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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
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ACCELERAD DOCUMENT DIST BUTION SYSTEM REGULATORY INFORMATION DISTRIBUTIO SYSTEM (RIDS)
ACCESSION NBR:9302030096 DOC.DATE: 93/01/25 NOTARIZED: NO DOCKET ¹ FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUSiW.H. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 92-007-00:on 921224,turbine runback occurred & "A" EDG started & tied into safeguard buses 14 & 18.Caused by loss D' of power to safeguards.Restored normal power to safeguards buses 14 & 18.W/930125 ltr.
DZSTRZBUTZON CODE: ZE22T COPZES RECEZVED:LTR ( ENCL ( SZZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 Ai RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCQ-PD1-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB8H3 1 1 RR T/S SB8D1 1 1 NRR/DST/SRXB 8E 1 1 REG FILE 02 1 1 RES/DSIR/EIB 1 1 RGN1 FILE 01 1 1 EXTERNAL 'G&G BRYCE i J H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POOREgW. 1 1 NUDOCS FULL TXT 1 1
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NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE( CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 29 ENCL 29
N$ b V 5 ~ ~ I~ 4 Jhf /I'ii
/ 'lOtC j 5Ts'lt I
ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER, N.Y. 14649-0001 546.2700 7CLCPnOhf,'+cA cooE 715 January 25, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 92-007, Loss of Offsite Power Circuit 751,~ Due To Wind Storm Induced Debris, Causes Automatic Actuation of An ESF and RPS System (i.e. Emergency Diesel Generator Operation and Turbine Runback)
R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires a report of, "any event or- condition that resulted in manual or automatic actuation of any Engineered. Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached Licensee Event Report LER 92-007 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecre xco U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of- Prussia, PA 19406 Ginna USNRC Senior Resident Inspector
~()P 9302030096.930i25 PDR ADOCK 05000244 PDR
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (64) 9) APPROVED 0MB NO. 31504104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPI.Y WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT ILER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (Pyr30), V.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (11 DOCKET NVMBER (2) PA E 3 R.E. Ginna Nuclear Power Plant 0500024410F10 Loss of Offsite Power Circuit 751, Due To Hind Storm I'nduced Debris, Causes 'Automatic EVENT DATE (5) LER NUMBER (6) OTHER FACILITIES INVOLVED (6)
MONTH DAY YEAR YEAR ~ SEQUENTIAL NSi NUMBER REVtSION MO~'
REPORT DATE (7)
DAY YEAR FACILITYNAMES DOCKET NUMBERISI 0 5 0 0 0 1 2' 4 0 7 0 5 0 0 0
' THIS REPORT IS SUBMITTED PURSUANT T 0 THE REQUIREMENTS OF 10 CF R ('I t IChrch onr or more of thr followinPl (11 OPERATING MODE (9) 20.402(b) 20.405(cl 50,7 3 ( ~ I (2)(le) '3.7((b)
POWER 20 406N)(1)IB 60.36(c) (1) 60,73( ~ )(2)(e) 73.71(c)
LEVEL (10) 20.405(sl(1)(6) 60.36(c) (2) 60,73(s)(2) (r9) OTHER ISprcify in Abstract below end In Feet, HRC Form 20.405(s) ((l(iiil 60.73( ~ I (2)(i) 60.73( ~ ) (2)(eII0(A) 3BSAI 20.405(s) (I )(IY) 60.73( ~ l(2)(iil 50,73 (s) (2) (yiii)(6) 20.406 (~ l (I)(s) 50.73(el(2) (iii) 50.'73( ~ )(2)(s) .
