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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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AC CK1Z RATED Dl FTKBUTION DZMONSTRKT10N SYSTK-y REGULAT . INFORMATION DISTRIBUTIOh,SYSTEM (RIDS)
ACCESSION NBR':8908300230 . DOC'DATE: 89/08/22 NOTARIZED: NO DOCKET 4 FACZL:STN-50-530 Palo Verde Nuclear Station, Unit 3, -Arizona Publi 05000530 AUTH. NAME AUTHOR AFFILIATION SHRIVER,T.D.. Arizona Public Service Co. (formerly Arizona Nuclear Power HAYNES,J.G. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 89-009-00:on 890728,inadvertent Train A fuel bldg essential ventilation actuation signal:initiated.
W/8 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR Q ENCL TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
~ SIZE:
NOTES:Standardized plant. 05000530 RECIPIENT COPIES RECIPIENT COPIES ZD CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 DAVIS P M. 1 1 INTERNAL: ACRS MZCHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLZE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 P RPB 10 2 2 NUDOCS-ABSTRACT 1 1 REG F LE 02 1 1 RES/DSIR/EZB 1 1 R E 01 1 1 R
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Arizona Public Service Company P.O, BOX 53999 PHOENIX, ARIZONA 85072-3999 192-00510-JGH/TDS/DAO August 22, 1989 U. S. Nuclear Regulatory Commission NRC Document Control Desk Washington, D;C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 3 Docket No. STN 50-530 (License No. NPF-74)
Licensee Event Report 89-009-00 File: 89-020-404 Attached please find Licensee Event Report (LER) No. 89-009-00 prepared and submitted pursuant to IOCFR 50.73. In accordance with IOCFR 50.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V office.
If you have any questions, please contact T. D. Shriver, Compliance Hanager at (602) 393-2521.
Very trul yours, J. G. Haynes Vice President Nuclear Production JGH/TDS/DAJ/kj Attachment cc: W. F.. Conway (all w/a)
D. B. Karner E. E. Van Brunt, Jr.
J. B. Hartin T. J. Polich H. J. Davis A. C. Gehr INPO Records Center 8908300~30 @908~@
ADQCK 05000530 S PNU
If NRC Form 344 0 UA. NUCLEAR REOULATORY COEMCISSION (SO)3)
APPROVED DMS NO. 3)%04)04 UCENSEE EVENT REPORT LER) EXPIRES: SISIISS FACILITY NAME (II DOCKET NUMBER (1) PA TITLE (CI Palo Verde Unit 3 0 s o o 0 530ioF07 Inadvertent Fuel Building Essential Ventilation ESF Actuation EVENT DATE (5) LER NUMBER (SI REPORT DATE (7I OTHER FACILITIES INVOLVED ISI MONTH DAY YEAR YEAR 4 E 0 O'E NT I A L REVS~ MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(S)
NUM4ER y.r3 NUMBER N/A i) 0 5 0 0 0 0 728 8 9 8 9 009 000 82 28 9 N/A 0 5 0 0 0 OPE RATINO THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR )I (Cool onr or moto ol thr Iollornnp) (III MODE ( ~ I 6 20A02(41 20A05(cl 50.73(o) (2) (h) 73.71(41 POWER 20A05( ~ l(1)(il 50.34(cl(ll 50.73(o)(2)hl 73.71(cl LEVEL p p p 20.405(o l)1) iii) 50,34 (c) (2) 50.73 (I I l2) (r W I 'OTHER (Sorrily In Aptttrtt priory onp In Tort, IYIIC Form 20A05( ~ llll(nil 50.73( ~ I(2) (il 50.73( ~ ) (2) (rii (Al SSSAI 20A05(x )(ll(h) 50.73(ol(1) (iil 50.73(o)(2l(riSIIS)
IPPWs. gr'L4@o.: 20A05( ~ )(1)(rl 50.73(o) (2)(iiil 50.73 (4) (2) (xl LICENSEE CONTACT FOR THIS LER (11)
NAME TELEPHONE NUMBER AREA CODE Timothy D. Shriver, Compliance Manager 6 02 39 3- 25 21 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC REPORTABLE MANUFAC. EPORTABLE TURER TO NPRDS COMPONENT ympm, TVRER X V I BK R G1 84 SUPPLEMENTAL REPORT EXPECTED (ICI MONTH DAY YEAR EXPECTED SU 5 M I SS ION YES Ill yH, complot ~ EXPECTED StlpotISSIOII DATEI DATE (15) 1 1 3 0 8 9 ABBTRAc'7 I(,imit to tctx) IprcrL I r., rpproximrtrly Attrrn tinplr corer typrwrittrn lmrd (14)
