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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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ACCELERATED DISTRIBVIION DEMONSTRATION SYSTEM REGULATORINFORMATION DISTRIBUTION .STEM (RIDE)
ACCESSION NBR:8901200173 DOC.DATE: 89/01/10 NOTARIZED: NO DOCKET N FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUS,W.H. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 88-010-00:on 881211,simultaneous loss od two "B" SG pressure channels due to sensing line freezing.
W/8 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR i ENCL TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc. j SZEE:
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 S RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 STAHLE,C 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADE SH 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB SH 1 1 NRR/DEST/ESB SD 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB SD 1 1
,NRR/DEST/RSB SE 1 1 NRR/DEST/SGB SD 1 1
'2 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/QAB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/DREP/RAB 10 1 1 NRR/DREP/RPB 10 2 2 N~R-DR- I S B 9A 1 1 NUDOCS-ABSTRACT 1 1 RZ~~ 1 1 R
RES/DSIR/EIB 1 1 DSR/PRAB 1 1 RGN1 FILE 01 1 1 I
EXTERNAL EG&G WILLIAMSI S 4 4 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 D NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS F G 1 1
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TOTAL NUMBER OF COPIES REQUIRED:. LTTR 45 ENCL 44
NIIC Sorer SOS UA. IIUCLKAR REOULATOIIY COaaMQSION IS42 I ASSROVED OMS NO.SISO DION LICENSEE EVENT REPORT HLER) EXSIRES ~ 0/Sa/() S SACILITY NAME Il) DocxKT IIUMEKR Ql tA R.E. Ginna Nuclear Power Plant 0 5 0 0 0 4 4 1 OF1 0 TITLE (a) Zmu aneOuS SS O earn enera or ressure nne s, e ' ensuing Line Freezin , Causes a Co()mon Mode Failure Condition.
EVENT DATE ISI LKR NVMSKR (S) RESORT DATE (7) OTHER SACILITIKS INVOLVED ISI MDIITaa DAY YEAR YKAR aaOVINTIAL MONTH OAY YEAR SACILITY NAaaaa DOCKET NUMSER($ )
e& NV<<oah 2 rruaaaah 0 5 0 0 0 12 11888 8 01 000 11089 0 5 0 0 0 0 KRATI IO THIS REtOR'T IS SUSAIITTEO SURSUANT T 0 THE REOUIREMKNTS OS IOCSR $ a ICAeCC Orre Or m<<e Of aae IoalorrMSI (ll MOOS (Ol 20.402(O) 20.aoa( a I 24) (2 I llal 72.7) (a)
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LICKNSKE CONTACT tOll THIS LKR l12)
NAME TELESHONE NVMSER Nesley kI. Backus AREA COOK Technical Assistant to the rations Mana er 3 1 COMtLK'TE ONE LINK SOR EACH CDMSONKNT SAILURK OESCRISED IN THIS REtORT (12)
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D PIT F)l 8 0 Y SVSSLKMKNTAL RESOR'T EXSECTEO (Ia) ~ aONTH DAY YEAR EXtECTEO 1V 2 M1$ 1 ION DATE II E)
YES IIItaa, camtae<<SxtEctf 0 susoNssIOH DA TEI NO ASST R ACT IVmla IO laOO acre<<, I A, chere atara<<at IN<<ee aleteeaaaae Crtrreratree Iwra) II~ I On December 100% full power ll, 1988 at 1124 EST with the reactor at approximately one of the three 1B steam generator pressure channels began drifting high. At approximately 1144 EST a second 1B steam generator pressure channel began drifting high.
The underlying cause of the above events was the freezing of the affected pressure transmitter sensing lines leading to the simultaneous loss of two independent safety related steam generator pressure channels.
Tmmediate operator action was to declare the affected pressure channels inoperable and commence a load reduction to hot shutdown per Technical Specification action statement.
Corrective action taken was to thaw out the affected sensing lines and calibrate and return to service the affected pressure channels.
