|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
[Table view] |
Text
k'.l CO H.I "E'Y IACCELLRATEDBIDS !3ROCI'.SSli REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9412050138 DOC.DATE: '94/11/21 NOTARIZED: NO DOCKET FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION GRABO,B.A. Arizona Public Service Co. (formerly Arizona Nuclear Power LEVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 94-006-00 on 941021,identified actual flow rates on Unit 1 spray pond pumps may be exceeding design flow rates.
Caused by oversized orifices in Unit 1 spray pump return Established admin controls.W/941121 ltr. 'ines.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:STANDARDIZED PLANT 05000528 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR 'ENCL ID CODE/NAME LTTR ENCL PD4-2 PD 1 HOLIAN, B 1 1 TRAN,L 1 1 INTERNAL: ACRS 1 1 AEOD++OAB/~S P 2 2 AEOD/SPD/RRAB 1 1 CENTER 02 1 1 NRR/DE/EELB 1 1 /DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NRR/PMAS/IRCB-E 1 1 RES/DSIR/EIB 1 1 RGN4 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHY I G A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE KVKSTE! CONTACTTI IE DOC!:iIENTCONTROL DESk, ROOM PI-37 (EXT. 504-~OS3 ) TO FLIXIINATE)OL'R iAXILFROil DISTRIBU'I'IOY, LIS'I'S I'OR DOC!. 5 IEN'I'S 5'Ol,'ON" I'L'I:.D!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28
0 sl,
Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O. BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00913-JML/BAG/BE'ovember JAMES M. LEVINE 21, 1994 VICE PRESIDENT NUCLEAR PRODUCTION U. S. Nuclear Regulatory Commission ATIN: Document Control Desk Mail Station P1-37.
Washington, DC 20555
Dear-Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 (Ucense No. NPF&1)
Ucense Event Report 94<06%0 File: 9420-404 Attached please find Licensee Event Report. (LER)94-006 prepared and submitted pursuant to 10CFR50.73. This LER reports the identication of a condition that resulted in the unit being outside .the design basis of the plant. In accordance with 10CFR50.73(d), a copy of this LER is being forwarded to the Regional Acfministrator, NRC Region IV.
If you have any questions, please contact Burton A. Grabo, Section Leader, Nuclear Regulatory Affairs, at (602)'-393-6492.
Sincerely, JML/BAG/BE/pv Attachment cc: W. L Stewart (all with attachment)
L J. Callan K. E. Perkins K. E. Johnston INPO Records Center 94Y>0~0Y38 94YY~Y PDR ADDCK 05000528
'PDR
Ol I1'
LICENSEE EVENT REPORT (LER)
FACILITYNAME (1) DOCKET NUMBER (2) PAGE (3) 0 0 0 0 2 OF 0 8 Palo Verde Unit 1 5 5 8 1 ITLE (4)
S ra Pond Pum Flow Greater than Desi n Basis Calculation EVENT DATE 5 LER NUMBER 6 REPORT DATE 7 OTHER FACIUTIES INVOLVED 8 MONTH DAY SEQUENTIAL REVISION MONTH OAY FACILITYNAMES KET NUMBERS NUMBER NA 0 5 0 0 0 1 0 2 1 9 4 9, 4 0 0 6 NA 0' 0 0 0 OPERATING REPORT IS SUBMITTED PURSUANI'O THE REQUIREMENTS OF 10 CFR C (Check one or mora of tha folkrrring) (11)
MODE (9) 20.402(b) ~ 20.405(c) 50.73(a)(2)(iv) 73.71(b) 20.405(a)(1)Qi 50.38(c)(1) 50.73(a)(2)(v) 73.71(c)
LEVEL(10) 9 6 20.405(a) (1)(ii) 50.38(c)(2) 50.73(a) (2) (vii) OTHER (Speofy in Abstract 20.405(a) (1)(iii) SO.73(a)(2)g 50.73(a)(2)(viii)(A) below and in Text, NRC Form
- 20. 405(a) (1) (iv) X 50,73(a) (2) (ii) 50.73(a)(2)(VIIB(B) 366A) 20,405(a)(1) (V) 50.73(a)(2)(iii) 50.73(a)(2)(x)
UCENSEE CONTACT FOR THIS LER (1 2)
LEPHONE NUMBER Burton A. Grabo, Supervisor, Nuclear Regulatory Affairs EA CODE COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBED IN T)ES REPORT (1 3) 602393-6492 CAUSE MANUFAC- REPORTABLE MANUFAC- REPORTABLE;:.jg@
TURER TO NPRDS TURER SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY'EAR SUBMISSION YES 0f yes, complete EXPECTED SUBMISSION DATE) ouzel N I 400 ~ I~ ynam4olg shies regrI-Ipecac At approximately
~ law) o a 1305 MST on October 21, 1994, DATE (1 5)
Palo Verde Unit 1 was in Mode 1 (POWER OPERATIONS), when it was identified by Design Engineering personnel (utility, non-licensed) that the actual flow rates on the Unit 1 Spray Pond (SP) pumps may be exceeding design flow rates. This increased flow rate is due to'versized orifices in the Unit 1 SP return lines. The increased flow rate causes higher water losses -from the spray ponds. Therefore, inventory may be depleted faster than the design analysis.
