ML060390424

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IR 05000454-05-011; 05000455-05-011; on 10/01/2005-12/31/2005; Byron Station, Units 1 and 2; Inservice Inspection Activities, Permanent Plant Modification, Emergency Action Level and Emergency Plan Changes
ML060390424
Person / Time
Site: Byron  Constellation icon.png
Issue date: 02/03/2006
From: Richard Skokowski
NRC/RGN-III/DRP/RPB3
To: Crane C
Exelon Generation Co
References
IR-05-011
Download: ML060390424 (65)


See also: IR 05000454/2005011

Text

February 3, 2006

Mr. Christopher M. Crane

President and Chief Nuclear Officer

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

BYRON STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION

REPORT 05000454/2005011; 05000455/2005011

Dear Mr. Crane:

On December 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an

integrated inspection at your Byron Station, Units 1 and 2. The enclosed report documents the

inspection findings which were discussed on January 6, 2006, with Mr. S. Kuczynski and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, one NRC-identified and one self-revealed findings of

very low safety significance (Green) are documented in this report. One of these finding was

determined to involve a violation of NRC requirements. In addition, a third issue was reviewed

under the NRC traditional enforcement process and determined to be a Severity Level IV

violation of NRC requirements. However, because these violations were of very low safety

significance or Severity Level IV violation and because the issues were entered into your

corrective action program, the NRC is treating these findings as Non-Cited Violations in

accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.

20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the

Resident Inspector office at the Byron facility.

C. Crane

-2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its

enclosure will be made available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs document

system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Richard A.Skokowski, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454; 50-455

License Nos. NPF-37; NPF-66

Enclosure:

Inspection Report 05000454/2005011; 05000455/2005011

w/Attachment: Supplemental Information

cc w/encl:

Site Vice President - Byron Station

Plant Manager - Byron Station

Regulatory Assurance Manager - Byron Station

Chief Operating Officer

Senior Vice President - Nuclear Services

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing

Manager Licensing - Braidwood and Byron

Senior Counsel, Nuclear

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

State Liaison Officer, State of Illinois

State Liaison Officer, State of Wisconsin

Chairman, Illinois Commerce Commission

B. Quigley, Byron Station

DOCUMENT NAME: C:\\MyFiles\\Roger\\Ml060390424.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

RIII

NAME

RSkokowski:dtp

DATE

02/03/06

OFFICIAL RECORD COPY

C. Crane

-3-

ADAMS Distribution:

GYS

JBH1

RidsNrrDirsIrib

GEG

KGO

RAS

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-454; 50-455

License Nos:

NPF-37; NPF-66

Report Nos:

05000454/2005011; 05000455/2005011

Licensee:

Exelon Generation Company, LLC

Facility:

Byron Station, Units 1 and 2

Location:

4450 N. German Church Road

Byron, IL 61010

Dates:

October 01, 2005, through December 31, 2005

Inspectors:

D. Schroeder, Acting Senior Resident Inspector

R. Orlikowski, Acting Senior Resident Inspector

J. Taylor, Acting Senior Resident Inspector

B. Bartlett, Acting Senior Resident Inspector

R. Ng, Resident Inspector

C. Acosta Acevedo, Reactor Engineer

M. Wilk, Reactor Engineer, Region III

M. Holmberg, Reactor Inspector, Region III

J. House, Radiation Specialist

J. Jandovitz, Reactor Inspector, Region III

R. Jickling, Emergency Preparedness Analyst

J. Robbins, Reactor Engineer, RIII

M. Jordan, Consultant

C. Thompson, Resident Inspector, Illinois Emergency

Management Agency

Approved by:

R. Skokowski, Chief

Branch 3

Division of Reactor Projects

Enclosure

2

SUMMARY OF FINDINGS

IR 05000454/2005011; 05000455/2005011; on 10/01/2005-12/31/2005; Byron Station,

Units 1 and 2; Inservice Inspection Activities, Permanent Plant Modification, Emergency

Action Level and Emergency Plan Changes.

This report covers a 3 month period of baseline resident inspection and announced baseline

inspections on radiation protection, heat sink performance, EP inspection and inservice

inspection. The inspections were conducted by resident and inspectors based in the NRC

Region III office. One Severity Level IV Non-Cited Violation and two Green findings, one

of which was a violation of NRC requirements, were identified. The significance of most findings

is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC)

0609, Significance Determination Process (SDP). Findings for which the SDP does not apply

may be Green or be assigned a severity level after NRC management review. The NRCs

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

Green. A finding having very low safety significance (Green) was self-revealed when the

newly installed Digital Electrohydraulic System (DEH) failed to respond to operator input

to initiate a turbine runback that subsequently resulted in a reactor trip. The inspectors

determined that the algorithm required for turbine runback was deleted from the software

database due to a compiler fault. Modification review and testing performed by the

licensee failed to discover the software error. To correct the problem the licensee

reinstalled the deleted software algorithm into the DEH system.

The finding was more than minor because it affected the design control attribute of the

Initiating Events cornerstone objective. The attribute objective limits the likelihood of

those events that upset plant stability and challenge critical safety functions during at-

power operations. Specifically, the lack of turbine runback capability contributed to a

reactor trip from a feedwater system transient. The finding was determined to be of very

low safety significance (Green), since it only contributed to the likelihood of a reactor trip.

No violation of NRC requirements occurred. (Section 1R17)

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding involving a Non-Cited Violation (NCV) of

10 CFR Part 50.55a(g)(4)ii having very low safety significance for failure to perform a

VT-2 examination at nominal operating pressure for six new residual heat removal

system welds that were returned to service. This finding was entered into the licensees

corrective action program.

This finding was of more than minor significance because the licensee returned these

six welds to service without completing the required pressure test and VT-2 examination,

which placed this system at increased risk for undetected leakage and component

Enclosure

3

failure. Operation of this system with improperly tested piping affected the mitigating

systems cornerstone objective of equipment reliability. This finding was of very low

safety significance because the required test and VT-2 examination were subsequently

completed and all welds passed. The finding was not suitable for a significance

determination process evaluation. This finding has been reviewed by NRC Management

and has been determined to be a Green finding of very low safety significance. (Section

1R08)

Cornerstone: Emergency Preparedness

Severity Level IV. The inspectors identified that the licensee had changed its standard

emergency action level (EAL) scheme by revising one EALs criteria for an Unusual

Event declaration that addressed an unplanned radiological release in excess of effluent

radiation monitor readings unless the release could be determined to be below Offsite

Dose Calculation Manual limits within 15 minutes for releases that could not be

terminated in 60 minutes or less. The inspectors determined that this EAL change

decreased the effectiveness of the emergency plan, and that the licensee did not obtain

prior NRC approval for this change, contrary to the requirements of 10 CFR 50.54(q).

The licensee is evaluating the options to correct the EAL.

This finding was more than minor because extending the time period required for the

appropriate emergency classification of a radiological release could adversely affect the

performance of both onsite and offsite emergency actions. Because the issue affected

the NRCs ability to perform its regulatory function, it was evaluated with the traditional

enforcement process as specified in Section IV.A.3 of the Enforcement Policy.

According to Supplement VIII of the Enforcement Policy, this finding was determined to

be a Severity Level IV because it involved a failure to meet a requirement not directly

related to assessment and notification. Further, this problem was isolated to one EAL

and was not indicative of a functional problem with the EAL scheme. Additionally,

because the violation was a Severity Level IV and the licensee entered this issue into its

corrective action program this finding is being treated as a Severity Level IV Non-Cited

Violation of 10 CFR 50.54(q). (Section 1EP4)

B.

Licensee Identified Violations

None.

Enclosure

4

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full power for the quarter except for the followings:

On December 8, 2005, Unit 1 ramped down to 98 percent to swap feedwater pumps.

On December 18, 2005, Unit 1 downpowered to 85 percent to perform a turbine

valve/governor valve surveillance.

Unit 2 started the quarter shutdown for a refueling outage. On October 18, 2005, Unit 2

returned to full power operation. The unit operated at or near full power for the quarter except

for the followings:

On October 19, 2005, Unit 2 tripped due to the loss of a condensate/condensate booster

pump resulting from a faulty motor. The unit subsequently returned to full power on

October 22, 2005.

On November 5, 2005, Unit 2 ramped down to 96 percent to swap feedwater pumps.

On November 19, 2005, Unit 2 downpowered to 95 percent to swap feedwater pumps.

1.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01

Adverse Weather Protection (71111.01)

a.

Inspection Scope

The inspectors completed a total of two samples in this area when they evaluated the

licensees preparation for adverse weather conditions during the winter months (i.e.,

below freezing temperatures and accumulation of ice and snow), which could potentially

lead to a loss of offsite power or a loss of mitigating systems. Specifically, the

inspectors reviewed the following two system/structures:

Primary Water Storage Tanks; and

Essential Service Water Cooling Towers.

The inspectors walked down the primary water storage tanks, the essential service water

cooling towers, and other areas of the station potentially affected by cold weather.

Insulated and trace heated piping and components, operation of area space heaters,

and closure of outside air dampers were inspected. The inspectors selected the two

structures listed because they were identified as risk significant in the licensees risk

analysis. The inspectors interviewed operations department personnel and reviewed

applicable portions of the Updated Final Safety Analysis Report (UFSAR). The

inspectors evaluated licensee performance by comparing actual performance to the

Enclosure

5

licensee management expectations and guidelines as presented in Byron Abnormal

Operating Procedures.

In addition, the inspectors reviewed the issues that the licensee entered into its

corrective action program to verify that identified problems were being entered into the

program with the appropriate characterization and significance. The documents listed in

the Attachment to this report were also used by the inspectors to evaluate this area.

b.

Findings

No findings of significance were identified.

1R04

Equipment Alignment (71111.04)

.1

Partial Walkdowns

a.

Inspection Scope

The inspectors performed two partial walkdown samples of accessible portions of trains

of risk-significant mitigating systems equipment during times when the trains were of

increased importance due to the redundant trains or other related equipment being

unavailable. The inspectors utilized the valve and electric breaker lineups and

applicable system drawings to determine that the components were properly positioned

and that support systems were lined up as needed. The inspectors also examined the

material condition of the components and observed operating parameters of equipment

to determine that there were no obvious deficiencies. The inspectors used the

information in the appropriate sections of the UFSAR and Technical Specification (TS) to

determine the functional requirements of the systems.

The inspectors verified the alignment of the following:

Unit 2 Station Air Compressors while 1B Auxiliary Feedwater System

was out of service for maintenance; and

Unit 1 Train A Essential Service Water System.

The documents reviewed during this inspection were listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

.2

Complete Walkdown

a.

Inspection Scope

During the inspection, the inspectors completed one complete system alignment

inspection of the accessible portions of the Unit 1 Auxiliary Feedwater system. This

system was selected because it was considered both safety related and risk significant

Enclosure

6

in the licensees probabilistic risk assessment. The inspection consisted of the following

activities:

Unit 1 Train A Containment Spray Pump during the 1B Containment Spray Pump

work window.

The inspectors reviewed the issues that the licensee entered into its corrective action

program to verify that identified problems were being entered into the program with the

appropriate characterization and significance. The documents reviewed during this

inspection are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05)

.1

Walkdowns

a.

Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of fire fighting equipment; the control of transient

combustibles and ignition sources; and on the condition and operating status of installed

fire barriers. The inspectors reviewed applicable portions of the Byron Station Fire

Protection Report and selected fire areas for inspection based on their overall

contribution to internal fire risk, as documented in the Individual Plant Examination of

External Events Report. In addition, during these inspections, the inspectors used the

following reference documents:

OP-AA-201-006; Control of Temporary Heat Sources, Revision 0;

OP-AA-201-009; Control of Transient Combustible Material, Revision 4; and

OP-MW-201-007; Fire Protection System Impairment Control, Revision 3.

The inspectors verified that fire hoses and extinguishers were in their designated

locations and available for immediate use; that fire detectors and sprinklers were

unobstructed; that transient material loading was within the analyzed limits; and that

fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The Byron Station Pre-Fire Plans applicable for each area inspected were used by

the inspectors to determine approximate locations of firefighting equipment.

The inspectors completed ten inspection samples by examining the plant areas listed

below to observe conditions related to fire protection:

Unit 2 Containment (Zone 1.1-2, Zone 1.2-2 and Zone 1.1-3);

Unit 1 Auxiliary Feedwater Tunnel & Main Steam Tunnel (Zone 18.3-1);

Turbine Building 451' (Zone 8.6-0);

Division 12 4KV Switchgear Room (Zone 5.1-1);

Enclosure

7

Division 12 Misc. Electrical Equipment Room (Zone 5.4-1);

Auxiliary Building 401' Elevation General Area (zone 11.5-0);

Unit 2 Train B Auxiliary Feedwater Pump Room (Zone 11.4A-2);

Lower Cable Spreading Room (Zone 3.2A-1);

Unit 2 Auxiliary Electrical Room (Zone 5.5-2); and

Unit 2 2A Diesel Generator Room (Zone 9.2-2).