8'7)01200173 8'7)0110 05000244 PDR ADOCK S
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U.S. NUCLE AR REOULATOIIY COMMISSION NRC /orm 9AAA i9491 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ARRAOVEO OME NO 9ISOWIOt ER ~ IREE EISI/9$
R AC I LIT Y NAME I I I OOCKET NUMEER 191 LEII NUMSER l ~ I ~ AOE ISI
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~ rUM th VUM to R.E. Ginna Nuclear Power Plant. o s o o o 244 8 0 1 0 000 2 DF 1 0 TExT Illmore NrrNe e eettteer. we ohetteerM HRc lrorhI ~'AI llll PRE-EVENT PLANT CONDITIONS The unit was at approximately 100% steady state full power with no ma)or activities in progress'. A cold weather walkdown per Administrative Procedure A-54.4.1 had been completed at 0842 EST December ll, 1988. r DESCRIPTION OP EVENT A. DATES AND APPROXIMATE TIMES FOR MAJOR OCCURRENCES:
0 December 11, 1988, 1124 EST: ".B" Steam Generator Pressure Channel PT-479 started to was declared inoperable and defeated per Ecpxipment drift high and Restoration Procedure ER-INST.1 (Reactor Protec-tion Bistable Defeat After Instrumentation Loop Failure).
0 December 11, 1988, 1144 EST: "B" Steam Generator Pressure Channel PT-483 started to was declared inoperable.
drift high and 0 December ll, 1988, 1144 EST: Event date and time.
December 11, 1988, 1144 EST: Discovery date and time. I 0 December 11, 1988, 1230 EST: Started unit load reduction.
0 December 11, 1988, 1428 EST: "B" Steam Generator Pressure Channel PT-483 declared operable.
0 December 11, 1988, 1428 EST: Stopped unit load reduction.
0 December Pressure ll, 1988, 1522 Channel PT-479 EST: "B" Steam Generator declared operable.
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U.S. NUCL'EAA AECULATOAY COMMISSION NAC Fons SEEA AFFAOVEO OMS NO, 5IEOWI04 15@El LICENSEE EVENT REPORT ILER) TEXT CONTINUATION EXFIAES SITIIS5 LEA NUMSEA I ~ I ~ AOE ISI FACILITY NAME III SEQVEHTIAL NVM EA R.E. Ginna Nuclear Power Plant o 5 o o o 2 4 4 8 8 0 1 0 0 0 0 3 oF l 0 TEXT IIF mort AMoI A movFMI. vM ~WIC Fame ~'FI llll B. EVENT:
On December ll, 1988 at 1124 EST with the reactor at approximately 1004 full power, steam generator 1B pressure channel PT-479 began drifting high and was declared inoperable and defeated per Equipment Restoration Procedure ER-INST.l, (Reactor Protection Bistable Defeat After Instrumentation Loop Failure).
At, 1144 EST, steam generator 1B pressure channel PT-483 also started drifting high and was declared inoperable.
At this time, the Control Room operators determined that the probable cause of the 1B steam generator pressure channel problems was freezing'of the trans-mitter sensing lines, as all other indication of plant status was normal. Auxiliary operators were dis-patched to the area where the 1B steam generator pressure transmitters were located and reported back that it was extremely cold in the area. This condition was found to be due to outside cold air, (approximately 10 F) being drawn into the building through the inlet air dampers located near the affected pressure transmitters. Actions were immediately taken to reclose the outside air dampers and supply additional heat to the area.
At 1230 EST, a load reduction of 20% per hour was commenced due to Technical Specifications section 3.55 action statement 95 which requires, "at any time the number of operable channels is less than the minimum operable channels required, be at hot shutdown within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and at an RCS temperature less than 350 F within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, (i.e.
the number of channels at this time was one less than the minimum operable channels required.)