Unit 1 has established administrative controls to counter this condition until the correct orifices are installed. The work is being scheduled for the next refueling outage (1R5') in April,.
1995. Also, pending Technical Specification (TS) and Updated Final Safety Analysis Report (UFSAR) amendments to reduce the SP inventory from 27 to 26 days may permit lifting some of the administrative controls or provide additional margin.
There have been no previously similar events reported. pursuant to 10CFR50.73.
II LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
'ACILITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR >~ SEQUENTIAL ";?>>,': EVISIO NUMBER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 4 ,0 0 6 0 2 OF 0 8 I. DESCRIPTION OF WH'AT OCCURRED:
A. Initial Conditions:
At approximately 1305 MST on October 21, 1994, PVNGS Unit 1 was in Mode 1 (POWER OPERATIONS) at 98'. power.
B. Reportable Event
Description:
Event Classification: Any event or condition that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded; or that resulted in the nuclear power plant being:
In a condition that was outside the design basis of the plant.
At approximately 1305 MST on October 21, 1994, Design Engineering personnel (utility, non-licensed) identified that the actual flow rates on the Unit 1 Spray Pond (SP) pumps may be exceeding design flow rates if instrument uncertainties are included. The increased flow rate causes higher water losses from the spray ponds. Therefore, inventory may be depleted faster than the design basis of 27 days. The increased flow rate is due to orifices in the SP return lines'eing oversized.
The Ultimate Heat Sink (UHS) at PVNGS is'he two SPs.
The Essential Spray Pond System (ESPS) consists of pumps, piping and heat exchangers. Water, taken from the SPs, removes heat from various safety-related components via the heat exchangers and dissipates this heat load to the atmosphere via the sprays. The UHS in conjunction with any one train of the ESPS, provides for 100% of the heat removal from the reactor core, and other auxiliaries required for safe shutdown during normal, forced or design basis accident related shutdowns. The combined inventory of both the SPs is required for long term cooldown, that is, post Loss of Coolant Accident (LOCA).
ig)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR g(j~ SEQUENTIAL $45~ EVISIO NUMBER P~< NUMBER, Palo Verde Unit 1 '.I >cj<
0 5 0 0 0 5 2 8 9 4 0 0 6 0 3 OF 0 8 EXT Each return header of the ESPS (two per Unit) is provided with an orifice. The purpose of the orifices is to ensure that the SP pumps operate at their design pressure and flow rate.
To meet the Updated Final Safety Analysis Report's (UFSAR) requirement that the ESPS operate at a higher pressure than the Essential Cooling Water System (ECWS),
the orifices were located downstream of the Essential Water (EW) heat exchangers. The orifice plates were fabricated, installed under a design change, and the system was tested in September 20, 1983.
Since September 20, 1983, potential opportunities were missed to identify that the wrong-sized orifices were installed in Unit 1. The close out review of the initial Design Change Package (DCP) did not identify the oversized orifices. Also, Surveillance Testing (ST),
performance monitoring, and self-assessments on the Design Basis Project for Service Water did not identify the oversized orifices. It was not until October 28, 1993, while replacing leaking orifice gaskets that it was identified that the wrong sized orifices were installed in Unit 1. Based on surveillance test flow data, this condition does not exist in Units 2 and 3.
A 10CFR50 59 ~ evaluation was performed on October 28, 1993, for the identified condition. The. evaluation was based on a SP flow rate of 17,950 gpm. The evaluation determined that the TS required volume in the SPs will provide an inventory for 26.2 days versus 27 days as currently stated in the UFSAR. Also, the calculation showed that the large bore sized orifices and the reduction of a nominal one day in water inventory will have no significant impact on the originally defined design criteria and safety analysis.
