ML14078A666

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IR 05000285-14-002; 01/01/2014 - 02/15/2014; Fort Calhoun Station; Integrated Resident Inspection Report and Confirmatory Action Letter Closeout Items & Notice of Violations
ML14078A666
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 03/19/2014
From: Hay M
NRC/RGN-IV/DRP
To: Cortopassi L
Omaha Public Power District
Hay M
References
EA-14-037 IR-14-002
Download: ML14078A666 (78)


See also: IR 05000285/2014002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

1600 E. LAMAR BLVD.

ARLINGTON, TX 76011-4511

March 19, 2014

EA-14-037

Lou Cortopassi, Vice President

and Chief Nuclear Officer

Omaha Public Power District

Fort Calhoun Station FC-2-4

P.O. Box 550

Fort Calhoun, NE 68023-0550

Subject: FORT CALHOUN - NRC INTEGRATED INSPECTION REPORT

NUMBER 05000285/2014002 AND NOTICES OF VIOLATIONS

Dear Mr. Cortopassi:

On February 15, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at the Fort Calhoun Station. On February 25, 2014, the NRC inspectors discussed

the results of this inspection with Mr. Michael Prospero, Plant Manager, and other members of

your staff. Inspectors documented the results of this inspection in the enclosed inspection

report.

During this inspection, the NRC staff examined activities conducted under your license as they

relate to public health and safety with the Commission's rules and regulations and with the

conditions of your license. Within these areas, the inspection consisted of selected examination

of procedures and representative records, observations of activities, and interviews with

personnel.

Based on the results of the inspection, the NRC has determined a Severity Level IV violation of

NRC requirments occurred. Additionally, the NRC identified an issue that was evaluated under

the risk significance determination process as having very low safety significance (green). The

NRC also determined that a violation was associated with this issue.

These violations were evaluated in accordance with the NRC Enforcement Policy. The current

Enforcement Policy is included on the NRCs Web site at

http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.

These violations are cited in the enclosed Notice and the circumstances surrounding them are

described in detail in the subject inspection report. The violations are being cited in the Notice

because one issue was repetitive in nature and the other issue involved the failure to restore

compliance (or demonstrate objective evidence of plans to restore compliance) within a

reasonable period of time after a violation is identified.

L. Cortopassi -2-

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. If you have additional information that you

believe the NRC should consider, you may provide it in your response to the Notice. The NRCs

review of your response to the Notice will also determine whether further enforcement action is

necessary to ensure your compliance with regulatory requirements.

Additionally, based on the results of the inspection, the NRC identified two additional Severity

Level IV violations of NRC requirements and five findings evaluated under the risk significance

determination process as having very low safety significance. The NRC determined that

violations were associated with these issues, however, these violations are being treated as

Non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy. These

NCVs are described in the subject inspection report. If you contest the violations or significance

of these NCVs, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Fort Calhoun

Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the

Fort Calhoun Station.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRCs Public

Document Room or from the Publicly Available Records (PARS) component of the NRC's

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Michael Hay, Chief

Project Branch F

Division of Reactor Projects

Docket: 50-285

License: DPR-40

Enclosure:

NRC Inspection Report 05000285/2014002

w/Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

L. Cortopassi -3-

Electronic distribution by RIV:

Regional Administrator (Marc.Dapas@nrc.gov)

Deputy Regional Administrator (Steven.Reynolds@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

Acting DRS Director (Jeff.Clark@nrc.gov)

Acting DRS Deputy Director (Geoffrey.Miller@nrc.gov)

Senior Resident Inspector (John.Kirkland@nrc.gov)

Resident Inspector (Jacob.Wingebach@nrc.gov)

Branch Chief, DRP/F (Michael.Hay@nrc.gov)

Senior Project Engineer, DRP/F (Nick.Taylor@nrc.gov)

Project Engineer, DRP/F (Chris.Smith@nrc.gov)

FCS Administrative Assistant (Janise.Schwee@nrc.gov)

RIV Public Affairs Officer (Victor.Dricks@nrc.gov)

RIV Public Affairs Officer (Lara.Uselding@nrc.gov)

NRR Project Manager (Lynnea.Wilkins@nrc.gov)

NRR Project Manager (Joseph.Sebrosky@nrc.gov)

RIV Branch Chief, DRS/TSB (Ray.Kellar@nrc.gov)

RIV RITS Coordinator (Marisa.Herrera@nrc.gov)

RIV Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

OEWEB Resource (Sue.Bogle@nrc.gov)

RIV/ETA: OEDO (Ernesto.Quinones@nrc.gov)

RIV RSLO (Bill.Maier@nrc.gov)

MC 0350 Panel Chairman (Anton.Vegel@nrc.gov)

MC 0350 Panel Vice Chairman (Louise.Lund@nrc.gov)

MC 0350 Panel Member (Michael.Balazik@nrc.gov)

MC 0350 Panel Member (Michael.Markley@nrc.gov)

R:\_Reactors\FCS\2014\FCS 2014-002-RP JCK.pdf ML14078A666

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials MCH

Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials MCH

SRI:DRP/F RI:DRP/F SPE:DRP/F PE:DRP/F OE C:DRP/F

JKirkland JWingebach NTaylor CSmith RBrowder MHay

/RA/ /RA/ /RA/ /RA/ /RA/ /RA/

03/18/14 03/18/14 03/13/14 03/18/14 03/19/14 03/19/14

OFFICIAL RECORD COPY

NOTICE OF VIOLATION

Omaha Public Power District Docket No: 50-285

Fort Calhoun Station License No: DPR-40

EA-14-037

During an NRC inspection conducted on August 26, 2013 through February 15, 2014, a

violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy,

the violation is listed below:

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that

measures shall be established to assure that conditions adverse to quality, such as

failures, malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected.

Contrary to the above, between August 12, 2008 and November 24, 2013, the licensee

failed to correct a condition adverse to quality. Specifically, actions were not taken to

correct NRC-identified runout concerns in the containment spray system until these

concerns were again raised by the NRC on July 18, 2013.

This violation is associated with a Green Significance Determination Process finding.

Pursuant to the provisions of 10 CFR 2.201, Omaha Public Power District is hereby required to

submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional

Administrator, Region IV, and a copy to the NRC Resident Inspector at the facility that is the

subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation

(Notice). This reply should be clearly marked as a "Reply to a Notice of Violation; EA-14-037"

and should include: (1) the reason for the violation, or, if contested, the basis for disputing the

violation or severity level, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will

be achieved. Your response may reference or include previous docketed correspondence, if

the correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

-1- Enclosure

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 19th day of March, 2014

-2-

NOTICE OF VIOLATION

Omaha Public Power District Docket No: 50-285

Fort Calhoun Station License No: DPR-40

EA-14-037

During an NRC inspection conducted on August 26, 2013 through February 15, 2014, a

violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy,

the violation is listed below:

10 CFR 50.73(a)(1), requires, in part, that the licensee submit a Licensee Event Report

(LER) for any event of the type described in this paragraph within 60 days after the

discovery of the event.

Contrary to the above, between June 14 and July 2, 2013, the licensee failed to submit a

LER for two events meeting the requirements for reporting specified in 10 CFR 50.73

within 60 days after the discovery of the event. Specifically, LERs 2013-101-0, HPSI

Pump Flow Imbalance, and 2013-017-0, Containment Spray Pump Design Documents

do not Support Operation in Runout, were submitted more than 60 days after the events

were discovered.

The NRC determined that this violation was repetive in nature as described in Paragraph

2.3.2(a)(3) of the NRC Enforcement Policy. A similar violation had been documented in

NRC Inspection Report 2013008 dated July 16, 2013 (ML13197A261). That report

included NCV 05000285/2013008-43, entitled Untimely Submittal of Licensee Event

Reports. The NCV documented nine examples of LERs that were submitted later than

required by 10 CFR 73(a)(1).

This is a Severity Level IV violation.

Pursuant to the provisions of 10 CFR 2.201, Omaha Public Power District is hereby required to

submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional

Administrator, Region IV, and a copy to the NRC Resident Inspector at the facility that is the

subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation

(Notice). This reply should be clearly marked as a "Reply to a Notice of Violation; EA-14-037"

and should include for each violation: (1) the reason for the violation, or, if contested, the basis

for disputing the violation or severity level, (2) the corrective steps that have been taken and the

results achieved, (3) the corrective steps that will be taken, and (4) the date when full

compliance will be achieved. Your response may reference or include previous docketed

correspondence, if the correspondence adequately addresses the required response. If an

adequate reply is not received within the time specified in this Notice, an order or a Demand for

Information may be issued as to why the license should not be modified, suspended, or

revoked, or why such other action as may be proper should not be taken. Where good cause is

shown, consideration will be given to extending the response time.

-3-

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), and be accessible from

the NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should

not include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 19th day of March, 2014

-4-

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000285

License: DPR-40

Report: 05000285/2014002

Licensee: Omaha Public Power District

Facility: Fort Calhoun Station

Location: 9610 Power Lane

Blair, NE 68008

Dates: January 1 through February 15, 2014

Inspectors: J. Kirkland, Senior Resident Inspector

J. Wingebach, Resident Inspector

N. Taylor, Senior Project Engineer

W. Smith, Project Engineer

W. Lyon, Senior Reactor Engineer

M. Chambers, Physical Security Inspector

A. Guzzetta, Reactor Systems Engineer

M. Farnan, Mechanical Engineer

A. Sallman, Senior Reactor Systems Engineer

Approved By: Michael Hay, Chief, Project Branch F

Division of Reactor Projects

-5-

SUMMARY

IR 05000285/2014002; 01/01/2014 - 02/15/2014; Fort Calhoun Station; integrated resident

inspection report and Confirmatory Action Letter closeout items.

The inspection activities described in this report were performed between January 1, 2014, and

February 15, 2014, by the resident inspectors at the Fort Calhoun Station, inspectors from the

NRCs Region IV office, and technical support from headquarters staff. Nine findings are

documented in this report. Seven findings were of very low safety significance (Green). All of

these findings involved violations of NRC requirements and three of these violations were

determined to be Severity Level IV violations under the traditional enforcement process. The

significance of inspection findings is indicated by their color (Green, White, Yellow, or Red),

which is determined using Inspection Manual Chapter 0609, Significance Determination

Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310,

Components Within the Cross-Cutting Areas. Violations of NRC requirements are

dispositioned in accordance with the NRCs Enforcement Policy. The NRC's program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG 1649, Reactor Oversight Process.

Cornerstone: Mitigating Systems

Green. A non-cited violation of 10 CFR 50, Appendix B, Criterion III, Design Control, was

identified involving the failure to translate the High Pressure Safety Injection (HPSI) pump

design and runout characteristics to design documents such as the Updated Safety Analysis

Report or design calculations. On June 21, 2013, the licensee completed Engineering

Change 59874, which permanently installed flow-limiting orifices in the discharge line of each

pump, effectively preventing HPSI runout conditions from occurring for all plant conditions.

This finding was more than minor because it adversely impacted the design control attribute of

the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences.

The inspectors reviewed NRC IMC 0609, Attachment 4, Initial Characterization of Findings,

Table 3 - SDP Appendix Router. While this issue was identified during a refueling outage, the

inspectors determined that the majority of the exposure time for this violation occurred with the

reactor at power. As such, the inspectors determined the finding should be evaluated using the

SDP in accordance with IMC 0609, The Significance Determination Process (SDP) for

Findings at-Power, Appendix A, Exhibit 2, Mitigating Systems Screening Questions. The

finding required a detailed risk evaluation because the high pressure safety injection system

was inoperable for some of the large break loss of coolant accident scenarios (at reactor

pressures less than 100 psi). A Region IV senior reactor analyst performed a bounding detailed

risk evaluation. The change to the core damage frequency was 8E-8/year and, therefore,

determined to be of very low safety significance (Green). The dominant core damage

sequences included loss of coolant accidents where the high and low pressure safety injection

systems failed during recirculation. The non-degraded low pressure safety injection system

contributed to minimize the risk. The inspectors determined there was no cross-cutting aspect

associated with this finding because events related to identification of needed procedures and

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specifications occurred in the 1970s and are not indicative of current performance. (Section

4OA3.2)

Green. Two examples of a non-cited violation of 10 CFR 50, Appendix B, Criterion III, Design

Control, were identified. The first example involved the failure to establish procedures or

Technical Specifications to accomplish required HPSI injection flow balancing. The second

example involved the failure to provide controls or testing to ensure that replacement parts for

HPSI injection valves were suitable for the application and were capable of supporting the

safety-related functions of the HPSI system. The licensee has since implemented Engineering

Change 59874 which included throttling of the HPSI loop injection valves. This change was

completed on August 20, 2013, restoring the original plant design and overcoming the

configuration control errors introduced on three of the eight injection valves. Post-work testing

for the completed modification included flow balance testing for the HPSI loop injection lines.

The inspectors reviewed the results of this testing and determined that the UFSAR assumptions

regarding balanced loop flows were adequately addressed by licensee corrective actions.

This finding was more than minor because it adversely impacted the design control attribute of

the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences.

The inspectors reviewed NRC IMC 0609, Attachment 4, Initial Characterization of Findings,

Table 3 - SDP Appendix Router. While this issue was identified during a refueling outage, the

inspectors determined that the majority of the exposure time for this violation occurred with the

reactor at power. As such, the inspectors determined the finding could be evaluated using the

SDP in accordance with IMC 0609, The SDP for Findings at-Power, Appendix A, Exhibit 2,

Mitigating Systems Screening Questions. The inspectors answered yes to the question of

Does the finding represent a loss of system and/or function? The inspectors determined the

finding required a detailed risk evaluation per IMC 0609 Paragraph 6.0, because the operability

of the high pressure safety injection system (both trains) was in question. A Region IV senior

reactor analyst performed a detailed risk evaluation and determined the flow imbalance did not

result in a loss of safety function. Since the high pressure safety injection system was capable

of meeting the functional success criteria, there was no quantifiable change to the core damage

frequency and therefore was determined to be of very low safety significance (Green). The

inspectors determined there was no cross-cutting aspect associated with this finding because

events related to identification of needed procedures and specifications occurred in the 1970s

and are not indicative of current performance. Additionally, the errant replacement of parts of

three HPSI injection valves occurred between 1993 and 2006, and are also not indicative of

current performance. (Section 4OA3.4)

SLIV and Green. A Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests, and

Experiments, and an associated Green finding was identified involving the failure to request a

license amendment for a facility change that required a change to the Technical Specifications.

This issue is also associated with a Green finding related to the licensees failure to follow

Procedure NOD-QP-3, 10 CFR 50.59 and 10 CFR 72.48 Reviews, and Procedure FCSG-23,

10 CFR 50.59 Resource Manual, both of which require submittal of a license amendment

request prior to making a facility change that requires a change to Technical Specifications.

The licensee initiated CR 2014-01029 on January 23, 2014, to document this violation and track

corrective actions.

-7-

This performance deficiency was considered to be of more than minor safety significance

because it was associated with the procedure quality attribute of the mitigating systems

cornerstone and it adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the failure to follow station procedures for the 10 CFR 50.59

process caused the Technical Specifications to become insufficient to ensure that the limiting

conditions for operation will be met. Using Inspection Manual Chapter 0609 Appendix G,

Checklist 4, the inspectors determined that the finding did not result in the loss of any accident

mitigation capability and did not require a quantitative risk assessment. This finding was

determined to be of very low risk significance.

This performance deficiency was also determined to be subject to traditional enforcement

because it impeded the regulatory process, in that the failure to submit a license amendment

and add required surveillance testing was in violation of 10 CFR 50.59(c)(1)(i) and caused the

NRC-approved Technical Specifications to be out of alignment with the safety analysis for the

facility. This violation is associated with a finding that has been evaluated by the SDP and

communicated with an SDP color reflective of the safety impact of the deficient licensee

performance. The SDP, however, does not specifically consider the regulatory process impact.

Thus, although related to a common regulatory concern, it is necessary to address the violation

and finding using different processes to correctly reflect both the regulatory importance of the

violation and the safety significance of the associated finding. This violation was determined to

be a Severity Level IV violation, because it is consistent with the examples in Paragraph 6.1.d of

the NRC Enforcement Policy. The finding had a cross-cutting aspect in the training aspect of

the human performance cross-cutting area because the licensees staff failed to understand and

misapplied NRC generic guidance related to discovery of inadequate Technical Specifications

[H.9]. (Section 4OA3.4)

Green. A non-cited violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings was identified involving the licensees failure to complete a 10 CFR 50.59

screening that met the requirements of Procedure NOD-QP-3, 10 CFR 50.59 and 10

CFR 72.48 Reviews, Revision 37. The licensees staff subsequently re-performed the 50.59

screening on November 29, 2013, and determined that a 10 CFR 50.59 evaluation was

required. The NRC staff reviewed the 10 CFR 50.59 screening and evaluation and determined

that they had been properly performed, and that a license amendment request was not required

prior to implementation of the activity. The licensee documented this procedural violation in

CR 2014-01357 on January 29, 2014.

This performance deficiency was considered to be of more than minor safety significance

because it was associated with the design control attribute of the mitigating systems

cornerstone and it adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the failure to follow station procedures for the 10 CFR 50.59

process prevented the licensees staff from evaluating the adverse impacts of the change on the

facility. Using Inspection Manual Chapter 0609 Appendix G, Checklist 4, the inspectors

determined that the finding did not result in the loss of any accident mitigation capability and did

not require a quantitative risk assessment. This finding was determined to be of very low risk

-8-

significance. The inspectors determined that this finding had a cross-cutting aspect of

conservative bias in the human performance area, because the licensees staff ensured that the

proposed design change was safe in order to proceed rather than unsafe to stop [H.14].

(Section 4OA3.8)

Green. Several examples of a non-cited violation of 10 CFR Part 50, Appendix B, Criterion III,

Design Control, were identified involving the failure to ensure the adequacy of the anchorage

for several raw water system and containment spray system pipe supports. Specifically the

anchorage design was non-conservative with respect to the design basis requirements. The

licensee entered these issues into the corrective action program as CR 2013-05304 and

performed an operability determination as immediate actions. Long term actions to resolve the

errors in the calculations are documented in the condition report.

The performance deficiency was determined to be more than minor because it was associated

with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone

objective of ensuring the availability, reliability, and capability of the containment spray system

and raw water system. Using Inspection Manual Chapter 0609, Attachment 4 Initial

Characterization of Findings, and Appendix A The Significance Determination Process (SDP)

for findings at-power, both dated 6/19/12, the inspectors determined the performance

deficiency affected the mitigating systems cornerstone and screened to Green because the

finding affected the design and qualification of a mitigating component but remained operable.

The inspectors used the at-power SDP because the condition existed since construction and

while the plant was predominantly at power. The inspectors determined there was no cross-

cutting aspect associated with this finding because the calculations were from the 1980s and

therefore were not reflective of current performance. (Section 4OA5.1)

Green. A non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was

identified involving the failure to ensure the adequacy of the U-bolts for containment air cooler

pipe supports VAS-1 and VAS-2. Specifically the U-bolt design was non-conservative with

respect to the design basis requirements. The licensee entered these issues into the corrective

action program as CR 2013-03722. The licensee revised the calculation to support operability.

In addition, the licensee generated engineering change EC59570 to fix the degraded VAS-1 and

VAS-2 supports.