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER Wesley H. Backus AREA CODE Technical Assistant to the Operations Manager 31 552 4- 444 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT (13)
MANUFAC. REPORTABLE MANUFAC EPORTABLE CAUSE SYSTEM 'COMPONENT TVRER TO NPRDS 54ISY@ CAUSE SYSTEM COMPONENT TURER TO NPRDS X E A CON X 9 9 SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY YEAR EXPECTED SUBMISSION DATE'151 YES III yet. complrtr EXPECTED SUBAIISSIOH DATEI NO ABsTRAcT I(imlt to f400 spree 5 I.r., epproelmrtr(y flftrrn tlnplr spree typrwriNrn linni (16)
On December 24, 1992, at 0435 EST, with the reactor at approxi-mately 984-steady state full power, a turbine runback occurred and the "A" Emergency Diesel Generator started and tied into safeguard buses 14 and 18.
The Control Room operators performed the appropriate actions of AP-TURB.2 (Automatic Turbine Runback) and verified that the "A" Emergency Diesel Generator was operating properly and that ,
safeguards buses 14 and 18 were'nergized. . The plant was sub-sequently stabilized at approximately 774 full power.
The cause of the event was the loss of power to safeguards buses 14 and 18 due to loss of offsite power 34.'5 KV Circuit 751. The underlying cause for the loss of Circuit 751 was determined to be windstorm induced debris intercepting the shield wire and phase conductor causing .a fault. (This event is NUREG-1022 (C) Cause Code) .
Corrective action was to restore normal power to safeguards- buses 14 and 18 from offsite power source 34.5 KV Circuit 767 and to stop the "A" Emergency Diesel Generator and realign -it for auto standby.
NRC Form 366 (64)9)
NRC FORM 368A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31500104 (689)
EXPIRES: 4/30/92 ESTIMATED 8)/ADEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IP430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1NE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR rice SEQUENTIAL NUM 4 4 g~ REVISION NVMSE4 R.E. (rinna Nuclear Power Plant 0 5 0 0 0 24 492 0 0 7 0 0 02 o" 10 TEXT /ffmoro g>>co /4 rtufrorf, u>> I/Rrur'>>f HRC Form 35649/ ()2)
PRE-EVENT PLANT CONDIT ONS The plant was at approximately 98% steady state power with no major operational activities in progress.
The offsite power configuration to the plant was as follows:
o Offsite power 34.5 KV Circuit 751 was feeding the "ALI train safeguards buses 14 and 18 through 12A 34.5 KV/4160V transformer and through the safeguards buses 4160V/480V transformers.
o Offsite power 34.5 KV Circuit 767 was feeding the "B" train safeguards buses 16 and 17 through 12B 34.5 KV/4160V transformer and through the safeguards buses 4160V/480V transformers.
-The weather conditions in the area were high winds, blowing snow, and subfreezing temperatures.
DESCRIPTION OP EVENT A. DATES AND APPROXIMATE TIMES OP MAZOR OCCURRENCES 0 December 24, 1992, 0435 EST: Event date and time 0 December 24, 1992, 0435 EST: Discovery date and time 0 December 24, 1992, 0435 EST: Control Room operators verify the "A"'mergency Diesel Generator (D/G) Operation and safeguards buses 14 and 18 energized.
December 24, 1992, 0436 EST: Control Room operators perform the appropriate actions of abnormal procedure AP-TURB.2 (Automatic Turbine Runback) and stabilize the plant.
0 December 24, 1992, 0501 EST: Safeguard buses 14 and 18 resupplied from offsite power 34.5 KV Circuit 767.
NR C Form 368A (689)
NAC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (669) APPROVED OMB NO.3150410E E X PI A ES: 6/30/92 ESTIMATED BURDEN PEA RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFOAMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PJ)30). U.S. NUCLEAR, REGULATORY COMMISSION. WASHINGTON, OC 20555, AND TO 1'HE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
Nk'I SEOVENTIAL REVISION RE YEAR ~
NVMSER NVM ER R.E. Gonna Nuclear TEXT /// IIKVS Sg>>Ct /S PNJV/RR/ uW ~ PDT9er Plant NRC Fee@ 36SAB/ (17) 050'0024492 007 0 0 0 3 QF 1 0 o
- December 24, 1992, 0510 EST: The <<A<< Emergency D/G was stopped and realigned for auto standby.
o December 28, 1992, 0920 EST: Offsite power 34.5 KV Circuit 751 declared operable.