Unit 1 indicated flow rates, plus an allowance for the appropriate instrument uncertainty, may result in an actual flow rate greater than the 17,950 gpm previously Used.
i+i
~ '
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACIUTY NAME DOCKET NUMBER LER NUMBER PAGE YEAR SEQUENTIAL:~g>< EVlSIO NUMBER ~Sj%'UMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 4 0 0 6 0 40F 0 8 EXT On October 21, 1994, another 10CFRS0.59 evaluation (considering instrument uncertainties) was performed on the Unit 1 SP orifices based on the revised calculation.
In this evaluation it'was determined that certain administrative controls needed to be placed on Unit 1 until that time when the orifices are replaced to conform to the original design. With these administrative controls in place the analysis has shown that the water inventory requirement of 27 days will be satisfied.
There were no component or system failures, nor any structures, systems or components were inoperable at the start of the event that contributed to the event. No safety system activation occurred and none were necessary.
II. ASSESSMENT OF THE SAFETY CONSEQUENCES AND IMPLICATIONS OF THIS EVENT:
The primary purpose of the orifice plates is to (1) provide adequate backpressure to ensure that the ESPS operates at a higher pressure than the ECWS, (2) ensure that the ESPS flow is adequate from a thermal performance standpoint and (3) limit the ESPS flow to a value such that the water inventory of the UHS is adequate. Per the UFSAR a 27 day water inventory is available for post LOCA cooldown (Currently, License Document Change Requests are in the review cycle to change the 27 days to 26 days in the UFSAR and TS Bases due to the as built ESPS having a higher flow rate than originally assumed in the water supply calculation).
The impact of a larger bore in the orifice on the system function follows.
as it pertains to its to date operation is as (1) A hydraulic analysis of the SP system concluded that, the maximum predicted flow for the ESPS is 16,954 gpm.
II i+[ I' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILE NAME DOCKET NUMBER LER NUMBER PAGE YEAR:,.j?':). SEOUENTIAL EVISIO NUMBER NUMBER Palo Verde Unit 1 0.5 0 0 0 5 2 8 9 4 0,0 6 0 5oF0'8 EXT The calculation demonstrates that for flows up to this value, the predicted pressures in the ESPS will be higher than the predicted pressures in the ECWS at the EW heat exchanger (this is consistent with the UFSAR). For flows greater than 16,954 gpm the calculation indicates that this criterion (of ESPS operating at a higher pressure than ECWS) should be verified by field measurements. An Engineering, Evaluation Request (EER) performed on January 1, 1988, documented (from data collected in the field) that an ESPS to ECWS differential of 12 psi for the A Train and 12.5 psi for the B Train at the EW heat exchanger existed. Therefore, the criterion of maintaining the ESPS at a higher pressure than ECWS has been met even with the larger bore sized orifices.
(2) The SP/EW system thermal performance Design Bases Analysis concludes that an ESPS flow of 16,000 gpm is required for safe shutdown after a design basis LOCA.
The system hydraulic calculation demonstrates that the minimum predicted flow of any ESPS train will exceed the 16,000 gpm requirement. A larger bore size orifice results in higher flows. Therefore, the minimum flow requirement from a thermal standpoint has been met.
(3) Per Regulatory Guide (RG) 1.27, Rev 2, Ultimate Heat Sink for Nuclear Power Plants, Regulatory Position C.1, The ultimate heat sink should be capable of providing sufficient cooling for at least 30 days.
Furthermore it also states that, 2 cooling capaci,ty of less than 30 days may be acceptable ifit can be demonstrated that replenishment or use of an alternate water supply can be effected to assure the continuous capability of the sink to perform it's safety functions, taking into account the availabili ty of replenishment equipment and limi tations that may be imposed on "freedom of movement" following an accident or the occurrence of severe natural phenomena.
~I II C
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR SEQUENTIAI.,'-"I-'UMBER EVISIO NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 4 0 0 6 0 6oFO 8 EXT Per earlier UFSAR submittals to the NRC, procedures have been put in place and actions taken to ensure makeup is made available to the UHS prior to the depletion of the available inventory of 27 days to meet the RG requirements. These actions/provisions are discussed in Emergency Plan Implementing Procedure (EPIP) -56, VZ timate Heat Sink Emergency Water Supply. One of the provisions is to have a well functional within 15 days from the start of an accident. The NRC in their review (as documented in SER Supplement 3, dated September 1982, Scca 2.4.4.2) found the actions/provisions acceptable and concluded that PVNGS 1-3 meet the guidelines of RG 1.27 and the requirements of General Design Criteria (GDC) 44.