At approximately 0430 MST .on July 28, 1989, Palo Verde Unit 3 was in Mode 6 (REFUELING) with the Reactor Coolant System. at ambient temperature and core reloading in progress when an inadvertent Train HAH Fuel Building Essential Ventilation Actuation Signal (FBEVAS) was initiated on the Balance of Plant Engineered Safety Feature Actuation System. The Train '"A" FBEVAS resulted in the designed cross-trips of Train "BR FBEVAS and Train "AR and RB" Control Room Essential Filtration Actuation Signals (CREFAS). The actuati.on occurred when a Maintenance individual reset the Spent, Fuel Pool Area Radiation. Monitor (RU-31) Remote Indicating and Control Unit without ensuring that the channel was placed in "bypass." Following the actuation, Control Room Essential Ventilation System Train "BH fan tripped. All other components operated as designed. Radiation Protection personnel verified .that no actual high radiation levels existed in the area of the Spent Fuel Pool Area Monitor.
The root cause of this event was a cognitive personnel error by an APS Maintenance individual who did not ensure that RU-31 was placed in bypass in accordance with approved procedures. As corrective action, the individual has been counseled.
Previous similar events were reported in LER's 528/85-033 and 528/87-026.
NRC farm 344
NRC Felte SSSA I90>l US. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT'(LER)'TEXT CONTlNUATlON APPROYEO OMS NO 3150-0104 EXPIRE5: 4/31/IEI FACILITY NAME III COCKET NUMSER Ql LER NUMSER IS) PAGE ISI SSQI/SNT/AL REVISION NUMFSA NUMSSR Palo Verde Unit 3 0 s 53 08 0 0 00 02 ttxt /// ee>>e eeeee N NNeeed. ceo ee/eeeee/ ///IC Feee ~ 9/ I 'It) 0 0 0 9 9 QF 0 7 DESCRIPTION OF WHAT OCCURRED:
A. Initial Conditions:
At approximately 0430 HST on July 28, 1989, Palo Verde Unit 3 was in Mode 6 (REFUELING) with the Reactor Coolant System (RCS)(AB) at ambient temperature. Core (AC) reloading was in progress.
B. Reportable Event Description (Including Dates and Approximate Times of Hajor Occurrences):
Event Classification: Engineered Safety Feature Actuation.
At approximately 0430 HST on July 28, 1989, an inadvertent Train "A" Fuel Building Essential Ventilation Actuation Signal (FBEVAS)(VG)(JE) was initiated on the Balance of Plant Engineered Safety Feature Actuation System (BOP ESFAS)(JE). The Train "AU FBEVAS resulted- in the designed cross-trips of Train UBU FBEVAS and Train UA" and "B" Control Room Essential Filtration Actuation Signals (CREFAS)(VI)(JE). The actuations occurred when a maintenance individual (utility, non-licensed) reset the Spent Fuel Pool Area Radiation Honitor (RU-31)(ND)(IL)(RI) Remote Indicating and Control Unit (CPU) without ensuring that the channel was placed in "bypass." Following the actuation, Control Room Essential Ventilation System (VI) Train "B" fan (FAN) tripped. All other
-components operated as designed. Radiation Protection personnel (utility, non-licensed) verified that no actual high radiation levels existed in the area of the Spent Fuel Pool Area Honitor (RU-31).
RU-31 monitors for a release of activity due to a fuel handling accident in the Fuel Building (ND). This monitor provides a HIGH-HIGH dose rate alarm (RA) initiation signal via its Remote Indicating and Control Unit to BOP ESFAS which performs the safety function of isolating the normal ventilation system (VG) and activating the essential ventilation system. To prevent inadvertent ESF actuations during testing, troubleshooting, or calibration activities, it is necessary that the radiation monitor be removed from the on-line mode and placed in the bypass mode ai the BOP ESFAS panel (PNL). The bypass mode allows the operation of the various monitor interlocks (IEL) and trips for functional
.testing, but does not allow the monitor to actively interface with BOP ESFAS. Therefore, trip signals generated as a normal consequence of testing and calibration activities do not result in unnecessary ESF actuations.