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U.S. NUCLEAR RKOULATORY COMMITSION NRC Forrrr A4A I 045 I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMR NO. T154&105 TR ~ IRTS d(TI(55 FACILITY NAMK III OOCKCT NUMRKR LTI LCR NUMRIR ldl 1
550V5NTIAL 11 5 V 15 10 rr NVM dk r(VM dw R.E. Ginna Nuclear Power Plant o 5 o o o 24 488 010 0 0 0 4 OF fg(7 I(F rrr(rrd AMdd N red((re (rdd d(NRN((N (YRC Forrrr ~'ll ill I
At approximately 1300 EST, the 1B steam generator pressure channel PT-479 started decreasing from its highest pressure reached of 1091 psig.
thought at this time that the sensing lines for PT-It was 479 were thawing and that the channel pressure would return to actual steam generator pressure but PT-479 indication continued to decrease below actual steam generator pressure. At approximately 1315 EST, the 1B steam generator pressure channel PT-483 started decreasing from its pegged high position. With PT-479 defeated and PT-483 decreasing, the possibility existed of an inadvertent safety in)ection signal being generated from 2/3 lo lo steam generator pressure of 514 psig if PT-483 continued to decrease in the same manner as PT-479. With PT-479 at approxi-mately 120 psig, .the Operations Shift Supervisor instructed the Instrument and Control (I&C) Technician to insert a simulated signal of approximately 700 psig into the defeated channel PT-479. PT-479 was to remain defeated until it was determined whether PT-483 would decrease past the safety injection initiation setpoint of 514 psig. When PT-483 decreased below 600 psig, PT-479's low and lo lo pressure bistables were reinstated and PT-483 was placed in the defeat mode.
The 1B steam generator pressure channel PT-483 did decrease below 514 psig but safety injection was not actuated due to the simulated signal in PT-479. With PT-483 defeated the safety in)ection coincidence was 1/1 with 1B steam generator pressure channel PT-478 being the only operable channel.
At approximately 1410 EST the I&C department had completed. thawing the sensing lines to PT-479 and .PT-483 and their pressure indication had returned to normal. At approximately 1428 EST the I&C department completed calibration and return to operable status of PT-483. As the Technical Specifications for minimum operable channels was met with the return of PT-483 to operable status the load reduction was terminated. PT-479 was calibrated and returned to operable status at approximately 1522 EST.
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U.S. NUCLfAR RlOULATORY COMMISSION NRC %%dr~ S44A
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AFFROVEO OMl NO. SI50M<04 E<< ~ <RES 4<SI<SS OOC<<ET NUMSER ISI ~ AOE IS)
FACILITY NAME III I.ER NUMOER I ~ I S~ QUS<<T<AL <ISVIS<0<<
NUM ~R <<UM Sh R.E. Ginna Nuclear Power Plant: o so oo244 8 8 0 0 0 0 5 OF 1 0 TEXT I<F m<<<4 <<M<<4 <<<44<<<44<. <<44 ~ <<<<<h<<F HRC %%dhh JINA'4 I II TI C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
E. METHOD OF DISCOVERY:
The event was immediately apparent due to alarms and indication in the Control Room.
F. OPERATOR ACTION:
Immediate operator action was to defeat the inoperable 1B steam generator pressure channel PT-479 and with the failure of the second 1B steam generator pressure channel, to determine the cause of these two pressure channels failing simultaneously.
The Control Room operators, after determining that freezing of the pressure channel sensing lines was the probable cause, took immediate action to reduce the amount of cold air coming into the pressure channel sensing line area and to supply additional heat to this area.
After declaring two of the three 1B steam generator pressure channels inoperable, the Control Room operators started reducing unit power per technical specification action statement.
During this event period, the plant was operating with known system integrity which would not warrant the need for safety injection actuation.