The performance deficiency was determined to be more than minor because it was associated

with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone

objective of ensuring the availability, reliability, and capability of several safety injection tank

valves. Specifically, the one-directional U-bolts for VAS-1 and VAS-2 are not designed to

withstand two-directional loading and the condensate drain piping line has the potential to

adversely impact the safety injection tank discharge isolation valves HCV-2934 and HCV-2974

during a design basis event. The licensee updated calculation FC05918 and provided an

operability evaluation to address the degraded condition. The inspectors reviewed the

information and did not find any issues. Using Inspection Manual Chapter 0609, Attachment 4

Initial Characterization of Findings, and Appendix A The Significance Determination Process

(SDP) for findings at-power, both dated June 19, 2012, the inspectors determined performance

deficiency affected the mitigating systems cornerstone and screened to Green because the

finding affected the design and qualification of a mitigating SSC but remained operable. The

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inspectors used the at-power SDP because the condition existed since construction and while

the plant was predominantly at power. The inspectors determined there was no cross-cutting

aspect associated with this finding because the calculation was from the 1980s, and therefore

was not reflective of current performance. (Section 4OA5.2)

Cornerstone: Barrier Integrity

Green. A cited violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was

identified involving the failure to take timely corrective action for a condition adverse to quality.

Specifically, the licensee failed to restore compliance following NRC identification of the

licensees failure to correct a runout condition of the containment spray system (CS)

documented in NCV 05000285/2008003-05, in August 2008. Licensee corrective actions to

correct the issue included completion of an analysis of containment spray pump operation

during the main steam line break (MSLB) event; revision of CS design documentation; analysis

of motor performance by an electrical vendor; and completion of a temporary modification to

throttle the CS pump discharge valves to provide additional system resistance preventing pump

runout. Future corrective actions include a permanent design change to prevent CS pump

runout. The licensee initiated CR 2014-02242 on February 19, 2014, to document this failure to

restore compliance.

This finding was more than minor because it adversely impacted the Barrier Integrity

cornerstone objective to provide reasonable assurance that physical design barriers

(containment) protect the public from radionuclide releases caused by accidents or events. The

inspectors reviewed NRC IMC 0609, Attachment 4, Initial Characterization of Findings, Table 3

- SDP Appendix Router. While this issue was identified during a refueling outage, the

inspectors determined that the majority of the exposure time for this violation occurred with the

reactor at power and should be evaluated using the Significance Determination Process in

accordance with IMC 0609, The Significance Determination Process (SDP) for Findings at-

Power, Appendix A, Exhibit 3, Barrier Integrity Screening Questions. The inspectors

determined that the finding did not represent an actual open pathway in containment or

containment isolation logic, nor did the finding represent an actual reduction in the function of

containment hydrogen igniters. Based on the guidance in the Exhibit 3 checklist the inspectors

determined that the finding was of very low safety significance.

The inspectors determined that the finding had a cross-cutting aspect of avoiding complacency

in the human performance area, because the licensees staff failed to recognize latent issues

even while expecting successful outcomes [H.12]. (Section 4OA3.8)

Other Findings and Violations

SL-IV. A Severity Level IV non-cited violation of 10 CFR 50.46, Acceptance criteria for

emergency core cooling systems (ECCS) for light-water nuclear power reactors, was identified

involving the failure to submit a report within 30 days of discovery of a significant change in the

application of the ECCS model that affected the peak cladding temperature. The licensee

submitted the required 10 CFR 50.46 report late on September 20, 2013 (ML13266A108). This

report was subsequently reviewed by the NRC staff date October 2, 2013, and determined to be

- 10 -

acceptable. The NRC staff determined that while the configuration change to the HPSI system

resulted in a higher peak cladding temperature, it is within the regulatory requirements of

10 CFR 50.46(b)(1). The licensee initiated CRs-2014-00674 and 2014-01356 to address

issuance of the late report.

This performance deficiency was determined to be subject to traditional enforcement because it

impeded the regulatory process, in that the failure to submit a timely report of significant ECCS

analytical changes prevented the NRC technical staff from independently evaluating the

potential safety implications of reductions in safety injection flow into the reactor during an

accident. This violation was determined to be a Severity Level IV violation because it is

consistent with the examples in Paragraph 6.9.d of the NRC Enforcement Policy. Because this

violation is subject to traditional enforcement, no cross-cutting aspects have been assigned.

(Section 4OA3.2)

SL-IV. Two examples of a cited Severity Level IV violation of 10 CFR 50.73, Immediate

Notification Requirements for Operating Nuclear Power Reactors, were identified involving the

failure to submit a required licensee event report (LER) within 60 days following discovery of an

event requiring a report. In the first example, LER 2013-010-0 was submitted on July 2, 2013,

seventy-nine days after the flow imbalance was observed by the licensees staff. In the second

example, LER 2013-017-0 was submitted to the NRC on December 27, 2013, 62 days after the

event date on the licensees reportability evaluation and sixty-six days after a condition report

documented the reportable condition. The licensee initiated CR 2014-01358 on

January 29, 2014 to document this repetitive violation.

The violation was evaluated using Section 2.2.4 of the NRC Enforcement Policy, because the

failure to submit a required LER may impact the ability of the NRC to perform its regulatory

oversight function. As a result, this violation was evaluated using traditional enforcement. In

accordance with Section 6.9(d)(9) of the NRC Enforcement Policy, this violation was determined

to be a Severity Level IV violation. The inspetors determined that a cross-cutting aspect was

not applicable to this performance deficiency because the failure to make a required report was

strictly associated with a traditional enforcement violation. (Section 4OA3.4)

- 11 -

PLANT STATUS

The plant began the reporting period at 100% power. On January 9, 2014, the plant shutdown

in accordance with Technical Specification 2.0.1 because an intake structure river sluice gate

would not close. Following repairs, the plant reached citicality on January 12, 2014, and was

manually tripped shortly thereafter due to a control element assembly that would not move.

Following repairs the plant started up on January 13, 2014, and reached 100% power on

January 15, 2014, where it remained for the duration of the inspection period.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness to Cope with External Flooding

a. Inspection Scope

On January 8, 2014, the inspectors completed an inspection of the stations readiness to

cope with external flooding. After reviewing the licensees flooding analysis, the

inspectors chose one plant area that was susceptible to flooding:

  • Intake Structure, due to failure of sluice gates

The inspectors reviewed plant design features and licensee procedures for coping with

flooding. The inspectors walked down the selected areas to inspect the design features,

including the material condition of seals, drains, and flood barriers. The inspectors

evaluated whether credited operator actions could be successfully accomplished.

These activities constituted one sample of readiness to cope with external flooding, as

defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

- 12 -

1R04 Equipment Alignment (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant

systems:

  • January 6, 2014, Auxiliary Building Ventilation

The inspectors reviewed the licensees procedures and system design information to

determine the correct lineup for the systems. They visually verified that critical portions

of the systems were correctly aligned for the existing plant configuration.

These activities constituted one partial system walk-down sample as defined in

Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status

and material condition. The inspectors focused their inspection on two plant areas

important to safety:

  • January 28, 2014, Room 13, Mechanical Penetration Area, Fire Area 13
  • January 28, 2014, Room 18, Component Cooling Heat Exchanger Area, Fire

Area 33

For each area, the inspectors evaluated the fire plan against defined hazards and

defense-in-depth features in the licensees fire protection program. The inspectors

evaluated control of transient combustibles and ignition sources, fire detection and

suppression systems, manual firefighting equipment and capability, passive fire

protection features, and compensatory measures for degraded conditions.

These activities constituted two quarterly inspection samples, as defined in Inspection

Procedure 71111.05.

- 13 -

b. Findings

No findings were identified.

.2 Annual Inspection

a. Inspection Scope

On February 4, 2014, the inspectors completed their annual evaluation of the licensees

fire brigade performance. This evaluation included observation of one announced fire

drill. During this drill, the inspectors evaluated the capability of the fire brigade

members, the leadership ability of the brigade leader, the brigades use of turnout gear

and fire-fighting equipment, and the effectiveness of the fire brigades team operation.

The inspectors also reviewed whether the licensees fire brigade met NRC requirements

for training, dedicated size and membership, and equipment.

These activities constituted one annual inspection sample, as defined in Inspection

Procedure 71111.05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On February 11, 2014, the inspectors observed simulator training for an operating crew.

The inspectors assessed the performance of the operators and the evaluators critique of

their performance.

These activities constitute completion of one quarterly licensed operator requalification

program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

On January 22, 2014, the inspectors reviewed a risk assessment performed by the

licensee prior to to performing a maintenance run on Diesel Generator 1 and the risk

management actions taken by the licensee in response to the elevated risk.

- 14 -

The inspectors verified that this risk assessment was performed timely and in

accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant

procedures. The inspectors reviewed the accuracy and completeness of the licensees

risk assessment and verified that the licensee implemented appropriate risk

management actions based on the result of the assessment.

Additionally, on February 12, 2014, the inspectors observed portions of one emergent

work activity that had the potential to affect the functional capability of mitigating

systems. This activity involved the failure of the turbine driven auxiliary feedwater pump

steam admission Valve YCV-1045.

The inspectors verified that the licensee appropriately developed and followed a work

plan for these activities. The inspectors verified that the licensee took precautions to

minimize the impact of the work activities on unaffected structures, systems, and

components (SSCs).

These activities constitute completion of two maintenance risk assessments and

emergent work control inspection samples, as defined in Inspection Procedure 71111.13

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed three operability determinations that the licensee performed for

degraded or nonconforming structures, systems, or components (SSCs):

downstream of heat exchanger AC-1A

structure

10 recirculation valve), due to non essential parts

The inspectors reviewed the timeliness and technical adequacy of the licensees

evaluations. Where the licensee determined the degraded SSC to be operable, the

inspectors verified that the licensees compensatory measures were appropriate to

provide reasonable assurance of operability. The inspectors verified that the licensee

had considered the effect of other degraded conditions on the operability of the

degraded SSC.

These activities constitute completion of three operability and functionality review

samples, as defined in Inspection Procedure 71111.15.

- 15 -

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed two post-maintenance testing activities that affected risk-

significant SSCs:

  • January 30, 2014, Post-maintenance testing following the overhaul of the Diesel

Auxiliary Feedwater Pump FW-54

  • January 10, 2014, Post-maintenance testing Hot Leak Check following

mechanical penetration M-45 piping swagelock replacement

The inspectors reviewed licensing- and design-basis documents for the SSCs and the

maintenance and post-maintenance test procedures. The inspectors observed the

performance of the post-maintenance tests to verify that the licensee performed the tests

in accordance with approved procedures, satisfied the established acceptance criteria,

and restored the operability of the affected SSCs.

These activities constitute completion of two post-maintenance testing inspection

samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed five risk-significant surveillance tests and reviewed test results

to verify that these tests adequately demonstrated that the SSCs were capable of

performing their safety functions:

In-service tests:

  • January 29, 2014, AC-10C Raw Water Pump Quarterly Inservice

Test, OP-ST-RW-3021

Reactor coolant system leak detection tests:

  • February 4, 2014, Manual leak rate calculation

Other surveillance tests:

- 16 -

  • January 23, 2014, Quarterly functional test of Power Range Safety Channels

A/B/C/D, IC-ST-RPS-0002/3/4/5

  • February 12, 2014, Operability Test of instrument air valve IA-YCV-1045-C and

Close Stroke Test of YCV-1045, IC-ST-IA-3009

Check Valve Tests, OP-ST-AFW-3011

The inspectors verified that these tests met technical specification requirements, that the

licensee performed the tests in accordance with their procedures, and that the results of

the test satisfied appropriate acceptance criteria. The inspectors verified that the

licensee restored the operability of the affected SSCs following testing.

These activities constitute completion of five surveillance testing inspection samples, as

defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Security

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items

entered into the licensees corrective action program and periodically attended the

licensees condition report screening meetings. The inspectors verified that licensee

personnel were identifying problems at an appropriate threshold and entering these

problems into the corrective action program for resolution. The inspectors verified that

the licensee developed and implemented corrective actions commensurate with the

significance of the problems identified. The inspectors also reviewed the licensees

problem identification and resolution activities during the performance of the other

inspection activities documented in this report.

b. Findings

No findings were identified.

- 17 -

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) LER 05000285/2012-013-00: Inadequate Calculation of Uncertainty Results in a

Technical Specification Violation

Technical Data Book Procedure (TDB)-III.40, Technical Specification Required SIRWT

Levels, lists the administrative requirements to maintain the Technical Specification (TS)

required Safety Injection Refueling Water Tank (SIRWT) levels. The required SIRWT level

for TS 2.3 accounts for instrument uncertainty, as described in the basis for TS 2.3.

However, the required SIRWT levels listed in TDB-III.40 for TS 2.2.7 and 2.2.8 do not

account for instrument uncertainty. Therefore, the TS described levels in TS 2.2.7 and 2.2.8

did not adequately account for SIRWT instrument level uncertainty. As a result, using the

levels described in TDB-III.40 for compliance with TS 2.2.7 and 2.2.8 was non-conservative.

The causal analysis (2011-9956) concluded that there was inadequate/incomplete

procedural guidance for developing Administrative Limits used to protect TS Limits. This

includes guidance for understanding how to evaluate and apply uncertainties when

developing TS Administrative Limits.

The licensee has revised procedures to include guidance on the development of new

Technical Specification limits and the associated administrative limits. The licensee

performed an extent of condition based on criteria in RG 1.97, Criteria for Accident

Monitoring Instrumentation for Nuclear Power Plants.

This Licensee Event Report is Closed.

.2 (Closed) Licensee Event Report 05000285/2013-003-01: Calculations Indicate the HPSI

Pumps will Operate in Run-out During a DBA

a. Inspection Scope

On January 30, 2013, the licensee identified that design basis calculations indicated that

the high pressure safety injection pumps would operate in a run out condition during

postulated accident conditions. The licensee issued Revision 0 of the LER to report that

this represented an unanalyzed condition, and that it was also an event or condition that

could have prevented the fulfillment of the safety function of the HPSI system.

The preliminary causal analysis identified that the cause of the condition was that the

station had failed to obtain vendor technical information on HPSI pump performance in a

10 CFR 50, Appendix B, quality assurance validated format. Corrective actions

identified in the LER included revising procedures to prevent HPSI operation in runout;

design changes to prevent HPSI operation in runout; and improving engineering

guidance related to review of vendor information and documentation of engineering

evaluations.

On November 27, 2013, the licensee submitted Revision 01 to the LER to update the

cause and corrective actions taken for the condition.

- 18 -

The inspectors reviewed both revisions of the LER, and identified a number of

observations and findings as described later in this report.

This Licensee Event Report is closed.

b. Review of OPPD Report 30-Day Report of a Significant Change in the Loss-of-Coolant

Accident (LOCA)/Emergency Core Cooling System (ECCS) Models Pursuant

to 10 CFR 50.46

Due to a deficiency associated with high pressure safety injection (HPSI) pump runout,

the licensee determined that a physical plant modification was required involving

installation of flow orifices to the HPSI discharge lines. The installation of these orifices

affected HPSI flow rate, which changed the emergency core cooling system (ECCS)

performance that is predicted using an evaluation model pursuant to the requirements of

10 CFR 50.46.

The inspectors reviewed the licensees report which was submitted to the NRC staff on

September 20, 2013, (ADAMS Accession number ML13266A108), per the requirements

of 10 CFR 50.46(3)(ii). The report included evaluation of the HPSI flow reduction for

both the Large Break Loss of Coolant Accident (LBLOCA) and Small Break Loss of

Coolant Accident (SBLOCA).

For the evaluation of LBLOCA, the licensee reported that the reduction in HPSI flow had

no impact on the predicted peak cladding temperature (PCT). The PCT for LBLOCA

continues to be 1581 degrees Fahrenheit. The inspectors observed that HPSI is a

system primarily designed to mitigate the effects of small break LOCAs, and did not

identify any issues with this estimate.

The licensee estimated the effect of HPSI flow reduction on the SBLOCA analysis,

and determined that the limiting break size decreased from a 3.5 inch diameter break to

a 3.0 inch diameter break. The HPSI flow reduction also caused an increase in PCT of

309 degrees Fahrenheit. The resulting PCT for SBLOCA is 1746 degrees Fahrenheit.

The inspectors determined that the revised PCT for the SBLOCA analysis reflects that

the licensee considered, in its estimate, both the effect of the change on the predicted

PCT for the limiting break size, and the potential for a new break size to be more

limiting. The licensees estimate also indicates that the estimated PCT remains below

the 2200 °F acceptance criterion contained at 10 CFR 50.46(b)(1).

The inspectors did not identify any issues of significance related to the technical content

of the 10 CFR 50.46 report. A violation was identified regarding the timeliness of this

report, as discussed in section 4OA3.2.d.1 of this report.

c. Review of Emergency Core Cooling System Performance

A review of Emergency Core Cooling System (ECCS) design and performance was

conducted by staff from the Reactor Systems Branch (SRXB) in the Office of Nuclear

Reactor Regulation (NRR). The review included an audit of High Pressure Safety

- 19 -

Injection (HPSI) pump operability, containment spray (CS) pump operability, vortex

issues, and void transport characteristics.

HPSI Pump Characteristics

A historical OPPD document was reviewed which listed developed head data for the

HPSI 2A, 2B, and 2C pumps as a function of flow rate. Recent pump vendor (Sulzer

Pumps, Inc.) analyses were reviewed which addressed expected degradation due to

wear by assuming that internal clearances may be postulated to increase by multiples of

1.5 and 2.0 applied to the nominal design clearances. Analysis results were determined

to be reasonable and the methodology appears to have been successfully applied by

Sulzer for other applications.

The original seal water cyclone separators did not have sufficient flow to provide self-

cleaning and were replaced. Recent evaluations of the replaced separators established

that the seal water system will operate acceptably.

HPSI Pump Runout Control

The licensees 2013 modification to the HPSI system acceptably limited HPSI pump flow

rate to less than 450 gpm. This was accomplished by inserting orifices in the pump

discharge pipes followed by testing that showed that the maximum flow rate occurred

with HPSI Pump 2B at 402 gpm with no flow in the mini-flow lines. Historical information

acceptably showed that open miniflow lines would increase runout flow rate by about

2 gpm, a negligible effect.

Orifice installation affected predicted ECCS evaluation model performance pursuant to

the requirements of 10 CFR 50.46. This was addressed by the licensee consistent with

the requirements of 10 CFR 50.46(3)(ii). The licensee reported that there was no impact

on the predicted peak cladding temperature (PCT) for the large break loss-of-coolant

accident (LBLOCA) and that PCT for the small break loss-of-coolant accident (SBLOCA)

increased by 309 °F to 1746 °F. Predicted PCTs remained below the 2200 °F

acceptance criterion contained at 10 CFR 50.46(b)(1). SRXB did not identify any issues

of significance.

Containment Spray (CS) Pump Runout Control

The CS pumps were recognized as subject to runout for two scenarios and the licensee

elected to address this issue by throttling the discharge valves to limit flow rate.

Containment aspects were found acceptable by the NRR Containment & Ventilation

Branch (SCVB) and valve characteristics were addressed by the Division of Engineering

Mechanical and Civil Engineering Branch and found acceptable. SRXBs assessment of

pump and motor issues is covered in the following paragraph.

The licensee used PROTO-FLO software to conclude that runout would be controlled

by changing flow rate from 1885 to 1500 gpm and from 3770 to 2800 gpm for the

single pump and two pump operating conditions, respectively. This was determined

to be achieved if each pump discharge valve was throttled to achieve a flow rate of

- 20 -

2515 +/- 25 gpm in a lineup where one CS pump draws from and recirculates back to the

Safety Injection Refueling Water Tank (SIRWT). 43 cases were analyzed by PROTO-

FLO plus another 10 cases to tune the code. SRXB determined that PROTO-FLO

acceptably calculated flow behavior. SRXB also determined that flow rate could be

acceptably controlled by the number of valve turns that correlated to calculated valve

opening.