The water losses from an operating spray pond are comprised of four components: (i) evaporation losses (because of the spray action), (ii) drift losses (because of the wind), (iii) surface evaporation losses (losses from the unsprayed area of the pond), and (iv) air to water heat transfer losses (occurring when the air temperature is higher than the water temperature) with (i) and (ii) being the major components. Since the system is operated normally with all valves wide open, a larger bore sized orifice results in a higher total system flow. The larger flow in turn results in a higher spray height which results in higher water losses through drift and evaporation depleting 'the available inventory sooner.
Thus the only system function that has been affected by the incorrect orifices is the available water inventory in the UHS. An evaluation has been conducted using the same methodology previously used in calculations with the following three input exceptions: (i) a Spent Fuel Pool (SFP) heat load of 9.0 E6 BTU/Hr, which is less than the bounding heat load, but greater than the current heat load, based on the actual SFP inventory, (ii) a SP pump flow of 18,400 gpm versus the original 17,950 gpm and (iii) an initial SP temperature of 89'F versus the previous 97'F have been used in this analysis.
4I 4>
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR SEQUENTIAL EVISIO kk NUMBER NUMBER Palo Verde Unit 1
- 0 5' 0 0 5 2 8 '-.9 4 0 0 6 0,7 OF 0 8 EXT The input exceptions used bound Unit 1 operations to date. As stated earlier, all other inputs to this evaluation are identical to the current design bases analysis and would be 'collectively more conservative than any maximum actuals experienced.
The results of this evaluation indicate that even with the higher flow rate, the water inventory in the UHS would have always been in excess of 25 days. This inventory would have thus still provided adequate margin between the time that a makeup source would have been made available and the depletion of the SP inventory.
The continuous cooling capability as required by the RG and the safety design bases of the system would have still been met (albeit with a slightly reduced margin) with the higher flows.
The event did not result in any challenges to the fission product barriers or result in any releases of radioactive materials. Therefore, there were no adverse safety consequences or implications as a result of this event.
This event did not adversely affect the safe operation of the plant or the health and safety of the public.
III. CORRECTIVE ACTION:
A. Immediate:
On October 21, 1994, a 10CFR50.59 evaluation was completed and presented to the Plant Review Board (PRB) for review. The 50.59 evaluation placed three administrative restrictions on Unit 1 SP operations. The restrictions are as follows:
~ A maximum actual spray pond temperature of 89'F.
~ An actual minimum spray pond usable level of 12'5." of water in each of the ponds.
~ A SFP heat load less than or equal to 9.0 E6 BTU/HR.
0 Ql t
C
LICENSEE'EVENT REPORT (LER) TEXT CONTINUATION FACILITYNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL EVISIO NUMBER NUMBER Palo Verde unit 1 0 5 0 0 0 5, 2 8 9 4 0 0 6 0 8 oF0 8 EXT With these restrictions in place the calculation has shown that the water inventory requirement of 27 days will be satisfied. Instrument loop uncertainties have been factored into the implementation of. these restrictions.
B. Action to Prevent Recurrence:
APS is reviewing its ability to replace these orifices during the fifth refueling outage (1R5) of Unit 1. The fifth refueling outage is scheduled to begin on April 1, 1995. If both orifices are unable to be replaced during the 1R5 refueling outage, the work will be completed at the next available outage of sufficient duration.
IV. PREVIOUS SIMILAR EVENTS:
There have been no similar events of this type of failure reported pursuant to 10CFR50.73.
V. ADDITIONAL INFORMATION:
Further evaluation indicated that though the specified maximum flow rate will ensure that the water inventory requirement is satisfied, it will be necessary to impose an additional control of throttling the SP flow rate back to a lower value post LOCA during long-term cooldown to ensure that when the usable inventory in the ponds is depleted, the SP pump Net Positive Suction Head (NPSH) requirements will still be met.
An action to reduce SP system flow to an indicated value of 17,000 gpm has been added to the LOCA EOPs to ensure that the SP pump NPSH requirements will be met. This change to the LOCA EOP will only be in effect until 'the Unit 1 SP orifices are changed out.
This action will further ensure the 27 day requirement is maintained.
II II s
I