The inspectors also reviewed selected issues documented in condition reports (CRs), to

determine if they had been properly addressed in the licensees corrective action

program. The documents reviewed during this inspection are listed in the Attachment to

this report.

b.

Findings

No findings of significance were identified.

.2

Drill Observation

a.

Inspection Scope

The inspectors assessed the fire brigade performance and the drill evaluators critique

during a fire brigade drill conducted on November 18, 2005. This was not counted as an

inspection sample since the required annual sample had been completed. The

inspectors determined that this drill was of importance since it involved local fire

department participation. The drill simulated an airplane crash in the protected area.

The inspectors focused on command and control of the fire brigade activities; fire

fighting and communication practices; material condition and use of fire fighting

equipment; implementation of pre-fire plan strategies, the coordination of fire fighting

actions between station fire brigades and offsite resources and access control of offsite

resources. The inspectors evaluated the fire brigade performance using the licensees

established procedures and guidance.

b.

Findings

No findings of significance were identified.

1R06

Flood Protection Measures (71111.06)

a.

Inspection Scope

During the week of October 31, 2005, the inspectors evaluated the licensees controls

for mitigating internal flooding by completing a semi-annual sample. The specific areas

evaluated included the auxiliary building elevations 330', 346', and 364'. During the

evaluation, inspectors performed the following:

Reviewed the licensees design basis documents including UFSAR, and Safety

Evaluation Report, to identify the design basis for flood protection and to identify

those areas susceptible to internal flooding;

Enclosure

8

Interviewed members of the licensee engineering and operations staff in regards

to system design and flood response actions;

Reviewed selected abnormal operating procedures for identifying and mitigating

flooding events;

Reviewed plant configuration that may impact external flooding controls;

Inspected areas for control of materials that could potentially clog drains; and

Inspected the watertight doors and flood seals.

The documents reviewed during this inspection are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

1R07

Heat Sink Performance

.1

Annual Sample of Heat Sink Performance (71111.07A)

a.

Inspection Scope

The inspectors completed one annual testing and performance review inspection sample

by observing and evaluating the licensees inspection of the following safety-related heat

exchanger:

Unit 2, Train B Auxiliary Feedwater Right Angle Lube Oil Cooler.

This heat exchanger was selected for review because essential service water was

ranked high in the plant specific risk assessment and the heat exchanger was a support

system directly connected to the safety-related auxiliary feedwater system.

In addition to observing the inspection and reviewing the heat exchanger inspection

results, the inspectors discussed the results and heat exchanger performance with the

licensees engineer responsible for the heat exchanger inspection program.

The inspectors also reviewed selected issues documented in condition reports (CRs),

to determine if they had been properly addressed in the licensees corrective action

program. The documents reviewed during this inspection are listed in the Attachment

to this report.

b.

Findings

No findings of significance were identified.

Enclosure

9

.2

Biennial Review of Heat Sink Performance (71111.07B)

a.

Inspection Scope

The inspectors reviewed the performance of the Unit 1 service water pump room cooler

and lube oil cooler, and the Unit 2 emergency diesel generator engine jacket water

cooler (a total of three heat exchangers). These heat exchangers were chosen for

review based on their high risk achievement worth in the licensees probabilistic safety

analysis. This review resulted in the completion of three inspection samples. While

onsite, the inspectors reviewed completed surveillance tests, and associated

calculations. The inspectors reviewed the documentation to confirm that the test and/or

inspection methodology was consistent with accepted industry and scientific practices.

This review was based on heat transfer texts and an Electrical Power Research Institute

standard (EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines). The

inspectors also reviewed documentation to verify that acceptance criteria was consistent

with design basis values, as outlined in the UFSAR and TS. The inspectors reviewed

documentation to verify that the licensee took appropriate actions to verify physical

integrity of the heat exchangers. The inspectors also reviewed documentation to verify

that the licensee had appropriate controls in place to ensure availability of the ultimate

heat sink under adverse conditions.

The inspectors reviewed corrective action documents, concerning heat exchanger or

heat sink performance issues to verify that the licensee had an appropriate threshold for

identifying issues. The inspectors also evaluated the effectiveness of the corrective

actions for identified issues, including the engineering justification for operability.

The documents that were reviewed are included in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R08

Inservice Inspection (ISI) Activities (71111.08)

.1

Piping Systems ISI

a.

Inspection Scope

The inspectors conducted a review of the implementation of the licensees ISI program

for monitoring degradation of the reactor coolant system boundary and the risk

significant piping system boundaries for Unit 2. The inspectors selected components

based upon the ISI activities available for review during the onsite inspection period.

The inspectors observed the following two types of nondestructive examination activities

to evaluate compliance with the ASME Code Section XI and Section V requirements and

to verify that indications and defects (if present) were dispositioned in accordance with

the ASME Code Section XI requirements.

Enclosure

10

Ultrasonic examination (UT) of two feedwater system welds (2FW03DD-16, C01,

C02) on a 16 inch diameter line in the Unit 2 main steam isolation valve (MSIV)

room, five feedwater system welds (2FW87CA-6, C05, C06, C07, C08, C09)

outside the missile barrier inside containment and three reactor coolant system

welds (2RC28A-3, J03, J04, J05) inside the missile barrier within containment;

and

Magnetic particle examination of a support weld (2MSS07AD-28, E-2) for a

28 inch main steam line located in the MSIV room.

The inspectors reviewed a Code VT-3 examination from the previous outage with

relevant indications identified on snubber support 2RC18001S to determine if the

licensees corrective actions and extent of condition reviews were in accordance with

the ASME Code requirements.

The inspectors reviewed pressure boundary welds for the Code Class 2 and 3 portions

of the Unit 2 residual heat removal (RH) system, to determine if the welding acceptance

and preservice examinations (e.g., pressure testing, visual, dye penetrant, and weld

procedure qualification tensile tests and bend tests) were performed in accordance with

ASME Code Sections III, V, IX, and XI requirements. Specifically, the inspectors

reviewed records of six field welds associated with the installation of two new valves and

piping components in a 3 inch diameter line within the RH system.

The inspectors performed a review of ISI related problems that were identified by the

licensee and entered into the corrective action program, conducted interviews with

licensee staff, and reviewed licensee corrective action records to determine if:

the licensee had described the scope of the ISI related problems;

the licensee had established an appropriate threshold for identifying issues;

the licensee had evaluated industry generic issues related to ISI and pressure

boundary integrity; and

the licensee implemented appropriate corrective actions.

The inspectors performed these reviews to ensure compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

The reviews as discussed above counted as one inspection sample.

b.

Findings

Introduction: The inspectors identified a finding involving a Non-Cited Violation (NCV)

of 10 CFR Part 50.55a(g)(4)ii having very low safety significance (Green) for failure to

perform a VT-2 examination at nominal operating pressure for six new RH system welds

returned to service.

Enclosure

11

Description: On September 28, 2005, the inspectors identified that the licensee had not

completed a VT-2 examination at nominal operating system pressure upon returning six

newly fabricated pressure boundary welds in a 3 inch RH system line to service.

Following construction of a new weld in a safety-related Code Class 1, 2 or 3 system,

a VT-2 examination is required at hydrostatic test pressure as specified by article

IWA-4000 of Section XI of the ASME Code. As an alternative to completing a VT-2

examination at hydrostatic test pressure, the licensee elected to implement Code

Case 416-1 and substitute a VT-2 examination at nominal operating pressure and

temperature for six new RH system welds installed under work order No. 00366731.

During shutdown cooling the RH system operates at pressures up to 350 pounds per

square inch gage (psig). On September 18, 2003, the licensee returned six newly

fabricated welds to service in accordance with work order No. 00366731 and performed

a VT-2 examination with the system at only 50 psig. Subsequently, on five occasions

during RH pump surveillance testing, the licensee subjected these welds to pressures

exceeding 200 psig without performing VT-2 examinations. The inspectors were

concerned that subjecting these new welds to pressures above that previously tested

without examination could have resulted in undetected leakage associated with a weld

defect or failure. On March 23, 2004, the licensee performed a preplanned VT-2

examination of the six new RH system welds with system pressure at 350 psig with no

evidence of weld leakage. The licensee performed this test to fulfill the Code Case 416-

1 requirements as documented on a Code NIS-2 data form. However, the licensee staff

did not recognize that these welds had been subjected to pressures above that seen

during the initial VT-2 examination. Because, the licensee had not completed a VT-2

examination at 350 psig prior to, or immediately upon return of these welds to service,

the inspectors determined that the requirements of paragraph (b) of Code Case 416-1

had not been met.

Analysis: The inspectors determined that the failure of the licensee to perform a VT-2

examination of six RH system welds at nominal operating system pressure prior to, or

immediately upon return to service was a performance deficiency that warranted a

significance evaluation. This finding was of more than minor significance because the

licensee returned these six welds to service without completing a VT-2 examination at

the required pressure, which placed the RH system (mitigating system) at increased risk

for undetected leakage and component failure. Therefore, operation of the RH system

with improperly tested piping affected the mitigating system cornerstone objective of

equipment reliability. This finding was of very low safety significance because a VT-2

examination at the required pressure was subsequently completed with all welds

passed. The inspectors determined that the finding could not be evaluated using the

Significance Determination Process (SDP) in accordance with NRC IMC 0609,

Significance Determination Process, because the SDP for the Mitigating Systems

Cornerstone applied to degraded systems/components, not to the testing and

examination activities intended to detect degraded components. Therefore, this finding

was reviewed by a Regional Branch Chief in accordance with IMC 0612, Section 05.04c,

who agreed with the inspectors that this finding was of very low safety significance.

Enclosure

12

Enforcement: On September 28, 2005, while performing the NRC baseline procedure

71111.08, the inspectors identified an NCV of 10 CFR Part 50.55a(g)(4)ii.

10 CFR 50.55a(g)(4)ii requires compliance with Section XI Edition of the ASME Code

issued within 12 months of the start of the interval or the ASME Code Cases identified in

Regulatory Guide 1.147 for examination of components and system pressure tests.

Regulatory Guide 1.147 identified Code Case 416-1 as an NRC approved Code Case.

Paragraph (b) of Code Case CC 416-1 required that prior to or immediately upon return

to service, a visual examination VT-2 shall be performed at nominal operating pressure.

Contrary to these requirements, on September 18, 2003, the licensee returned six RH

system welds (Code Class 2 and 3 system) to service under work order No. 00366731

without performing VT-2 examination at nominal operating pressure. This violation

existed until March 23, 2004, when these welds were subjected to a VT-2 examination at

nominal operating pressure. The finding was not suitable for SDP evaluation, but has

been reviewed by NRC Management and has been determined to be a Green finding of

very low safety significance. Because of the very low safety significance of this finding

and because the issue was entered into the licensees corrective action program

(AR 00380389), it is being treated as an NCV, consistent with Section VI.A.1 of the

Enforcement Policy (NCV 05000455/2005011-01).

.2

Pressurized Water Reactor Vessel Head Penetration ISI

a.

Inspection Scope

The inspectors conducted a review of the licensees activities associated with a bare

metal visual examination of the Unit 2 reactor vessel head and vessel head penetration

nozzles to meet NRC Order EA 03-009. Specifically, the inspectors observed the

licensee performing direct and remote VT-2 type examinations of portions of five vessel

head penetration nozzles and reviewed the video-taped examination records for other

penetration locations. Additionally, the inspectors completed an independent direct

visual examination for portions of six peripheral vessel head penetration nozzle locations

and reviewed the final written examination records documenting the extent of the

licensees visual examination coverage.

The inspectors completed these reviews and observations to confirm that the licensee

had criteria for visual examination quality, appropriately resolved interference or masking

issues, dispositioned indications and defects in accordance with the ASME Code (if

present), and that the examination scope met the requirements of NRC order EA-03-

009.

Procedure 71111.08, Steps 02.02.c and 02.02.d associated with recordable indications

accepted for continued service and welded repairs were not performed because no

recorded indications had been identified and no welded repairs had been completed.

Therefore, inspectors concluded that the reviews discussed above did not count as a

completed inspection sample as described in Section 71111.08-5 of the inspection

procedure, but the sample was completed to the extent possible.

Enclosure

13

b.

Findings

No findings of significance were identified.

.3

Boric Acid Corrosion Control (BACC) ISI

a.

Inspection Scope

The inspectors reviewed the Unit 2 BACC inspection activities conducted pursuant to

licensee commitments made in response to NRC Generic Letter 88-05, Boric Acid

Corrosion of Carbon Steel Reactor Pressure Boundary.

The inspectors observed the licensee during BACC visual examinations of the reactor

coolant and other borated systems conducted on September 25, 2005, to evaluate

compliance with licensee BACC program requirements and 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. In particular, the

inspectors observed these examinations to determine if the licensee focused on

locations where boric acid leaks could cause degradation of safety significant

components and that degraded or non-conforming conditions were properly identified

in the licensees corrective action system.

The inspectors reviewed engineering evaluations performed for boric acid found on

reactor coolant system piping and components to verify that the minimum design code

required section thickness had been maintained for the affected component(s).

Specifically, the inspectors reviewed:

Evaluation No. 2004-315 for Component 2CV128, Minor Packing Leak;

Evaluation No. 2004-466 for Component 2RH029A, Valve Cap found Leaking at

1/2 Drop per Second; and

Evaluation No. 2004-404 for Component 2SI121A, Boric Acid Leak at Base of

Relief Valve.

The inspectors reviewed licencee corrective actions implemented for evidence of boric

acid leakage to confirm that they were consistent with requirements of Section XI of the

ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI. Specifically, the inspectors

reviewed the following ARs

AR 00377795, Body to Bonnet Leakage from 2RC8045D, September 26, 2005;

AR 00379178, Boric Acid Packing Leak, Dry 2CV236, September 29, 2005; and

AR 00381103, Boric Acid Leakage at Kerotest Check Valve Cap,

October 3, 2005.

The documents reviewed during this inspection are listed in the Attachment to this

report. The reviews as discussed above counted as one inspection sample.

b.

Findings

No findings of significance were identified.

Enclosure

14

.4

Steam Generator (SG) Tube ISI

a.

Inspection Scope

The inspectors performed an on-site review of SG tube examination activities conducted

pursuant to TS and the ASME Code Section XI requirements.

The inspectors observed acquisition of eddy-current test (ET) data, interviewed ET data

analysts, and reviewed documents related to the SG ISI program to determine if:

In-situ SG tube pressure testing screening criteria and the methodologies used to

derive these criteria were consistent with EPRI TR-107620, Steam Generator In

Situ Pressure Test Guidelines;

The in-situ SG tube pressure testing screening criteria were properly applied in

terms of SG tube selection based upon evaluation of the list of tubes with

measured/sized flaws;

The numbers and sizes of SG tube flaws/degradation identified was bound by the

licensees previous outage Operational Assessment predictions;

The SG tube ET examination scope and expansion criteria were sufficient to

identify tube degradation based on site and industry operating experience by

confirming that the ET scope completed was consistent with the licensees

procedures, plant TS requirements and EPRI 1003138, Pressurized Water

Reactor Steam Generator Examination Guidelines, Revision 6;

The SG tube ET examination scope included tube areas which represent ET

challenges such as the tubesheet regions, expansion transitions and support

plates;

The licensee identified new tube degradation mechanisms;

The licensee implemented repair methods which were consistent with the repair

processes allowed in the plant TS requirements;

The licensee primary-to-secondary leakage (e.g., SG tube leakage) was below

the detection threshold during the previous operating cycle; and

The licensee initiated evaluations for unretrievable loose parts identified in the 1D

SG;

The ET probes and equipment configurations used to acquire data from the SG

tubes were qualified to detect the known/expected types of SG tube degradation

in accordance with Appendix H, Performance Demonstration for Eddy Current

Examination, of EPRI 1003138, Pressurized Water Reactor Steam Generator

Examination Guidelines, Revision 6; and

The licensee identified deviations from ET data acquisition or analysis

procedures.

The inspectors performed a review of SG ISI related problems that were identified by the

licensee and entered into the corrective action program, conducted interviews with

licensee staff and reviewed licensee corrective action records to determine if:

The licensee had described the scope of the SG related problems;

The licensee had established an appropriate threshold for identifying issues;

Enclosure

15

The licensee had evaluated industry generic issues related to SG tube integrity;

and

The licensee implemented appropriate corrective actions.

The inspectors performed these reviews to ensure compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

The inspectors also reviewed licensee in-situ pressure test results for tube R49-C50,

which was pressure tested during the Byron Unit 2 Refueling Outage No. B2R11. The

inspectors performed this review to determine if the in-situ SG tube pressure testing

screening criteria and test pressures were consistent with EPRI TR-107620, Steam

Generator In Situ Pressure Test Guidelines.

The inspectors concluded that the reviews discussed above did not count as a

completed inspection sample as described in Section 71111.08-5 of the inspection

procedure, but the sample was completed to the extent possible.

The specific activities which were not available for the inspectors review to complete the

procedure sample and the basis for their unavailability is identified below.

Procedure 71111.08, Steps 02.04.a.3 and 02.04.a.4 associated with review of

in-situ pressure testing and tube performance criteria were not available for

review because none of the degraded SG tubes examined during the current

refueling outage No. 12 met the screening requirements for pressure testing.

Procedure 71111.08, Step 02.04.d associated with review of licensee activities

for new SG tube degradation mechanisms was not available for review because

no new tube degradation mechanisms were identified; and

Procedure 71111.08, Step 02.04.h associated with review of corrective actions

for primary-to-secondary leakage greater than 3 gallons per day was not

available for review because primary-to-secondary leakage was below the

minimum detectable threshold during the previous operating cycle.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification (71111.11)

.1

Resident Inspector Quarterly Review

a.

Inspection Scope

The inspectors completed one inspection sample by observing and evaluating an

operating crew during an Anticipated Transient Without Scram (ATWS) requiring a

manual reactor shutdown. The inspectors evaluated crew performance in the areas of:

Clarity and formality of communications;

Ability to take timely actions;

Enclosure

16

Prioritization, interpretation and verification of alarms;

procedure use;

Control board manipulations;

Supervisors command and control;

Management oversight; and

Group dynamics.

Crew performance in these areas was compared to licensee management expectations

and guidelines as presented in the following documents:

OP-AA-101-111, Roles and Responsibilities of On-Shift Personnel, Revision 1;

OP-AA-103-102, Watchstanding Practices, Revision 3;

OP-AA-103-103, Operation of Plant Equipment, Revision 0; and

OP-AA-104-101, Communications, Revision 1.

The inspectors verified that the crew completed the critical tasks listed in the above

simulator guide. The inspectors also compared simulator configurations with actual

control board configurations. For any weaknesses identified, the inspectors observed

the licensee evaluators to determine whether they also noted the issues and discussed

them in the critique at the end of the session.

The documents reviewed during this inspection are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors completed one inspection sample by evaluating the licensees

implementation of the maintenance rule, 10 CFR 50.65, as it pertained to identified

performance problems associated with the following structures, systems, and/or

components:

Unit 2, 2D Reactor Coolant Pump motor move to Unit 2 containment with fuel in

the core.

The inspectors evaluated the licensee's appropriate handling of SSC condition problems

in terms of appropriate work practices and characterizing reliability issues. Equipment

problems were screened for review using a problem oriented approach. Work practices

were observed which related to the reliability of equipment maintenance during the

inspection period. Items chosen are risk significant, and extent of condition was

reviewed as applicable. Work practices were reviewed for contribution to potential

degraded conditions of the affected SSCs. Related work activities were observed and

corrective actions were discussed with licensee personnel. Exelon's handling of the

issues being reviewed were evaluated under the requirements of the maintenance rule

Enclosure

17

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed the licensees management of plant risk during emergent

maintenance activities or during activities where more than one significant system or

train was unavailable. The inspectors chose activities based on their potential to

increase the probability of an initiating event or impact the operation of safety-significant

equipment. The inspectors verified that the evaluation, planning, control, and

performance of the work were done in a manner to reduce the risk and the work duration

was minimized where practical. The inspectors also verified that contingency plans were

in place where appropriate.

The inspectors reviewed configuration risk assessment records, UFSAR, TS, and

Individual Plant Examination. The inspectors also observed operator turnovers,

observed plan-of-the-day meetings, and reviewed other related documents to determine

that the equipment configurations had been properly listed, that protected equipment

had been identified and was being controlled where appropriate, and that significant

aspects of plant risk were being communicated to the necessary personnel. The

inspectors verified that the licensee controlled work activities in accordance with the

following documents:

ER-AA-600, Risk Management, Revision 4;

ER-AA-310, Implementation of the Maintenance Rule, Revision 4;

OU-AA-103, Shutdown Safety Management Program, Revision 4;

OU-AP-104, Shutdown Safety Management Program, Revision 8;

WC-AA-101, On-Line Work Control Process, Revision 11;

Byron Operating Department Policy 400-47, June 23, 2004, Revision 7; and

Byron Nuclear Power Station Probabilistic Risk Assessment, Revision 5B.

The inspectors completed five inspection samples by reviewing the following activities:

Unit 1 Train A Auxiliary Feedwater pump work window concurrent with Unit 1

Train A Station Air maintenance;

Emergent work on the Feedwater Isolation Valve 2FW009C;

Emergent work on the 1A Emergency Diesel Generator;

Planned maintenance on the Essential Service Water makeup pump concurrent

with Auxiliary Building HVAC maintenance; and

Unit 1 Solid State Protection System Surveillance while a Main Control Room

Door was removed for maintenance.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

Enclosure

18

b.

Findings

No findings of significance were identified.

1R14

Personnel Performance Related to Non-routine Plant Evolutions and Events (71111.14)

a.

Inspection Scope

The inspectors completed two inspection samples by observing or evaluating control

room and equipment operators during the following non-routine evolutions:

Unit 2 startup testing from the B2R12 outage; and

Unit 2 reactor trip.

The inspectors evaluated crew performance in the areas of:

Prioritization, interpretation and verification of alarms;

Procedure use;

Control board manipulations;

Supervisors command and control

Management oversight; and

Group dynamics.

Crew performance in these areas was compared to licensee management expectations

and guidelines as presented in the following documents:

OP-AA-101-111, Roles and Responsibilities of On-shift Personnel;

OP-AA-103-102, Watchstanding Practices;

OP AA-103-103, Operation of Plant Equipment; and

OP-AA-104-101, Communications.

Additional documents reviewed during this inspection are listed under Section 4OA3 of

the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors evaluated plant conditions, selected condition reports, engineering

evaluations and operability determinations for risk-significant components and systems

in which operability issues were questioned. These conditions were evaluated to

determine whether the operability of components was justified.

The inspectors completed two inspection samples by reviewing the following evaluations

and issues:

Enclosure

19

Unit 1Train B Emergency Diesel Generator undervoltage relay failed surveillance

criteria; and

Unit 2 Feedwater Isolation Valve 2FW009C failed inservice testing.

The inspectors compared the operability and design criteria in the appropriate section of

the TS including the TS Basis, the Technical Requirements Manual (TRM) and UFSAR

to the licensees evaluations to determine that the components or systems were

operable. The inspectors determined whether compensatory measures, if needed, were

taken, and determined whether the evaluations were consistent with the requirements of

licensees Procedure LS-AA-105, Operability Determination Process, Revision 1. The

inspectors also discussed the details of the evaluations with the shift managers and

appropriate members of the licensees engineering staff.

The inspectors utilized the following references during the completion of their review:

NRC Inspection Manual Part 9900, Technical Guidance, Operability

Determinations & Functionality Assessments for Resolution of Degraded or

Nonconforming Conditions Averse to Quality or Safety; September 26, 2005; and

NRC Regulatory Issue Summary RIS-05-020, Revision to Guidance Formerly

Contained in NRC Generic Letter 91-18, Information to Licensees regarding Two

NRC Inspection Manual Sections on Resolution of Degraded and Nonconforming

Conditions and on Operability.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

The inspectors completed one operator workaround sample. The inspectors evaluated

the impact of an existing operator challenge and corrective actions taken or proposed to

correct the problem:

Unit 1, 1D Main Steam Isolation Valve high Pressure Alarm.

During this review, the inspectors interviewed operating and engineering department

personnel and reviewed applicable documents.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

Enclosure

20

b.

Findings

No findings of significance were identified.

1R17

Permanent Plant Modification (71111.17)

a.

Inspection Scope

The inspectors completed one inspection sample by reviewing the following permanent

plant modification:

Unit 2 Digital Electrohydraulic System Modification

The inspectors reviewed the digital electrohydraulic system modification installed during

B2R12 to verify that the design basis, licensing basis, and performance capability of risk

significant systems were not degraded by the installation of the modification. The

inspectors considered the design adequacy of the modification by performing a review of

the modifications impact on plant electrical requirements, material requirements and

replacement components, response time, control signals, equipment protection,

operation, failure modes, and other related process requirements.