SIRWT Draining, Vortex, and Void Movement Considerations

The SIRWT is a 25 ft by 100 ft rectangular tank with two ECCS 19.25 inch inside

diameter suction lines at one end. A cruciform vortex suppresser that extends into the

tank is installed in the entrance to each suction line. The SRXB inspectors performed an

exhaustive review of previous modeling of the SIRWT performance by a vendor, Fauske

& Associates. The inspectors noted that the analysis performed by Fauske &

Associates, and accepted by OPPD, contains a number of conservative as well as non-

conservative errors. The licensee documented the inspectors observations in

CRs 2013-21824 and 2013-21936. The licensee performed an immediate operability

determination which demonstrated that the cumulative impact of the errors did not

threaten the safety function of the SIRWT or the associated ECCS systems. The

inspectors reviewed this operability determination and concluded that it acceptably

addressed the inspectors concerns. The licensee also assigned several corrective

actions to update the affected analyses. Lastly, the licensee entered Action 2 from

CR 2013-21936 into the Performance Improvement Integrated Matrix (PIIM 2013-0086)

to track the licensees response to the inspectors observations prior to startup from the

next refueling outage.

Measurement of Flow Rate

The licensee documented inaccuracies in the installed HPSI flow rate instrumentation

that required installation of temporary ultrasonic flow rate meters (UFMs). The

inspectors determined that the UFMs provided accurate indication of flowrate. The

inspectors also noted that the installed instrumentation was of sufficient accuracy to

support use by operations during emergency conditions, but the inaccuracies prevented

appropriate flow indications for periodic pump testing as required by Technical

Specifications.

Water Hammer

Fauske described an experimental and analysis methodology program to assess water

hammer. The program showed that: (1) the gas void fraction for the initial stratified gas-

water configuration is essentially preserved during the water hammer event, (2) the peak

water hammer pressure is determined by the initial gas pressure and volume, the pump

shutoff head and whether the system is flushed before the test conditions are

established, (3) the peak force generated by the gas-water water hammer event is

determined by the peak pressure and the rate of rise of the water hammer

pressurization, (4) if the system piping includes a swinging check valve, the closure

induced by the water hammer event can cause subsequent forces, in both axial

directions (upstream and downstream), that are larger than the water hammer induced

- 21 -

force, and (5) the peak forces are a function of both the piping configuration and the

initial gas volume.

The licensee provided a water hammer evaluation of voids in suction piping. The

evaluation assumed that the moving gas/water column would instantaneously encounter

a rigid wall that corresponded to the HPSI suction location in an approach similar to that

provided by Fauske. There appear to be no cases where water hammer due to

compression of gas voids has caused actual pipe breaks. Therefore, SRXB judged that

water hammer is not of significant concern with respect to HPSI operation.

A violation was identified regarding the design control attributes of this inspection, as

discussed in Section 4OA3.2.d of this report.

d. Findings

i. Failure to Make Required 10 CFR 50.46 Report Within Required Time

Introduction. The inspectors identified a SLIV non-cited violation of 10 CFR 50.46,

Acceptance criteria for emergency core cooling systems for light-water nuclear

power reactors, for the licensees failure to submit a report within 30 days of

discovery of a significant change in the application of the ECCS model that affected

the peak cladding temperature.

Description. 10 CFR 50.46(a)(3)(i) states, in part, that each licensee shall estimate

the effect of any change in the application of an ECCS cooling evaluation model, to

determine if the change is significant. A change is considered significant if it results

in a calculated peak fuel cladding temperature different by more than 50° F from the

calculation of record. Paragraph (ii) requires that any significant change be reported

within 30 days to the NRC staff. 10 CFR 50.46(b)(1) provides an upper limit of

2200°F for maximum fuel element cladding temperature.

In early 2013, the licensee determined that a plant modification would be necessary

to prevent the runout of the installed high pressure safety injection (HPSI) pumps

during accident scenarios. This modification, which was installed in June 2013,

included installation of flow-restricting orifices in the discharge line of each HPSI

pump. As a result of the lower injection flows expected after the modification, the

licensee contracted an engineering firm to complete an analysis of the expected

increase in fuel temperatures that could be expected in an accident. The vendor

completed the analysis on July 26, 2013, which showed that in the most limiting

scenario, a small break loss of coolant accident, the reduced HPSI flow rates would

cause a 309° F increase in the peak cladding temperature. The licensee adopted

the vendors result in Engineering Analysis13-023, Fort Calhoun SBLOCA Analysis

with Reduced HPSI Flow (AREVA Calc. 32-9130020-001) on August 16, 2013, and

determined that the peak cladding temperature in the most limiting scenario (small

break loss of coolant accident) would be 1846°F, still well below the limit of 2200°F

specified in 10 CFR 50.46.

- 22 -

On August 1, 2013, the licensees staff initiated CR 2013-15442, documenting that

the AREVA report demonstrated the need to submit a 30 day report as required by

10 CFR 50.46(a)(ii). An action was assigned in the condition report to complete a

reportability evaluation by August 9 2013. A draft 10 CFR 50.46 report was created

by the condition report originator and provided to the Regulatory Assurance

department on August 12, 2013.

The licensees Regulatory Assurance department subsequently canceled the

reportability determination on August 27, 2013, and documented that the

10 CFR 50.46 reporting requirement did not apply. To justify this action, the

Regulatory Assurance staff provided the following quote from Nuclear Energy

Institute (NEI) Guide 07-05, 10 CFR 50.46 Reporting Guidelines, July 2008,

Section 2.2.11, Input Information:

The first category of input information is the basic engineering information that

describes a specific plant A change to input information of this type is not

considered a change to the evaluation model. Changes and error corrections in

this category are not reportable under 10 CFR 50.46.

The licensees position was that this type of change was not controlled by

10 CFR 50.46, and that any required action would be identified through compliance

with 10 CFR 50.59, Changes, Tests, and Experiments. The inspectors noted that

NEI 07-05 was not endorsed by the NRC staff, and sought guidance from the staff

responsible for reviewing 10 CFR 50.46 ECCS analysis at the Office of Nuclear

Reactor Regulation. Headquarters staff confirmed that the position described in

NEI 07-05 was not endorsed by the NRC and contradicts the requirement of

10 CFR 50.46(a)(3)(ii) which states, in part, that:

For each change toan acceptable model or in the application of such a model

that affects the temperature calculation, the holder of an operating

licenseshall report the nature of the change or error

Additionally, the inspectors noted that the NRC has endorsed NEI 96-07, Guidance

for Implementation of 10 CFR 50.59, Changes, Tests and Experiments, Revision 1.

NEI 96-07 specifically identifies that changes in anticipated fuel cladding temperature

are controlled by 10 CFR 50.46 and would not be subject to the process defined by

10 CFR 50.59.

The inspectors noted that the licensees procedure for completing reportability

determinations contributed to this error. Procedure SO-R-1, Reportability

Determinations, Attachment 8, paragraph 3.4.2 directs the licensees staff to follow

the format provided in NEI 07-05 for preparation of 30 day written reports. While the

report format in NEI 07-05 is generally consistent with 10 CFR 50.46, NEI 07-05

contains reportability guidance that is contrary to NRC regulations. This position

was communicated to the licensee by the NRC staff on September 12, 2013, and

the licensee was informed that the required report had not been submitted within

30 days as required by 10 CFR 50.46(a)(ii).

- 23 -

The licensee submitted the required 10 CFR 50.46 report September 20, 2013

(ML13266A108). This report was subsequently reviewed by the NRC staff date

October 2, 2013, and determined to be acceptable. The NRC staff determined that

while the configuration change to the HPSI system resulted in a significantly higher

peak cladding temperature, it is within the regulatory requirements of

10 CFR 50.46(b)(1).

The licensee initiated CR-2014-00674 on January 16 2014 to document the late

report submittal. The licensee initiated CR 2014-01356 on January 29, 2014 to

document the fact that Procedure SO-R-1 refers to NEI guidance, which is not

endorsed by the NRC.

Analysis. The failure to submit a written report within 30 days of discovery of a

significant change to the ECCS peak cladding temperature analysis is contrary to the

requirements of 10 CFR 50.46(a)(ii) and is a performance deficiency. This

performance deficiency was determined to be subject to traditional enforcement

because it impeded the regulatory process, in that the failure to submit a timely

report of significant ECCS analytical changes prevented the NRC technical staff from

independently evaluating the potential safety implications of reductions in safety

injection flow into the reactor during an accident. This violation was determined to be

a Severity Level IV violation, because it is consistent with the examples in

Paragraph 6.9.d of the NRC Enforcement Policy. Because this violation is subject to

traditional enforcement, no cross-cutting aspects have been assigned.

Enforcement. 10 CFR 50.46, Acceptance criteria for emergency core cooling

systems for light-water nuclear power reactors, states, in part, that any

significant change to a limiting ECCS analysis shall be reported to the NRC

within 30 days. Contrary to this requirement, the licensee determined that a

significant change had been made on August 1, 2013, but failed to submit the

required report until September 20, 2013. This violation is being treated as an

NCV, consistent with Section 2.3.2.a of the Enforcement Policy. The violation was

entered into the licensees corrective action program as CR 2014-00674.

(NCV 05000285/2014002-01, Failure to Make Required 10 CFR 50.46 Report

Within Required Time)

ii. Failure to Translate HPSI Pump Design Requirements to Design Documents

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50,

Appendix B, Criterion III, Design Control. Specifically, the licensee failed to

translate HPSI pump design and runout characteristics to design documents such as

the Updated Safety Analysis Report or design calculations.

Description. The emergency core cooling systems (ECCS) at Fort Calhoun Station

are designed to provide safety injection flow during various loss of coolant scenarios.

One of these systems, the high pressure safety injection (HPSI) system, contains

three centrifugal pumps which are capable of injecting water at high pressures into

- 24 -

each of the four reactor coolant loops. The inspectors noted that the original pump

curves provided by the manufacturer demonstrated expected pump performance to a

maximum tested flow of 425 gpm. Pump flows beyond the tested limits are

generally considered to be runout conditions, which can lead to rapid degradation of

pump internals and overload of pump motors.

The inspectors reviewed pre-operational testing reports from 1972 that demonstrated

initial attempts to prevent runout of the HPSI pumps. Additionally, special testing

was documented in 1976 that adjusted loop injection flows to avoid runout of the

pumps. Despite the constraints of the original design, on April 29, 1977, the licensee

removed the limit switch settings from the loop injection valves in an attempt to

increase HPSI injection flow based on un-validated information from the vendor that

HPSI pump runout for short periods of time was acceptable. The licensees

emergency procedures still contained steps that directed the operators to maintain

HPSI total flow below 400 gpm by manually throttling the loop injection valves, so the

net effect of this design change was to move the flow limiting design feature from an

automatic to a manual action. In a letter dated June 30, 1977, the NRC staff notified

OPPD of the safety importance of avoiding runout conditions in HPSI and LPSI

systems, and requested that the licensee determine if throttle valves were used in

the design to perform this function.

Other operational and design changes were made in the ensuing years that reduced

margins to runout conditions. These changes included changes to emergency

operating procedures that required HPSI to run at full capacity until certain throttling

criteria were met; cross-connecting HPSI trains to pressurize a containment

penetration; and ECCS logic changes which extended length of HPSI injection phase

prior to Recirculation Actuation Signal (RAS) beyond the limit proposed by the

vendor.

On January 30, 2013, while performing analysis in support of a planned modification,

the licensees staff determined that design basis calculations indicated that the HPSI

pumps would operate in a run out condition in some design basis accident

conditions. The licensee documented this condition in CR 2013-02100, which was

screened as Significance Level 2 and assigned a low-tier apparent cause evaluation.

The low-tier apparent cause evaluation was completed on March 21, 2013, and

documented that the apparent cause was that the station failed to obtain vendor

technical information in a 10 CFR 50, Appendix B, validated format. One

contributing cause was identified in that design basis documentation for the HPSI

system was lacking. The licensee submitted LER 2013-003-0 to the NRC on

April 1, 2013, reporting the unanalyzed condition. This LER also described the

apparent cause and planned corrective actions.

On May 21, 2013, due to a documented concern of potential NRC escalated

enforcement action, CR 2013-02100 was re-categorized as Significance Level 1 and

assigned a root cause investigation. The subsequent root cause evaluation was

completed on July 4, 2013. The licensee identified that the root cause was a lack of

rigorous engineering processes that allowed reductions in margin to runout. The

- 25 -

report also identified two contributing causes, in that the pump vendor had supplied

inaccurate information to the licensee, and incomplete design basis documentation.

One action to prevent recurrence was identified, as well as four new corrective

actions.

On July 11, 2013, NRC inspectors met with the licensee to discuss inspector

concerns with the root cause analysis. The inspectors shared a concern that over-

reliance on technical information from the pump vendor without adequate technical

review had prevented the licensee from recognizing this design control issue. The

licensee documented the inspectors concerns in CR 2013-14177. Following this

meeting, the licensees staff revised the root cause analysis on August 27, 2013.

This revised report identified a different root cause, in that HPSI pump impeller

design and runout characteristics identified during pre-operational testing were not

translated into FCS design and licensing basis documents. Several contributing

causes were also identified, including: limited staff understanding of HPSI pump

design; informal engineering evaluation of vendor-supplied information; failure to

internally communicate significance of identified concerns; and failure of the

corrective action program to react to adverse trend in vendor calculation

inaccuracies. This report also identified two actions to prevent recurrence and

19 corrective actions.

On August 28, 2013, NRC inspectors met again with the licensees staff to discuss

details from the July 4, 2013 version of the root cause analysis and LER 2013-003-0.

The licensee again revised the root cause analysis on September 12, 2013, adding

another contributing cause in that the licensee had failed to appropriately respond to

the NRCs June 1977 letter that specifically warned of the runout concern.

On June 21, 2013, the licensee completed Engineering Change 59874, which

permanently installed flow-limiting orifices in the discharge line of each pump,

effectively preventing HPSI pump runout conditions from occurring in any plant

condition. The inspectors reviewed this design change package, performed field

inspections of the completed modifications, and reviewed the results of the

completed post-modification testing. The inspectors also noted that the licensee had

completed a number of actions and has planned a broad range of programmatic

corrective actions to improve maintenance and knowledge of the plants design and

license basis.

On November 27, 2013, the licensee submitted Revision 1 to the LER to update the

cause and corrective actions taken for the condition.

Analysis. The inspectors determined that the licensees failure to translate HPSI

pump design and runout characteristics to design documents such as the Updated

Safety Analysis Report or design calculations was a performance deficiency. This

finding was more than minor because it adversely impacted the design control

attribute of the Mitigating Systems Cornerstone objective of ensuring the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences.

- 26 -

The inspectors reviewed IMC 0609 Attachment 4, Initial Characterization of

Findings, Table 3 - SDP Appendix Router. While this issue was identified during a

refueling outage, the inspectors determined that the majority of the exposure time for

this violation occurred with the reactor at power. As such, the inspectors determined

the finding should be evaluated using the SDP in accordance with IMC 0609, The

Significance Determination Process (SDP) for Findings at-Power, Appendix A,

Exhibit 2, Mitigating Systems Screening Questions. The finding required a detailed

risk evaluation because the high pressure safety injection system was inoperable for

some of the large break loss of coolant accident scenarios (at reactor pressures less

than 100 psi). Therefore, a Region IV senior reactor analyst performed a detailed

risk evaluation.

The analyst used the Fort Calhoun Standardized Plant Analysis Risk (SPAR) model,

Revision 8.20 with a truncation limit of E-11 to evaluate this performance deficiency.

Two Pumps Running Scenario: The licensees vendor calculated the expected

pump runout conditions. The vendor determined that runout conditions would occur

at a pump flow of 467 gallons per minute. At this flow rate, the pump discharge

pressure would be 244 psia. This particular scenario assumed two high pressure

safety injection pumps were running into two headers. The corresponding reactor

vessel pressure would be about 100 psia. Its important to note that the low pressure

safety injection system can support early injection and recirculation at this reactor

pressure. Experts from the NRCs Office of Nuclear Reactor Regulation reviewed

the calculation and found no significant errors.

For an initial risk estimate, the analyst set the failure to run basic events for the high

pressure safety injection pumps to a failure of 1.0. This included the train A and B

pumps as well as the swing Pump C. However, the analyst noted that the model

was not properly failing the pumps in some instances. Each time a high pressure

safety injection pump was included in the cutsets, the pump should have failed with a

probability of 1.0. In some instances the model failed the pump for other reasons

with a nominal failure probability (such as 3.8E-3 for being in test and maintenance).

To account for these errors, the analyst set the remaining high pressure safety

injection pump basic events (failure to start, and test and maintenance) to a failure

probability of 1.0.

Next the analyst determined that only the loss of coolant accident sequences were

affected by the performance deficiency. The analyst considered the following

definitions from the SPAR model documentation:

Small Loss of Coolant Accident - The small loss of coolant accident initiating

event is defined as a steam or liquid break in the reactor coolant system other

than a steam generator tube rupture which exceeds normal charging flow. In this

break size range, normally defined as between 3/8 in. and 2 in., normal charging

cannot maintain pressurizer level.

Medium Loss of Coolant Accident - The medium break loss of a coolant

accident initiating event is defined as a steam or liquid break that is large enough

- 27 -

to remove decay heat without using the steam generators but small enough that

RCS pressure is above the accumulator and low pressure injection system

shutoff pressure.

Large Loss of Coolant Accident - The large loss of coolant accident initiating

event is defined as a steam or liquid break that is large enough to rapidly

depressurize the reactor coolant system pressure to a point below the low

pressure injection and safety injection tank shutoff pressure. This break size is

generally defined as being greater than 5 in.

Interfacing System Loss of Coolant Accidents - Interfacing system loss-of-

coolant accidents are a class of accidents that can result in the over-

pressurization and rupture of systems that interface with the reactor coolant

system outside containment. These accidents have been a concern with regard

to public health risk due to the potential for fission product release directly to the

environment, bypassing the containment structure.

The analyst determined that only the large break and interfacing system loss of

coolant accidents should be quantified for this first scenario. In short, small and

medium break loss of coolant accidents would result in reactor pressure remaining

above the low pressure safety injection (195 psig) and safety injection tank

(240 psig) shutoff head conditions, especially considering that a high pressure safety

injection pump would be initially running. While it was possible to depressurize

below 195 psig as part of a normal shutdown, the residual heat removal system

would be employed for this purpose. This would aid operators in that they would

have control over decay heat removal and plant pressure. With the residual heat

removal system in operation, the high pressure safety injection system was not as

risk important.

Thus far, with the previously noted assumptions, the Delta-CDF was 2.8E-6/year.

The analyst noted that the SPAR model loss of coolant accident event tree did not

credit the low pressure safety injection system for early recirculation. If the high

pressure safety injection pumps failed during early recirculation, the event tree

transitioned directly to core damage. This was inconsistent with Emergency

Operating Procedure 20, Functional Recovery Procedure, Revision 25, in that the

procedure directed operators to inject with the low pressure safety injection system

for certain conditions (which include low pressure recirculation).

The low pressure safety injection pumps were capable of supporting recirculation

provided the reactor pressure was sufficiently low to allow pump operation. The low

pressure safety injection pumps provided a nominal discharge pressure of 175 psi.

The shutoff head for the pumps was approximately 194 psi. Since, however, the

reactor pressure of concern was 100 psi or less, the low pressure safety injection

pumps were capable of providing the recirculation function.

Given a high pressure safety injection system failure, the analyst determined that

credit for low pressure safety injection recirculation should be provided. To provide

- 28 -

credit, the analyst solved the low pressure recirculation fault tree to determine the

overall system failure probability (1.3E-3). Since the pumps automatically tripped on

a recirculation actuation signal, operators would need to manually start and align the

pumps for injection. The nominal human error probability from NUREG/CR-6883,

The SPAR-H Human Reliability Analysis Method, was 1.1E-2. The analyst added

these two values together for a total failure probability of 1.2E-2.