B. EVENT:
On December 24, 1992, at 0435 EST, with the reactor at approximately 984 steady state full power, the Control Room received numerous annunciator alarms.
The Control Room operators immediately determined that the following events had occurred:
o Safeguards buses 14 and 18 had lost their normal power supply. E 0 A turbine runback of approximately 204 full power had occurred.
0 The <<A<< Emergency D/G had started and was tied to safeguards buses 14,and 18.
The Control Room operators immediately performed the appropriate actions of AP-TURB.2 (Automatic Turbine Runback), transitioned to AP-ELEC.1 (Loss of 12A And/Or 12B Transformer) and verified that the <<A<<
Emergency D/G was operating properly and that safe-guards buses 14 and 18 were energized. The plant was subsequently stabilized at approximately 774 full power. The Control Room operators observed that 4160V bus 12A and offsite power 34.5 KV Circuit 751 displayed zero (0) voltage. The Control Room operators performed the appropriate actions of AP-,ELEC.l and contacted Power Control. The Power Control Dispatcher informed them that offsite power 34.5 KV Circuit 751 had tripped at, substation 204.
~ NRC Foe> 366A (669)
NRC FORM 366A (6 J)9) t LICENSEE EVENT REPORT ILER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3(500104 E XP I R ES: O/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BUADEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, 00 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE IS)
- $ N: SEQUENTIAL Ngi'EVISION YEAR NUM ER 44 NUM ER R.E. Ginna Nuclear Power Plant TEXT ///mare r/IOOO/O r/O/ver/ IIOO ///OrrO/HRC FOrrrr 36//rEB/ I)7) 050002gg9 00 7 00 0 OF Subsequently, at 0452 EST, the Control Room operators, using Equipment Restoration procedure ER-ELEC.1 (Restoration of Offsite Power) energized 4160V Bus 12A from offsite power 34.5 KV Circuit. 767. At 0501 EST safeguard buses 14 and 18 were resupplied by offsite power.
At 0510 EST, December 24, 1992, the "A" Emergency D/G was stopped and realigned for auto standby.
At 0920 EST, December 28, 1992, after offsite power 34.5 KV Circuit 751 had been cleared for use, normal offsite power from Circuit 751 was made available to the plant. The current operating alignment utilizing 34.5 KV Circuit 767 is being maintained to supply the
'safeguards trains. Offsite power 34.5 KV Circuit 751 was maintained as the plant's backup supply of offsite power.
C INOPERABLE STRUCTURESP COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None.
D. OTEGPR SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
E. METHOD OF DISCOVERY:
The event was immediately apparent due to alarms and indications in the Control Room.
NAG Form 366A (649)
NRC FOAM 366A UA. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 31500104 E XP I R ES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P.530), U.S, NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3(500(04), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503, FACILITY NAME n) DOCKET NUMBER (2) LFR NUMBER (6) PAGE IS)
YEAR @R SEQUENTIAL NUM ER j~J
..A REVISION NUM ER R.E. Gonna Nuclear Power Plant o s o o o 244 92 00 7 000 5 OF 1 0 TEXT /// mare 4/race Et tertu/red, u>> add/r/arre/NRC Farm 36649/ ((7)
OPERATOR ACTION:
Following the turbine runback, buses 14 and 18 under-voltage, and the "A" Emergency D/G automatic start, the Control Room operators immediately performed the appropriate actions of AP-TURB.2 (Automatic Turbine Runback) and verified that the "A" Emergency D/G was operating properly and that safeguards buses 14 and
- 18. were energized.
Subsequently, the Control Room operators restored normal power to bus 14 and 18 and stopped and realigned the "A" Emergency D/G for Auto standby.
SAFETY SYSTEM RESPONSES:
The "A" Emergency D/G automatically started, displayed proper voltage and frequency and closed into safeguards buses 14 and 18 to supply emergency power.