Prior to the event, at approximately 0425 HST on July 28, 1989, the Unit 3 Spent Fuel Pool Area Radiation Honitor (RU-31) went off-line (i.e., would not communicate with its Remote Indicating and Control
'lee I /IAM esse 19 4)s
NRC PSIIII 444A I94A US. NUCLEAR REOULATORY COMMIEE1ON LlCENSEE EVENT REPORT (LER) TEXT'CONTlNUATION APPROVEO OME NO 9150~144 EXPIRES: 4/3111EI PACILITY NAME 111 OOCKET NUMEER Ql LER NVMEER 141 ~ ACE LTI YEAR gj?, SEOVENTIAL VVII~ %% ' I AEVISIQN gL HVMOSA Palo Verde Unit TEXT Nt IIIoIS SOoCe It ~. IIm ~ 3 HRC FOnn 3$ 5l LU 1171 o 5 o o o-53 08 Unit). RU-31 was declared inoperable and Fuel Building Essential 9 0 0 9 0 0 0 3 OF 0' Ventilation was initiated pursuant to Technical Specification 3.3.3. 1 ACTION requirements. Radiation Protection personnel (utility, non-licensed) were unsuccessful in attempts to reset the monitor; therefore, they contacted Instrumentation & Control (I&C)
Haintenance personnel (utility, non-licensed) for assistance. A maintenance individual went to the Remote Indicating and Control (RIC) Unit for RU-31 and noted that the RIC was not functioning properly (i.e., locked-up). The individual was aware of an investigation of a ground isolation elsewhere in the plant and believed that this had resulted in power supply (JX) perturbations which would cause RU-31 to Ulock-up" and go off-line.
In order to reset the RIC, it is necessary to momentarily de-energize the Unit by either pressing the reset button or pulling the power supply fuse (FU). However, since a loss of power to the RIC and/or RU-31 will cause a Train "ALv FBEVAS, it is necessary to place Train RAU FBEVAS in bypass prior to de-energizing the RIC to prevent an inadvertent ESF actuation.
At approximately 0430 HST, the individual de-energized the RIC without first contacting Control Room personnel (utility, licensed) and having Train RA" FBEVAS placed in bypass per approved procedures. This resulted in a Train RA" FBEVAS and designed cross trips of Train UBU FBEVAS and Train "A" and UB" CREFAS's. The BOP ESF actuation signals resulted in actuations of the Fuel Building Essential Ventilation System (VG) Trains UAR and "B", the Control Room Essential Ventilation System (VI) Trains UAR and "B", the Essential Chilled Water System (KH) Trains RAU and UB", the Essential Cooling Water System (BI) Trains RAR and UB" and the Essential Spray Pond System (BS) Trains UAU and "BR. Following the actuations, the Train "BR Control Room Essential Ventilation System fan tripped. All other components operated as designed.
The BOP ESF actuations were identified by Control Room personnel (utility, licensed) as a result of main control board (HCBD) annunciations (ANN). There were no operator actions which contributed to the cause of this event. No other ESF actuations occurred and none were necessary. Operations personnel verffied.
that the ESF actuations did not occur as a result of high radiation levels in the Fuel Building.
C. Status of structures, systems, or components that were inoperable at the start of the event that contributed to the event:
Prior to the event, the Spent Fuel Pool Area Radiation Honitor (RU-31) was inoperable as discussed in,Section I.B. No other structures, systems, or components were inoperable at the start of the event which contributed to the event.
~ AC ~ I?A V 944 4 IS 4SI
NRC Po<co SSSA 198) I US. NUCLEAII AECULATOAYCOMMISSIONJ LICENSEE EVENT REPORT (I ER)'TEXT CONTINUATION APPROVED OMS NO SISOMIOC EXPIRES: S/31/SS PACILITY NAME Ill OOCXET NUMSEA QI LER NUMSEII 191 ~ ACE 131 gg SEOUENT/*L AEVcoOcc NVMOOR NVMOPO Palo Verde Unit 3 o s o ohio 53 0 8 9 0 0 9 00 04 oF 0 TEXT ///cocoo cpoco N cooooocL'op ecoooooo/A/RC Focco ~'c/ Illl D. Cause of each component or system failure, if known:
The cause of Control Room Essential Ventilation System Train "B",
fan tripping was an intermittent failure in the fan's power supply breaker (BKR). The cause of the power supply breaker malfunction is under investigation in accordance with the APS root cause evaluation program. The investigation to determine the root cause is expected to be completed by October 31, 1989. The results of the investigation will be reported in a supplement to this LER expected to be submitted by November 30, 1989.
The cause of the Spent Fuel Pool. Area Radiation Monitor (RU-31) communication problem discussed in Section I.B could not be determined. Troubleshooting was conducted in accordance with an approved work authorization document and no problems were discovered. After resetting the monitor, the monitor operated properly and was returned to service't approximately 2151 HST on July 28, 1989.
E. Failure mode, mechanism, and effect of each failed component, if known:
The cause of the intermittent failure in the Control Room Essential Ventilation System Train "B" fan power supply breaker is under investigation as described in Section I.D. The intermittent failure resulted in a loss of power to the Control Room Essential Air Handling Unit fan which resulted in Train "B" Control Room Ventilation not functioning (i.e., no air flow). This did not result in a loss of Control Room Ventilation since the 'A" Train started and operated properly. Each train is designed to provide 100 percent capacity.
The Spent Fuel Pool Area Radiation Monitor (RU-31) problem discussed in Sections I.B and I.D resulted in the inability to remotely access RU-31 indicated radiation levels and the inability of the monitor to initiate a FBEVAS if a HIGH-HIGH alarm condition occurred.
F. For failures of components with multiple functions, list of systems or secondary functions that were also affected:
Not applicable - no component failures occurred which had multiple functions.
G. For failures that rendered a train of a safety system inoperable, estimated time elapsed from the discovery of the failure until the train was returned to service:
Control Room Essential Ventilation System Train UB" was inoperable 4AC /4AM I~ Oo 19 Slc
J HRC Perm 444A US. HUCLEAR AECULATORY COMMIEQOH 19S) I Il LlCENSEE'EVENT REPORT (LER) TEXT CONTINUATlON AI'PROYED OMS HO 4140MISa EXPIRES: SINAI ISS PACILITY HAME Ill DOCKET HUMSEA IEI L'ER HUMSER 141 ~ ACE ISI 4 4 0 V 4 H T I A I. a191 nn4 v n4 no H
~ rvnnaaa nrvMaaa TEXT N'are Pal o Verde Uni aaace H eaareverE nnaa ~t 3 IYIIC fcvm Jul Sl II7) from approximately 0430 0 s HST on 0 0 0 July 28; 5 3 0 1989 until 0 0 it was 9 0 0 returned 05oFO 7.:
to service at approximately 0041 HST.,on August 12, 1989. Train RBR was inoperable approximately 14 days 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />. During this period of inoperability, RA" Train Control Room Essential Ventilation remained operable.
No other failures occurred which rendered a train of a safety system inoperable; however, the Spent Fuel Pool Area Radiation 0425 HST on July Honitor (RU-31) was inoperable from approximately 28, 1989 until it was returned to service at approximately 2151 HST RU-31 was inoperable approximately 17 hours 26 on July 28, 1989.
minutes.
H. Hethod of discovery of each component or system failure or procedural error:
The intermittent failure in the Control Room Ventilation System Train RBR fan power supply breaker was discovered during troubleshooting conducted after the event. The Spent Fuel Pool discovered Area Radiation Honitor (RU-31) communication problem was annunciation in the Control by Control Room personnel via local Protection Room and subsequent investigation by Radiation personnel. There were no procedural errors discovered.
I. Cause of Event:
The cause of the event was a cognitive personnel error on the part of the APS individual (utility, non-licensed) responsible for resetting the Spent Fuel Pool Area Radiation Honitor (RU-31) Remote Indicating and Control Unit (RIC) without first notifying Control Room personnel and ensuring that the monitor was placed in bypass.