With this credit, the resultant Delta-CDF was:

Delta-CDF = 2.8E-6 * 1.2E-2 = 4E-8/year

This result was conservative because the analyst provided no credit for operator

recognition of runout conditions or mitigating actions to preclude pump damage.

Operators received training on runout conditions but it was unclear if adequate

indications were available in the control room.

One Pump Operating Scenario: The analyst considered a second scenario where

only one of the high pressure safety injection pumps was available for injection - the

other two pumps were unavailable because of random failures or for maintenance.

For this scenario, the analyst could not conclude that reactor pressure would be

sufficiently low to allow the low pressure safety injection system to inject. Therefore,

no credit was provided for this function.

The SPAR model specified that the failure probability for a single high pressure

safety injection pump (including unavailability for maintenance) was 5.1E-3. Since

there are two normally aligned pumps, either pump could be unavailable. The

probability that either the A or B pump was unavailable was approximately 1.2E-2. In

addition, if one pump failed or was unavailable, operators could place the swing high

pressure safety injection pump into service. The analyst considered that operators

could fail to properly perform this action. The nominal human error probability for an

operator manual action was 1.1E-2. As with the A and B pumps, the pump could

fail once placed into service, or otherwise be unavailable because of maintenance.

The total unavailability for the C pump was 1.2E-2 + 1.1E-2 = 2.3E-2. Therefore,

the total probability that only one pump would be available for injection

was 1.2E-2 * 2.3E-2 = 2.8E-4.

The analyst used the SPAR model and set the high pressure safety injection pump

common cause failure to run probability to 2.8E-4. This meant that if two pumps

were unavailable, the third pump would fail. The nominal common cause failure to

run probability was E-7.

This particular scenario was identified during plant simulator demonstrations.

Specifically, for a 3 inch pipe break, and one pump running, the inspectors identified

that it was possible for the high pressure safety injection pump to fail without first

lowering reactor pressure to less than the low pressure safety injection pump

discharge head. This correlated to the medium break loss of coolant accident in the

- 29 -

NRCs SPAR model. Therefore, the analyst solved the medium break loss of coolant

accident and the intersystem loss of coolant accident sequences.

The analyst noted that this assumption was generally inconsistent with the SPAR

model bases document, in that the medium break loss of coolant accident pressure

could drop below the accumulator shutoff pressure (about 275 psig). Plant pressure

would need to drop below this pressure to establish the runout conditions where

pump damage could occur.

The Delta-CDF was 4.2E-8/year.

Total Delta-CDF: The total Delta-CDF was:

Delta-CDF = 4E-8 + 4.2E-8 = 8.2E-8/year

The analyst determined that the finding was of very low safety significance (Green).

The dominant core damage sequences included large break loss of coolant

accidents where the high and low pressure safety injection systems both failed

during early low pressure recirculation. The low pressure safety injection system

helped to minimize the risk.

Since the change to the core damage frequency was less than E-7, the analyst was

not required to evaluate 1) external events, or 2) the effect on the large early release

frequency.

The inspectors determined there was no cross-cutting aspect associated with this

finding because events related to identification of needed procedures and

specifications occurred in the 1970s and are not indicative of current performance.

Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control states, in part,

that measures shall be established to assure that applicable regulatory

requirements and the design basis, as defined in 10 CFR 50.2, for those structures,

systems, and components to which this appendix applies are correctly translated into

specifications, drawings, procedures, and instructions. Contrary to this requirement,

from April 29, 1977 to June 21, 2013, the licensee failed to translate HPSI pump

design and runout characteristics to design documents. This violation is being

treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy. The

violation was entered into the licensees corrective action program as

CR 2013-02100. (NCV 05000285/2014002-02, Failure to Translate HPSI Pump

Design Requirements to Design Documents)

.3 (Closed) LER 05000285/2013-007-01: Containment Air Cooling Units (VA-16A/B) Seismic

Criteria

CR 2013-02260 identified that a summary structural analysis (FC03901) indicated that

VA-15A/B (Containment Air Cooler/Filter) plenum was overstressed by 100 percent and that

VA-16A/B (Containment Air Cooler) plenum would have been overstressed during a design

- 30 -

basis seismic event. At the time of discovery, FC03901 indicated that VA-15A/B required

cross-bracing, which was added resulting in the equipment being operable. Since VA-16A/B

was overstressed, they were considered inoperable.

The licensee causal analysis determined that the design basis information was incomplete

at the beginning of commercial operation. A weakness in licensing basis knowledge and a

failure to internalize the importance of the design basis, resulted in the organization missing

repeated opportunities to correct the initial deficiencies and additional errors were created

over time. Also, the early culture established standards and expectations for the

organization that resulted in behaviors demonstrating that the operation of the facility was

more important than maintaining the license and design basis of the Station. This resulted

in long-standing, reinforced, and institutionalized behaviors that resisted external and

internal efforts to change.

The NRC identified the overstressed containment air cooler issue, and documented

non-cited violation NCV 05000285/2013012-04, Failure to adequately design containment

air coolers structural bracing in Inspection Report 0500285/2013-012 (ML 13144A772).

After the inspection report was issued, the licensee performed additional analysis that

concluded the containment coolers were inoperable, but would have been able to perform

their safety function. In addition, containment air coolers VA-16A and VA-16B were modified

to add structural bracing prior to plant restart.

This Licensee Event Report is Closed.

.4 (Closed) Licensee Event Report 05000285/2013-010-01: HPSI Pump Flow Imbalance

a. Inspection Scope

On May 3, 2013, it was identified that the high pressure injection pump injection flows to

the reactor coolant system were not balanced in accordance with the Fort Calhoun

Station (FCS) Updated Safety Analysis Report Section 14.15.5.2.

The licensee submitted LER 2013-010-0 on July 2, 2013 to report a condition that could

have prevented the fulfillment of a safety function, and as a condition that caused

multiple trains of a safety system to become inoperable. The initial revision of this LER

contained very little detail and stated that a supplemental report would be made

following completion of a causal analysis. The licensee completed an apparent cause

evaluation in CR-2013-09949 on October 2, 2013, and subsequently issued Revision 1

of this LER on October 23, 2013.

The licensee determined that the cause of the event was failure to translate the plant

physical design into design documents, which allowed plant engineers to modify

important plant design aspects without understanding the potential safety impact. The

licensee implemented a design change to restore balanced flows in the HPSI injection

lines and updated design documents to reflect the importance of maintaining balanced

injection flows.

- 31 -

This Licensee Event Report is closed.

b. Findings

i. Failure to Maintain Design Control of HPSI Injection Valves

Introduction. The inspectors identified two examples of a Green non-cited violation

of 10 CFR 50, Appendix B, Criterion III, Design Control. The first example involved

the licensees failure to establish procedures or technical specifications to

accomplish required HPSI injection flow balancing. The second example involved

the failure to provide controls or testing to ensure that replacement parts for HPSI

injection valves were suitable for the application and were capable of supporting the

safety-related functions of the HPSI system.

Description. The emergency core cooling systems (ECCS) at Fort Calhoun Station

are designed to provide safety injection flow during various loss of coolant scenarios.

One of these systems, the high pressure safety injection (HPSI) system, contains

three centrifugal pumps which are capable of injecting water at high pressures into

each of the four reactor coolant loops. Each loop is provided with an injection line

from the A and B HPSI train, and as such the HPSI system provides a total of eight

injection lines into the reactor coolant system. Each injection line is provided with a

motor-operated injection valve to allow isolation or throttling of flow.

The original safety evaluation report for Fort Calhoun Station did not specifically

describe the balancing of HPSI loop injection flow rates. Injection line flow balancing

was, however, part of original plant design, and was accomplished by the use of limit

switches on each injection valve that stopped the valve travel at a pre-defined

position. The inspectors reviewed pre-operational testing reports from 1972 that

established these balanced flows. Additionally, special testing was documented in

1976 that adjusted loop injection flows to maintain this balance.

Despite the constraints of the original design, in April 1977 the licensee removed the

limit switch settings from the loop injection valves in an attempt to increase HPSI

injection flow. This had the unrecognized and undesirable effect of defeating the

original design intent of maintaining balanced loop injection flows. The licensees

emergency procedures still contained steps that directed the operators to maintain

balanced injection flows, so the net effect of this design change was to move the flow

balancing design feature from an automatic to a manual action.

In a letter dated June 30, 1977, the NRC staff notified OPPD of the safety

importance of maintaining balanced loop injection flow rates from the HPSI and LPSI

systems, and requested that the licensee determine if throttle valves were used in

the design to achieve the required flow balance. The letter further requested that if

throttle valves were used, the licensee should propose changes to technical

specifications to add a specific set of surveillance requirements that were included as

an attachment to the NRC letter.

- 32 -

The licensee provided a brief response to this letter on August 22, 1977, which

stated that throttle valves were not used to obtain the needed flow distribution from

the HPSI or LPSI systems. The licensee failed to inform the NRC that they had

originally been designed with throttled loop injection valves, but had removed this

important design feature just prior to receiving the letter from the NRC. As a result,

the surveillance requirements described in the June 30, 1977 letter were not added

to the Fort Calhoun Station Technical Specifications. The NRC staff reviewed this

correspondence against the requirements of 10 CFR 50.9, Completeness and

Accuracy of Information, and determined that due to the age of the issue no

enforcement action was appropriate (this regulation did not exist at the time of the

inaccurate communication). The inspectors noted that the licensee has documented

this inaccurate communication in CR 2013-09949.

Paragraph 14.15.5.2 of the Updated Final Safety Analysis Report (UFSAR)

describes that the analysis of record for the small-break loss of coolant accident

scenario assumes that the HPSI system flow was modeled to be evenly distributed to

the four reactor coolant system cold legs. UFSAR Paragraph 6.2.1 states that the

HPSI pump minimum flow rate is designed to provide sufficient injection capacity

assuming 25% spillage in the event that one of the four loop injection lines fails.

On April 14, 2013, the license performed a test on HPSI system to benchmark a

hydraulic flow model and determine if runout conditions were possible under Work

Order 480114. CR 2013-08300 was initiated on April 15, 2013, and included the raw

data from the testing, which also demonstrated that the injection flow was not

adequately balanced between the reactor coolant loops as described in the UFSAR.

The licensees safety analysis expected loop flows to be balanced within 10 gpm of

each other. Data collected during the test (see table below) showed differences as

high as 60 gpm between the highest and lowest loop injection flows. As a result, the

assumption in the safety analysis that HPSI could provide minimum flow with 25%

spillage was not satisfied, in that imbalanced injection flows could cause greater than

25% spillage should the line with the highest flow rate fail in an accident.

Valve Number RCS Loop Measured

Flow (gpm)

HCV-311 1B 80

HCV-314 1A 75

HCV-317 2A 135

HCV-320 2B 110

CR 2013-09949 was written on May 3, 2013, documenting a concern with the

observed flow imbalance. On June 17, 2013, the licensee calculated the flow

coefficients (Cv) for the eight HPSI injection valves as follows:

- 33 -

Valve Number RCS Loop Measured Cv

HCV-311 1B, Train B 13

HCV-312 1B, Train A 18*

HCV-314 1A, Train B 10

HCV-315 1A, Train A 18*

HCV-317 2A, Train B 22*

HCV-318 2A, Train A 11

HCV-320 2B, Train B 13

HCV-321 2B, Train A 13

  • identifies those valves which did not meet design Cv < 13

The licensee discovered that two of the injection valves (HCV-312 and HCV-315)

had been replaced in May 2005 and November 2003, (respectively) with valves from

a different vendor (Flowserve) than the original valves. The licensee specification

sheets for the replacement valves called for a maximum Cv of 13 to match the

existing design. Documents produced by the licensee demonstrated that quality

control issues with the supplied valves required the valves to be returned to the

vendor for disc and seat repairs prior to installation. The post-work testing performed

after these valve replacements included stroke-time testing and motor testing. No

post-maintenance testing was performed to ensure that the as-received valves met

the flow characteristic design requirement to ensure UFSAR assumptions regarding

balanced loop injection flows was sustained. Additionally, the licensee discovered

that the disc for HCV-317 had been replaced in November 1993, with a part that had

been provided meeting the original specification. As with the other valves discussed,

no post-maintenance testing was performed to ensure that the rebuilt valve met the

flow characteristic design requirement.

Licensee Event Report (LER) 2013-010-0 was submitted to the NRC on July 2, 2013

to report that the imbalanced flow issue could have prevented the HPSI system from

performing its safety function. This LER, however, lacked any meaningful details as

the licensee had yet to complete a causal evaluation for the loss of safety function.

The licensees apparent cause evaluation was completed on July 20, 2013 as a

Tier 2 apparent cause report. The initial version of the evaluation identified that the

apparent cause of the flow imbalance problem was inadequate post-maintenance

testing following engineering changes and maintenance to the HPSI loop injection

valves. Related causal factors included failure to identify a surveillance test for flow

balancing, lack of engineering understanding of the HPSI design and licensing basis,

and lack of supervisory technical oversight. Proposed corrective actions included

development of a periodic flow balancing test, revision to post-maintenance testing

- 34 -

instructions, improved technical training and documentation, and an audit of the

vendor who supplied the incorrect valves.

The licensee has since implemented Engineering Change 59874 which includes a

number of design modifications for the HPSI system. One of the included

modifications was re-throttling of the HPSI loop injection valves. This change was

completed on August 20, 2013, restoring the original plant design and correcting the

configuration control errors introduced on three of the eight injection valves. Post-

work testing for the completed modification included flow balance testing for the

HPSI loop injection lines. The inspectors reviewed the results of this testing and

determined that the UFSAR assumptions regarding balanced loop flows are now

reflected by HPSI system performance data.

NRC inspectors began onsite inspection activities related to HPSI system issues on

August 26, 2013. Based upon questions asked by NRC inspectors regarding the

actions proposed for CR 2013-09949, the licensee initiated CR 2013-17630 on

September 13, 2013, entitled Potentially inadequate cause evaluation for an LER.

The text of this CR included the following: Given the current regulatory interest in

this issue it appears that the cause analysis for this issue should receive a more

rigorous cause analysis and station management approval.

The licensee subsequently re-performed the apparent cause evaluation for

CR 2013-09949, and documented the results on October 2, 2013. While the

underlying CR was not upgraded to a higher status, the scope of the revised

apparent cause report scope included Updated the analysis to satisfy ACA Tier 1

requirements due to potential upgrade to ACA Tier 1 per CR 2013-17630. The

updated causal analysis included use of multiple analytical tools and identified two

underlying root causes that were not described in the initial apparent cause report.

The revised report also identified that the apparent cause was more fundamental in

nature, in that the original design of the HPSI loop injection valves was not translated

into design documents, which affected the quality of many processes including post-

maintenance testing. The revised report also identified a contributing cause related

to the licensee failing to appropriately respond to the NRCs June 30, 1977 letter that

provided specific direction to licensees to carefully control the configuration of throttle

ECCS injection valves.

Analysis. The inspectors determined that the licensees failure to establish

procedures or specifications to accomplish required HPSI flow balancing or to

provide appropriate controls or testing for replacement parts was a performance

deficiency. This finding was more than minor because it adversely impacted the

design control attribute of the Mitigating Systems Cornerstone objective of ensuring

the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences.

The inspectors reviewed IMC 0609 Attachment 4, Initial Characterization of

Findings, Table 3 - SDP Appendix Router. While this issue was identified during a

refueling outage, the inspectors determined that the majority of the exposure time for

- 35 -

this violation occurred with the reactor at power. As such, the inspectors determined

the finding should be evaluated using the SDP in accordance with IMC 0609, The

Significance Determination Process (SDP) for Findings at-Power, Appendix A,

Exhibit 2, Mitigating Systems Screening Questions. The inspectors answered yes

to the question of Does the finding represent a loss of system operability and/or

function? The inspectors therefore determined that the finding would require a

detailed risk evaluation per IMC 0609 Paragraph 6.0, because the operability of the

high pressure safety injection system (both trains) was in question. Therefore, a

Region IV senior reactor analyst performed a bounding detailed risk evaluation.

The analyst noted that the NRCs Standardized Plant Analysis Risk model included

system functional success criteria. The high pressure safety injection system

functional success criteria specified: delivery of water to the reactor vessel using

one high pressure safety injection pump and at least two out of four intact cold legs.

The flow imbalance specified in the functional success criteria was much worse than

the actual flow imbalance identified by the finding. Probabilistic risk assessments

focus on severe core damage whereas design basis requirements are focused on

the potential to exceed emergency core cooling system success criteria and 10 CFR

Part 100 limits, which are much more conservative. Since the high pressure safety

injection system was capable of meeting the functional success criteria, there was no

quantifiable change to the core damage frequency. The finding was not a significant

contributor to the large early release frequency.

The analyst determined that the finding was of very low safety significance (Green).

The dominant core damage sequences included loss of coolant accidents. However,

the high pressure safety injection system remained functional for its probabilistic risk

assessment function, which minimized the risk.

The inspectors determined there was no cross-cutting aspect associated with this

finding because events related to identification of needed procedures and

specifications occurred in the 1970s and are not indicative of current performance.

Additionally, the errant replacement of parts of three HPSI injection valves occurred

between 1993 and 2006, and are also not indicative of current performance.

Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control states, in part,

that measures shall be established to assure that applicable regulatory

requirements and the design basis, as defined in 10 CFR 50.2, for those structures,

systems, and components to which this appendix applies are correctly translated into

specifications, drawings, procedures, and instructions and that measures be

established for the selection and review for suitability of application of materials,

parts, equipment, and processes that are essential to the safety-related functions of

the structures, systems, and components.

Contrary to this requirement, from June 30, 1977 to present, the licensee failed to

establish procedures or Technical Specifications to accomplish required HPSI

injection flow balancing. Additionally, since October 1993, the licensee has failed to

provide controls or testing to ensure that replacement parts for HPSI injection valves

were suitable for the application and were capable of supporting the safety-related

- 36 -

functions of the HPSI system. This violation is being treated as an NCV, consistent

with Section 2.3.2.a of the Enforcement Policy. The violation was entered into the

licensees corrective action program as CR 2014-02305

(NCV-05000285/2014002-03, Failure to Maintain Design Control of HPSI Injection

Valves).

ii. Failure to Request a License Amendment for Required Change to Technical

Specifications

Introduction. The inspectors identified a Severity Level IV non-cited violation of

10 CFR 50.59, Changes, Tests, and Experiments, and an associated Green

finding, for the licensees failure to request a license amendment for a facility change

that required a change to the Technical Specifications. This issue is also associated

with a Green finding related to the licensees failure to follow Procedure NOD-QP-3,

10 CFR 50.59 and 10 CFR 72.48 Reviews, and Procedure FCSG-23,

10 CFR 50.59 Resource Manual, both of which require submittal of a license

amendment request prior to making a facility change that requires a change to

Technical Specifications.

Description. The emergency core cooling systems (ECCS) at Fort Calhoun Station

are designed to provide safety injection flow during various loss of coolant scenarios.

One of these systems, the high pressure safety injection (HPSI) system, contains

three centrifugal pumps which are capable of injecting water at high pressures into

each of the four reactor coolant loops. Each loop is provided with an injection line

from the A and B HPSI train, and as such the HPSI system provides a total of eight

injection lines into the reactor coolant system. Each injection line is provided with a

motor-operated injection valve to allow isolation or throttling of flow in the injection

line.