NRC +ORM S44A
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V.E. NVCLEAN AEOULATOIIYCOMMIEEION NAC rrorrrr 555A IW51 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION AeelIOVEO OME NO, 5150WI05 EAelllE5 EI)1t55 FACILITY NAME III OOCKET NUMEEII IEI LEII NUMEEII I51 ~ AOE 151 55QUErrellL NUM Eo lrUM
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~1 R.E. Ginna Nuclear Power Plant o 5 o o o 244 8 010 0 6 OF 1 0 Tz@T ]It more mooe ~ reooeeeI. rree ~ tooorot HtIC term 5$ $A EI I ITI Because the pressure indication was decreasing toward the safety injection initiation setpoint in the two inoperable 1B steam generator pressure channels, the Operations Shift Supervisor instructed the I&C Technician to insert a simulated signal into one of the inoperable pressure channels to avoid an in-advertent safety injection actuation. The decision that a safety injection actuation was not needed and the simulator should be installed was reviewed and concurred on by the Shift Supervisor (SRO), the Control Room Foreman (SRO), and the Reactor Engin-eer/Technical Manager acting as Shift Technical Advisor. During the time this signal was inserted the Control Room operator's were monitoring the 1B steam generator parameters and reactor coolant system parameters very closely for the steam break accident.
G. SAFETY SYSTEM RESPONSES:
None.
III. CAUSE OF A. IMMEDIATE CAUSE:
The immediate cause of the event was the common mode failure of two of the three 1B steam generator-pressure channels.
B. INTERMEDIATE CAUSE:
The common mode failure of the two 1B steam generator pressure channels was due to the freezing of the pressure channels sensing lines.
C ~ ROOT CAUSE:
The freezing of the two 1B steam generator pressure channels sensing lines was due to inadequate cold weather operations and procedures.
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U,S NUCLEAR RKOULATORY COMMISSION HRC form 054A AttROVSO OM4 NO S150&I04 1045 I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION SXtlh4$ 4ISI/4$
OOCKST NUM44R ~ AOS ISI tACILITYNAMS Ill 141 LKR NUM44R I ~ I U I rr 5 I A 5 II 0HUM AIVISIOH Ih NUM Ih R.E. Ginna Nuclear Power Plant o 5 o o o 24 488 010 00 07 OF 1 0 TTXT (IT mort tooot A neural ow odohtohtt ANC %%de JOSA'tl 1171 IV. ANALYSIS OP EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2)(vii)(D) which requires a report of, "any event where a single cause or condition caused at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a system designed to mitigate the consequences of an accident".
The common mode failure of the two independent 1B steam generator pressure channels was an event where" a single condition caused two independent. channels to become inoperable in a system designed to mitigate the consequences of an accident.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences attributed to the common mode failure of the two 1B steam generator pressure channels because:
0 The failures and failure mode were determined very quickly.
0 One pressure channel remained fully operable throughout the event.
0 Unit load was reduced in preparation for taking unit off the line in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> per plant Technical Specifica-tion action statement.
0 A simulated signal was inserted into one of the inoperable pressure channels to avoid an inadvertent safety injection actuation and potential for a subsequent detrimental transient on the plant.
The inoperable pressure channels were repaired, calibrated and returned to service quickly.
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U.5. NUCLEAR REOULATORY COMM14410N NAC Sei~ 344A I 043 l LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AeeROVEO OM4 NO, 2ISOW104 ERelRES 4ISIISS OOCRET NUM44R I21 LER NUM4ER ISI ~ AOE ISI SACILITY NAME I)l 55OVINTIAL I A V i@10 H HVM 4R Nvv Ie R.E. Ginna Nuclear Power Plant o 5 o o o 2 4488 0 l 0 0 0 8 OF 1 0 TExT Irt epee Meee N NeveeeL eee edeeeeeve NRC fcnn ~'el I Ill There was the following safety implication attributed to the common mode failure of the two 1B steam generator pressure channels:
o Was the plant still protected against the steam line break accident with the 2 inoperable 1B steam generator pressure channels?