The inspectors utilized the following references during the completion of their review:

Updated Final Safety Analysis Report; and

Technical Specifications.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

b.

Findings

Introduction: A finding having very low safety significance (Green) was self-revealed

when the recently modified Digital Electrohydraulic System failed to respond to operator

input to initiate a turbine runback and subsequently resulted in a reactor trip. The failure

was due to a software error missed during the modification review and testing.

Description: From September 25 through October 12, 2005, Unit 2 conducted refueling

outage B2R12 during which the Digital Electrohydraulic (DEH) system was modified. On

October 18, 2005, with Unit 2 at full power, the operators removed the 2D

condensate/condensate booster (CD/CB) pump from service for planned maintenance.

Several hours later on October 19, 2005, the 2A CD/CB pump tripped and the operators

executed procedure 2BOA SEC-1, Secondary Pump Trip. Per procedure, the

operators tried to initiate turbine runback through the newly modified DEH system.

However, the system failed to respond to operator input. A load reduction was then

initiated by placing the turbine in manual and rapidly closing the turbine governor valves

to about 24 percent. However, by this time steam generator levels were approaching

Enclosure

21

the Reactor Protection System (RPS) trip setpoint. The operators then initiated actions

to trip the reactor but a reactor trip from low steam generator level was actuated by RPS

before the manual trip was accomplished.

Following the reactor trip, the licensee determined that the algorithm required for turbine

runback was deleted from the software database due to a compiler fault. An

undocumented length limitation on the software code caused the compiler fault. The

vendor and the licensee did not realize this limitation even though an error log existed

after compilation. In addition, the licensee did not test the turbine runback function at

power. The licensee also determined that the same condition existed in Unit 1 since the

DEH system was modified in March 2005. Based on these shortcomings in verification

and testing, the inspectors considered the post maintenance testing of the DEH

modification to be inadequate and contributed to a reactor trip.

Analysis: The inspectors determined that the failure to discover the software error for

the DEH modification was a performance deficiency because the licensees

modification process specified the need to perform post modification testing and

because it was within the licensees ability to foresee and prevent the error.

Traditional enforcement did not apply because the issue did not have any actual safety

consequences or potential for impacting the NRCs regulatory function and was not the

result of any willful violation of NRC requirements or licensees procedures. This finding

warranted a significance evaluation in accordance with Inspection Manual Chapter

(IMC) 0612 Power Reactor Inspection Reports, Appendix B, Issue Disposition

Screening issued on September 30, 2005. The inspectors determined that the finding

was more than minor because it affected the design control attribute of the Initiating

Events cornerstone. The initiating Events cornerstone objective is to limits the likelihood

of those events that upset plant stability and challenge critical safety functions during at-

power operations as the lack of turbine runback capability contributed to a reactor trip

from a feedwater system transient.

The inspectors determined that the finding could be evaluated using the Significance

Determination Process (SDP) in accordance with IMC 0609, Significance Determination

Process, because the finding was associated with the transient initiator contributors of

the Initiating Events cornerstone. The finding was determined to be of very low safety

significance (Green), since it only contributed to the likelihood of a reactor trip.

Enforcement: There were no violations of NRC regulatory requirements because the

affected equipment was not safety-related. The licensee entered this finding into their

corrective action program as AR 387581387581and subsequently reinstalled the missing

software algorithm into both Unit 1 and Unit 2 DEH systems.

(FIN 05000455/2005011-02)

1R19

Post Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed the post maintenance testing activities associated with

maintenance or modification of mitigating, barrier integrity, and support systems that

were identified as risk significant in the licensees risk analysis. The inspectors reviewed

Enclosure

22

these activities to determine that the post maintenance testing was performed

adequately, demonstrated that the maintenance was successful, and that operability was

restored. During this inspection activity, the inspectors interviewed maintenance and

engineering department personnel and reviewed the completed post maintenance

testing documentation. The inspectors used the appropriate sections of the TS, TRM,

and UFSAR, and other related documents to evaluate this area. The inspectors verified

that the licensee controlled post maintenance testing in accordance with the following:

BAP 1600-11, Work Request Post Maintenance Testing Guidance, Revision 12;

and

MA-AA-716-012, Post Maintenance Testing, Revision 5.

The inspectors completed five inspection samples by observing and evaluating the post

maintenance testing subsequent to the following maintenance activities:

Unit 2 Train B RH Suction from Sump Isolation Valve;

Unit 2 Train A Centrifugal Charging Pump;

Unit 1 Train A Emergency Diesel Generator Voltage Regulator Repair;

Unit 1 Train B Emergency Diesel Generator Output Relay failure and

Unit 1 Essential Service Water Discharge Cross-Tie Isolation Valve Breaker

Replacement.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R20

Refueling and Outage Activities (71111.20)

a.

Inspection Scope

The inspectors observed the licensees performance during B2R12 conducted

October 1, 2005 through October 12, 2005. This inspection sample was carried over

from last quarter.

The inspectors evaluated the licensees conduct of refueling outage activities to assess

the licensees control of plant configuration and management of shutdown risk. The

inspectors reviewed plant configuration to verify that the licensee maintained defense-in-

depth commensurate with the shutdown risk plan; reviewed major outage activities to

ensure that correct system lineups were maintained for key mitigating systems; and

observed refueling activities to ensure that fuel handling operations were performed in

accordance with TS, TRM, UFSAR and approved procedures. The inspectors

interviewed operations, engineering, work control, radiological protection, and

maintenance department personnel during their inspection activities. The inspectors

Enclosure

23

also attended outage-related status and pre-job briefings as well as Radiation Protection

ALARA [As Low As Reasonably Achievable] briefings. Other major outage activities

evaluated included the licensees control of:

Containment penetrations in accordance with the TS;

Structures, systems for components (SSCs) which could cause unexpected

reactivity changes;

Flow paths, configurations, and alternate means for reactor coolant system

inventory addition;

SSCs which could cause a loss of inventory;

Reactor coolant system pressure, level, and temperature instrumentation;

Spent fuel pool cooling during and after core offload;

Switchyard activities and the configuration of electrical power systems in

accordance with the TS and the shutdown risk plan; and

SSCs required for decay heat removal.

The inspectors observed portions of the plant startup, including the transition from

Mode 3 to Mode 2, to verify that the licensee controlled the plant startup and testing in

accordance with the TS. In addition, the inspectors completed numerous visual

inspections inside the Unit 2 containment. This included a tour of the Unit 2 containment

at Mode 3 before startup so that the inspectors could assess the material conditions of

equipments inside containment before the start of an operating cycle. During the visual

inspections the inspectors focused on the material condition of the equipment and

particularly on any indication of boric acid leakage.

The inspectors utilized the following references during the completion of their review:

ER-AP-331-1002; Boric Acid Corrosion Program Identification, Assessment,

and Evaluation;

HU-AA-104-101; Procedure Use and Adherence;

OP-MW-109-101; Clearance and Tagging;

OU-AA-103; Shutdown Safety Management Program;

OU-BY-204; Fuel Handling Activities in the Spent Fuel Pool for Byron and

Braidwood; and

OU-BY-205; Fuel Handling Activities in Containment During Refuel Outages for

Byron and Braidwood.

The documents reviewed during this inspection are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

Enclosure

24

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors witnessed selected surveillance testings and/or reviewed test data to

determine that the equipment tested using the surveillance procedures met the TS, the

TRM, the UFSAR and licensee procedural requirements. The inspectors also reviewed

applicable design documents including plant drawings, to verify that the surveillance

tests demonstrated that the equipment was capable of performing its intended safety

functions. The activities were selected based on their importance in ensuring mitigating

systems capability and barrier integrity.

The inspectors completed three inspection samples by observing and evaluating the

following surveillance tests:

Unit 2 Flow Balance of Charging and Safety Injection System to Cold Leg;

Unit 2 Train B Safety Injection Pump Discharge Outside Containment Isolation

Valve Stroke and Position Indication Test; and

Unit 2 Containment Floor Drain Level Transmitter Calculation.

Additionally the inspectors used the documents listed in the Attachment to this report to

determine that the testing met the frequency requirements; that the tests were

conducted in accordance with procedures that the test acceptance criteria were met;

and that the results of the tests were properly reviewed and recorded. The inspectors

verified that the individuals performing the tests were qualified to perform the test in

accordance with the licensees requirements, and that the test equipment used during

the test were calibrated within the specified periodicity. In addition, the inspectors

interviewed operations, maintenance and engineering department personnel regarding

the tests and test results.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors completed one inspection sample by evaluating the following temporary

plant modification on risk-significant equipment:

Removal of Tachometer Pickup Guard from Diesel Generator 1B.

The inspectors reviewed this temporary plant modification to determine that the

instructions were consistent with applicable design modification documents and that the

Enclosure

25

modification did not adversely impact system operability or availability. The inspectors

verified that the licensee controlled temporary modifications in accordance with Nuclear

Station Procedure NSP CC-AA-112, Temporary Configuration Changes, Revision 9.

The documents reviewed during this inspection are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The inspectors performed a screening review of Revision 16 of the Byron Station

Emergency Plan Annex to determine whether the changes made in Revision 16

decreased the effectiveness of the licensees emergency planning. This screening

review of Revision 16 was not documented in a Safety Evaluation Report and does not

constitute an approval of the changes. Therefore, the changes are subject to future

NRC inspection to ensure that the emergency plan continues to meet NRC regulations.

These activities completed one inspection sample.

b.

Findings

Introduction: The licensee changed one Emergency Action Level (EAL) that addressed

events related to unplanned radiological releases. This change was determined to

decrease the effectiveness of the licensees emergency plan, however, the licensee did

not submit this change to NRC for prior approval. This is a violation of 10 CFR 50.54(q)

and, because it impacted the regulatory process, traditional enforcement was applied.

Since this issue was entered into the licensees corrective action program and because

this item involved a failure to meet a regulatory requirement not directly related to

assessment or notification, this issue was determined to be a Severity Level IV Non-

Cited Violation (NCV).

Description: The licensees site-specific EALs were based on the guidance in

NUMARC/NRSP-007. In 1995, the licensee upgraded the RU2 EAL threshold value to

include criteria for confirming the validity of the effluent radiation monitor release

indications within 15 minutes by comparison with greater than or equal to two times the

Offsite Dose Calculation Manual limit. An Unusual Event would not be declared if the

comparison did not support the effluent monitors indication of a release. Revision 15 to

the Byron Station Emergency Plan Annex reflected this 15-minute criteria and appeared

as follows:

Enclosure

26

Revision 15 RU2 EAL Threshold Value In Part:

Unplanned Radiological release in excess of Table R1 Unusual Event value

unless releases can be determined to be below available Table R2 Unusual

Event thresholds within 15 minutes.

Revision 16 RU2 Threshold Value In Part:

Unplanned radiological release in excess of Table R1 Unusual Event threshold

for >60 minutes UNLESS release can be determined to be below available

Table R2 Unusual Event thresholds within this period.

Discussions with the licensee emergency preparedness staff and inspection of the

10 CFR 50.54(q) review records indicated this change was made to rearrange the EAL

with the more accurate indicators first and due to control room crews interpretation that

they had 75 minutes to declare an Unusual Event in this EAL. Also, the licensees

10 CFR 50.54(q) review indicated that the change did not decrease the effectiveness of

the emergency plan.

In contrast, the inspectors determined that the change to this indicator represented a

decrease in effectiveness of the emergency plan because the re-worded EAL threshold

removed the NRCs 1995 approved 15-minute requirement and replaced it with a

60-minute requirement for determining whether releases were below specified effluent

monitor thresholds.

The requirements of 10 CFR 50.54(q) allow the licensee to make changes to the

emergency plan without Commission approval as long as the change does not decrease

the effectiveness of the emergency plan. The inspectors noted that this change could

potentially delay the declaration of an Unusual Event by as much as 45 minutes.

However, since the licensee had concluded in its 10 CFR 50.54(q) review that the

change to this EAL threshold did not decrease the effectiveness of the emergency plan,

this change was not submitted to the NRC for review prior to implementation of the

revised EAL threshold.

Analysis: The inspectors determined that the failure to request NRC approval of the EAL

change was a performance deficiency. Furthermore, the failure to request NRC

approval of the EAL change potentially impeded the NRCs regulatory process and

was therefore, in accordance with Section 2.2.e of Appendix B to NRC Manual

Chapter 0609, evaluated using the guidance in Section IV of NUREG-1600, General

Statement of Policy and Procedure for NRC Enforcement Actions (Enforcement Policy),

rather than the NRC Significance Determination Process (SDP). This finding was more

than minor because extending the time period required for the appropriate emergency

classification of a radiological release could adversely affect the performance of both

onsite and offsite emergency actions. The finding is not suitable for SDP evaluation, but

has been reviewed by NRC management. The finding was therefore dispositioned as a

Severity Level IV violation according to Supplement VIII (Emergency Preparedness) of

the Enforcement Policy because it involved the licensees failure to meet an emergency

planning requirement (namely, 10 CFR 50.54(q)) not directly related to assessment of

and notification.

Enclosure

27

Enforcement: 10 CFR 50.54(q) states, in part, that the licensee may make changes to

these plans without Commission approval only if the changes do not decrease the

effectiveness of the plans. Proposed changes that decrease the effectiveness of the

approved emergency plans may not be implemented without application to and approval

by the Commission. Contrary to this, in Revision 16 of the Byron Station Emergency

Plan Annex, the licensee made a change to its standard EAL scheme that reduced the

effectiveness of the emergency plan. This change was not submitted to the NRC for

approval prior to implementation. The licensee entered this issue into their corrective

action program as Condition Report (CR) 00437193.

Changing an emergency plan commitment without prior NRC approval impacts the

NRCs ability to perform its regulatory function and is therefore processed through

traditional enforcement, as specified in Section IV.A.3 of the Enforcement Policy, issued

May 1, 2000 (65 FR 25388). According to Supplement VIII of the Enforcement Policy,

this finding was determined to be a Severity Level IV because it involved a failure to

meet a requirement not directly related to assessment and notification. Further, this

problem was isolated to one EAL and was not indicative of a functional problem with the

licensees EAL scheme. Additionally, because this was a Severity Level IV violation and

the licensee entered this issue into its corrective action program, this finding is being

treated as Non-Cited Violation (Severity Level IV) consistent with Section VI.A.1 of the

Enforcement Policy. (NCV 50-454/05-11-01).

1EP6

Drill Evaluation (71114.06)

a.

Inspection Scope

On November 14, 2005, the inspectors completed one inspection sample by observing

an Emergency Preparedness drill. The inspectors assessed the licensees exercise

performance and looked for weaknesses in the risk significance areas of emergency

classification, notification and protective action development. The inspectors observed

the licensees performance from the simulator control room and from the technical

support center. The inspectors compared issues noted during their observations to

those identified during the licensees critique as contained in the licensees exercise

findings and observation report. Additionally, the inspectors verified that items identified

during the licensees critique were appropriately entered into their corrective action

program. The drill scenario observed was:

Loss of offsite power to unit 1 and partial loss of offsite power to Unit 2 and

security event.

The inspectors also reviewed selected issues documented in CRs, to determine if they

had been properly addressed in the licensees corrective action program. The

documents reviewed during this inspection are listed in the Attachment to this report

b.

Findings

No findings of significance were identified.

Enclosure

28

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1

Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone

a.

Inspection Scope

The inspectors discussed performance indicators (PI) with the radiation protection (RP)

staff and reviewed data from the licensee's corrective action program to determine if

there were any performance indicators in the occupational exposure cornerstone that

had not been reported and reviewed. This review represented one sample.

b.

Findings

No findings of significance were identified.

.2

Plant Walkdowns and Radiation Work Permit Reviews

a.

Inspection Scope

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials (nonfuel) stored within the spent fuel or other

storage pools. This included discussions with cognizant licensee representatives.

This review represented one sample.

b.

Findings

No findings of significance were identified.

.3

Problem Identification and Resolution

a.

Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, and condition reports

(CRs) related to the access control program to determine if identified problems were

entered into the corrective action program for resolution. This review represented one

sample.

Corrective action reports related to access controls and high radiation area radiological

incidents (non-PI occurrences identified by the licensee in high radiation areas less than

1 Rem/hr) were reviewed. Staff members were interviewed and corrective action

documents were reviewed to determine if follow-up activities were being conducted in an

effective and timely manner commensurate with their importance to safety and risk

based on the following:

Enclosure

29

Initial problem identification, characterization, and tracking;

Disposition of operability/reportability issues;

Evaluation of safety significance/risk and priority for resolution;

Identification of repetitive problems;

Identification of contributing causes;

Identification and implementation of effective corrective actions;

Resolution of NCVs tracked in the corrective action system; and

Implementation/consideration of risk-significant operational experience feedback.

This review represented one sample.

The inspectors evaluated the licensees process for problem identification,

characterization and prioritization in order to determine if problems were entered into the

corrective action program and resolved. For repetitive deficiencies and/or significant

individual deficiencies identified in the problem identification and resolution process, the

inspectors determined whether the licensees self-assessment activities also identified

and addressed these deficiencies. This review represented one sample.

The inspectors discussed PIs with the RP staff and reviewed data from the licensee's

corrective action program to determine if there were any PIs for the occupational

exposure cornerstone that had not been reported and reviewed. There were none.

This review represented one sample.

b.

Findings

No findings of significance were identified.

.4

Radiation Worker Performance

a.

Inspection Scope

Radiological problem reports, which found that the cause of an event resulted from

radiation worker errors, were reviewed to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. This review

represented one sample.

b.

Findings

No findings of significance were identified.

.5

Radiation Protection Technician Proficiency

a.

Inspection Scope

Radiological problem reports, which found that the cause of an event was RP technician

error, were reviewed to determine if there was an observable pattern traceable to a

Enclosure

30

similar cause and to determine if this perspective matched the corrective action

approach taken by the licensee to resolve the reported problems. This review

represented one sample.

b.

Findings

No findings of significance were identified.

2OS2 As Low As Is Reasonably Achievable (ALARA) Planning And Controls (71121.02)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed plant collective exposure history, current exposure trends along

with ongoing and planned activities in order to assess current performance and

exposure challenges. This included determining the plants current 3-year rolling

average collective exposure. This review represented one sample.

Site specific trends in collective exposures and source-term measurements were

reviewed to evaluate the effect of the plants source term on worker exposure. This

review represented one sample.

b.

Findings

No findings of significance were identified.

.2

Verification of Dose Estimates and Exposure Tracking Systems

a.

Inspection Scope

The inspectors reviewed the assumptions and bases for the current annual collective

exposure estimate. Procedures were reviewed in order to evaluate the licensees

methodology for estimating work activity-specific exposures and the intended dose

outcome. Dose rate and man-hour estimates were evaluated for reasonable accuracy.

This review represented one sample.

b.

Findings

No findings of significance were identified.

.3

Problem Identification and Resolution

a.

Inspection Scope

The inspectors determined if the licensees self-assessment program identified and

addressed repetitive deficiencies and significant individual deficiencies that were

identified in the licensee's problem identification and resolution process. This review

represented one sample.

Enclosure

31

b.

Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

2PS3

Radiological Environmental Monitoring Program (REMP) And Radioactive Material

Control Program (71122.03)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed the 2003 and 2004 annual Radiological Environmental

Operating Reports and licensee assessment results to determine if the radiological

environmental monitoring program (REMP) was implemented as required by the

Radiological Environmental TSs (RETS) and the ODCM. The inspectors reviewed the

report for changes to the ODCM with respect to environmental monitoring and

commitments in terms of sampling locations, monitoring and measurement frequencies,

land use census, interlaboratory comparison program, and data analysis. The

inspectors reviewed the ODCM to identify environmental monitoring stations and

evaluated licensee self-assessments, audits, licensee event reports, and interlaboratory

comparison program results. The inspectors reviewed the UFSAR for information

regarding the environmental monitoring program and meteorological monitoring

instrumentation. The inspectors also reviewed the scope of the licensees audit program

to determine if it met the requirements of 10 CFR 20.1101c. This review represented

one sample.

b.

Findings

No findings of significance were identified.

.2

Onsite Inspection

a.

Inspection Scope

The inspectors accompanied the REMP vendor representative during his weekly sample

collection surveillance of all eight environmental air sampling stations and 16 of the

40 environmental thermoluminescent dosimeters to verify that their locations were

consistent with their descriptions in the ODCM and to evaluate the material condition of

these stations. This review represented one sample.

The inspectors observed the collection and preparation of a variety of environmental

samples including ground and surface water, and air. They also observed the technician

perform air sampler field check maintenance to determine if the air samplers were

functioning in accordance with vendor and licensee procedures. The inspectors

determined if environmental sampling was representative of the release pathways as

specified in the ODCM and that sampling techniques were in accordance with

procedures. This review represented one sample.

Enclosure

32

The meteorological monitoring site was observed and meteorological equipment

maintenance records were reviewed to evaluate the condition of the meteorological

instruments and to determine if the equipment was operable, calibrated, and maintained

in accordance with guidance contained in the UFSAR, annual report, NRC Safety

Guide 23, and licensee procedures. The inspectors reviewed the 2003 and 2004 Annual

Radiological Environmental Operating Reports and a sampling of monthly reports to

evaluate the onsite meteorological monitoring programs data recovery rates, routine

calibration, and maintenance activities. The inspectors determined if the meteorological

data readout and recording instruments, including computer interfaces and data loggers,

at the tower were operable; that readouts of wind speed, wind direction, delta

temperature, and atmospheric stability measurements were available on the licensees

computer system which was available in the control room, and that the computer system

was operable. This review represented one sample.

The inspectors reviewed each event documented in the Radiological Environmental

Operating Reports which involved missed samples, inoperable samplers, lost

thermoluminescent dosimeters, or anomalous measurements for the cause and

corrective actions. The licensees assessment of positive sample results (i.e., licensed

radioactive material detected above the lower limits of detection) were reviewed along

with the associated radioactive effluent release data that was the likely source of the

released material. This review represented one sample.

The inspectors reviewed the ODCM for significant changes resulting from land use

census modifications, or sampling station changes made since the last inspection. This

included a review of technical justifications for changed sampling locations. The

inspectors also determined if the licensee performed the reviews required to ensure that

the changes did not affect their ability to monitor the impacts of radioactive effluent

releases on the environment. This review represented one sample.

Calibration and maintenance records for the eight air samplers were reviewed to

determine if the equipment was being maintained as required. The inspectors reviewed

calibration records for radiation measurement (counting room) instrumentation that could

be used for environmental sample analysis and verified that the appropriate detection

sensitivities would be utilized for counting samples, in that the instrumentation could

achieve the RETS/ODCM required environmental lower level of detection. The

inspectors reviewed quality control data used to monitor radiation measurement

instrument performance, and actions taken for degrading detector performance.

The inspectors reviewed a licensee audit of the vendor laboratory that analyzed the

licensees REMP samples as the licensee does not perform radio-chemical analyses of

REMP samples. Additionally, results of the vendors interlaboratory comparison

program were reviewed to evaluate the effectiveness of the vendors analytical and

quality assurance programs. Corrective actions for deficiencies identified in the audit

were reviewed along with the vendors interlaboratory comparison program to verify the

adequacy of the vendors analytical and quality assurance programs.

The inspectors also evaluated the results of the licensees interlaboratory comparison

program to evaluate the adequacy of radio-chemical analyses performed by the

licensee. Licensee quality assurance audit results of the REMP were reviewed to

Enclosure

33

determine whether the licensee met the TS/ODCM requirements. This review

represented one sample.

b.

Findings

No findings of significance were identified.

.3

Unrestricted Release of Material from the Radiologically Restricted Area

a.

Inspection Scope

The inspectors observed the access control location where the licensee monitored

potentially contaminated material leaving the radiologically restricted area and inspected

the methods used for control, survey, and release of material from this area. The

inspectors observed the performance of personnel surveying and releasing material for

unrestricted use to verify that the work was performed in accordance with plant

procedures. This review represented one sample.

The inspectors verified that the radiation monitoring instrumentation was appropriate

for the radiation types present and was calibrated with appropriate radiation sources

that represented the expected isotopic mix. The inspectors reviewed the licensees

criteria for the survey and release of potentially contaminated material and verified

that there was guidance on how to respond to an alarm indicating the presence of

licensed radioactive material. The inspectors evaluated the licensees equipment to

determine if radiation detection sensitivities were consistent with the NRC guidance

contained in IE Circular 81-07 and IE Information Notice 85-92 for surface

contamination, and HPPOS-221 for volumetrically contaminated material.

The inspectors reviewed the licensees procedures and records to verify that the

radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters such as counting times and background radiation

levels. The inspectors determined if the licensee had established a release limit by

altering the instruments typical sensitivity through such methods as raising the energy

discriminator level or locating the instrument in a high radiation background area. This

review represented one sample.

b.

Findings

No findings of significance were identified.

.4

Identification and Resolution of Problems

a.

Inspection Scope

The inspectors reviewed self-assessments, audits, condition reports, and special reports

related to the radiological environmental monitoring program since the last REMP

inspection to determine if identified problems were entered into the corrective action

program for resolution. This included (1) the results of recent focus area self-

assessments of the REMP and Radioactive Material Control programs; (2) a Nuclear

Enclosure

34

Oversight Continuous Assessment Report and field observations; and (3) the licensees

CR database generated in calendar years 2003 - 2005. The inspectors evaluated the

effectiveness of these processes to identify, characterize and prioritize problems, and to

develop and implement corrective actions. The inspectors also verified that the

licensee's self-assessment program was capable of identifying and addressing repetitive

deficiencies or significant individual deficiencies that were identified by the problem

identification and resolution process.

The inspectors also reviewed corrective action documents related to the REMP that

affected environmental sampling and analysis, and meteorological monitoring

instrumentation. Staff members were interviewed and documents were reviewed to

determine if the following activities were being conducted in an effective and timely

manner commensurate with their importance to safety and risk:

Initial problem identification, characterization, and tracking;

Disposition of operability/reportability issues;

Evaluation of safety significance/risk and priority for resolution;

Identification of repetitive problems;

Identification of contributing causes;

Identification and implementation of effective corrective actions;

Resolution of NCVs tracked in the corrective action system; and

Implementation/consideration of risk significant operational experience feedback.

This review represented one sample.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

Cornerstones: Occupational and Public Radiation Safety

.1

Radiation Safety Strategic Area

a.

Inspection Scope

The inspectors sampled the licensees PI submittals for the periods listed below. The

inspectors used PI definitions and guidance contained in Revision 3 of Nuclear Energy

Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, to

verify the accuracy of the PI data. The following PIs were reviewed:

Occupational Exposure Control Effectiveness: Units 1 and 2

The inspectors reviewed the licensees assessment of the PI for occupational

radiation safety, to determine if indicator related data was adequately assessed

and reported during the previous four quarters. The inspectors compared the

Enclosure

35

licensees PI data with the condition report database, reviewed radiological

restricted area exit electronic dosimetry transaction records, and conducted

walkdowns of accessible locked high radiation area entrances to verify the

adequacy of controls in place for these areas. Data collection and analysis

methods for PIs were discussed with licensee representatives to determine if

there were any unaccounted for occurrences in the Occupational Radiation

Safety PI as defined in Revision 3 of Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline. This review

represented one sample.

Radiological Environmental TS/Offsite Dose Calculation Manual Radiological

Effluent Occurrences: Units 1 and 2

The inspectors reviewed data associated with the RETS/ODCM PI to determine if

the indicator was accurately assessed and reported. This review included the

licensees condition report database for the previous four quarters, to identify any

potential occurrences such as unmonitored, uncontrolled or improperly calculated

effluent releases that may have impacted offsite dose. The inspectors also

selectively reviewed gaseous and liquid effluent release data and the results of

associated offsite dose calculations and quarterly PI verification records

generated over the previous four quarters. Data collection and analyses

methods for PIs were discussed with licensee representatives to determine if the

process was implemented consistent with industry guidance in Revision 3 of

Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance

Indicator Guideline. This review represented one sample.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to determine that they were

being entered into the licensees corrective action system at an appropriate threshold,

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Minor issues entered into the licensees

corrective action system as a result of inspectors observations are generally denoted in

the list of documents reviewed at the back of the report.

b.

Findings

No findings of significance were identified.

Enclosure

36

.2

Annual Sample - Root Cause Evaluation for the Contamination of 0A and 0B Essential

Service Water Diesel Fuel Oil Storage Tanks

Introduction: On August 16, 2005, during a routine sampling of the diesel fuel oil storage

tank for the 0A Essential Service Water Make-up Pump Diesel Engine, the licensee

identified fuel oil contamination. The licensees associated extent of condition review

identified additional contamination of the 0B Essential Service Water Make-up Pump

diesel fuel oil storage tank. Both Essential Service Water Pumps were declared

inoperable as a result of these discoveries. The licensees subsequent root cause

analysis determined that this contamination was a result of improper tank cleaning work

that had been performed in June of 2005. The licensees root cause analysis cited

inadequate work instructions, the contract procurement process, and inadequate post

maintenance testing as contributors to this event.

a.

Prioritization and Evaluation of Issues

(1)

Inspection Scope

The inspectors reviewed the root cause evaluation associated with AR 353560353560and

discussed the technical aspects of these issues with members of the licensees

engineering, maintenance, and contract services staff. The licensee identified four

causal factors and four contributing causes. The root cause analysis identified seven

immediate, eight interim, and 12 long term corrective actions. After a review of the

completed and planned corrective actions the inspectors concluded that the issues

associated with this event were appropriately prioritized and adequately evaluated.

(2)

Issues

The licensee determined that the tank cleaning evolution was unsuccessful due to

programmatic and organizational issues. Four specific areas were noted:

The work package development process failed to recognize tank cleaning as an

activity requiring detailed instructions. The licensee relied upon the vendors

previous record of successful tank cleaning, supervision, and post maintenance

testing to produce the desired outcome;

Additional Operating Experience (OPEX) citing fuel contamination as a result of

cleaning activities was available but not included in the work package;

The licensee determined that the post maintenance test for this activity did not

completely address the scope of work performed. Additionally, there was no

requirement for fuel oil sampling upon tank fill completion; and

The contract requisition did not provide sufficient guidance for cleaning the fuel

tanks. A review of Service Procurement Procedure SM-AC-402, Revision 0

showed the policy provided inadequate direction for the inclusion of technical

scope in contract requests.

The inspectors review of the root cause evaluation found that the licensee completed it

using the analytical method of Tap Root. The inspectors considered the evaluation to be

of appropriate scope and depth for the situation. The inspectors considered the

associated extent of condition review to be extensive and appropriate.

Enclosure

37

b.

Effectiveness of Corrective Actions

(1)

Inspection Scope

The inspectors assessed the licensees immediate, interim, and long term corrective

actions associated with the fuel contamination root cause investigation to determine if

the corrective actions were appropriately focused to address the problems identified.

(2)

Issues

The inspectors reviewed the licensees root cause evaluation and determined that the

corrective actions addressed the causes identified. Corrective actions taken by the

licensee include:

Additional detail added to work instructions for the cleaning of diesel fuel oil

storage tanks;

Additional OPEX included in work instructions;

Review of open and ongoing contract releases and corresponding work

instructions for other vendor supported activities; and

Review and revision of contract guidance to ensure sufficient technical detail is

provided for future contractor work packages.

The inspectors determined that the immediate corrective actions focused on operability

concerns and were appropriate. The intermediate corrective actions addressed

procedural, programmatic, and extent issues and were appropriate. In regards to the

long term corrective actions, the inspectors considered them to be appropriate; however,

not all of the long term actions have been implemented. Those that have been

implemented lack sufficient historical depth to allow for assessment of effectiveness.

.3

Annual Sample - Essential Service Water Cooling Tower Concrete Degradation

Introduction: During this and previous report periods, the inspectors have noted a

number of issues entered into the corrective action program related to concrete

degradation of the circulating water natural draft cooling towers and essential service

water cooling towers. Since the essential service water system provides cooling water

to safety-related plant equipment under both normal and emergency conditions, the

degradation of the concrete structure could affect the heat removal capability of the

plant.

To access the extend of condition associated with the concrete degradation, the

inspectors performed a search on the licensees corrective action program database and

reviewed selected condition reports associated with this issue. The inspectors identified

that the licensee started experiencing concrete degradation in the essential service

water cooling towers back in 1998 and continued with the repairs since that time. Due to

the length of time that this problem existed, the inspectors selected this issue as one

annual sample of the licensees problem identification and resolution program.

Enclosure

38

Documents reviewed as part of this inspection were listed in the attachment to this

report.

a.

Prioritization and Evaluation of Issues

(1)

Inspection Scope

The inspectors reviewed selected action requests associated with the essential service

water tower concrete degradation and the related extent of condition review. The

inspectors considered the licensees evaluation and disposition of performance issues

and application of risk insights for prioritization of issues.

(2)

Issues

The inspectors found that the licensee prioritized and evaluated issues appropriately.

No significant issues were identified in this area.

b.

Effectiveness of Corrective Actions

(1)

Inspection Scope

The inspectors reviewed work orders associated with the concrete repair to determine if

the issues were repeated and if they were resolved promptly.

(2)

Issues

The inspectors determined that while concrete degradation in the cooling towers was

being addressed as early as 1998, the required functions of the cooling towers were not

affected due to its redundant design. However, as different modes of degradation were

discovered during repair work, the repair scope had to be changed by the licensee and

rescheduled, which in turn extended the work completion time. In addition, upon

questioning by the inspectors, the licensee also discovered that one of the work orders

for the repair work was inadvertently cancelled. This work order was reinstated.

In conclusion, the inspectors determined that the corrective actions to repair the cooling

towers were adequate and they were being addressed in a timely manner. No

significant issues were identified in this area.

.4

Semi-Annual Trending Review - Status of Human Performance Cross-Cutting Issue

Corrective Actions and Comprehensive Improvement Program

a.

Inspection Scope

During the mid-cycle assessment for the 2005 calendar year inspection program, the

NRC staff identified a substantive cross-cutting issue in the area of human performance.

The results of this assessment were provided to the licensee on August 30, 2005, in the

Byron Mid-Cycle Performance Review letter. Per the Mid-cycle Performance Review

Enclosure

39

letter, the inspectors conducted an annual inspection and trend review using Inspection

Procedure 71152, Identification and Resolution of Problems, to focus on human

performance issues.

The inspectors reviewed the licensees common cause analysis related to human

performance issues and station clock resets, self-assessment on human performance

and technical human performance, and selected departmental trend improvement plans.

The inspectors discussed these programs and reports with the applicable members of

the licensees staff.

Documents reviewed as part of this inspection were listed in the attachment to this

report.

b.

Issues

No findings of significance were identified. Over the course of the 2005 mid-cycle

assessment period, the inspectors identified 10 findings/violations of very low safety

significance (Green) where human performance was not adequate. The breakdown by

cornerstone for these findings/violations was as follows:

Initiating Events: 1 finding/violation;

Mitigating Systems: 5 findings/violations;

Barrier Integrity: 2 findings/violations; and

Occupational Radiation Safety: 2 findings/violations.

Specifically, the findings/violations were attributed to inadequate human performance in

manipulation of plant equipment outside of the normal work control processes, failing to

comply with procedural requirements, and failure to comply with contaminated and high

radiation area posting requirements.

The inspectors found that the licensee had given an appropriately high priority to the

actions intended to address the substantive cross-cutting issue in human performance.

Individual departmental human performance improvement plans were developed.

The licensee also conducted a Focused Area Self-assessment (FASA) in June and

August 2005 and a Common Cause Analysis (CCA) completed in December 2005.

The licensee has also established a new human performance coordinator. The licensee

did not have a station wide comprehensive improvement program, but was reviewing the

comprehensive improvement program developed at LaSalle for incorporation at Byron.

Many of the actions identified by the FASA and the CCA had completion dates in the

November 2005 and early 2006. The results of these efforts were considered

indeterminate since many of the actions were new or had not been completed.

However, the actions the licensee took to make station personnel aware of the human

performance problems including individual department human performance

improvement plans have had some effect in reducing human performance errors. In the

third and forth quarter inspection periods only two additional human performance

findings/violations of very low safety significance were identified. Based on the review

performed, the inspectors did not identify any additional trends.

Enclosure

40

4OA3 Event Follow-Up

.1

(Closed) Licensee Event Report (LER) 05000454, 455-2005-005-00: Both Trains of the

Ultimate Heat Sink Water Makeup Trains Exceeded TS Required Action Completion

Time Due to Contaminated Fuel Oil Resulting From Inadequate Tank Cleaning

Procedure.

On August 16, 2005, the licensee identified that diesel fuel oil for the safety related

Ultimate Heat Sink Water Makeup system diesel engine pumps contained water and

sediment contamination, which rendered both trains of the makeup system inoperable.

The licensee then entered into the appropriate TS limiting condition for operation (LCO),

drained, cleaned, flushed, refilled, and sampled the diesel fuel oil tanks and exited the

LCO. The licensee later determined that inadequate cleaning procedure and post

maintenance testing requirements for the diesel fuel oil tank cleaning process for each

tank in June 2005 resulting in contamination of the diesel fuel oil. The licensee

evaluated the safety significance of the water makeup system inoperability and the

inspectors reviewed the licensees evaluation. The inspectors determined that this issue

involved a violation of T.S. 5.4.1.a. The enforcement aspects of this issue were

discussed in Section 1R12 of NRC Inspection Report 05000454/455/2005009. This met

the requirements of 10 CFR 50.73 and is closed.

.2

Unit 2 Reactor Trip Response

a.

Inspection Scope

On October 19, 2005, the inspectors responded to the control room after being notified

that the reactor had automatically tripped from full power. The trip was caused by low

steam generator level as one of the CD/CB pump developed a fault in the motor and

tripped offline. The extra CD/CB pump was not available due to maintenance. A turbine

runback was initiated by the Operators in an attempt to match steam flow and feed flow.

However, the turbine control system failed to respond. Following the repair to the

CD/CB pump, the unit returned to full power on October 22, 2005. The inspectors

assessed control room operator performance immediately following the reactor trip and

reviewed the post trip report.

b.

Findings

No findings of significance were identified.

4OA5 Other Activities

.1

Pressurizer Penetration Nozzles and Steam Space Piping Connections in U.S.

Pressurized Water Reactors (TI 2515/160)

a.

Inspection Scope

On May 28, 2004, the NRC issued Bulletin 2004-01, Inspection of Alloy 82/182/600

Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping

Enclosure

41

Connections at Pressurized-Water Reactors (PWR). The purpose of this Bulletin was

to:

Advise PWR licensees that current methods of inspecting Alloy 82/182/600

materials used in the fabrication of pressurizer penetrations and steam space

piping connections may need to be supplemented with additional measures to

detect and adequately characterize flaws due to primary water stress corrosion

cracking;

Request PWR addressees to provide the NRC with the information related to the

materials from which the pressurizer penetrations and steam space piping

connections at their facilities were fabricated; and

Request PWR licensees to provide the NRC with the information related to the

inspections that have been and those that will be performed to ensure that

degradation of Alloy 82/182/600 materials used in the fabrication of pressurizer

penetrations and steam space piping connections will be identified, adequately

characterized, and repaired.

The objective of TI 2515/160, Pressurizer Penetration Nozzles and Steam Space Piping

Connections in U.S. Pressurized Water Reactors, was to support the NRC review of

licensees activities for inspecting pressurizer penetrations and steam space piping

connections made from Alloy 82/182/600 materials, and to determine whether the

inspections of these components are implemented in accordance with the licensee

responses to Bulletin 2004-01. In response to Bulletin 2004-01, the licensee committed

to perform a bare metal visual inspection of 100 percent of the five susceptible Inconel

pressurizer penetrations in the upper pressurizer head using a VT-2 qualified examiner.

On September 28, 2005, the inspector observed the licensee performing this inspection

on Unit 2 and performed a review, in accordance with TI 2515/160, of the licensees

controls and personnel used for pressurizer penetration nozzles and steam space piping

connections examinations to confirm that the licensee met commitments associated with

Bulletin 2004-01. The results of the inspectors review included documenting

observations and conclusions in response to the questions identified in TI 2515/160.

b.

Observations

Summary: Based upon a bare metal visual examination of the Unit 2 pressurizer upper

head nozzles, the licensee did not identify any indications of boric acid leaks.

Evaluation of Inspection Requirements

In accordance with the requirements of TI 2515/160, inspectors evaluated and answered

the following questions:

1.

For each of the examination methods used during the outage, was the

examination performed by qualified and knowledgeable personnel?

Enclosure

42

Yes. The licensee conducted a direct visual examination of the bare metal

surface of the upper pressurizer head heater penetration nozzles with a

knowledgeable staff member certified to Level III as a VT-2 examiner in

accordance with procedure TQ-AA-122, Qualification and Certification of

Nondestructive (NDE) Personnel. This qualification and certification procedure

referenced the industry standards SNT-TC-1A, Personnel Qualification and

Certification in Nondestructive Testing, and ANSI/ANST CP-189, Standard for

Qualification and Certification of Nondestructive Testing Personnel.

2.

For each of the examination methods used during the outage, was the

examination performed in accordance with demonstrated procedures?

Yes. The inspectors observed the licensee performing the bare metal inspection

of the pressurizer nozzles in accordance with work order 00745675 which

referenced procedure ER-AP-331-1001. This procedure required licensee

examination staff to use the VT-2 visual examination method in accordance with

procedure, ER-AA-33-015, VT-2 Visual Examination. The licensee examiner

conducted this inspection with a flashlight in accordance with ER-AA-33-015, and

demonstrated adequate illumination on an 18 percent neutral gray card with a

1/32 inch black line. Based on ensuring adequate illumination and resolution, the

inspectors considered this procedure demonstrated for the purpose of a bare

metal visual examination of the pressurizer upper head nozzles.

3.

Able to identify, disposition, and resolve deficiencies?

Yes. The inspectors concluded that the licensees direct visual examinations

were capable of detecting leakage from cracking in pressurizer penetrations if it

had existed. This conclusion was based upon the inspectors direct observations

of pressurizer penetration locations which were free of debris or deposits that

could mask evidence of leakage in the areas examined.

4.

Capable of identifying the leakage in pressurizer penetration nozzle or steam

space piping components, as discussed in NRC Bulletin 2004-01?

Yes. The inspectors basis is discussed in the answer to question 3 above.

5.

What was the physical condition of the penetration nozzle and steam space

piping components in the pressurizer system (e.g., debris, insulation, dirt, boron

from other sources, physical layout, viewing obstructions)?

The upper pressurizer head Inconel penetrations included three safety relief

valve penetration nozzles, a power operated relief valve nozzle and a spray line

penetration nozzle. The inspectors observed that the canned metal reflective

insulation had been removed from the pressurizer at these penetration locations

to allow a direct bare metal visual examination. The inspector performed a direct

visual inspection for these pressurizer penetrations. Based on this examination,

the area examined was clean and free of debris or deposits or other obstructions

which could mask evidence of leakage.

Enclosure

43

6.

How was the visual inspection conducted (e.g., with video camera or direct visual

by the examination personnel)?

The licensee conducted a direct bare metal visual examination of these

pressurizer penetrations. No video or photography equipment was used.

7.

How complete was the coverage (e.g., 360 degrees around the circumference of

all the nozzles)?

The licensee performed a bare metal inspection of the five steam space piping

connections/nozzles which included 360 degrees around the circumference of

each penetration nozzle.

8.

Could small boron deposits, as described in the Bulletin 2004-01, be identified

and characterized?

Yes. The inspectors determined through direct observation of the licensees

efforts that the licensee staff were capable of detecting pressurizer nozzle

leakage, if any had existed. The work order contained specific instructions for

acceptance criteria and reporting requirements. The licensee relied on the

corrective action system process to make decisions on how to characterize

deposits. Because the licensee did not identify any deposits indicative of

leakage in the areas examined, the inspectors could not assess the licensees

plans to characterize leakage on pressurizer components.

9.

What material deficiencies (i.e., cracks, corrosion, etc.) were identified that

required repair?

The licensee did not identify any material deficiencies that required repair.

10.

What, if any, impediments to effective examinations, for each of the applied

methods, were identified (e.g., centering rings, insulation, thermal sleeves,

instrumentation, nozzle distortion)?

The licensee did not identify any impediments to an effective examination. All of

the insulation had been removed around the nozzles to allow a direct visual

examination of the bare metal for 360 degrees around the circumference of each

penetration nozzle.

11.

If volumetric or surface examination techniques were used for the augmented

inspection examinations, what process did the licensee use to evaluate and

dispose any indications that may have been detected as a result of the

examinations?

Not applicable. The licensee did not perform augmented volumetric or surface

examinations.

12.

Did the licensee perform appropriate follow-on examinations for indications of

boric acid leaks from pressure-retaining components in the pressurizer system?

Enclosure

44

Not applicable. The licensee did not identify any indications of boric acid leaks

from pressure retaining components in the pressurizer system.

.2

Transportation of Reactor Control Rod Drives in Type A Packages (TI 2515/161)

a.

Inspection Scope

The inspectors conducted interviews and record reviews to verify that: (1) the licensee

had undergone refueling activities since calender year 2002; and (2) did not ship

irradiated control rod drive mechanisms in Department of Transportation Specification

7A, Type A packages during the time frame 2002 to the present.

b.

Findings

No findings of significance were identified.

.3

(Closed) Unresolved Item (URI) 5000454/2005003-06: Unverified Vessel Head

Temperatures Used in Effective Degradation Year (EDY) Calculation

The inspectors had previously reviewed the licensees Unit 1 vessel head

penetration nozzle susceptibility ranking calculation to verify that it complied with NRC

Order EA-03-009. During the review, the inspectors had identified that the licensee

lacked reference data to support the best estimated values for vessel head temperatures

used in the susceptibility ranking calculation EC-354172, B1R13 End of Cycle 13

Effective Degradation Years In Accordance with NRC Order EA-03-009.

The inspectors reviewed the licensees corrective actions for this issue. The licensee

corrective actions for this issue included revising calculation EC-354172 to include new

vessel head temperature data. The inspectors confirmed that the new data used in

Revision 1 of EC-354172 was traceable to plant specific values for each operating cycle

and concluded that the revised calculation met the NRC Order EA-03-009. The

licensees failure to use best estimate head temperature values in Revision 0 of

calculation EC-354172, was an example of a violation of Section IV.A of NRC Order

EA-03-009. Because the best estimated head temperatures changed by only a few

degrees from Revision 0 to Revision 1 of EC-354172, the overall effect on the

calculation output was 0.05 EDY which did not affect the head susceptibility ranking or

required inspections. Therefore, the inspectors determined that this was a violation of

NRC Order EA-03-009 of minor significance. URI 05000454/2005003-06 is closed.

Closure of this URI also completes TI 2515/150 Reactor Pressure Vessel Head and

Vessel Head Penetration Nozzles, for Unit 1.

.4

(Closed) Unresolved Item (URI) 050000454/455/2005004-05: Review of Missed

Ventilation and Filtration System TS Surveillance Requirements

On January 13, 2005, during a Nuclear Oversight Audit, the licensee identified that

15 TSs required ventilation surveillance tests were not performed. The licensees

subsequent root cause evaluation and investigation determined that the missed

surveillance tests were due to willful falsification of documents by a non-licensed

employee. The licensees associated extent of condition review identified 12 additional

Enclosure

45

TS required ventilation surveillance tests that were also falsified. Upon performing the

27 falsified surveillance requirements, six failed. The NRC determined that this issue

was a violation of Byron Station TSs. By providing false information regarding the

surveillances, the non-licensed employee also caused the licensee to be in violation of

10 CFR 50.9, Completeness and Accuracy of Information. In addition, the activities of

the employee also placed himself in violation of 10 CFR 50.5, Deliberate Misconduct.

The enforcement aspects of this issue were described in the Notice of Violation EA-05-

159, Byron Station - Notice of Violation [NRC Office of Investigations Report No. 3-

2005-008, from James L. Caldwell to Christropher M. Crane, dated October 27, 2005.

This URI is closed.

4OA6 Meetings

.1

The inspectors presented the inspection results to Mr. S. Kuczynski and other members

of licensee management on January 6, 2006. The inspectors asked the licensee

whether any materials examined during the inspection should be considered proprietary.

No proprietary information was identified.

.2

Interim Exit Meetings

Interim exits were conducted for:

Temporary Instruction 2515/160, and Procedure 71111.08 with Mr. D. Hoots and

other members of licensee management at the conclusion of the inspection on

October 6, 2005. The inspectors returned proprietary information reviewed

during the inspection and the licensee confirmed that none of the potential report

input discussed was considered proprietary;

Radiation Protection inspection with Mr. S. Kuczynski on October 14, 2005;

Biennial heat sink inspection with Mr. S. Kuczynski and other members of

licensee management at the conclusion of the inspection on December 2, 2005;

and

Emergency Preparedness inspection with Mr. S. McCain and Mr. D. Drawbaugh

by telephone call on December 28, 2005.

4OA7 Licensee Identified Violations

None.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Kuczynski, Site Vice President

D. Hoots, Plant Manager

B. Adams, Engineering Director

D. Drawbaugh, Emergency Preparedness Manager

T. Fluck, NRC Coordinator

S. Gackstetter, Operations Training Manager

T. Green, Level III NDE

W. Grundmann, Regulatory Assurance Manager

S. Kerr, Chemistry Manager

S. Koernschild, Engineering

W. Kouba, Nuclear Oversight Manager

B. McBride, ISI Engineer

S. McCain, Corporate Emergency Preparedness Manager

M. Marchionda, Shift Operations Supervisor

D. Palmer, Radiation Protection Manager

M. Prospero, Operations Manager

J. Smith, Steam Generator Engineer

M. Snow, Work Management Director

T. Spelde, Asset Management

E. Steinke, Chemistry

N. Vakili, 89-13 Program Owner

B. Youman, Maintenance Manager

Nuclear Regulatory Commission

R. Skokowski, Chief, Division of Reactor Project

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None.