The original safety evaluation report for Fort Calhoun Station did not specifically

describe the balancing of HPSI loop injection flow rates. Injection line flow balancing

was, however, part of original plant design, and was accomplished by the use of limit

switches on each injection valve that stopped the valve travel at a pre-defined

position. The inspectors noted that pre-operational testing reports from 1972

established these balanced flows. Additionally, special testing was documented in

1976 that adjusted loop injection flows to maintain this balance.

Despite the constraints of the original design, in April 1977 the licensee removed the

limit switch settings from the loop injection valves in an attempt to increase HPSI

injection flow. This had the unrecognized and undesirable effect of defeating the

original design intent of maintaining balanced loop injection flows. The licensees

emergency procedures still contained steps that directed the operators to maintain

balanced injection flows, so the net effect of this design change was to move the flow

balancing design feature from an automatic design feature to a manual operator

action.

- 37 -

In a letter dated June 30, 1977, the NRC staff notified OPPD of the safety

importance of maintaining balanced loop injection flow rates from the HPSI and LPSI

systems, and requested that the licensee determine if throttle valves were used in

the design to achieve the required flow balance. The letter further requested that if

throttle valves were used, the licensee should propose changes to the Technical

Specifications to add a specific set of surveillance requirements that were included

as an attachment to the NRC letter.

The licensee provided a brief response to this letter on August 22, 1977, which

stated that throttle valves were not used to obtain the needed flow distribution from

the HPSI or LPSI systems. The licensee failed to inform the NRC that they had

originally been designed with throttled loop injection valves, but had removed this

important design feature just prior to receiving the letter from the NRC. As a result,

the surveillance requirements described in the June 30, 1977 letter were not added

to the Fort Calhoun Station Technical Specifications.

Paragraph 14.15.5.2 of the Updated Final Safety Analysis Report (UFSAR) currently

describes that the analysis of record for the small-break loss of coolant accident

scenario assumes that the HPSI system flow was modeled to be evenly distributed to

the four reactor coolant system cold legs. Additionally, UFSAR Paragraph 6.2.1

states that the HPSI pump minimum flow rate is designed to provide sufficient

injection capacity assuming 25% spillage in the event that one of the four loop

injection lines fails.

On April 14, 2013, the licensee performed a test on HPSI system to benchmark a

hydraulic flow model and determine if runout conditions were possible under Work

Order 480114. The data collected during this test demonstrated that the injection

flow was not adequately balanced between the reactor coolant loops as described in

the UFSAR. As a result, the assumption in the safety analysis that HPSI could

provide minimum flow with 25% spillage was not satisfied, in that imbalanced

injection flows could cause greater than 25% spillage should the line with the highest

flow rate fail in an accident. CR 2013-09949 was written on May 3, 2013, to evaluate

the flow imbalance problem. The initial version of the evaluation identified that the

apparent cause of the flow imbalance problem was inadequate post-maintenance

testing following engineering changes and maintenance to the HPSI loop injection

valves. The licensee also documented a conclusion that the request from the NRC

to initiate a Technical Specification Surveillance to periodically verify balanced flow

was not responded to properly.

On June 17, 2013, the licensee determined the flow characteristics through each

HPSI injection line. During this testing, three of the eight injection valves failed to

meet the flow characteristics expected by the licensee. The licensee subsequently

discovered that injection valves in these three lines had been modified without

controlling their configuration to ensure the flow balancing characteristics of the

design were sustained.

- 38 -

The licensee has since implemented Engineering Change (EC) 59874 which

includes a number of design modifications for the HPSI system. One of the included

modifications was re-throttling of the HPSI loop injection valves. This change

restored the original plant design, and corrected the configuration control errors

introduced on three of the eight injection valves. Post-work testing for the completed

modification included flow balance testing for the HPSI loop injection lines. The

inspectors reviewed the results of this testing and determined that the UFSAR

assumptions regarding balanced loop flows are now reflected by plant performance.

While the design of the facility now supports the safety analysis, the plant Technical

Specifications no longer meet the criteria of 10 CFR 50.36. Specifically,

10 CFR 50.36(c)(3) requires that Technical Specifications include sufficient

surveillance requirements to assure that....facility operation will be within safety

limits, and that limiting conditions for operation will be met. As specified in the

NRCs letter of June 30, 1977, the use of throttle valves to ensure balanced loop

injection flow rates requires periodic surveillance testing. Current Technical

Specifications at Fort Calhoun Station do not include these surveillance tests. The

inspectors determined that the need for a Technical Specification change was

recognized by station personnel early in 2013. In a meeting with station

management on July 30, 2013, engineering staff who were leading the design

change effort documented their plans to submit a license amendment request to add

the needed surveillance requirement to the Technical Specifications prior to

completion of the modification.

On September 18, 2013, the proposed design change in EC 59874 was presented to

the Station Modification and Acceptance Review Team (SMART) for review in

preparation for approval by the Plant Review Committee. According to the minutes

of the meeting, the licensees staff initially proposed that the needed flow balancing

tests would be performed as surveillance tests in the future as required by

10 CFR 50.36(c)(3). The meeting minutes record that the decision was made by the

SMART to perform future flow balancing as a preventative maintenance task rather

than as a surveillance test. Discussions with participants in the meeting suggest that

station personnel expected that a license amendment request (LAR) would be

submitted sometime in the future to formalize the new maintenance procedure as a

surveillance test.

The final modification package for EC 59874 included a 10 CFR 50.59 applicability

determination form which was completed on October 2, 2013. This applicability

determination form required the reviewer to determine if the proposed activity

involved a change to the Technical Specifications or operating license. This question

was incorrectly answered in the negative. This response was contrary to the

licensees procedure. Procedure NOD-QP-3, 10 CFR 50.59 and 10 CFR 72.48

Reviews, Step 4.8.3 states the following; Any activity requiring prior NRC approval

or requiring a change to the Technical Specifications shall not be approved for

implementation until NRC approval has been obtained. Additionally, FCSG-23,

10 CFR 50.59 Resource Manual, step 4.2.1.H.1 states the following;

- 39 -

Per 10 CFR 50.59(c)(1), proposed activities that require a change to the Technical

Specifications.must be made via the license amendment process, 10 CFR 50.90.

Contrary to the requirements of NOD-QP-3 and FCSG-23, EC 59874 was

implemented on October 9, 2013, without the licensee requesting or receiving a

Technical Specification change to add the necessary surveillance requirements for

balancing HPSI injection line flow rates.

The inspectors also noted that during the final review process for EC 59874, a plant

employee serving as the modification independent reviewer documented the

following question: Why is it acceptable to proceed with this EC without a licensing

amendment request? In response the Regulatory Assurance staff incorrectly stated

that it was acceptable to implement the change, and then treat the Technical

Specifications as inadequate. In Paragraph 3.5.1 of EC 59874, the licensee clearly

stated the intention to use the guidance of NRC Administrative Letter (AL) 98-10 to

defer the needed Technical Specification change.

NRC Administrative Letter 98-10, Dispositioning of Technical Specifications That

Are Insufficient to Assure Plant Safety, dated December 29, 1998, was issued to

reiterate to addressees the NRC staffs expectations regarding correction of facility

Technical Specifications (TS) when they are found to contain non-conservative

values or specific incorrect actions. The inspectors contacted NRC staff responsible

for this guidance and validated that AL 98-10 was never intended to allow a facility to

avoid a necessary Technical Specification change prior to implementing a plant

modification. The licensees misapplication of this NRC guidance contributed directly

to a violation of 10 CFR 50.59(c)(1).

The licensee initiated CR 2014-01029 on January 23 2014, to document this

violation and track corrective actions.

Analysis. The failure to follow station procedures which required submittal of a

license amendment request prior to implementing the design change that throttled

HPSI injection line admission valves was a performance deficiency. This

performance deficiency was considered to be of more than minor safety significance

because it was associated with the procedure quality attribute of the mitigating

systems cornerstone and it adversely affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. Specifically, the failure to follow station

procedures for the 10 CFR 50.59 process caused the Technical Specifications to

become insufficient to ensure that the limiting conditions for operation will be met.

Using Inspection Manual Chapter 0609 Appendix G, Checklist 4, the inspectors

determined that the finding did not result in the loss of any accident mitigation

capability and did not require a quantitative risk assessment. This finding was

determined to be of very low risk significance (Green).

This performance deficiency was also determined to be subject to traditional

enforcement because it impeded the regulatory process, in that the failure to submit

- 40 -

a license amendment and add required surveillance testing was in violation of

10 CFR 50.59(c)(1)(i) and caused the Technical Specifications to be deficient with

respect to balanced HPSI injection flows assumed in the facility safety analysis.

This violation is associated with a finding that has been evaluated by the SDP and

communicated with an SDP color reflective of the safety impact of the deficient

licensee performance. The SDP, however, does not specifically consider the

regulatory process impact. Thus, although related to a common regulatory concern,

it is necessary to address the violation and finding using different processes to

correctly reflect both the regulatory importance of the violation and the safety

significance of the associated finding. This violation was determined to be a Severity

Level IV violation, because it is consistent with the examples in Paragraph 6.1.d of

the NRC Enforcement Policy.

The finding had a cross-cutting aspect in the training aspect of the human

performance cross-cutting area because the licensees staff failed to understand and

misapplied NRC generic guidance related to discovery of insufficient technical

specifications (H.9).

Enforcement. 10 CFR 50.59, Changes, Tests, and Experiments states in section

(c)(1), in part, that a licensee may make changes in the facility as described in the

final safety analysis report (as updated)without obtaining a license amendment

pursuant to paragraph 50.90 only if: (i) A change to the technical specifications

incorporated in the license is not required Contrary to this requirement, on

October 9, 2013, the licensee made a change to the facility as described in the final

safety analysis report without obtaining a license amendment pursuant to paragraph

50.90 when a change to the technical specifications incorporated in the license was

required. Specifically, the licensee completed a design change that throttled the

HPSI branch line injection valves and invoked a new required surveillance test

without obtaining a license amendment to add the surveillance requirement to

technical specifications. Because this finding was of very low safety significance

(Green), the associated violation was screened as Severity Level IV, and the

violation was entered into the licensees corrective action program as CR 2014-

01029, this violation is being treated as an NCV, consistent with Section 2.3.2.a of

the Enforcement Policy. (NCV 05000285/2014002-04, Failure to Request a License

Amendment for Required Change to Technical Specifications).

iii. Untimely Submittal of Required Licensee Event Reports

Introduction. The inspectors identified two examples of a cited Severity Level IV

violation of 10 CFR 50.73, Immediate Notification Requirements for Operating

Nuclear Power Reactors, for the licensees failure to submit a required licensee

event report within 60 days following discovery of an event requiring a report.

Description.

Example 1:

- 41 -

Paragraph 14.15.5.2 of the Updated Final Safety Analysis Report (UFSAR)

describes that the analysis of record for the small-break loss of coolant accident

scenario assumes that the HPSI system flow was modeled to be evenly distributed to

the four reactor coolant system cold legs. UFSAR Paragraph 6.2.1 states that the

HPSI pump minimum flow rate is designed to provide sufficient injection capacity

assuming 25% spillage in the event that one of the four loop injection lines fails.

On April 14, 2013, the licensee performed a test on HPSI system to benchmark a

hydraulic flow model and determine if runout conditions were possible under Work

Order 480114. The data collected during this test suggested a possible vibration

concern with the 2B HPSI pump. CR 2013-08300 was initiated on April 15, 2013 to

document the vibration concern. Included with the CR was the raw data from the

troubleshooting, which also demonstrated that the injection flow was not adequately

balanced between the reactor coolant loops as described in the UFSAR. The

licensee sent this data to an off-site vendor for review and analysis.

On May 3, 2013, the licensees staff initiated CR 2013-09949 to document the results

of the evaluation of the April 14 test data. This CR documented the conclusion that

the HPSI injection flows measured on April 14, 2013, were imbalanced, and that as a

result, the assumption in the safety analysis that HPSI could provide minimum flow

with 25% spillage was not satisfied.

An action was assigned from CR 2013-09949 to complete a reportability evaluation

for the condition. This reportability evaluation was assigned on May 17, 2013, and

given a due date of May 24, 2013. The due date for this action was subsequently

extended five times by the licensees staff prior to completion of the reportability

evaluation on June 14, 2013, sixty-one days after the data was observed on

April 14, 2013. Throughout this process, the event date listed was the date that

CR 2013-09949 documented the results of the evaluation of the data, rather than the

date the data was observed by the licensees staff. Additionally, the inspectors noted

that contrary to Procedure SO-R-1, Reportability Determinations, the reportability

evaluation was not reviewed by the Plant Review Committee. After being informed

of this process error, the licensee initiated CR 2014-00958. The inspectors

determined that this process error was of minor safety significance and did not

represent a finding.

The license submitted LER 2013-010-0 on July 2, 2013, sixty days after the initiation

of the CR on May 3, 2013, but seventy-nine days after the flow imbalance was

observed by the licensees staff. The licensee submitted an LER supplement on

October 23, 2013, as LER 2013-010-1.

The inspectors reviewed the LER to determine if it had been submitted with the time

required by 10 CFR50.73. Section 50.73(a)(1), requires, in part, that the licensee

submit a LER for any event of the type described in this paragraph within 60 days

after the discovery of the event. The inspectors noted that the licensees internal

procedure SO-R-1, Reportability Determinations, Revision 31 states in

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Paragraph 4.1.1 that Reportabilities shall be made based on the discovery date for

the event rather than the date when an evaluation of the event is completed in

accordance with NUREG 1022.

The inspectors reviewed the guidance of NUREG 1022, Event Report Guidelines:

10 CFR 50.72 and 50.73, Revision 3, and determined that the language in the

licensees procedure is generally consistent with that of NUREG 1022, Section 2.5,

Time Limits for Reporting. The inspectors noted that the NUREG 1022 guidance

also recognizes that some conditions require evaluation to determine if a reportable

condition exists. In these cases, the NUREG guidance explains that the evaluation

should proceed on a time scale commensurate with the safety significance of the

issue, and that when operability of the affected equipment is in doubt, appropriate

actions such as reporting should be commenced. The inspectors reviewed the

operability determination attached to CR 2013-08300 on April 15, 2013, (which

included the flow imbalance data) and noted that the licensee completed the

associated operability evaluation on same day the CR was written (April 15, 2013).

This operability evaluation documented that the HPSI system was already inoperable

due to the unrelated HPSI runout condition. Additionally, the flow imbalance

condition represented a loss of safety function for the HPSI system, a condition that

would normally require action to place the station in hot shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

and cold shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The inspectors determined that the eighteen day

delay between recording of the flow imbalance data in CR 2013-08300 and the

event date in the licensees reportability evaluation was not appropriate, and was

inconsistent with Procedure SO-R-1 and NUREG 1022. Based upon an event date

of April 15 2013, the LER should have been submitted no later than June 14, 2013,

as required by 10 CFR 50.73(a)(1).

Example 2:

On July 25, 2013, while responding to questions by NRC inspectors regarding runout

susceptibility of the containment spray pumps, the licensee discovered that

anticipated operating conditions during accident scenarios may exceed analyzed

limits for the pumps. The licensee documented this concern in CR 2013-15047.

Specifically, design basis calculations and vendor information for the containment

spray system did not describe acceptable pump operations at flows greater than

3000 gpm, which would exist in some accident scenarios. Additionally, no analysis

had been performed for a potential pump/motor coupling failure, which would require

the remaining containment spray pump to provide flow through both containment

spray headers.

On July 26, 2013, the licensee documented in the immediate operability

determination for CR 2013-15047 that no reportable condition existed due to

reportability evaluations written for CRs 2007-01530, 2007-02241, and 2008-01683.

CR 2013-19722 was written on October 22, 2013, which documented that new pump

curve for containment spray pumps revealed that anticipated motor loads would be

significantly above the horsepower rating for the motor. The containment spray

- 43 -

pump motors are rated for a nominal 300 BHP, and can be acceptably operated at

115 percent of this nominal motor load (i.e. up to a service factor of 1.15). Prior to

this evaluation, the design basis assumed that maximum containment spray pump

flow would be 3200 gpm, resulting in a motor load of 344 BHP and a service factor of

1.15. The new pump curve documented in CR 2013-19722 demonstrated that actual

motor load at 3200 gpm would be 365 BHP, for an unacceptable service factor

of 1.22. The motor vendor determined that under this load, the motors would be

expected to fail within approximately 10 minutes.

Based on questions from the NRC resident inspectors, the licensee initiated

CR 2013-19930 on October 25, 2013 to document the need to reconsider

reportability for the condition identified in CR 2013-15047. A reportability evaluation

was subsequently assigned as an Action Item 005 to CR 2013-15047 on October 26,

and completed on October 31,2013. This evaluation determined that the issues

described required reporting in accordance with 10 CFR 50.73. Licensee Event

Report 2013-017-0 was submitted to the NRC on December 27, 2013. This report

was submitted 57 days after the completion date of the reportability evaluation, but

62 days after the event date of October 26, 2013 on the reportability evaluation.

The inspectors also noted that the report was sent 66 days after CR 2013-19722

documented the potential overload condition.

Enforcement Policy Discussion:

The inspectors determined that this violation was repetitive in nature, as described in

the NRC Enforcement Policy. Paragraph 2.3.2(a)(3) of the NRC Enforcement Policy

provides that one of the criteria that must be met for a violation to be screened as a

non-cited violation is that the violation must not be repetitive, or if repetitive must

not have been identified by the NRC. Repetitive, with regard to this aspect of the

Enforcement Policy, is defined as follows:

A violation is considered repetitive if it could reasonably be expected to have

been prevented by the licensees corrective action for a previous violation. In

addition, a violation is considered repetitive if a previous licensee finding

occurred within the past 2 years of the inspection at issue, or the period between

the last two inspections, whichever is longer.

The inspectors noted that a similar violation had been documented in NRC

Inspection Report 2013008 dated July 16, 2013 (ML13197A261). That report

included NCV 05000285/2013008-43, entitled Untimely Submittal of Licensee Event

Reports. The NCV documented nine examples of LERs that were submitted later

than required by 10 CFR 73(a)(1). The NCV also documented that the late reports

were caused by a backlog of significant technical issues as well as a fundamental

misunderstanding about what constituted the time of discovery. Corrective actions to

address knowledge gaps involving the reportability process were initiated under

Condition Report CR 2012-03796, completed in July 2012. The inspection report

documented that following completion of these corrective actions, LERs submitted

- 44 -

after August 2012 were generally timely and met the 60 day requirement specified in

10 CFR 50.72(a)(1).

The inspectors reviewed the completion status of the licensees corrective actions for

NCV 05000285/2013008-43 as documented in CR 2012-03796. All but one of the

assigned corrective actions was completed prior to submittal of untimely

LER 2013-010-0 and LER 2013-017-0. The one remaining item was classified as a

long term corrective action assigned an original due date of August 31, 2012. The

scope of this action was to revise Procedure SO-R-1 to more closely align with the

Exelon fleet model. The due date for this remaining action has since been extended

nine times and is currently scheduled for completion in February 2014. The most

recent due date extension emphasized that the pending changes are enhancements

to the procedure... and Shift Managers have demonstrated the ability to perform

reportability determinations. The inspectors also noted that Procedure SO-R-1 has

been revised seven times since CR 2013-03796 was initiated on May 8, 2012, yet

the action in CAP has not been recorded as completed and errant reportability

evaluations continue to occur.

Given that most of the licensees corrective actions for NCV 05000285/2013008-43

were completed prior to the performance of the reportability evaluation for

CR 2013-09949 or CR 2013-15047, and that less than two years have transpired

since the violation was documented, the inspectors determined that this violation

meets the enforcement policy definition of a repetitive violation.