The R.E. Ginna Nuclear Power Plant Updated Final Safety Analysis Report (Ginna/UFSAR) section 15.1 states in'art that the following systems provide the necessary protection against a steam pipe rupture.
- 1. Safety in)ection system actuation on the following:
- a. Two-out-of-three pressurizer low pressure signals.
- b. Two-out-of-three low pressure signals in any steam line.
- c. Two-out-of-three high containment pressure signals.
Based on this review of the UFSAR, blocking of the steam generator low pressure safety in)ection signal has negli-gible effect on the most limiting transient involved.
Based on the above it can be concluded that safety in)ection actuation for the steam line break would still have taken place from either low pressurizer pressure or high contain-ment pressure thus assuring the public's health and safety at all times.
CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
o The cold air situation in the area of the affected pressure transmitter sensing lines was immediately rectified.
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AUCLSAA ASOULATOAY COMMISSIOII IIAC carer SISA 10451 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION'.S. ASSAOVSO OMS HO, 3150MI04 S x ~ I AS 5 4 Ill /SS 4ACILITY HAMS 111 OOCAST IIVMSSA 111 LSA HUMSSA I ~ I ~ AOS ISI 55QV err TIAL AIYISIQrr
~ rVQ Sll rrvv Ih R.E. Ginna Nuclear Power Plant p 5 p p p 2 4488 0 1 0 0 0 0 9 OF l 0 TACT Illmare Awae ~ reaveerL rree arHAArheT HAC few SATA0 I 1171 o The frozen sensing lines were thawed out and the affected pressure channels calibrated satisfac-torily and returned to service.
o Unit load was returned to full power.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
0 Rewrite Administrative Procedure A-54.4.1 (Cold Weather Walkdown Procedure) to provide a better trigger mechanism for initiation and to provide specific quantitative guidance for areas, components, and temperature criteria.
0 Add thermometers in temperature sensitive areas of affected buildings.
0 Add temperature readings of temperature sensitive areas to Aux. Operators Log.
0 Initiate Engineering Work Request to review the adequacy of HVAC systems in the Intermediate Building.
0 Evaluate the integrity of the affected steam generator pressure instrument tubing.
0 Evaluate relocation/replacement of the affected steam generator pressure instrument tubing.
0 Replace existing outside air louver with manual positive sealing louver.
0 Review other potential corrective action to preclude freezing of instrument lines.
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U.S. NUCLKAN XSOULATOAY COMMISSION NIIC Fee~ SttA IOeSI LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AFFIIOVSO OMS NO, SISO&104 S X ~ 11 t$ NISI ISS FACILITY HAMS 111 OOCKST NUMSSII ISI LSII NUMSSII I ~ I ~ AOS ISI YSAn SSQVtNTIAL ntvlSlov vvM n vvM tn R.E. Ginna Nuclear Power Plant 24 488 0 1 0 0 10 DF1 0 TExT llfnxxe NxNe ~ recvee. we eeetNnel HIIc Fenn ~'IlIITI ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
None B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar .LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Station could be identified.
C. SPECIAL COMMENTS:
Sensing line for PT-479 also froze on 12-5-80, which did not result in a LER. A main feedwater instrument line also froze on 12-7-84. This entire issue of instrument line operability is discussed in NRC Inspection Report 88-26.
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V ST@it ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER, N.Y. 14649-0001 r
IL'LCPHO<c inca cooa 7se 546-2700 January 10, 1989 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER-88-010, Simultaneous Loss of Two Safety Related "B" Steam Generator Pressure Channels, Due to Sensing Line Freezing, Causes a Common Mode Failure Condition R.E. Ginna Nuclear Power Plant Docket No. 50-244 (
In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(vii)(D) which requires a report of, "any event where a single cause or condition caused at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a system designed to mitigate the consequences of an accident",
the attached Licensee Event Report LER 88-010 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Me redy General Manager Nuclear Production xce U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector