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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCELERATED DISTRJBUTION DEMONSTRATION SYSTEM REGULATORY INFORv&TZON DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9206250008 DOC.DATE: 92/06/17 NOTARIZED: NO DOCKET FACIL:'50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUSPW.H. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas a Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 92-006-00:on 920518,steam generator high level feedwater isolat'ons occurred. Caused by secondary sys pressure transient. After SG levels stabilized, main feedwater ltr.
regulating valve returned to automatic control.W/920617 DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ] ENCL TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
J SIZE:
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72) . 05000244 RECIPIENT COPIES RECIPIENT ,COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDl-3 LA 1 1 PD1-3 PD 1 1 JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPBll 2 2. NRR/DST/SELB 8D 1 1 NRR/DST/SICB8H3 1 1 NRB/ T/SPLB8Dl 1 1 NRR/DST/SRXB 8E 1 1 G FI 02 1 1 RES/DSIR/EIB 1 1 RGN1 FILE 01 1 1 EXTERNAL: EGGG BRYCEEJ.H 3 3 L ST LOBBY NARD 1 1 NRC PDR 1 1 NSIC MURPHYPG.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1
~gg pqyc0') Kpt~
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: : TTR 30 ENCL 30
cg ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER N.Y. 14649-0001 ROBERT C MECREDY TELESsSSOt'E Vj<e i'sesident astca COOE7 i 6 546 2700 Cinne Nucleus Production June 17, 1992 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 92-006, Feedwater Control Perturbations, Due To A Secondary Side Transient, Causes Steam Generator High Level Feedwater Isolations R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10CFR50.73, Licensee Event Report System, item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached Event Report LER 92-006 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecredy xc'.S. Region I Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector cy20617 920b2>000 0500024+
PDR ADQC PD 8
I NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION (669) APPAOVED OMB NO. 3150d104 E XP IR ES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFOAMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT ILER) COMMENTS REGARDING BURDEN ESTIMATE TO THE AECOADS AND REPORTS MANAGEMENT BRANCH (F630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITYNAME (Il DOCKET NUMBER (2) PAGE 3 R.E. Ginna Nuclear Power Plant o 5 o o o2 441oF08 Feedwater Control Perturbations, Due To A Secondary Transient, Causes Steam Generator Hi h EVENT DATE(5) LE'R NUMBER (6) REPORT DATE (7I OTHER FACILITIES INVOLVED IS)
MONTH YEAR "q: SEQUENTIAL rrrvrsroN MONTH FACILI1'Y NAMES DOCKET NUMBER(SI OAY YEAR NUMBER &r NVMSER OAY YEAR 0 5 0 0 0 0 518 929 2 006 0 0 0 6 1 7 9 2 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT 7 0 THE REQUIREMENTS OF 10 CFR (): IChrcc onr or morr of thr followinp/ (Ill MODE (9) 20A02(itl 20.405(c) 50,73 I~ ) (2) (iv) 73.71(II)
POWER 20A05(el(1)(i) 60.36(cl(1) 50.73( ~ ) (2)(vl 73.71(cl LEVEL 0 20.405(c )II((SI 50.36(c) l2) 50.73 ( ~ ) (2) (vill OTHER /Sorrily in Ahrtrrcr Oriow rnd ln Text, HRC Form 20.405(e) II)(ilil 50.73(e) l2) (Il 60.73( ~ )(2Hviii)(AI 3SSAl k4 20A05(e l(1 l(ivl 50.73(el(2)(ii) 50,73(c) (2((viSI (B)
P44 V4 20.405(e) (1)(v) 50.73(c) (2)(iii) 50.73(el(2) (x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER Wesley H. Backus AREA CODE Technical Assistant to the Operations Manager 31 552 4-4 446 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBEO IN THIS REPOAT (13)
CAUSE SYSTEM COMPONENT MANVFAC. E PORTA 8 LE MANUFAC.
TVRER TO NPRDS SYSTEM COMPONENT TVRER kKFC~
SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)
X YES IllyrL complrrr EXPECTED SIJSJIISSIOII DATE/ NO 07 01 ABSTRACT ILimlt to lr00 rprrrr, I r.. rpproxlmrtrly lifrrrn rlnplr.rpecr typrwrlNrn linNJ (16)
On May 18, 1992 at approximately 1339 EDST, with the Reactor at approximately 974 full power, Main Feedwater Isolations occurred on the "A" Steam Generator (S/G). These feedwater isolations were caused by overfeeding the "A" S/G while in manual control, following a secondary system pressure transient.
Immediate operator action was to manually control the Main Feedwater Regulating Valves (FRV) to reduce the steam generator water levels and stabilize the plant.
The immediate cause of the event is due to a secondary system pressure transient. (This event is NUREG-1022 (X) cause code.)
The root cause is undetermined at this time.
Corrective action taken or planned are discussed in Section V of the text.
NRC Form 366 (669)
l NRC FORM 366A (BJ)9)
LICENSEE EVENT REPORT {LER)
UA. NUCLEAR REGULATORY COMMISSION e APPROVED OMB NO. 31600104 EXPIRES: S/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUESTI 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IPJ)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT 13)600)OS), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME Il) DOCKET NUMBER 12) LER NUMBER I6) PAGE 13)
~'jj REVISION YEAR 4 5 6 SSOUSNTIAL NUMSSR N NUMBER R.E. Ginna Nuclear Power Plant o s o o o 2 449 2 006 0 0 2 or- 0 8 TEXT /l/ mom <<Moo /s mqo/t<</ ooo oI/I/ll/ooo/ HRC FomI 36643/ I)T)
PRE-EVENT PLANT CONDITIONS The plant was at approximately 974 steady state power with no major activities in progress. Instrument and Control (I&C) Department personnel were investigating the Advanced Digital Feedwater Control System (ADFCS) due to some feedwater oscillations that had occurred at'pproximately 1110 EDST, May 18, 1992. These feedwater oscillations were being caused by the "A" and "B" Steam Generator (S/G)
Main Feedwater Regulating Valves (FRVs) cycling (between 434 and 48%), at twice their normal frequency and in opposite phase from each other. This feedwater response (instability while in automatic control) was new and unexpected by the operators.
DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAJOR OCCHBGUBTCES:
0 May- 18, 1992, 1337 EDST: A Secondary Side Transient. occurs.
0 May 18, 1992, 1339 EDST: Event Date and Approximate Time.
o May 18, 1992, 1339 EDST: Discovery Date and Approximate Time.
0 May 18, 1992, 1342 EDST: Control Room operators restore S/G levels to normal and place Main FRVs in automatic.
NRC Form 366A IBB9)
NAC FORM 355A (LS. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150010O (BJ)9)
EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY Wl'H THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50J) HRS. FORWARD COMMENTS REQARDINQ BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IP430), U.S. NUCLEAR AEGULATOAYCOMMISSION, WASHINGTON, DC 20555, AND TO 1)IE PAPERWOAK REDUCTION PROJECT 131500104), OFFICE OF MANAQFMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LEA NUMBER (5) PAGE (3)
YEAR .WiS SEQUENTIAL Pe NVMOER
/~4'EV SKIN
'.:.: NUMBER R.E. Ginna Nuclear Power Plant o s o o o 24 4 92 0 06 0 0 0 3 OF 0 8 TEXT ///mo>> opo>> b Ioh)II/IPC o>> oCh//Conn/NRC Form 355AB/ (12)
B. EVENT-On May 18, 1992, at approximately 1337 EDST, with the Reactor at approximately 974 full power, a secondary side condensate system decreasing pressure transient occurred. This pressure decrease traveled throughout the entire secondary side and was reflected as low feedwater header pressure and corresponding decrease in differential pressure across both FRVs. The ADFCS responded to the low feedwater header pressure by increasing the open demand signal to the main FRVs in order to maintain the proper feedwater flow. At this same time, the "C" Condensate Pump automatically started on low condensate system header pressure.
Combined with a condensate header pressure low alarm, this alerted the Control Room operators to an abnormal condition. The Control Room operators, after observing that the main FRVs open demand signals were higher than normal and increasing, and that feedwater flow to the "B" S/G was higher than appropriate, took manual control of the Main FRVs to prevent further opening of the valves.