III. CAUSE OF EVENT A. IMMEDIATE CAUSE:
The automatic turbine runback was caused by a dropped rod signal from the Nuclear Instrument System (NIS) power range N-42 and/or from the Microprocessor Rod Position Indication (MRPI) System.1 The automatic actuation of the "A" Emergency D/G was due to undervoltage on safeguards buses 14 and 18.
NRC Farm 366A (64)9)
1 NRC FORM 366A US. NUCI.EAR AEGULATOAYCOMMISSION (689) APPROVED OMB NO. 31504106 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPOATS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (21 'LER NUMBER (6) PAGE (3)
YEAR SEQVENTIAL REVISION HVMllER '?49: NVMSEA R.E. Gonna Nuclear P016er Plant TEXT //! nxve HM>> ls /Poult, u>> sddhiond HRC Ann 366AB/ ()7) 050002gg92 007 0 0 0 6 OF 1 0 B. INTERMEDIATE CAUSES:
The dropped Rod signal from NIS power range N-.42 was due to the momentary loss of the "B" instrument bus which supplied power to N-42. The loss of bus was due to. the momentary loss of MCC-1C the'B!'nstrument which supplied power to the constant voltage trans-former for the "B" instrument bus..
The dropped rod signal from the MRPI System was due to the momentary loss of MCC-1K which supplied power to the MRPI System. The loss of MCC-1K was due to the momentary loss of MCC-1C which .supplied power to MCC-1K.
The loss of MCC-1C was due to the momentary loss of power to safeguards bus 14.
The loss of power to safeguards bus 14 was due to the loss of offsite power 34.5 KV Circuit 751.
The undervoltage on safeguards buses 14 and 18 was due to the loss of offsite power 34.5 KV Circuit 751.
C. ROOT CAUSE:
On January 15, 1993 34.5 KV Circuit 751 was patrolled using bucket trucks. At pole T-424 on Lake .Road a burned phase conductor was found.
Based on the above the underlying cause of the loss of offsite power 34.5 KV Circuit 751 was determined to be windstorm induced debris intercepting the shield wire and phase conductor causing a fault.
(Wind gusts of up to 33.5 mph)
NRC Form 366A (669)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 31500104 EXPIRES: 4/30)92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE. EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 505) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PS30), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, OC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (II DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAI. REVISION NUMSER NUM ER I
R.E. 'Ginna Nuclear Power Plant 0 5 0 0 0 2 4 4 9 007 0 0 0 7 " 1 0 TEXT illIROIP <<coo lo toquiod, uoo oddldonol HRC Foun 36SAS I (12),
IV. ANALYSIS OF WHFNT The event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of, "any event or condition 'hat resulted'in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protection System (RPS)", in that the automatic turbine runback was an automatic actuation of the RPS and the starting of the
""A" Emergency D/G was an automatic actuation of an ESF system.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
o All reactor control and protection systems performed as designedt thus limiting the overall effects of the turbine runback transient.
o The "A" Emergency D/G operated as designed by starting and supplying emergency power to safeguards buses 14 and 18.
o Offsite power 34.5 KV Circuit 767 was still in operation supplying power to the "B" train safeguards buses and subsequently was lined up to also .supply power to the "A" train safeguards buses as permitted by plant technical specifications.
Based on the above, health and safety was assured at it can be concluded that all times.
the public(s
'I NRC Form 366A (64)9)
NRC FORM 366A UA. NUCLEAR REGULATORY COMMISSION
'(64) 9) ~ APPROVED OMB NO. 31504))04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REOUESTI 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IP4)30), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (3)504))04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME ul DOCKET NUMBER 12) LER NUMBER IS) ~ PAGE IS)
YEAR SEOUENTIAL REVISION NUMSER NUM ER R. E. Ginna Nuclear Power .Plant 0 6 0 0 0 2 44 92 0 0 7 0 0 08oF 1 0 TEXT /I/more Eoece l) reovter/, v>> er/drT/one/HRC Form 3ÃA'4) 117)
V. CORRE IVE ACTION A. ACTION TAKEN TO M%URN AFFECTED SXSTEMS TO PRE-EV19lT NORMAL STATUS:
After the plant had been stabilized, safeguards buses 14 and 18 normal power supplies were restored via offsite power 34.5 KV Circuit 767 and the "A" Emergency D/G was stopped and aligned for auto standby.
