|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
[Table view] |
Text
CATEGORY 3 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9701020016 DOC.DATE: 96/12/17 NOTARIZED: NO FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi DOCKET I 05000528 AUTH. NAME AUTHOR AFFILIATION MARKS,D.G. Arizona Public Service Co. (formerly Arizona Nuclear Power OVERBECK,G.R. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 96-007-00:on 961119,surveillance test deficiencies were found during GL 96-01 review leading to TS 3.0.3 entries.
Caused by increase in scope of required testing. Supplement will be submitted.W/961217 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. E NOTES:STANDARDIZED PLANT 05000528 G RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD4-2 PD 1 1 CLIFFORD,J 1 1 INTERNAL: ACRS 1 1 AEOD S 2 2 AEOD/SPD/RRAB 2 2 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 D RES/DET/EIB 1 1 RGN4 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC MURPHYiG.A 1 1 NOAC POOREgW. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 N
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON', NEED!
FULL TEXT CONVERSZON REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26
II 41 I
I
Comotitmoot. /nnorotloo. Energy.
Gregg R. Overbeck Mail Station 7602 Palo Verde Nuclear Vice President TEL 602/393-5148 P.O. Box 52034 Generating Station Nuclear Production FAX 602/393-6077 'Phoenix, AZ 85072-2034 192-00984-GRO/DGM/KR December 17, 1996 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station P1-37 Washington, D.C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS).
Units1,2, and 3 Docket Nos. STN 50-528, 50-529, and 50430 License Nos. NPF41, NPF-51, and NPF-74 Licensee Event Report 9640740 Attached please find Licensee Event Report (LER) 96407-00 prepared and submitted pursuant to 10CFR50.73. This LER reports Technical Specifications,3.0.3 entries due to
.surveillance. test deficiencies found during the Generic Letter 9641, "Testing of Safety Related Logic Circuits" review. In accordance with 10CFR50.73(d), a copy of this LER is being forwarded to the Regional Administrator, NRC Region IV. If you have any questions, please contact Daniel G. Marks, Section Leader,'Nuclear Regulatory Affairs, at (602) 393-6492.
Sincerely, GRO/DGM/KR/kr Attachment cc: L. J. Callan (all with attachment)
K E. Perkins K. E. Johnston INPO Records Center u040J<
970i0200i6 96i2i7 05000528 PDR ADOCK S PDR
Ol LICENSEE EVENT REPORT (LER)
DOCKET NUMBER (2) PAGE (3)
ACIUTYNAME(I )
0 5 0 0 0 5 2 8 1OFO 8 Palo Verde Unit 1 ITLE (4)
Surveillance Test Deficiencies Found Durin GL 96-01 Review Lead to TS 3.0.3 Entries LER NUMBER 6 REPORT DATE OTHER FACIUTIES INVOLVED 8 EVENT DATE 6 REVISCN MONTH FACIIITYNAMES T NUMBERS MONTH DAY YEAR YEAR NUMBER 0 5 0 0 0 5 2 9 1 9 9 6 9 6 0 0 7 0 0 1 2 1 7 9 6 05000530 REPORT IS SUBMITTED PURSUANT TO THE RECUbtEMENTB oF 10 cFR C (cbears one or more at tbe ooaorrrng) (11) 20.402(b) 20<<5(c) 5073(a)(2)(n) 73.71(b) 20.45(a)(1)Qi 5(t38(c)(1 ) 50.73(a)(2)(r) 73.71(c) 5(t38(c)(2) 50.73(a)(2)(i4r) OTHER (SpecEY in Abstract 20,45(a)(1)(ri)
LEvEL(to) 1 p p 5073(aN2)(r) 5(L73(a)(2) Y)(A) beknii and In TrarL NRC Form 20.45(a)(1)(ib) 20.45(a)(1)(n) 50.73(a)(2Krr) 5073(a)(2)(riaNO 20 405(a)(t)(r) 5073(a)(2K~) 50.73(a)(2)(r)
UCEN SEE CONTACT FOR THIS LER (1 2)
E NUMBER E
Daniel G. Marks, Section Leader, Nuclear Regulatory Affairs - 6 4 9 2 6 0 2 3 9 3 COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBED IN TI8S REPORT (13)
MANUFAC- REPORTABLE 'ANUFAC. REPORTABLE ~,, ra nt TURER TO NPRDS TURER TO NPRDS SUPPLEMENTAL REPORT EXPECTED (I4)
~
SUBMISSCN DATE (I 5)
TRACT (Umit to 1400 spaces, la, apprradmateIY fiiieen sbryle.space lines) (1 8)
On November 19, 1996, at approximately 1125 MST, Palo Verde Units 2 and 3 were in Mode 1 (POWER OPERATION), when Control Room personnel entered Technical Specification Limiting Condition foz Operation (TS LCO) 3.0.3 due to noncompliance with the operability requirements of TS LCO 3.3.2. Control Room personnel invoked the provisions of TS Surveillance Requirement (SR) 4.0.3 to allow up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the missed surveillance. The surveillance was satisfactorily completed within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Control Room personnel exited TS LCO 3.0.3 at approximately 1921 MST on November 19, 1996.