The increased feedwater header pressure was caused by the auto start of the "C" Condensate Pump. Coupled with manual operation of the Main FRVs, the result was momentary overfeeding of the "AL( S/G after the "B" FRV was throttled. During this time period, the operator manually secured the "C" condensate pump to decrease feedwater header pressure. At 1339 EDST, May 18, 1992, Main Feedwater Isolation on high level (i.e. >/= 674 narrow range level) occurred three (3) times to the "A" S/G over a period of ten (10) seconds.
The Control Room operators manually restored S/G levels to normal, and at approximately 1342 EDST restored the "A" and "B" Main FRVs to automatic control.
NAC Form 3$ 5A (559)
NRC FORM SSSA US. NUCLEAR REGULATORY COMMISSION (Beo) APPROVEO OMB NO. 31500(OE E XP I R ES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REQUESTI 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150010E), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITYNAME (1 I DOCKE'T NUMBER (2) LER NUMBER (5) PAGE (3)
YEAR "j SEOUENZIAL,g+b N:: NUM ER REVISION
.PA NUMSER R.E. Ginna Nuclear Power Plant 0 5 0 0 0 2 4 4 2 006 0 0 0 4oF 0 8 TEXT llfmore toete lt ee)rdted, Irte eddldonel iVRC Forrrt 3554't) (17)
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE &GHAT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
E. METHOD OF DISCOVERY.
The event was immediately apparent due to alarms and indications in the Control Room.
OPERATOR ACTION:
The Control Room operators took immediate manual actions to control S/G levels and stabilize the plant. Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10 CFR 50.72, Non-Emergency, 4 hour Notification.
G. SAFETY SYSTEM RESPONSES:
r The "A" S/G Main FRV began to close automatically as a result of the feedwater isolation signal. Due to the short duration that the signal was present, the valve never fully closed.
III. CAUSE OF EVENT A. IMMEDIATE CAUSE:
The feedwater isolation signal to the "A" S/G Main FRV was due to the "A" S/G narrow range level being
>/= 674.
NRC Form 355A (BB9)
NRC FORM 355A UA. NUCLEAR REGULATORY COMMISSION (549) APPROVEO OMB NO. 3'I500I04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFOAMATION COLLECTION AEGUESTI 500 HAS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3(504)104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (I l DOCKET NUMBER (2) LER NUMBER (Sl PAGE (3)
YEAR :'SQ SEOUENTIAL ~~+ REVISION C%> NUMBER '.%'> NUMSER R.E. Ginna Nuclear Power Plant 0 5 0 0 0 2 4 4 9 0 06 00 05 oF 0 8 TEXT ///more SPeoe /I nN)lr/red, oee edd/abns/HRC form 3654'4/ (12)
B. INTERMEDIATE CAUSES:
The "A" S/G narrow range level was >/= 674 due to increased flow to the "A" S/G, caused by the perturbations in main feedwater header pressure during manual operation. This situation resulted in inadvertent overfeeding of the "A" S/G. It should also be noted here that just prior to this event, feedwater automatic control had been experiencing instability with flow oscillations, and the operators were sensitive to abnormal indications with ADFCS in automatic control of the FRVs.
C ROOT CAUSE:
The root cause is believed to be the control instability problems being experienced with the FRVs.
These instabilities caused operators to place ADFCS in manual following observation of FRV response.
After extensive troubleshooting, the" specific root cause has not been determined. Various contributing causes have been identified, and intermediate and long-term corrective actions (see Section V.B) address the need to determine the root cause.
ANALYSIS OP This event is reportable in accordance with 10CFR50.73, Licensee Event Report system, item (a)(2)(iv), which requires reporting of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protection System (RPS)". The feedwater isolation of the "A" S/G was an automatic actuation of an ESF system.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
NAC Form 35SA (54)9)
NRC FORM 355A US. NUCLEAR REGULATORY COMMISSION (589) APPROVED OMB NO. 31500(04 EXP IR ES: 5/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT {LER) INFORMATION COLLECTION REOUESTI 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION ANO REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3(SOOIOE), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITYNAME ll) DOCKET NUMBER (2) I.ER NUMBER (5) PAGE (3)
YEAR @3 sEQUENTIAL ':.:5
)g~o REVISION NUMBER NUMBER R.E. Ginna Nuclear Power Plant 0 s 0 0 o 24 492 0 0 600 06 oF0 8 TEXT //IIBo>> EOooo lr>>EUPR/, II>> BI/I/IT/ono/NRC %%drm 35BA3/ (17)
There were no operational or safety consequences or implications attributed to the feedwater isolations because:
o The feedwater isolation signals occurred at the required S/G level.