The licensee initiated CR 2014-01358 on January 29, 2014 to document this

repetitive violation.

Analysis. The inspectors determined that the failure to submit a required LER was a

violation of 10 CFR 50.73. The violation was evaluated using Section 2.2.4 of the

NRC Enforcement Policy, because the failure to submit a required LER may impact

the ability of the NRC to perform its regulatory oversight function. As a result, this

violation was evaluated using traditional enforcement. In accordance with

Section 6.9(d)(9) of the NRC Enforcement Policy, this violation was determined to be

a Severity Level IV violation. The team determined that a cross-cutting aspect was

not applicable to this performance deficiency because the failure to make a required

report was strictly associated with a traditional enforcement violation.

Enforcement. Title 10 of the Code of Federal Regulations, Section 50.73(a)(1),

requires, in part, that the licensee submit a LER for any event of the type described

in this paragraph within 60 days after the discovery of the event. Contrary to the

above, between June 14 and July 2, 2013, the licensee failed to submit a LER for an

event meeting the requirements for reporting specified in 10 CFR 50.73. This

violation is not being treated as a new violation. Instead, it is considered as a related

violation to the non-cited violation issued in July 2013, which dealt with nine

examples of a failure to submit timely LERs. This violation is being treated as a cited

violation, consistent with Section 2.3.2(a)(3) of the NRC Enforcement Policy:

- 45 -

VIO 05000285/2014002-05, Untimely Submittal of Required Licensee Event

Reports. (EA-14-037)

.5 (Closed) Licensee Event Report 05000285/2013-015-00: Unqualified Coating used as a

Water Tight Barrier in Rooms 81 and 82

On September 13, 2013, it was identified that the floor coatings in Rooms 81 and 82 may

not maintain its integrity during a high energy line break environment allowing water to

migrate into the rooms below which contain the diesel generators and safety related

switchgear. This was reported on September 23, 2013, under 10 CFR 50.72(b)(3)(ii)(8),

Unanalyzed Condition (Event Notification 49378). Fort Calhoun Station was shutdown in

MODE 5 when the condition was identified and entered into the station's corrective action

program as Condition Report 2013-17605.

Engineering is reviewing this condition and the evaluation performed in 2009 for a previous

condition. The completed results of this review will be used to update this report.

This Licensee Event Report is closed. Revision 1 of this Licensee Event Report was

submitted on February 14, 2014.

.6 (Open) Licensee Event Report 05000285/2013-015-01: Unqualified Coating used as a

Water Tight Barrier in Rooms 81 and 82

On September 23, 2013, it was identified that the floor structure in Rooms 81 and 82 may

not maintain its integrity during a high energy line break environment allowing water to

migrate into the rooms below that houses the diesel generators and safety related

switchgear. This was reported on September 23, 2013, under 10 CFR 50.72(b)(3)(ii)(B),

Unanalyzed Condition (Event Notification 49378). Fort Calhoun Station was shutdown in

MODE 5 when the condition was identified and entered into the station's corrective action

program as Condition Report 2013-18103.

A cause evaluation was completed and determined that corrective actions in CR 2009-0687

root cause analysis (RCA) did not resolve water intrusion into Auxiliary Building rooms

containing safety related equipment due to lack of technical rigor and flawed decision

making.

The floor in Room 82 was recoated. The seismic gap between containment and the

auxiliary building was sealed. All penetrations that had openings below 2 feet above the

floor were coated and the area around the impingement plate was sealed. Cracks in the

ceilings of the switchgear and upper electrical penetration rooms were repaired.

.7 (Open) Licensee Event Report 05000285/2013-016-00: Reporting of Additional High Energy

Line Break Concerns

On October 18, 2013, as part of an extent of condition for LERs 2012-017 and 2013-011,

Fort Calhoun Station (FCS) personnel identified a potential additional high energy line break

(HELB) concern with the piping associated with the letdown heat exchanger (LDHX).

- 46 -

Subsequently on November 5, 11, 16, and 20, additional HELB impacts were also identified.

These impacts involved increased loads on supports in the piping subsystem MS-4099

(main steam supply to FW-10), high energy line cracking (HELC) related to auxiliary steam

in various rooms in the power block, the assumptions made regarding diesel generator

operability during a HELB, and the quality of the steam to FW-10, the steam-driven auxiliary

feedwater pump.

It was previously determined and reported that FCS did not fully implement and/or maintain

the Electrical Equipment Qualification (EEQ) program to meet the requirements of

10 CFR 50.49. As a consequence, the equipment included in the EEQ program, the

systems included in the High Energy Line Break (HELB) Analysis and the environmental

conditions used by the EEQ program have not been maintained current or in an auditable

manner. In addition to the corrective actions (CA) to resolve the EEQ/HELB program issues

previously reported, additional CAs are being pursued to address the individual conditions

listed above.

.8 (Closed) Licensee Event Report 05000285/2013-017-00: Containment Spray Pump Design

Documents do not Support Operation in Runout

a. Inspection Scope

On July 25, 2013, in response to a question from the NRC, the licensee identified that

the containment spray pumps could experience runout conditions in some accident

scenarios, and that design basis documents for the system did not support operability.

Specifically, in the event that one of the two installed containment spray pumps

experienced a pump/motor coupling failure, the remaining pump would have attempt to

provide flow to both containment spray headers and would have failed due to motor

overload.

The licensee issued the LER 2013-017-0 on December 17, 2013 to report a condition

not allowed by Technical Specifications, that could have prevented the fulfillment of a

safety function, and as a condition that caused multiple trains of a safety system to

become inoperable. As a corrective action, the licensee implemented a temporary

modification that throttled a valve at the discharge of each containment spray pump to

prevent runout conditions from occurring. The licensee described plans to complete a

permanent modification in the future to prevent runout.

The required reduction in containment spray flow rates required further analysis by the

licensee to determine if the current Main Steam Line Break (MSLB) analysis in USAR

Table 14.16-3 is still bounding. The NRC technical staff reviewed the results of the

licensees evaluation of the impact of the modification on containment peak pressure

and temperature, and determined that the licensees MSLB accident containment

analysis was acceptable, and that the reduction in the containment spray system

flowrates did not require a license amendment.

- 47 -

In addition to the findings described below, the inspectors determined that this LER was

not submitted within the time required by 10 CFR 50.73(a)(1). The enforcement aspects

of this issue are discussed in Section 4OA3.4 of this report.

This Licensee Event Report is closed.

b. Findings

i. Failure to Restore Compliance for Containment Spray Runout Conditions

Introduction. The inspectors identified a cited Green violation of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action, for the licensees failure to take timely

corrective action for a condition adverse to quality. Specifically, the inspectors noted

that the licensee failed to restore compliance following NRC identification of the

licensees failure to correct runout conditions in the containment spray system

documented as NCV 05000285/2008003-05 in August 2008.

Description. The containment spray system at Fort Calhoun Station consists of two

safety-related centrifugal pumps which are designed to provide flow through either of

two spray headers in containment to lower the peak containment pressure during the

first twenty minutes of a main steam line break accident. Open cross-connect valves

between the discharge piping on each pump allow each pump to supply flow to both

headers. This configuration challenges the operability of the pumps in that a failure

of one of the pumps could cause the remaining pump to provide flow through both

spray headers and result in runout of the remaining pump and eventual pump failure

due to high vibrations or motor overload. This design vulnerability was identified by

the licensee as early as 1990, and interlocks were added to prevent both spray

header isolation valves from opening unless both containment spray pump motors

were running.

During an inspection performed under Inspection Procedure 95002, Supplemental

Inspection for One Degraded Cornerstone or Any Three White Inputs in a Strategic

Performance Area, on March 17, 2008, NRC inspectors identified an operability

concern with the response of the containment spray system. Specifically, the

inspectors identified a potential vulnerability in that a mechanical failure of a

containment spray pump (such as a pump shaft shear or a stuck discharge check

valve) could result in the runout failure of the remaining pump. These two scenarios

of concern were documented by the licensee in CR 2008-1666 and CR 2008-1683

respectively. Given the similarity of the pump shaft shear and failed check valve

scenarios, the licensee consolidated many of the needed corrective actions and

tracked them under CR 2008-1683.

In response to CR 2008-1666 and CR 2008-1683, station operators completed an

operability evaluation on March 19, 2008. This operability evaluation contained the

following discussion of the scenarios of concern:

The two events that credit Containment Spray are a Loss of Coolant Accident

(LOCA) and a Main Steam Line break (MSLB).During a MSLB the containment

- 48 -

heat removal capability of the CS system is provided in addition to the heat

removal capability of the containment Coolers.therefore the LOCA response

will be the one mainly addressed.

The licensee completed Safety Analysis for Operability (SAO) 2008-02 on

March 22, 2008 to define the conditions which must exist to assure operability until

final corrective action were taken. These steps included updating plant procedures

and the UFSAR to define operator actions to recognize pump shaft shear and check

valve failures; adding procedural requirements to ensure all containment fan coolers

remained operable until the start of the 2008 refueling outage; and completion of

Engineering Change 30663, GSI 191 Implementation, during the 2008 refueling

outage, after which SAO 2008-002 could be closed. The inspectors noted that the

purpose of EC 30663 was to provide the engineering justification for retaining the

existing containment sump strainer design. A necessary input to this EC was

completion of EC 40070, which eliminated the containment spray function for a

LOCA.

On May 5, 2008, the licensee completed an apparent cause evaluation for this

condition. The cause was determined to be less than adequate evaluation of the

single failure impact of CS system subcomponents on the containment spray

system. Several actions were identified to correct the condition, including closure of

SAO 2008-02; conducting training for engineering staff on identification of single

failures; and training for staff on procedure changes. Several additional actions were

identified to prevent recurrence including procedure revisions to clarify plant

modification procedural controls and clarify single failure criteria.

On May 28, 2008, the Plant Review Committee approved closure of SAO 2008-002

following completion of EC 30663. In the supporting memorandum to the Plant

Review Committee, the licensees staff wrote that After implementation of this EC,

the CS Pumps are no longer credited for a LOCA event. The inspectors noted,

however, that completion of EC 30663 did nothing to resolve the vulnerability of the

pump failure in the other design basis event for which containment spray was

credited (MSLB). Finally, the inspectors noted that on January 15, 2010, the

licensee documented that all actions necessary to address NCV 2008003-05 had

been completed, and on January 19, 2010, CR 2008-1683 was closed.

On July 18, 2013, NRC inspectors again inquired about the runout susceptibility of

the containment spray pumps. In response to these questions by the inspectors, the

licensee discovered that anticipated operating conditions during a MSLB scenario

may exceed analyzed limits for the pumps. The licensee documented this concern in

CR 2013-15047 on July 25, 2013. Specifically, design basis calculations and vendor

information for the containment spray system did not describe acceptable pump

operations at flows greater than 3000 gpm, which would exist within the first twenty

minutes of a main steam line break scenario. Additionally, no analysis had been

performed for a potential pump/motor coupling failure, which would require a single

containment spray pump to provide flow through both containment spray headers.

After subsequent analysis of the MSLB scenario by the motor vendor, the licensee

initiated CR 2013-19722 on October 22, 2013, which described that the acceptance

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review of a new pump curve for the containment spray pumps identified the motor

horsepower required was beyond the service factor of 1.15. A subsequent

reportability evaluation further documented that Additional evaluations performed by

an electric motor vendor to determine if the CS Pump motor can support operation in

a runout condition determined that the motor may fail after approximately 10 minutes

of operation. On December 27, 2013, the licensee reported this condition in

Licensee Event Report 2013-017-0 as a condition which was prohibited by the

plants Technical Specifications and as a condition that could have prevented the

fulfillment of the safety function of containment spray system.

Corrective actions taken for CR 2013-15047 included completion of an analysis of

containment spray pump operation in an MSLB event; revision of CS design

documentation; analysis of motor performance by electrical vendor; and completion

of a temporary modification which throttles the CS pump discharge valves to provide

additional system resistance and prevent runout. The action to change the system

resistance was completed on November 24, 2013, which put the station back into

compliance by correcting the condition adverse to quality originally identified by NRC

in NCV 2008003-05. Future corrective actions will include a permanent design

change to prevent CS pump runout.

Inspectors determined that this violation demonstrated that the licensee had failed to

restore compliance within a reasonable period of time after the previous violation

was identified, as described in Paragraph 2.3.2(a)(2) of the NRC Enforcement Policy.

Specifically, the inspectors noted that NCV 05000285/2008003-05, entitled

Inadequate Corrective Actions for a Containment Spray Design Deficiency,

described that the licensee had initiated CR 2008-01683 to document the violation.

The inspectors reviewed the disposition of CR 2008-01683, and determined that

neither the actions taken to correct the violation, nor the actions taken to prevent

recurrence were sufficient to resolve the performance deficiency. At the time that the

concern was again raised by NRC inspectors on July 18, 2013, CR 2008-01683 and

all of its associated corrective actions were already completed and closed.

During an extent of condition review for a runout concern in the HPSI system, the

licensee identified that design basis calculations FC07077 and FC07078 predicted

flowrates beyond the manufacturers pump curve. Action 2013-02100-008 was

assigned on April 17, 2013 to validate and document the CS pumps can operate

successfully and meet design requirements in their extended flow region The

language of the action item presumed a successful outcome, and on May 17, 2013

the action item was closed based upon previous vendor correspondence (i.e. no new

analysis was conducted), and the licensee documented that the CS pumps are

acceptable as is. No additional actions are required. This action and the

inadequate response represent a recent opportunity to identify and correct this

condition prior to NRCs actions in the matter.

The licensee initiated CR 2014-02242 on February 19, 2014 to document this failure

to restore compliance.

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Analysis. The inspectors determined that the licensees failure to correct a condition

adverse to quality was a performance deficiency. This finding was more than minor

because it adversely impacted the SSC and barrier performance attribute of the

Barrier Integrity cornerstone objective to provide reasonable assurance that physical

design barriers (containment) protect the public from radionuclide releases caused

by accidents or events.

The inspectors reviewed IMC 0609 Attachment 4, Initial Characterization of

Findings, Table 3 - SDP Appendix Router. While this issue was identified during a

refueling outage, the inspectors determined that the majority of the exposure time for

this violation occurred with the reactor at power. As such, the inspectors determined

the finding should be evaluated using the SDP in accordance with IMC 0609, The

Significance Determination Process (SDP) for Findings at-Power, Appendix A,

Exhibit 3, Barrier Integrity Screening Questions. The inspectors determined that

the finding did not represent an actual open pathway in containment or containment

isolation logic, nor did the finding represent an actual reduction in the function of

containment hydrogen igniters. Based on the guidance in the Exhibit 3 checklist the

inspectors determined that the finding was of very low safety significance.

The inspectors determined that finding had a cross-cutting aspect of avoiding

complacency in the human performance area, because the licensees staff failed to

recognize latent issues even while expecting successful outcomes (H.12).

Enforcement. Title 10 CFR 50, Appendix B, Criterion XVI, Corrective Action,

requires, in part, that Measures shall be established to assure that conditions

adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective

material and equipment, and nonconformances are promptly identified and

corrected. Contrary to the above, between August 12, 2008 and

November 24, 2013, the licensee failed to take adequate corrective action to assure

that a condition adverse to quality was corrected. Specifically, actions were not

taken to correct NRC-identified runout concerns in the containment spray system

until these concerns were again raised by the NRC on July 18, 2013. This violation

is not being treated as a new violation. Instead, it is considered as a continuation of

the non-cited violation issued in August 2008, which identified the licensees failure

to take corrective actions for runout concerns in the containment spray system. This

violation is being treated as a cited violation, consistent with Section 2.3.2(a)(2) of

the NRC Enforcement Policy: VIO 05000285/2014002-06, Failure to Restore

Compliance for Containment Spray Runout Conditions. (EA-14-037)

ii. Inadequate 10 CFR 50.59 Screening for Containment Spray Design Change

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings for the licensees

failure to complete a 10 CFR 50.59 screening that met the requirements of

NOD-QP-3, 10 CFR 50.59 and 10 CFR 72.48 Reviews, Revision 37.

Description. 10 CFR 50.59, Changes, Tests, and Experiments, contains

requirements for the process by which licensees may make changes to their

- 51 -

facilities and procedures as described in the safety analysis report, without prior

NRC approval, under certain conditions. Through the issuance of Regulatory

Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and

Experiments, the NRC endorsed industry-developed guidance for compliance with

10 CFR 50.59. This industry guidance, documented in NEI 96-07, Guidelines for

10 CFR 50.59 Evaluations, Revision 1, provides methods that are acceptable to the

NRC staff for complying with the provisions of the rule.

Section 4.2 of NEI 96-07 describes the process used to screen plant changes to

determine if further evaluation is required. This process involves answering a

number of screening questions. If any of these questions is answered in the

affirmative, the NEI guidance requires that the change be subjected to a evaluation

to determine if NRC review and approval is required prior to making the change.

The inspectors noted that the licensees guidance on implementation of the

10 CFR 50.59 rule is contained within two documents: NOD-QP-3, 10 CFR 50.59

and 10 CFR 72.48 Reviews, Revision 37, and FCSG-23, 10 CFR 50.59 Resource

Manual, Revision 8. Step 4.4.1.A of NOD-QP-3 requires plant personnel to

complete the screening activity using Form FC-154A and the guidance within

FCSG-23. Step 4.4.1.C requires the performer to provide written justification for

each of five questions to demonstrate that the overall conclusion is that an evaluation

is not required.

The inspectors reviewed the completed 10 CFR 50.59 screening that was performed

for Engineering Change (EC) 62416 on November 14, 2013. This EC was

implemented to change the normal position for the containment spray pump

discharge isolation valve from full open to throttled. This new position was required

to prevent the runout of the containment spray pumps in certain accident conditions,

and involved using the normally-open gate valve to throttle flow rates of up to

3000 gpm during accident conditions. During these operating conditions, the new

position of the gate valve would be approximately 80 percent closed, exposing the

valve to high differential pressures and creating a number of potentially unanalyzed

degradation mechanisms in the downstream piping, including vibration, flow erosion,

and debris blockage.

The inspectors noted that the completed FC-154A screening form answered no to

all five screening questions. The inspectors developed a concern with the licensees

response to Question 1, which asks the screener to answer the following question:

1. Does the proposed activity involve a change to an SSC that adversely affects

a UFSAR described design function?

The inspectors determined that this response was in error, in that the proposed

change adversely affected the UFSAR described design function of the containment

spray system, due to the possible adverse effects of throttling the gate valves on

the system valves and piping. The inspectors determined that in answering

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no to this question, the licensee failed to properly implement Step 4.4.1.C of

Procedure NOD-QP-3. After sharing this concern with the licensee, the licensee

initiated CR 2013-22007 documenting the procedural error. CR 2013-22007

recorded that the initial FC-154A screen had incorrectly determined that a

10 CFR 50.59 evaluation was not required. The licensees staff subsequently re-

performed the FC-154A screening form on November 29, 2013, and determined that

a 10 CFR 50.59 evaluation was required. The NRC staff reviewed the resulting

10 CFR 50.59 screening and evaluation and determined that they had been properly

performed, and that a license amendment request was not required prior to

implementation of the activity.

The licensee documented this procedural violation in CR 2014-01357 on

January 29, 2014.

Analysis. The failure to follow station procedures which required completion of an

accurate 10 CFR 50.59 screening of a design change was a performance deficiency.

This performance deficiency was considered to be of more than minor safety

significance because it was associated with the design control attribute of the

mitigating systems cornerstone and it adversely affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the failure to follow

station procedures for the 10 CFR 50.59 process prevented the licensees staff from

evaluating the adverse impacts of the change on the facility. Using Inspection

Manual Chapter 0609 Appendix G, Checklist 4, the inspectors determined that the

finding did not result in the loss of any accident mitigation capability and did not

require a quantitative risk assessment. This finding was determined to be of very low

risk significance (Green).

