanks and Associated Piping The inspectors did not identify any past use of the above.TSCs that resulted in exceeding the action'equirements of the associated technical specification. The inspectors concluded that the safety significance'f the TSC 'errors were minimal.

The inspectors concluded that the licensee's approval of TSCs without appropriate technical justification was a weakness. At the end of the inspection, the licensee committed to. review all remaining TSCs to ensure they were still necessary and could be justified."

Review Sco e The NRC inspection report indicated that 37 TSCs were in effect at the time. of the inspection. A review of the active TSCs from the TSC index indicated that there were actually 35 active TSCs.

The three TSCs discussed in the inspection report were canceled.

The scope of the TSC review was of the remaining 32 active, TSCs.

Observation and Findin s Nine TSCs were canceled. They are as follows.

TSC ¹5 Operable - Operability Definition - Attendant

'nstrumentation TSC ¹12 D.C. Distribution - Operating TSC .¹26 Steam Generator Stop Valve Operability TSC ¹37 Definition of Maintenance on Emergency Core Cooling System Valves TSC ¹38 Turbine Driven Auxiliary Feedwater Pump Operability TSC ¹45 Snubber Functional Test Retest Results TSC ¹47 10 CFR 50 Appendix R Equipment Operability TSC ¹60 Auxiliary Feedwater System and Essential Service Water System TSC ¹61 Auxiliary Feedwater System Surveillance

'equirements Of,this group, two . TSCs (¹5 and ¹12), were canceled due to insufficient technical bases to support the implied operability provided by the TSC. Three TSCs (¹37, ¹60 and ¹61). were canceled

Attachment to AEP:NRC:1238F Page 14 k

as they were implemented in a manner inconsistent with current expectations. Four TSCs (¹26, ¹38, ¹45 and ¹47) were determined to .

be unnecessary.

One TSC (¹65), boric acid transfer pump operability, was revised to properly reflect its technical bases (refer to section 08.1 of the NRC inspection report).

The remaining 22 TSCs remain active.

Conclusion Based on the review of the existing TSCs, it follows that the TSCs were not well defined and were implemented 'in a manner inconsistent with current expectations. The program was utilized to capture many event driven decisions that would more appropriately operability program, or should be translated into appr'oved fit an procedural controls.

An improved TSC program will be developed by June 27, 1997. This program will provide a review of proposed new clarifications to ensure adequate technical justification is present prior to approval, and 'that a clarification does not change or alter the requirement of the specification being clarified.

Additionally, the new program will require plant 'mpact reviews as part of the implementation process. The impact reviews will ensure appropriate review and incorporation of clarification information into plant procedures and programs. The impact review process is being incorporated into the implementation process to address a SOPI concern involving integration of TSC ¹7 into the plant's ZST program.

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