The Unit 1 suzveillances had been completed within the required surveillance interval during the recent refueling outage. On December 4, 1996, at approximately 1315 MST, Palo Verde Units 1, 2, and 3 were in Mode 1, when Control Room personnel entered TS LCO 3.0.3 due to noncompliance with the operability requirements of TS LCO 3.3.1. Control Room personnel invoked the provisions of TS SR 4.0.3. The surveillance was satisfactorily completed within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Control Room personnel exited TS LCO 3.0.3 by 0056 MST on December 5, 1996 in the three units.
An investigation team performing the requested. actions zel'ated to Generic Letter (GL) 96-01, "Testing of Safety Related Logic Circuits" concluded that in both cases the surveillance procedures did not meet the TS testing requirements. Similar deficiencies discovered during the ongoing GL 96-01 review of safety systems will be included in a supplement to this LER.
There have been no .previous similar events reported pursuant to 10CFR50.73.
t LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AClulYNAME DOCKET NUMBER LER NUMBER PAGE YEAR SEOUENllAL RENQO NUMBER 'UMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 6 0 0 7 0 0 0 2 of08 1 ~ REPORTING REQUIREMENT:
This LER 529/96-007-00 is being written to report events that resulted in a condition prohibited by the plant's Technical Specifications (TS) as specified in 10 CFR 50.73(a)(2)(i)(B).
Specifi.cally, at approximately 1125 MST on November 19, 1996, Palo Verde Units 2 and 3 were in Mode 1 (POWER OPERATION), operating at approximately 100 percent power when Control Room personnel (utility-licensed operators) declared both trains of Auxiliary Feedwater (AFW) (BA) Engineered Safety Features Actuation System (ESFAS) (JE) instrumentation (AFAS-1 and AFAS-2) inoperable due to exceeding the specified surveillance interval including the maximum allowable extension of 25 percent as specified in TS Surveillance Requirement (SR) 4.0.2, and entered TS Limiting Condition for Operation (LCO) 3.0.3. Control Room personnel invoked the provisions of TS SR 4.0.3 to allow up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the missed surveillance prior to commencing a. plant shutdown to comply with TS LCO 3.0.3. The surveillance was satisfactorily completed within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Control Room personnel exited TS LCO 3.0.3 at approximately 1921 MST on November 19, 1996. The Unit 1 surveillances 'had been completed within the required surveillance interval during the recent refueling outage.
Similarly, at approximately 1315 MST on December 4, 1996, Palo Verde Uni.ts 1, 2, and 3 were in Mode 1, operating at approximately 100 percent power when Control Room personnel declared the four channels of the reactor protection system (RPS) (JC) reactor trip breakers inoperable due to exceeding the maximum allowable surveillance interval, and entered TS LCO 3.0.3. Control Room personnel invoked the provisions of TS SR 4.0.3 The ~
surveillance was satisfactorily completed within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Control Room personnel exited TS LCO 3.0 ' by 0056 MST on December 5, 1996 in the three units.
- 2. EVENT DESCRIPTION:
Prior to the events, on January 10, 1996, NRC issued Generi.c Letter No.
96-01 (GL 96-01), "Testing of Safety-related Logic Circuits, " which zequested that all addressees compare electrical schematic drawings and logic diagrams for the reactor protection system, emergency diesel generator (EK) load shedding and sequencing, and actuation logic for the ESF systems against plant surveillance test procedures to ensure that all portions of the logic circuitry, including the parallel logi.c,, i.ntezlocks, bypasses, and inhibit circuits, aze adequately covered in the surveillance procedures to fulfill the TS requirements. An APS engineering team (other
LICENSEE EVENT REPORT (LER): TEXT CONTINUATION ACUlYNAME DOCKET NUMBER LER NUMBER PAGE YEAR ., RBASO NUMBER NUMBER Palo Verde Unit 1 05'000528 9 6 0 0 7 0 0 0 3 Cf 0 8 utility personnel) was created to perform the requested action specified in GL 96-01.
A. NOVEMBER 19, 1996 TS LCO 3.0.3 ENTRY An additional letter was issued on March 27, 1996 from the NRC to the Nuclear Energy Institute (NEI) summarizing the results of a workshop regarding GL 96-01. The workshop provided an opportunity for the NRC to clarify their position and to respond to industry concerns regarding GL 96-01. Specifically related to the November 19th event was a response to Question 32 located in enclosure 3 of the letter. Question 32 was stated as follows:
Frequently, an ESF signal is used to preclude inadvertent operator action (for instance, pzecludes an operator from stopping a SI pump until SI is reset). Do these seal-in contacts need to be tested if the failure of those seal in contacts do not affect the safety function of the system or component? (and if they are not referenced in TS).
Answer 32 of the letter was stated as follows:
IEEE 279[-1971, "IEEE Standard Criteria for Protection Systems foz Nuclear Power Generating Stations"], Section 4.16 requires that protective functions go to completion once initiated and seal-in circuits are generally provided to meet this requirement.
Therefore, seal-in circuits perform a safety function and should be tested as part of the ESF logic.
During the GL 96-01 review process, on November 6, 1996, APS Engineering personnel (other utility personnel) determined that this clarification provided the basis necessary to increase the scope of TS equipment associated with the ESFAS instrumentation and that the ESFAS lockout relays were not being tested on a quarterly basis as required by TS SR 4.3.2.1, ESFAS instrumentation. An evaluation was initiated in accordance with the APS Corrective Action Program.
At, Palo Verde, lockout relays aze designed to seal in actuations to ensure that they proceed to completion even if the initiating condition clears.
This is a requirement of IEEE-279-1971, section 4.16, "Completion of Protective Action Once It Ks Initiated." The ESFAS lockout relays are tested every 18 months. The Plant Protection System (PPS) (JC) also uses lockout relays on each of the four initiation paths for every ESFAS function except AFAS-1 and AFAS-2. When an initiation path is tripped, the trip condition must be cleared and a keylocked reset pushbutton
0 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ACUITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR REWSK)
NUMBER Palo Verde Unit 1 0500052896 0 0 7 0 0 0 4of0 8 pressed to reset the initiation path. The PPS lockout relays are tested every quarter. The initial condition under evaluation was not considered an OPERABILITY concern because the redundant lockout relays in the PPS system were being tested quarterly. Further evaluation was pursued to verify that the testing of the PPS lockout relays met the necessary requirements.
As previously stated, AFAS-1 and AFAS-2 do not have PPS lockout relays in order to prevent reactor coolant system (AB) overcooling or steam generator (SG). (AB) overfilling during an AFAS actuation. The AFAS-1 and AFAS-2 provide essential auxiliary feedwater to intact SG(s) following a main steam line (SB) break or loss of main feedwater (SJ) . If the difference between SG pressures is greater than 1B5 psi, the system will not feed the low pressure SG. AFAS-1 and AFAS-2 are unique in that the actuation signals are either "in" or "reset" after the actuation signal clears. When SG level increases to 40.B percent, the valves which feed the SG will close unless Control Room personnel have overridden them. All other ESFAS signals must be reset manually after the parameter returns to within normal values to operate the equipment or the equipment must be manually overridden by Control Room personnel.
On November 19, 1996, APS Engineering personnel determined that the quarterly surveillances for AFAS-1 and AFAS-2 lockout relays were not being satisfied since there were no redundant lockout relays for AFAS in the PPS system. It was also determined that only Units 2 and 3 were affected because the Unit 1 surveillances were completed within the required surveillance interval during the recent refueling outage. APS Engineering personnel informed Control Room personnel in both Units 2 and 3, and at approximately 1125 MST on November 19, 1996, Control Room personnel declared both'rains of AFW ESFAS instrumentation inoperable due to exceeding the specified surveillance interval of TS SR 4.3.2.1 including the maximum allowable extension of 25 percent as specified in TS SR 4.0.2, and entered TS LCO 3.0.3. Control Room personnel invoked the provisions of TS SR 4.0.3 to allow up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the missed surveillance prior to commencing a plant shutdown to comply with TS LCO 3.0.3. The AFAS-1 and AFAS-2 lockout relays were tested satisfactorily under a corrective maintenance work document. The Plant Review Board approved the test results crediting a satisfactory completion of SR 4 '.2.1 within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Control Room personnel exited TS LCO 3.0.3 at approximately 1921 MST on November 19, 1996. There were no safety system responses and none were necessary.
4! Il
~I
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER LER NUMBER PAGE YEAR Palo Verde Unit 1 0 5 0 0 0'5 2 8 9 6 0 0 7 0 '0 0 5of0 8 B. DECEMBER 4, 1996 TS LCO 3.0.3 ENTRY During the GL 96-01 review process, on December 4, 1996, APS Engineering personnel determined that an approved surveillance procedure may not independently verify the reactor trip breaker undervoltage and shunt trips as specified in TS SR 4.3.1.1. The surveillance procedure testing method ensured that each of the trip coils of the two respective trip circuits successfully trip the reactor trip breakers. However, the testing method did not independently verify that both the undezvoltage and shunt trip initiating circuit contacts change state. The contacts are designed to enexgize the shunt trip and de-energize the undexvoltage coils to trip the reactor trip breakers.
On December 4, 1996, APS Engineering personnel determined that the 18-month suzveillances for the reactor trip breakers, were not being satisfied since the surveillance test did not demonstrate proper operation of the entire logic for both the undervoltage and shunt trips. APS Engineering personnel informed Control Room personnel in the three units, and .at approximately 1315 MST on December 4, 1996, Control 'Room personnel entered TS LCO 3.0.3 due to noncompliance with TS LCO 3.3.1, Reactor Protection Instrumentation. Control Room personnel invoked the, provisions of TS SR 4.0.3 to allow up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the missed surveillance prior to commencing a plant shutdown to comply with TS LCO 3.0 '. The reactor trip breakers were tested satisfactorily under a corrective maintenance work document. The Plant Review Board approved the test results crediting a satisfactory completion of SR 4.3.1.1 within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Control Room personnel exited TS LCO 3.0.3 by 0056 MST on Decembex 5, 1996 in the thzee units. There were no safety system responses and none were necessary.
3 ~ ASSESSMENT OF THE SAFETY CONSEQUENCES AND IMPLICATIONS OF THIS EVENT:
The ESFAS lockout relays were tested in Units 1, 2, and 3 and no failures were found. A review of corrective maintenance history revealed only one instance where a lockout relay had failed (Unit 1 in 1990). The relay would not energize following testing. The relays are designed as fail safe, therefore, no failures have occurred that would have prevented an ESF actuation lock-in. If an ESFAS signal cleared pxior to completing the actuation, and if a lockout relay failed to ensure that the signal is not automatically reset once it was initiated, some of the affected safety related equipment would stop movement to the actuated position, and the sequencer would stop sequencing. If the ESFAS signal returned, the same equipment would resume to its actuated position, and the sequencer would xesequence.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ACIUTYNAME DOCKET NUMBER LER NUMBER PAGE YEAR Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 6 0 0 7 0 0 0 6of0 8 The reactor trip breakers'ndervoltage and shunt trip initiating circuits for the RPS, Supplementary Protection System (SPS) and the manual trip were tested in Units 1, 2, and 3 and no failures were found. The testing deficiency could not have resulted in a loss of safety function without an additional failure that would have been detectable by existing test procedures. A failure of one of the redundant trip initiating circuits in each channel could have been present and remained undetected as long as the other redundant trip circuit remained operable to allow the reactor trip breaker to function properly during the quarterly channel functional test. If all of the reactor trip breakers were assumed to have one of the redundant, trip initiating devices fail, a failure of the remaining trip device in two of the four reactor trip breakers would be required for a 1'oss of safety function.
These events did not adversely affect the safe operation of the plant or health and safety of the public. The events did not result in any challenges to the fission product barriers or results in any releases of radioactive materials. Therefore, there were no adverse safety consequences or implications as a result of the events.
CAUSE OF THE EVENT:
Independent investigations of these events are being conducted in accordance with the APS Corrective Action Program. As part of the investigations, a determination of the cause of the events has been performed.
The surveillance testing procedures for RPS and ESFAS instrumentation were developed based on requirements specified in the Palo Verde TS, corresponding TS bases, IEEE 279-1971, and IEEE 338-1975, "IEEE Standard Criteria for the Periodic Testing of Nuclear Power Generating Station Class 1E Power and Protection Systems". These standards require system testing from sensor to actuated devices.
The seal-in function of the lockout relays was not included in the testing program because it was not in the signal'ath from the sensor to the actuated device. APS'osition has been that the lockout relays had no safety function, and therefore were not TS equipment. The proper operation of the lockout relay was verified every 18 months during shutdown under a preventative maintenance (PM) program. Since the lockout relays were not included i.n the TS surveillance testing for the ESF automatic actuation logic, the refueling interval was considered sufficient to maintain the reliability of the relays. Information provided by the NRC as clarification to GL 96-01 stated that the seal-in circuit performs a safety-related function and should be included in the ESF logic testing.
II C'
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AQUTYNAME DOCKET NUMBER LER NUMBER PAGE YEAR SEQUENTlAL,, REVISO NUMBER . NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 6 0 0 7 0 0 0 7 of 0 8 Based on this clarification, APS Engineering personnel determined that the lockout relays should be considered part of the ESF automatic actuation logic, and therefore were required to be tested in accordance with TS LCO 3.3.2, ESFAS instrumentation. The cause of the event was attributed to an increase in the scope of required testing following clarification provided by the NRC related to GL 96-01 (SALP Cause Code X: Other).
Current Palo .Verde TS requize independent verification of the undervoltage and shunt trips for the reactor trip breakers, not the SPS, RPS initiating logic, or the manual trip. There is no specific TS requirement for independent testing of redundant parallel circuits within a channel.
Therefore, it would not have been obvious to the procedure writer that the surveillance test should encompass the entire actuating circuit, from the initiating contacts down to the trip coils, not gust for the reactor trip breakers. Based on the intent of GL 96-01 and the potential for incomplete testing of safety systems as presented by GL 96-01, APS Engineering personnel took the conservative position that the surveillance test did not demonstrate proper operation of the entire logic for both the undervoltage and shunt trips (SALP Cause Code X: Other).
A previous review of Information Notice (IN) 93-15, "Inadequate Logic Testing of Safety-related Circuits" performed by APS personnel on June 3, 1993, provided an opportunity to discover the testing deficiency. IN 93-15 discusses inadequate testing of the trip functions at a Westinghouse plant.
There are significant differences between the Westinghouse and ABB-Combustion Engineering (ABB-CE) RPS designs. In addition, the Westinghouse TS have specific surveillances to test both the automatic contacts and manual trip switch contacts for the undervoltage and shunt trips. The APS review of IN 93-15 determined that the Palo Verde design does not use an automatic shunt trip relay, and therefore, the Palo Verde design was different than the design described in the IN. The review concluded that IN 93-15 did not apply to Palo Verde.
No unusual characteristics of the work location (e.g., noise, heat, poor lighting) directly contributed to these events. There were. no personnel or procedural errors which contributed to these events.
- 5. STRUCTURES SYSTEMS, OR COMPONENTS INFORMATION:
Although the RPS and ESFAS instrumentation was declared inoperable for a lapsed surveillance requirement, there were no component or system failures involved in these events. No failures of components with multiple functions were involved. No failures that rendered a train of a safety system inoperable were involved.
0 LICENSEE EVENT REPORT (LER) TEXT CONTINUATiON ACIUTYNAME DOCKET NUMBER LER NUMBER PAGE YEAR RE%GO NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 6 0 0 7 0 '0 0 8of0 8
- 6. CORRECTIVE ACTIONS TO PREVENT RECURRENCE:
Independent investigations of these events are being conducted in accordance with the APS Corrective Action Program. Actions to prevent recurrence are being developed based upon the results of the investigations and will be tracked to completion under the PVNGS Commitment. Action Tracking System (CATS). These actions include modifying surveillance test procedures as necessary to comply with the Technical Specifications.
The GL 96-01 review of the protective systems will continue to determine if other testing discrepancies exist. If other discrepancies are discovered, or if information is developed which would significantly change the readers'nderstanding of the events, a supplement will be submitted.
- 7. PREVIOUS SIMILAR EVENTS:
Although there have been previous events reported pursuant to 10CFR50.73 within the last three years for missing TS surveil'lance requirements, the causes discussed in the previous events have not been similar to these events. Therefore, the corrective actions of the previous events would not have prevented these events.
4l gi