The inspectors determined that this finding had a cross-cutting aspect of

conservative bias in the human performance area, because the licensees staff

ensure that the proposed design change was safe in order to proceed rather than

unsafe to stop (H.14).

Enforcement. Title 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings states, in part, that activities affecting quality shall be prescribed by

documented procedures and accomplished in accordance with these procedures.

The licensee established Procedure NOD-QP-3, as the implementing procedure for

10 CFR 50.59 Reviews, an acivity affecting quality. Contrary to this requirement,

between November 13 and November 29, 2013, the licensee failed to accomplish an

activity affecting quality in accordance with the procedure. Specifically, the licensee

completed a 10 CFR 50.59 screening that did not meet the requirements of NOD-

QP-3, 10 CFR 50.59 and 10 CFR 72.48 Reviews, Revision 37. This violation is

being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy.

The violation was entered into the licensees corrective action program as

CR 2014-01357. (NCV 05000285/2014002-07, Inadequate 10 CFR 50.59

Screening for Containment Spray Design Change)

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.9 Open) Licensee Event Report 05000285/2013-019-00: Non-Seismic Circulating Water Pipe

Could Disable Raw Water Pumps

On December 2, 2013, NRC inspectors questioned the validity of an operability

determination performed by the station on a non-safety grade pipe in the Raw Water pump

vaults. The concern was determined to be valid and on December 3, 2013 at 0038 CST, an

operability evaluation for Condition Report (CR) 2013-22090 confirmed operability of the RW

pumps with interim actions to prevent circulating water flow from the affected 12 inch pipe

into the raw water vault during a seismic event. Interim compensatory actions to maintain

operability of the raw water pumps are to secure the screen wash system and establish a

clearance.

A cause analysis is in progress and an update to this LER will be provided with additional

information.

A design change was completed to eliminate the adverse interaction noted above.

These activities constitute completion of five event follow-up samples, as defined in Inspection

Procedure 71153.

4OA4 IMC 0350 Inspection Activities (92702)

Inspectors continued implementing IMC 0350 inspection activities, which included follow-up of

the restart checklist items contained in the Confirmatory Action Letter (CAL) issued

February 26, 2013 (EA-13-020, ML 13057A287). The purpose of these inspection activities was

to assess the licensees performance and progress in addressing its implementation and

effectiveness of FCSs Integrated Performance Improvement Plan (IPIP), significant

performance issues, weaknesses in programs and processes, and flood restoration activities.

Inspectors used the criteria described in baseline and supplemental inspection procedures,

various programmatic NRC inspection procedures, and IMC 0350 to assess the licensees

performance and progress in implementing its performance improvement initiatives. Inspectors

performed on-site and in-office activities, which are described in more detail in the following

sections of this report. This section documents inspection activities that occurred prior to

closure of the CAL on December 17, 2013. Specific documents reviewed during this inspection

are listed in the attachment.

The following inspection scope, assessments, observations, and findings are documented by

CAL restart checklist item number.

.3 Adequacy of Significant Programs and Processes

Section 3 of the Restart Checklist addresses major programs and processes in place at

FCS. Section 3 reviews also include an assessment of how the licensee addressed the

NRC Inspection Procedure 95003 key attributes as described in Section 6.

.b Equipment Design Qualifications

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This item of the Restart Checklist verifies that plant components are maintained within

their licensing and design basis. Additionally, this item provides monitoring of the

capability of the selected components and operator actions to perform their functions.

As plants age, modifications may alter or disable important design features making the

design bases difficult to determine or obsolete. The plant risk assessment model

assumes the capability of safety systems and components to perform their intended

safety function successfully.

(1) Safety-Related Parts Program

i. Inspection Scope

The team reviewed the licensees assessment of issues related to the safety-

related parts program at FCS. The team assessed the licensees equipment

design quality classifications review for inconsistent quality classifications.

Additionally, the team assessed the licensees review of the use of non-safety-

related parts in safety-related applications. Specifically, the team assessed the

RCA for CR 2012-05615, for which the problem statement was:

FCS did not maintain compliance in all cases to the Updated Safety Analysis

Report, Appendix A, Section 4.0, Design Control, such that non-safety graded

parts would not be installed in safety grade applications. This would result in

failure to comply with the FCS design basis. Design basis compliance is not

assured.

The team also assessed the adequacy of the extent of condition, extent of

causes, and corrective actions (CL Items 3.b.1.1; 3.b.1.2; 3.b.1.3).

The teams assessment of this RCA was based on the evaluation criteria from

Section 02.02 of NRC Inspection Procedure 95001, which aligned with this item.

The inspection objectives were to:

  • Provide assurance that the apparent and contributing causes of risk-

significant issues were understood

  • Provide assurance that the extent-of-condition and extent-of-cause of

risk-significant issues were identified

  • Provide assurance that the licensee's corrective actions for risk-significant

performance issues were, or will be, sufficient to address the apparent

and contributing causes and to preclude repetition

ii. Observations and Findings

Determine that the problem was evaluated using a systematic methodology to

identify the root and contributing causes.

- 55 -

The team determined that the licensee evaluated this problem using a systematic

methodology to identify the root and contributing causes. Specifically,

RCA 2012-05615 employed the use of event and causal factor charting, barrier

analysis, common factor analysis, and the why staircase. The licensee identified

the following as the root cause for why FCS has allowed non-safety-related parts

to be installed in safety grade applications:

RC-1: Inadequate procedural guidance and an ineffective training/mentoring

process have resulted in an ineffective work planning and review process

with the potential for non-CQE parts being installed where CQE parts are

required.

(CQE stands for critical quality element and is synonymous with safety-

related).

The licensees RCA also identified the following contributing causes (CC):

CC-1: A lack of adequate reference documents and resources/tools for

planners, engineers, and maintenance personnel to reference exists.

CC-2: Ownership of important resources (Bill of Materials, CQE List, Asset

Suite) is not known by Station personnel.

CC-3: Overconfidence in Station personnel abilities to accomplish work has

resulted in inadequate use of human performance tools and a rationalization

that current expectations, standards, and performance are sufficient for

Station needs.

CC-4: Station personnel were willing to work around Station procedures

using tribal knowledge (experience) to complete tasks which resulted in a

procedure use and adherence issue.

CC-5: The CAP has not fully assessed and effectively resolved identified

CQE issues.

CC-6: A station personnel knowledge gap exists for the CQE classification

boundaries and dedication requirements.

The team determined that these root and contributing causes reasonably explain

why the safety-related parts program at FCS failed to maintain design control

such that non-safety graded parts have been installed in safety grade

applications. However, the team identified that the RCA appeared to be

incomplete because it did not address the licensees ability to properly classify

structures, systems, and components as safety-related. NRCs Manual

Chapter 0350 Panel FCS Restart Checklist Basis Document, Item 3.b.1, Safety-

Related Parts Program, specifically identified that the NRC will assess the

licensees equipment design quality classifications review for inconsistent quality

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classifications. The licensee performed an operability evaluation regarding

piping code of record concerns and plans to review their CQE documentation

during their design basis reconstitution.

Determine that the root cause evaluation was conducted to a level of detail

commensurate with the significance of the problem.

The team determined that the RCA was conducted to a level of detail

commensurate with the significance of the problem. Specifically, as discussed

above, the licensee conducted this evaluation not only by using event and causal

factor charting, barrier analysis, and the why-staircase, but also by conducting

interviews, reviewing documents, and attending meetings. The licensees RCA

techniques were generally thorough and identified the root and contributing

causes of deficiencies in the safety-related parts program relative to work

planning and work control.

Determine that the root cause evaluation included a consideration of prior

occurrences of the problem and knowledge of prior operating experience.

The team determined that the RCA included evaluations of both internal and

industry operating experience. The team determined that the licensees

evaluations of industry operating experience provided sufficient detail such that

general conclusions could be established regarding any similarities.

Determine that the root cause evaluation addressed the extent of condition and

the extent of cause of the problem.

The team reviewed the licensees RCA as it relates to extent of condition and

extent of cause.

For extent of condition, the licensee evaluated the extent to which the actual

condition exists with other plant processes, equipment, or human performance.

The licensees analysis used the same-same, same-similar, similar-same, and

similar-similar evaluation method. The licensee concluded that the extent of

condition does exist relative to other processes, procedures, or commitments

where nonconformity with established requirements could result in a non-

compliance with the FCS design basis. The licensee also found that an extent of

condition may exist for nuclear safety culture which has not been fully addressed

by causal analysis but can affect the stations commitment to written agreements

related to the FCS design basis. The licensee initiated CR 2012-17437 to

address this extent of condition issue.

The team noted that the licensee did not specifically document where the actual

condition of non-safety-related components may exist in safety-related

equipment as part of the extent of condition. This was determined to be a

documentation oversight since, through interviews, the team found that the

licensee had a comprehensive plan to address this element of extent of condition

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established under Action Item 29 of CR 2011-09459 and CA-13 of

CR 2012-05615. That plan reviewed safety-related WOs for the past two cycles

to identify where non-safety parts were inappropriately used in safety-related

applications. The team found that these corrective actions would reasonably

address any current issues where non-safety-related components were used in

safety-related applications. The team determined that while the licensees

strategy to address extent of condition was technically sound, the failure of the

RCA to address weaknesses in the ability to classify safety-related components

could result in a less than adequate extent of condition review.

For extent of cause, the licensee reviewed the root causes of an identified

problem to determine where they may have impacted other plant processes,

equipment, or human performance. The licensees analysis determined that an

extent of cause does exist related to the adequacy of non-accredited training

programs. The licensee initiated CR 2012-18335 to address the issues identified

with non-accredited training.

Determine that the root cause, extent of condition, and extent of cause

evaluations appropriately considered the safety culture components as described

in IMC 0310.

The root cause, extent of condition, and extent of cause evaluations

appropriately considered the safety culture components as described in

IMC 0310. Specifically, the licensee documented their consideration of the

IMC 0310 cross-cutting aspects in Attachment 11 of RCA 2012-05615. The

licensee identified several cross-cutting aspects in the area of human

performance, problem identification and resolution, and other components were

applicable to issues related to deficiencies in identifying degraded/nonconforming

conditions and operability evaluations. The final evaluation concluded that only a

small number of the safety culture attributes were not to be applicable to

RCA 2012-05615.

Determine that appropriate corrective actions are specified for each root and

contributing cause.

The team reviewed the licensees corrective actions for each of the root and

contributing causes. The team found that the corrective actions addressed the

root and contributing causes for why the licensee has allowed non-safety graded

parts to be installed in safety grade applications. The team noted that the

corrective actions focused primarily on work planning procedure changes and

development and implementation of training for work planners. The team also

found that Corrective Action 13 of CR 2012-05615 which implemented a review

of the past two cycles of safety-related work order adequately addressed the

extent of condition relative to where non-safety parts may have been

inappropriately used in safety-related applications. The team did note that the

licensees corrective action plan did not include any actions to address

weaknesses in the stations ability to classify structures, systems, and

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components. The team determined that the licensees corrective actions would

only be effective once weaknesses in the ability to classify safety-related

components are corrected.

Determine that a schedule has been established for implementing and

completing the corrective actions.

The team determined that a schedule has been established for implementing and

completing the corrective actions. The team found that corrective actions to

prevent recurrence had been scheduled or implemented which included

procedures changes and implementation of necessary training for work planners.

Additionally, corrective actions to address the contributing causes had been

scheduled. The team determined that that licensees schedule for implementing

corrective actions appeared to be commensurate with the significance of the

issues they are addressing.

Determine that quantitative or qualitative measures of success have been

developed for determining the effectiveness of the corrective actions to prevent

recurrence.

The team determined that quantitative or qualitative measures of success have

been developed for determining the effectiveness of the corrective actions to

prevent recurrence. The licensee established, in part, effectiveness reviews

consisting of independent self-assessments to determine if the necessary

guidance for planners to resolve CQE issues was incorporated into FCS

procedures. Additionally, the licensee identified interim and final effectiveness

reviews consisting of independent self-assessments to review condition reports

and WOs for CQE related issues. The review provided specific performance

measure to verify the frequency of CQE related issues is reduced. The team

determined that the licensees effectiveness criteria did meet the criteria

established in Procedure FCSG 24-7, Effectiveness Review of Corrective

Actions to Prevent Recurrence (CAPRs), Revision 1, in that the effectiveness

review specified specific success criteria.

iii. Assessment Results

The team concluded that for Root Cause Analysis 2012-05615: the root and

contributing causes of risk-significant issues were understood; the extent-of-

condition and extent-of-cause of risk-significant issues were identified; and, the

licensee's corrective actions for risk-significant performance issues were, or will

be, sufficient to address the root and contributing causes.

Restart Checklist items 3.b.1.1, 3.b.1.2, and 3.b.1.3 are closed.

.e Operability Process

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Improper evaluations of degraded and/or non-conforming conditions may result in

continued operation with a structure, system, or component that is not capable of

performing its design function.

(1) Inspection Scope

The team reviewed the licensees assessment of the Fundamental Performance

Deficiency (FPD) associated with Processes to Meet Regulatory Requirements

specifically related to the Operability Determination process. Specifically, the team

assessed the RCA for CR 2012-09494 Revision 1, which identified the following

programmatic and cultural deficiencies:

  • Deficiencies in the accurate identification of current licensing basis

degraded/nonconforming conditions

rigorous

  • Discrepant conditions are not always resolved in a timely manner

commensurate with the safety significance of the condition

  • Cause analysis and extent of condition are not consistently rigorous to

identify the underlying cause of the equipments deficient condition and the

broadness impact of the condition

  • The characteristics necessary for equipment to be fully qualified are not well

understood or applied

The team also assessed the adequacy of the extent of condition, extent of causes,

and corrective actions. (Restart Checklist Basis Document Items 3.e.1; 3.e.2; 3.e.3)

The teams assessment of this FPD was based on the evaluation criteria from

Section 02.02 of NRC Inspection Procedure 95001 which align with this item. The

inspection objectives were to:

  • Provide assurance that the root and contributing causes of risk-significant

issues were understood

  • Provide assurance that the extent-of-condition and extent-of-cause of risk-

significant issues were identified

  • Provide assurance that the licensee's corrective actions for risk-significant

performance issues were, or will be, sufficient to address the root and

contributing causes and to preclude repetition

(2) Observations and Findings

Determine that the problem was evaluated using a systematic methodology to

identify the root and contributing causes.

The team determined that the licensee evaluated this problem using a systematic

methodology to identify the root and contributing causes. Specifically,

RCA 2012- 09494 employed the use of barrier analysis to identify applicable causal

- 60 -

factors. The licensee further refined the results of the barrier analysis by use of a

Five Whys analysis to determine the root causes. The licensee then evaluated the

cause statements against cause testing established in FCS procedures to confirm

the root and contributing causes.

The licensee identified the following as root causes for the FPD:

RC-1: Leadership has not provided adequate governance and oversight for key

regulatory required programs and activities.

RC-2: Processes to perform, and support performance of, Degraded/Non-

Conforming Condition identification and Operability Determinations are not

adequate to ensure consistently accurate and timely determinations.

CC-1: The Operating Experience Program permitted a superficial review of NRC

Regulatory Issue Summary (RIS) 2005-20 Revision 1.

CC-2: Operations leadership did not recognize the risk associated with failing to

keep pace with the industry standard for an Operations led organization.

CC-3: Knowledge and skills to perform, and support performance of,

Degraded/Non-Conforming Condition identification and Operability

Determinations are not adequate to ensure consistently accurate and timely

determinations.

CC-4: Tools used to perform, and support performance of, Degraded/Non-

Conforming Condition identification and Operability Determinations are not

adequate to ensure consistently accurate and timely determinations.

Determine that the root cause evaluation was conducted to a level of detail

commensurate with the significance of the problem.

The licensees RCA employed various techniques to analyze the events. In general,

the quality of analysis was sound and identified several failed barriers in the process

for identification of degraded/nonconforming conditions and operability

determinations.

Determine that the root cause evaluation included a consideration of prior

occurrences of the problem and knowledge of prior operating experience.

The team determined that the RCA included evaluations of both internal and industry

operating experience. The licensees evaluations of industry operating experience

provided sufficient detail such that general conclusions could be established

regarding any similarities.

Determine that the root cause evaluation addressed the extent of condition and the

extent of cause of the problem.

- 61 -

The team reviewed the RCA as it relates to extent of condition and extent of cause.

For extent of condition, the licensees evaluation determined that an extent of

condition for deficiencies in identifying degraded/nonconforming conditions and

performance of operability determinations does exist at FCS. Consequently, the

licensee concluded that other regulatory-required programs, such as, the operability

determination process were not effectively implemented at FCS but the condition

was known as documented in CR 2012-08137, Regulatory Processes and

Infrastructure. The team generally agreed that the licensee had identified similar

processes, such as those documented in CR 2012-08137, which were not being

effectively implemented at FCS.

For extent of cause, the licensee identified extent of cause concerns involving

inadequacies in reinforcing high standards and accountability which was determined

to cross all department and work process boundaries. The licensee addressed the

extent of cause through the organizational ineffectiveness RCA performed under

CR 2012-03986. The licensee determined that corrective actions taken to address

the organizational ineffectiveness extent of cause fully address the extent of cause

for CR 2012-09494. The team found that the corrective actions generally addressed

the extent of cause related to root cause 1 and 2.

Determine that the root cause, extent of condition, and extent of cause evaluations

appropriately considered the safety culture components as described in IMC 0310.

The root cause, extent of condition, and extent of cause evaluations appropriately

considered the safety culture components as described in IMC 0310. Specifically,

the licensee documented their consideration of the IMC 0310 cross-cutting aspects

in Attachment 5 of RCA 2012-09494. The licensee identified H.1 Decision Making -

Licensee decisions demonstrate that nuclear safety is an overriding priority and O.1

Accountability - Management defines the line of authority and responsibility for

nuclear safety as the most applicable safety culture components.

Determine that appropriate corrective actions are specified for each root and

contributing cause.

The team reviewed the licensees corrective actions for each of the root and

contributing causes. In general, the corrective actions identified for the root and

contributing causes appear to be adequate to resolve the identified causes.

Determine that a schedule has been established for implementing and completing

the corrective actions.

The team determined that a schedule has been established for implementing and

completing the assigned corrective actions. Most of the corrective actions have been

completed.

- 62 -

Determine that quantitative or qualitative measures of success have been developed

for determining the effectiveness of the corrective actions to prevent recurrence.

The effectiveness review plan documented is problematic. Specifically, the licensee

has not established adequate quantitative or qualitative acceptance criteria

measures to assess the effectiveness of each corrective action to prevent recurrence

and the corrective actions to prevent recurrence collectively to prevent recurrence of

the root causes as required by FCSG-24-5, Cause Evaluation Manual. Specifically,

the current effectiveness review plan would allow inadequate operability calls to not

fail the effectiveness review as long as those calls were only on non-safety

significant equipment. In this instance the licensee defines safety significant

equipment as that which would put the station into a Technical Specification action

statement or change the Equipment out of service Risk color. In addition the

inspectors are not aware of a licensee mechanism to track this required information.

These observations were discussed with the licensee.

(3) Assessment Results

The team concluded that for Root Cause Analysis 2012-9494: the root and

contributing causes of risk-significant issues were understood; the extent-of-

condition and extent-of-cause of risk-significant issues were identified; and, the

licensee's corrective actions for risk-significant performance issues were, or will

be, sufficient to address the root and contributing causes.

Restart Checklist Items 3.e.1, 3.e.2, and 3.e.3 are closed.