The error was contrary to approved procedural controls and cautionary labeling affixed to the RIC. There were no procedural There were errors or deficiencies that contributed to the event. that directly no unusual characteristics of the work location contributed to the event.
The cause of the equipment malfunctions are described in Section I.D.
J. Safety System Response:
The following automatic safety system responses occurred:
Fuel Building Essential Ventilation Control Room Essential Ventilation Essential Chilled Mater System .-
nna 4 IOann 19 44 ~
NRC fere>> 544A e
19451 US. NUCLEAR RECULATORY COMM1551ON LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROYEO OMS RO 5150~145 EXPlRES: Eall&
f ACILI'TYNAME Ill OOCXET NUMEER 12)
LER NUMEER L91 PACK 151 rrLA>> 5KOUKIITIAL "' KVI5ION NUMeee Pre IIUIIeee Palo Verde Unit 3 ohio o o 5 30 89 0 0 9 0 0 '06 oe 0 7; TEXT Ef rrerre eeeee 4 Ieewed. eee ereerrejfeRC hnII JILL'el Ill)
Essential Cooling Mater System "Essential Spray 'Pond System K. Failed Component Information:
The failed breaker is manufactured by Brown Boveri Co. It is a 480 volt Model K-600S.
II. ASSESSMENT OF THE SAFETY CONSE(UENCES AND IMPLICATIONS OF THIS EVENT:
There were no safety consequences or implications resulting from the ESF actuation. The Spent Fuel Pool Area Honitor (RU-31) monitors for a release of activity due to a fuel handling accident in the Fuel.
Building. RU-31 performs the safety function of initiating an isolation of the normal ventilation system and activating the essential ventilation system on a HIGH-HIGH dose rate alarm. As discussed in Section I.B., Fuel Building Essential Ventilation was started by Control Room personnel when RU-31 became inoperable. RU-31 continued to monitor radiation levels at the time of the event initiation and no abnormal radiation levels were detected. Additionally, Radiation Protection personnel verified that no abnormal radiation levels existed. There was no fuel handling accident which initiated this event.
There were no safety consequences resulting from the malfunctioning Train- "B" Control Room Essential Ventilation fan/breaker as Train "A" started properly and provided 100 percent capacity Control Room Essential Ventilation.
I I I. CORRECTIVE ACTIONS:
A. Immediate:
As immediate corrective action, Radiation Protection personnel (utility, non-licensed) verified that no abnormal radiation levels existed and Control Room personnel (utility, licensed) verified that the FBEVAS was not the result .of a fuel handling accident.
B. Action. to Prevent Recurrence:
As corrective action to prevent recurrence, the involved individual was counseled. An 'investigation of this event is being conducted in accordance with the PVNGS Incident Investigation Program and is expected to be completed by August 30, 1989. The results of this investigation will be reported in the supplement to this LER if it would significantly change the reader's perception of the course, significance, implications, or consequences of the event; or if it results in substantial changes to the corrective actions described above.
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NRC PAIM 555A U4 NUCLEAR REGULATORY COMMIT/(ON 1S4)1~
LICENSEE EYENT REPORT (LER) TEXT CONTINUATION APPROVEO OME NO 5150&105 EXPIRES: b/lUN PAC1L1TV NAME 111 OOCKET NUMEER Ql LE11 NUMbER PAGE 151 011 SEAR SEQUENTIAL ASVISION
%Y ~ IuMSSA ~ III&4\A Palo Verde Unit s 53 089 0 09 00 07 oF 0 7 TEXT illmCW ance M ~. II>> rdaeenal 3
AIl1C FOIIII ~ bl Ill) o a a o IV., PREVIOUS SIMILAR EVENTS:
'Previous similar events were reported in Unit 1 LER's 328/85-033 and 528/87-026. As discussed in Section I.I, the cause of the event reported in this LER (530/89-009) was a cognitive personnel error.
Cognitive personnel errors are primarily the result of mental lapses and are not normally correctable with revised procedures or additional training. Therefore, the corrective actions for thenoted previous events would not have prevented this event. It should be that corrective actions for previous events were successful in preventing recurrence of the event for approximately two years and that this is the first event of this type which has occurred in Unit 3.
~ IAC 511IIM 555A IS 55I
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