Subsequently an extensive troubleshooting effort was undertaken to determine the root cause of offsite power 34.5 KV Circuit 751 tripping out at substation 204. This troubleshooting effort included the following:
o Performing a visual and instrument survey along the entire length of offsite power 34.5 KV Circuit 751 between the plant and substation 204
. to ascertain if there were any damaged insulators, tree limbs, or other debris on lines, or evidence of anything that had possibly fallen across the line and burned free. No abnormal conditions were detected.
0 Inspecting substation 204 for any abnormal conditions'i.e. breakers, wires, monitoring equipment, etc.). No abnormal conditions were detected, except a distance monitor did indicate a problem had occurred at a 'certain distance-from Station 204. This area -was checked out with no abnormal conditions detected.
NRC FonII 366A )669)
NRC FORM355A ILS. NUCLEAR REGULATORY COMMISSION APPRDYED 0MB No. 3150010e (SJ)B)
E XP I R ES: e/30/02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REOUESTI 508> HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504(04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER IS) PAGE (3)
YEAR seaveNTIAL;.y) RE VLs ION NIJMse II NVMSER R.E. Glnna Nuclear Power Plant TEXT ///mme rpoco /s roeIJPed, ooo ~ HRC FomI 3SSA'e/ (17)
'o s o o o 2 44 92 007 0 0 9 OF.l 0 o Placing a high potential test on Circuit 751*
(i.e. approximately 70 KV) to identify possible intermittent abnormal conditions. One abnormal condition was discovered on wire connecting links'of two phases of the Circuit. These links were found to have pinholes in the jacket covering. Rochester Gas and Electric Corporation (RG&E) Transmission and Distribution Department believes these pinholes were caused by the high potential test placed on the line. No correlation between the pinholes and the original initiating event could be drawn. The links were subsequently repaired and retested satisfactorily. No other abnormal conditions were detected.
o On December 28, 1992 at 0920 EST offsite power 34.5 KV Circuit 751 was declared operable and cleared for use.
ACTZON TAKEN OR PLANNED TO,PREVENT RECUMUDtCE As the underlying cause was determined to be windstorm induced debris intercepting the shield wire and phase conductor causing a fault, the following corrective action was taken to prevent recurrence:
0 Tree trimming efforts for 34.5 KV Circuit 751 were reviewed and additional trimming was completed as of January 11, 1993 at pole T-424 on Lake Road and T-25A and T-26A on Slocum Road.
The RG&E Transmission and Distribution Department will continue their practice of Aerial patrol of 34.5 KV Circuit 751 twice per year utilizing thermal imaging and visual assessment of encroachments and general line'ntegrity. Based on those assessments appropriate maintenance activities will be performed.
NRC FomI 355A (SJ)B)
NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION (689) OMB NO. 31600104 EXPIRES: E/30/92 CONTINUATION'PPROVED LICENSEE EVENT REPORT (LER) ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLFCTION REOUEST: 600 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT AND REPORTS MANAGEMENT BRANCH IP430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20556, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150410>>), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
VEARI,>PI SEQUENTIAL ~5i REVISION
'>A NUMBER NUMSER R.E. Gonna Nuclear Power Plant o s o o o 2 44 92 007 0 1 0 OF 1 0 TEXT /// more e/wc>> /e n /Ir/rerL e>> a//I/Oo>>/ HRC %%drIII SBSE3/ (12)
ADDITIONAL INFORMAT 0 A. FAILED COMPONENTS:
The wire connecting links are of unknown origin with
, no part number or model number.
B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Station could be identified.'owever, LER 91-002 was a similar event with a different root cause.
C SPECIAL COMMENTS:
None.
NRC FoIm 366A (669)
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