4OA5 Other Activities

On April 11, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed a reactive

inspection in accordance with NRC Inspection Procedure 93812, Special Inspection, at your

Fort Calhoun Station. This special inspection was conducted to gather information associated

with the improper design specifications associated with the raw water pump anchor bolts.

Inspection Report 05000285/2013-012, issued on May 24, 2013 (ML13144A772) documents the

results of this inspection. Documented in this report are two apparent violations (AV) that were

issued pending further evaluation by the licensee. The purpose of this section is document

closure of these two AVs.

.1 (Closed) Apparent Violation 05000285/2013012-08: Failure to Adequately Design

Anchorage for Containment Spray and Raw Water System Pipe Supports

a. Inspection Scope

The inspection report documented an apparent violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, for the failure to ensure the adequacy of the anchorage for

several raw water system and containment spray system pipe supports. Specifically the

anchorage design was non-conservative with respect to the design basis requirements.

This issue was and apparent violation because the final safety significance was to be

- 63 -

determined pending additional analysis of the as-found configuration of the anchorage

and associated pipe supports by the licensee.

b. Findings

Failure to Adequately Design Anchorage for Containment Spray and Raw Water System

Pipe Supports

Introduction. The inspection team identified several examples of a Green, non-cited

violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to

ensure the adequacy of the anchorage for several raw water system and containment

spray system pipe supports. Specifically the anchorage design was non-conservative

with respect to the design basis requirements.

Description. During a previous inspection, the NRC reviewed multiple calculations for

pipe supports on the raw water and containment spray systems and found that the

calculations had several errors related to the design requirements for anchorage. The

NRC issued an apparent violation AV 05000285/2013012-08, Failure to adequately

design anchorage for containment spray and raw water system pipe supports in NRC

Inspection Report 05000285/2013-012 (ML 13144A772).

The licensee performed an operability determination for the affected calculations and

found that the anchorage for the raw water and containment spray piping supports were

operable. The NRC reviewed the evaluations and concluded that reasonable assurance

of operability existed for the affected components.

Analysis. The inspectors determined that the failure to ensure adequacy of the

anchorage of the aforementioned Containment Spray Pipe Supports and Raw Water

Pipe Supports was not in accordance with design basis requirements and was a

performance deficiency. The performance deficiency was determined to be more than

minor because it required calculations to be re-performed to prove the system was

operable, and it was associated with the Mitigating Systems cornerstone attribute of

design control and affected the cornerstone objective of ensuring the availability,

reliability, and capability of the containment spray system and raw water system.

Using Inspection Manual Chapter 0609, Attachment 4 Initial Characterization of

Findings, and Appendix A The Significance Determination Process (SDP) for findings

at-power, both dated 6/19/12, the inspectors determined the performance deficiency

affected the mitigating systems cornerstone and screened to Green because the finding

affected the design and qualification of a mitigating SSC but remained operable. The

inspectors used the at-power SDP because the condition existed since construction and

while the plant was predominantly at power.

The inspectors determined there was no cross-cutting aspect associated with this finding

because the calculations were from the 1980s and therefore were not reflective of

current performance.

- 64 -

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control states, in

part, that the design control measures shall provide for verifying or checking the

adequacy of design, such as by the performance of design reviews, by the use of

alternate or simplified calculational methods, or by the performance of a suitable testing

program. Contrary to this requirement the inspectors identified that calculations

FC00607, FC01785, FC01786, FC01791, FC01864, FC01691, FC01902, FC02409,

FC02412, FC04228, FC02433, FC02436, and FC02425 for the raw water and

containment spray systems failed to ensure adequacy of the design. Specifically, these

anchorage calculations did not conform to applicable design requirements from

approximately 1980 until June 2013.

The licensee entered these issues into the corrective action program as CR 2013-05304

and performed an operability determination as immediate actions. Long term actions to

resolve the errors in the calculations are also implemented by the referenced CR. This

violation is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement

Policy. (NCV 05000285/2014002-08, Failure to Adequately Design Anchorage for

Containment Spray and Raw Water System Pipe Supports).

.2 (Closed) Apparent Violation 05000285/2013012-09: Failure to Adequately Implement

Design Requirements for Containment Air Cooler Pipe Supports

a. Inspection Scope

The inspection report documented an apparent violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, for the failure to ensure the adequacy of the U-bolts for

Containment Air Cooler pipe supports VAS-1 and VAS-2. This issue was an apparent

violation because the final safety significance was to be determined pending additional

analysis of the as-found configuration of the condensate drain line and associated pipe

supports by the licensee.

b. Findings

Failure to Adequately Implement Design Requirements for Containment Air Cooler Pipe

Supports

Introduction. The NRC identified a Green, non-cited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, for the failure to ensure the adequacy of the

U-bolts for containment air cooler pipe supports VAS-1 and VAS-2. Specifically the U-

bolt design was non-conservative with respect to the design basis requirements.

Description. During a previous inspection, the NRC reviewed calculations for VAS-1 and

VAS-2 pipe supports on the containment air cooling systems and found that the

calculations had an error in the design requirements for U-bolts. Specifically, calculation

FC05918 for the VAS-1 and VAS-2 U-bolts did not consider two-directional applied

loading, it only considered tensile loads. The NRC issued an apparent violation

AV 05000285/2013012-09, Failure to adequately implement design requirements for

containment air cooler pipe supports in NRC Inspection Report 0500285/2013-012

(ML 13144A772).

- 65 -

Analysis. The inspectors determined that the failure to ensure adequacy of the U-bolts

for containment air cooler pipe supports VAS-1 and VAS-2 in accordance with design

basis requirements was a performance deficiency.

The performance deficiency was determined to be more than minor because it required

calculations to be re-performed to prove the system was operable, and it was associated

with the Mitigating Systems cornerstone attribute of design control and affected the

cornerstone objective of ensuring the availability, reliability, and capability of several

safety injection tank valves. Specifically, the one-directional U-bolts for VAS-1 and VAS-

2 are not designed to withstand two-directional loading and the condensate drain piping

line has the potential to adversely impact the safety injection tank discharge isolation

valves HCV-2984 and HCV-2794 during a design basis event.

The licensee updated calculation FC05918 and provided an operability evaluation to

address the degraded condition. The inspectors reviewed the information and found the

analysis adequately supported the operability of the affected equipment.

Using Inspection Manual Chapter 0609, Attachment 4 Initial Characterization of

Findings, and Appendix A, The Significance Determination Process (SDP) for findings

at-power, both dated 6/19/12, the inspectors determined performance deficiency

affected the mitigating systems cornerstone and screened to Green because the finding

affected the design and qualification of a mitigating SSC but remained operable. The

inspectors used the at-power SDP because the condition existed since construction and

while the plant was predominantly at power.

The inspectors determined there was no cross-cutting aspect associated with this finding

because the calculation was from the 1980s, therefore was not reflective of current

performance.

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control states, in

part, that the design control measures shall provide for verifying or checking the

adequacy of design, such as by the performance of design reviews, by the use of

alternate or simplified calculation methods, or by the performance of a suitable testing

program.

Contrary to this requirement, the inspectors identified that calculation FC05918, from

1992 until May 2013, failed to ensure adequacy of the design. Specifically, the

calculation did not conform to the U-bolt requirements by applying two-directional

loading to a U-bolt restraint that is qualified for only one-directional loading. The

licensee revised the calculation to support operability. In addition, the licensee

generated engineering change EC59570 to fix the degraded VAS-1 and VAS-2

supports. The licensee entered these issues into the corrective action program

as CR 2013-03722. This violation is being treated as an NCV, consistent with

Section 2.3.2.a of the Enforcement Policy. (NCV 05000285/2014002-09, Failure to

Adequately Implement Design Requirements for Containment Air Cooler Pipe

Supports).

- 66 -

4OA6 Meetings, Including Exit

Exit Meeting Summary

On February 25, 2014, the inspectors presented the inspection results to Mr. M. Prospero, Plant

Manager, and other members of the licensee staff. The licensee acknowledged the issues

presented. The licensee confirmed that any proprietary information reviewed by the inspectors

had been returned or destroyed.

- 67 -

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

S. Anderson, Manager, Design Engineering

D. Bakalar, Manager, Security

J. Bousum, Manager, Emergency Planning and Administration

C. Cameron, Supervisor Regulatory Compliance

L. Cortopassi, Site Vice President

M. Ferm, Manager, System Engineering

K. Ihnen, Manager, Site Nuclear Oversight

T. Lindsey, Director, Training

E. Matzke, Senior Licensing Engineer, Regulatory Assurance

J. McManus, Manager, Engineering Programs

B. Obermeyer, Manager, Corrective Action Program

M. Prospero, Plant Manager

T. Orth, Director, Site Work Management

S. Shea, Supervisor, Operations Training

T. Simpkin, Manager, Site Regulatory Assurance

S. Swanson, Director, Operations

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Untimely Submittal of Required Licensee Event Reports05000285/2014002-05 VIO

(Section 4OA3.4)

Unqualified Coating used as a Water Tight Barrier in Rooms 81

05000285/2013-015-01 LER

and 82 (Section 4OA3.6)

Reporting of Additional High Energy Line Break Concerns

05000285/2013-016-00 LER

(Section 4OA3.7)

Failure to Restore Compliance for Containment Spray Runout

05000285/2014002-06 VIO

Conditions (Section 4OA3.8)

Non-Seismic Circulating Water Pipe Could Disable Raw Water

05000285/2013-019-00 LER

Pumps (Section 4OA3.9)

Closed

Inadequate Calculation of Uncertainty Results a Technical

05000285/2012-013-00 LER

Specification Violation (Section 4OA3.1)

Calculations Indicate the HPSI Pumps will Operate in Run-out

05000285/2013-003-01 LER

During a DBA (Section 4OA3.2)

Containment Air Cooling Units (VA-16A/B) Seismic Criteria

05000285/2013-007-01 LER

(Section 4OA3.3)

A-1 Attachment

Closed

05000285/2013-010-01 LER HPSI Pump Flow Imbalance (Section 4OA3.4)

Unqualified Coating used as a Water Tight Barrier in Rooms 81

05000285/2013-015-00 LER

and 82 Section 4OA3.5)

Containment Spray Pump Design Documents do not Support

05000285/2013-017-00 LER

Operation in Runout (Section 4OA3.8)

Failure to Adequately Design Anchorage for Containment Spray

05000285/2013012-08 AV

and Raw Water System Pipe Supports (Section 4OA5.1)

Failure to Adequately Implement Design Requirements for

05000285/2013012-09 AV

Containment Air Cooler Pipe Supports (Section 4OA5.2)

Opened and Closed

Failure to Make Required 10 CFR 50.46 Report Within

05000285/2014002-01 NCV

Required Time (Section 4OA3.2)

Failure to Translate HPSI Pump Design Requirements to

05000285/2014002-02 NCV

Design Documents (Section 4OA3.2)

Failure to Maintain Design Control of HPSI Injection Valve

05000285/2014002-03 NCV

(Section 4OA3.4)

Failure to Request a License Amendment for Required Change

05000285/2014002-04 NCV

to Technical Specifications (Section 4OA3.4)

Inadequate 10 CFR 50.59 Screening for Containment Spray

05000285/2014002-07 NCV

Design Change (Section 4OA3.8)

Failure to Adequately Design Anchorage for Containment Spray

05000285/2014002-08 NCV

and Raw Water System Pipe Supports (Section 4OA5.1)

Failure to Adequately Implement Design Requirements for

05000285/2014002-09 NCV

Containment Air Cooler Pipe Supports (Section 4OA5.2)

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

Procedures

Number Title Revision

FCS Technical Specifications

FC06747 SI Pump Room (Roon 21 & 22) Heat-up During Pump 6

Operation

USAR 9.10 Auxiliary Systems - Heating, Ventilating and Air 32

Conditioning System

A-2

Condition Reports (CRs)

2013-21373 2013-23302 2014-00211 2014-00203 2014-00373

Section 1RO5: Fire Protection

Procedures

Number Title Revision

OP-MW- Fire Protection System Impairment Control 7

201-0007

SO-G-102 Fire Protection Program Plan 17

SO-G-103 Fire Protection Operability Criteria and Surveillance Requirements 27

SO-G-28 Station Fire Plan 86

SO-G-91 Control and Transportation of Combustible Materials 30

Miscellaneous Documents

Number Title Revision

EA-FC-97-001 Fire hazards Analysis Manual 17

FC05814 UFHA Combustible Loading Calculation 11

USAR 9.11 Updated Safety Analysis Report, Fire Protection Systems 24

Section 1R06: Flood Protection Measures

Procedures

Number Title Revision

SO-G-124 Flood Barrier Impairment R4a

Condition Reports (CRs)

2014-00329

Section 1R11: Licensed Operator Requalification Program and Licensed Operator

Performance

Procedures

Number Title Revision

AOP-17 Loss of Instrument Air 15

A-3

Procedures

Number Title Revision

AOP-20 Loss of Bearing Water Cooling 5

AOP-30 Emergency Fill of Emergency Feedwater Storage Tank 12a

AOP-36 Loss of Spent Fuel Pool Cooling 10

EOP-00 Standard Post Trip Actions 31

EOP-01 Reactor Trip Recovery 14a

Miscellaneous Documents

Number Title Date

Simulator Fidelity Issues January 17, 2014

Simulator Walkdown Cycle 14-1 January 18, 2014

Simulator Loss of SFPC, Loss of Bearing Water and Emergency Fill of January 2, 2014

Scenario Guide the EFWST

82103e

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

Number Title Revision

FCSG-19 Performing Risk Assessments 17

SO-M-100 Conduct of Maintenance 57b

SO-M-101 Maintenance Work Control 103

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

Number Title Revision

FC-1137 Acceptance fro Operability (OPSAC) 21

OP-FC-108-115 Operability Determinations 0a

OP-FC-108-115-1001 Operability Evaluation Asset Suite Engineering Change 0

Desktop Guide

OP-FC-108-115-1002 Supplemental Consideration for On-Shift Immediate 0

Operability Determinations

A-4

Procedures

Number Title Revision

OP-FC-108-115-1003 Operability Determination Oversight and Monitoring 0

Calculations

Number Title Revision

FC08167 Acceptable Minimum Wall Thickness for Raw Water Piping 0

Downstream of Component Cooling Water Heat Exchanger

AC-1D

Miscellaneous Documents

Number Title Date

N-513-3 Cases of ASME Boiler and Pressure Vessel Code, January 26, 2009

Evaluation Criteria for Temporary Acceptance of Flaws in

Moderate Energy Class 2 or 3 Piping

Condition Reports (CRs)

2012-15755 2011-5244 2014-01963 2013-22937 2013-23166

Section 1R19: Post-Maintenance Testing

Procedures

Number Title Revision

EM-PM-EX-1000 480 Volt Motor Inspection 24

FC05571 HCV-2504A Leakage Rate compared to allowable limits 0

IC-CP-01-1112 Calibration of Auxiliary Feedwater Pump FW-54 Suction 3

Flow Loop F-1112

IC-CP-01-1117 Auxiliary Feedwater Pump FW-54 Discharge Flow 3

Indication

MM-PM-AFW-0002 Diesel Engine FW-56 Fluid Maintenance 8

MM-PM-AFW-0005 Diesel Engine FW-56 Maintenance 7

OP-PM-AFW-0004 Third Auxiliary Feedwater Pump Operability Verification 39

PBD-5 Containment Leak Rate 18

QC-ST-SL-3001 Primary Sample System RCS Sample Lines Pressure 6

Test

A-5

Condition Reports (CR)

2014-00522

Work Orders (WO)

506373 424138 472519 476594 476967

480835 437931 481784 481785 490755

Section 1R22: Surveillance Testing

Procedures

Number Title Revision

IC-ST-IA-3009 Operability Test of IA-YCV-1045-C and Close Stroke Test of 24

YCV-1045

OP-ST-AFW- Auxiliary Feedwater Pump FW-10, Steam Isolation Valve, 20

3011 and Check Valve Tests

OP-ST-RC-3001 Reactor Coolant System (RCS) Leak Rate Test 36

OP-ST-RW-3021 AC-10C Raw Water Pump Quarterly Inservice Test 39

Drawings

Number Title Revision

11405-M-253 Steam Generator and Blowdown Flow Diagram P&ID 98

Condition Reports (CR)

2012-15755 2014-01943 2014-01970 2014-01969

Work Orders (WO)

492131 491025

Section 4OA2: Problem Identification and Resolution (71152)

Procedures

Number Title Revision

FCSG-24-1 Condition Report Initiation 6

FCSG-24-3 Condition Report Screening 12a

FCSG-24-4 Condition Report and Cause Evaluation 8a

A-6

Section 4OA2: Problem Identification and Resolution (71152)

Procedures

Number Title Revision

FCSG-24-6 Corrective Action Implementation and Condition Report 12a

Closure

SO-R-2 Condition Reporting and Corrective Action 53b

Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion

Procedures

Number Title Revision

NOD-QP-3 10 CFR 50.59 and 10 CFR 72.48 Reviews 37

FCSG-23 10 CFR 50.59 Resource Manual 8

SO-R-1 Reportability Determinations 26 - 32

Condition Reports (CR)

2013-09949 2008-1666 2013-08300 2013-22007 2012-03796

2013-10910 2008-1683 2013-19722 2014-01029 2012-03796

2013-12508 2013-15047 2013-16417 2013-17630 2013-09949

2014-00958 2014-01358 2013-15442 2013-16241 2014-00674

2013-02100 2013-14177 2014-01629 2012-09494 2012-08137

2012-03986 2012-05615 2012-17437 2011-09459 2012-18.335

2012-05615 2011-09956

Other Documents

Number Title Revision /

Date

DEN Memorandum, 90% SMART Meeting Held on September 19,

Wednesday September 18, 2013 for EC 59874.HPSI Pump 2013

Runout Orifice Plates for SI-2A, SI-2B and SI-2C Revision

1,

EA 13-023 Fort Calhoun SBLOCA Analysis with Reduced HPSI Flow August 16, 2013

(AREVA Calc. 32-9130020-001)

A-7

Other Documents

Number Title Revision /

Date

EA 13-028 Fort Calhoun Safety Analysis Evaluation with Reduced August 16, 2013

HPSI Flow (AREVA Calc. 51-9130106-002)

EC 30663 GSI-191 Implementation 0

EC 59874 HPSI Pump Runout Orifice Plates for SI-2A, SI-2B and SI- July 30, 2013

2C, Rev 1 Kickoff Meeting

EC 59874 HPSI Pump Runout Orifice Plates for SI-2A, SI-2B and SI- 0,1

2C

EC 62416 Temporary Modification - Throttle Discharge Valves HCV- 1,2

2958, HCV-2968, and HCV-2978

FC 07470 Minimum Pump Performance Curve for HPSI Pump 0

FC-68C Applicability Determination, HPSI Pump Runout, SI-2A, SI- October 2, 2013

2B and SI-2C Part 3 of 3 (HPSI Loop Flow Balancing)

LER 2013-010-0 HPSI Pump Flow Imbalance July 2, 2013

LER 2013-010-1 HPSI Pump Flow Imbalance October 23, 2013

LIC 13-0133 30-Day Report of a Significant Change in the Loss-of- September 20, 2013

Coolant Accident (LOCA)/Emergency Core Cooling System

(ECCS) Models Pursuant to 10 CFR 50.46

LIC 77-0090 OPPD Letter to NRC August 22, 1977

NEI 0705 10 CFR 50.46 Reporting Guidelines July 2008

NRC 77-0060 NRC Letter to OPPD June 30, 1977

Section 4OA5: Other Activities

Condition Reports (CR)

2013-3722 2013-5304

A-8