o The plant was quickly stabilized and manual control of FRVs was accomplished to mitigate any consequences of the event.
o As the feedwater isolation signals occurred as designed, the assumptions of the FSAR for steam line break were met.
Based on the above, health it can be concluded that the and safety was assured at all times.
public's V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVICT NORMAL STATUS:
o After S/G levels were stabilized, the Main FRVs were returned to automatic control.
ACTION TAKEN OR PLANNED TO PR1W1PNT RECURRENCE:
After reviewing the results of troubleshooting and discussions with Nestinghouse, the following is an outline of the corrective actions being taken or planned in response to the feedwater control instability problems (and ADFCS transient response for secondary system transients):
NRC Fono 355A (589)
NRC FORM3SSA U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31500104 (SS9)
EXPIRES: S/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUESTI 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPOATS MANAGEMENT BRANCH (F430) U 9 NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1'HE PAPERWORK REDUCTION PROJECT (3(500(04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME Ii) DOCKET NUMBER (2l LER NUMBER (5) PAGE (3)
YEAR SEOVENTIAL REVISION NVMSSA NVMSSA R.E. Ginna Nuclear Power Plant 0 5 0 0 0 2 4 4 9 0 0 6 00 07 >>0 S TEXT ///moro sPom /s /II/rkrrd, Ir>> odd/done/HRC Form 35649/ (12) 0 Short Term Response:
a) IGC technicians loosened and lubricated the actuator to stem connection block for the "B" FRV.
b) Operations was directed to place the Main FRV bypass valves in full open position and in automatic control, to reduce the feedwater control instability problem.
c) The packing on both FRVs was relaxed to minimum torque, to reduce any potential friction of the valve stem.
0 Intermediate Term Response:
a) Westinghouse has evaluated ADFCS "tuning constants" and has supplied new ADFCS gain values, in an attempt to reduce the ADFCS impact on feedwater control instability problems.
b) New ADFCS gain values have been installed in the ADFCS software. Instability problems have not been eliminated as a result of these new gain values.
c) Diagnostic testing of FRV performance was completed. Testing focused on valve response to changes in current-to-pneumatic (I/P) transducers, valve positioners, and solenoids and associated instrument air tubing.
NRC Form 3OIA (SB9)
NRC FORM 388A UA. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31500104 (64)9)
E XP I 8 ES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 503) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, 00 20503.
FACILITY NAME (11 DOCKET NUMBER (21 LER NUMBER (8) PAGE (3)
YEAR w~O SEQUENTIAL Ir~N REVISION N'.6 NUMBER 'AS N U M 8 E R R.E. Ginna Nuclear Power Plant 0 5 0 0 0 2 4 4 9 0 0 6 0 0 08 oFO 8 TEXT ///more epeoe /4 mr/vtred, vee eddldooe/NRC Fomr 3//543/ (17) o Long Term Response:
a) Valve characteristic data (with and without valve shaft packing in place) will be reviewed.
b) The vendors of the Main FRV actuator and positioner will be consulted requesting their recommendations for valve packing and positioner operation, based on a more detailed review of the diagnostic testing.
c) The calibration procedures for the Main FRVs will be revised to include valve response characteristics during scheduled calibrations.
d) EWR 4773 will apply the information obtained from other actions, and is intended to enhance feedwater control and response to plant transients.
improvements will be obtained in both It is envisioned that electronic and pneumatic performance, as a result of these enhancements.
e) After additional actions are ,completed during the 1993 outage, and after a root cause determination is completed, a supplemental report to this LER will be submitted.
ADDITIONAL INFORMATION A. FAILED COMPONENTS:
None.
B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: LER 91-009 was a similar event with a different root cause.
C SPECIAL COMMZXZS:
None.
NRC Form 356A (689)