Opened and Closed

05000455/2005011-01

NCV

Failure to Perform a VT-2 Examination at Nominal

Operating Pressure Test for New RH System Welds

(Section 1R08)05000455/2005011-02

FIN

Failure to Perform Adequate Modification Testing for the

Digital Electrohydraulic System (Section 1R17)

Attachment

2

05000454/2005011-03

05000455/2005011-03

NCV

10 CFR 50.54(q) Violation for Decreasing the

Effectiveness of the Emergency Plan by Changing EAL

RU2 Threshold That Address Radiological Effluents

Without Prior NRC Approval or Adequate 10CFR50.54(q)

Review (Section 1EP4)

Closed

05000454-2005-005-00

05000455-2005-005-00

LER

Both Trains of the Ultimate Heat Sink Water Makeup

Trains Exceeded TS Required Action Completion Time

Due to Contaminated Fuel Oil Resulting From

Inadequate Tank Cleaning Procedure.05000454/2005003-06

URI

Unverified Vessel Head Temperatures Used in EDY

Calculation (Section 4OA5.3)05000454/2005004-05

05000455/2005004-05

URI

Review of Missed Ventilation and Filtration System TS

Surveillance Requirements (Section 4OA5.4)

Discussed

None.

Attachment

3

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01

Adverse Weather Protection

WO 637729, Freezing Temperature Protection - Protected Area Buildings, Ventilation,

and Tanks;

WO 755476, Freezing Temperature Protection - Non-Protected Area Buildings,

Ventilation, and Tanks;

WO 756245-01, Freezing Temperature Protection - SX Area Heaters Testing;

WO 756245-02, Freezing Temperature Protection - SX Area Heaters Testing;

WO 755031, Freezing Temperature Protection - Auxiliary Steam Boiler Testing;

WO 755475, Freezing Temperature Protection - Plant Ventilation System;

CR 399621, Unit 2 RWST Vent Heat Trace Temperature Controller Found

Mispositioned;

CR 398924, Freeze Protection - Need Gap Filled in Security Diesel Room;

CR 394858, Drain Condensate Tanks for Freeze Protection;

CR 272743, Essential Service Water Chemical Addition Piping not Insulated;

CR 265894, Louver Panel Broke, Turbine Building 401' C-23;

CR 385804, Heating Unit not Working;

CR 264434, Damaged Piping Insulation;

1R04

Equipment Alignment

OP-AA-108-112, Definition and Measurement of Mispositioned Plant Components,

Revision 1;

BOP-AF-M1A, Auxiliary FEEDWATER System Train A Valve Lineup, Revision 3;

BOP-AF-E1A, Auxiliary Feedwater Train A Electrical Lineup, Revision 1;

BOP-AF-E1C, Auxiliary Feedwater Train C Electrical Lineup, Revision 1;

BOP-AF-E1, Auxiliary Feedwater Electrical Lineup, Revision 8;

BOP-AF-M1, Auxiliary Feedwater System Lineup, Revision 14;

BOP SA-M2C, Service Air System Valve Lineup, Revision 2;

BOP SA-E2, Service Air Electrical Lineup, Revision 3;

BOP SA-M1, Service Air System Valve Lineup, Revision 28

1R05

Fire Protection

Byron Station Pre-Fire Plan for Zone 11.5-0 Auxiliary Building 401' Elevation General

Area, Revision 4;

Byron Station Pre-Fire Plan for Zone 3.2A-1, Lower Cable Spreading Room, Revision 4;

Byron Station Pre-Fire Plan for Zone 5.5-2, Unit 2 Auxiliary Electrical Room, Revision 4;

Byron Station Pre-Fire Plan for Zone 9.2-2, 2A Diesel Generator Room, Revision 4;

Byron Station Pre-Fire Plan for Zones 1.1-2, 1.2-2, 1.3-2, Containment Building;

Byron Station Pre-Fire Plan for Zone 18.3-1, Unit One Steam Tunnel;

Byron Station Pre-Fire Plan for Zone 11.4A-2, 2B Auxiliary Diesel Feedwater Pump

Attachment

4

Room;

Byron Station Pre-Fire Plan for Zone 5.4-1, Division 12 Misc Electrical Equipment and

Battery Room;

Byron Station Pre-Fire Plan for Zone 5.1-1, Division 12 ESF Switchgear Room;

Byron Station Pre-Fire Plan for Zone 8.6-0, Turbine Building;

1R06

Flood Protection Measures

BAR 0-38-A14, Turbine Building Fire/Oil Sump Flood Level, Revision 4;

1 BFR-Z.2, respond to Containment Flooding Unit 1, Revision 101;

2 BFR-Z.2, Respond to Containment Flooding Unit 2, Revision 101;

BHP 4200-81, Calibration of Magnetrol Flood Level Switch, Revision 4

1R07

Heat Sink Performance

WO 00588797, Inspection Heat Exchanger 2SX02K per Generic Letter 89-13,

October 6, 2005;

IR 381461, The end bells of Heat Exchanger 2SX02K were found with significant

deposits of mud and silt;

EC 357755, Past Operability Evaluation for Heat Exchanger 2SX02K;

IR 381941, The end bells and cover plates for Heat Exchanger 2SX02K had surface

imperfections after being sand blasted;

0BOA ENV-1; Adverse Weather Conditions Unit 0; Revision 102

0BOA-ENV-2; Rock River Abnormal Water Level Unit 0; Revision 100

0BOA ENV-4; Earthquake Unit 0; Revision 100

0BOA PRI-7; Lost of Ultimate Heat Sink Unit 0; Revision 0

0BOL 7.9; LCOAR Ultimate Heat Sink (UHS) Tech Spec LCO # 3.7.9; Revision 7

1BOA ENV-1; Adverse Weather Conditions Unit 1; Revision 100

1BVSR SX-4; Unit 1 Essential Service Water Flow Verification; Revision 3

1BVSR XII-12; Ultrasonic Thickness Examinations of Selected Essential Service Water

Components; Revision 3

2BOA Env-1; Adverse Weather Conditions Unit 2; Revision 100

BAP-560-3; Byron Cooling Water Chemistry Monitoring Program Description CW, WS,

SX; Revision 7

BOP SX-T2; SX Tower Operation Guidelines; Revision 12

BRW-95-218; Evaluation of Essential Service Water Pump Operation with Degraded

Lube Oil Coolers; Revision 0

BVP 200-19A1; Erosion/Corrosion Program; Revision 11

BVP 800-30; Service Water System (Essential Service Water) Fouling Monitoring

Program; Revision 8

BVP 800-30; Attachment D GL 89-13 HX Inspection Cover Sheet Inspection Results for

1A Sx Pump Room Cubicle Cooler; dated March 10, 2000

BVP 800-30; Attachment D GL 89-13 HX Inspection Cover Sheet Inspection Results for

1B Sx Pump Room Cubicle Cooler; dated April 3, 2000

CR 145070; 1A DG JW HX Corrosion; dated February 2, 2003

CR 154998; Potential Adverse Impact on Configuration Control; dated April 4, 2003

CR 157568; 1B DG JW Deficiencies; dated May 7, 2003

CR 168022; Incorrect Use of Grace Period for GL 89-13 HX Inspection Frequency;

dated July 17, 2003

CR 181006; Byron Station Review of OE 17031; dated October 15, 2003

CR 211766; Failed PMT on 2B DG Jacket Water Lower Cooler; dated March 30, 2004

Attachment

5

CR 255966; U0 CC HX GL 89-13 Inspection Past Critical Date; dated August 23, 2004

CR 282088; Inspection Date of 1DG01KB HX Too Close to Critical Due Date; dated

December 13, 2004

CR 291416; Filling and Venting Issues; dated January 17, 2005

CR 311626; As-Found Tube Blockage Accept Criter Not Met for 1AF01AB HX; dated

March 11, 2005

CR 335594; As-Found Tube Blockage In Excess of Limit in Calc BYR04-005; dated

May 16, 2005

CR 336162; 1A DG JW Cooler Tube Cleaning Issues; dated May 18, 2005

CR 353128; Deficiencies Identified During Heat Sink Performance FASA; dated

July 14, 2005

CR 389412; NOS ID - IR Review Not Per FASA Plan Evaluation Criteria; dated

October 24, 2004

CR 393026; EC 350427 Not Completed in Time; dated November 1, 2005

CR 394756; Results of Sr Mgr Challenge Mtg for Heat Sink Inspection; dated

November 4, 2005

CR 399041; 2A SX Pp Oil HX Fails As-Found GL 89-13 Tube Blockage Ac; dated

November 15, 2005

CR 399996; Time to Revisit Silting Issues at Byron; dated November 17, 2005

CR 428230; 1SX011 Valve Failed to Electrically Stroke Closed; dated

November 28, 2005

CR 428265; 1SX136 Did Not Stroke Full Open When Requested; dated

November 29, 2005

CR 428276; 1B SX Pp Oil HX Fails As-Found GL 89-13 Tube Blockage Ac; dated

November 29, 2005

CY-AA-120-4110; Raw Water Chemistry Strategic Plan; Revision 0

Drawing E6000-3001; Cubicle Cooler; Revision E

EC 336446; Cubical Cooler Tube Plugging; dated October 3, 2002

EC 339308; Develop Tube Plugging Criteria for GL 89-13 Heat Exchanger Work with

Harlan Kats to Determine Scope of HX in the Program; dated December 9, 2002

EC 344005; SX Pump Lube Oil Cooler Allowable Tube Blockage; Revision 0

EC 351458; Provide Justification for Extending GL 89-13 Inspection of 0CC01A Past Its

Critical Due Date of 9/22/2004; Revision 0

EC 355492; Justification for Inspection Frequencies; Revision 0

EC 357755; Past Operability Evaluation for 2B AF Pump Right Angle Gear Lube Oil

Cooler - 2SX02K; dated November 3, 2005

ER-AA-340; GL 89-13 Program Implementing Procedure; Revision 2

ER-AA-340-1001; GL 89-13 Program Implementation Instructional Guide; Revision 4

ER-AA-340-1002; Service Water Heat Exchanger and Component Inspection Guide;

Revision 2

FASA AT 278787-04; Focused Area Self-Assessment Heat Sink Performance; dated

November 7, 2005

Heat Exchanger Specification Sheet Ametek Job No. N80-40361; Sx Pump Lube Oil

Cooler; dated February 25, 1980

Specification F/L-2900; Cubicle Coolers; dated July 18, 1983

UT Analysis Report: Sub-component 2SXH01-1; dated October 2, 1993

UT Analysis Report: Sub-component 2SXH01-1; dated February 12, 1995

UT Analysis Report: Sub-component 2SXH02-2; dated October 1, 1993

UT Analysis Report: Sub-component 2SXH02-2; dated February 14, 1995

Attachment

6

UT Analysis Report: Sub-component 2SXH03; dated October 1, 1993

UT Analysis Report: Sub-component 2SXH03; dated February 14, 1995

UT Analysis Report: Sub-component 2SXL06; dated February 12, 1995

UT Analysis Report: Sub-component 2SXL06; dated August 29, 1996

VA-100; ESF Cubicle Energy Calculation; Revision 6

WO 584007; 2DG01KB - HX Inspection per GL 89-13

WO 604156; 2DG01KA - HX Inspection per GL 89-13; dated June 30, 2004

WO 661419; 1SX01AB - HX Inspection per GL 89-13; dated January 18, 2005

WO710086; 1DG01KA - HX Inspection per GL 89-13; dated May 9, 2005

WO 99157835; Perform SED Thermal Surveillance per BVP 800-30; dated

November 8, 2001

WO 99157896; 2DG01KA - HX Inspection per GL 89-13; dated January 15, 2002

WO 99230765; 1VA01SA - HX Inspection Per Generic Letter 89-13; dated July 21, 2003

CR Generated From Inspection:

CR 428932; 0DO088 Apparently Leaking; dated November 30, 2005

1R08

Inservice Inspection Activities

Corrective Action Program Documents

AR 00212270, 2A SG Waterbox Foreign Objects; March 31, 2004;

AR 00212575, Foreign Objects Identified in 2D SG Preheater; April 1, 2004;

AR 00218465, Error in EPRI Report Leads to Low SG In-Situ Test; May 3, 2004;

AR 00232331, OE 18620 Bottom Head Visual - Lack of Coverage; June 29, 2005;

AR 00233562, Harris SG Tube Leak from Loose Parts; July 2, 2005;

AR 00292042, Ultrasonic Examination Reveals Thin Areas in FP Pipe, January 19,

2005;

AR 00297866, Required QV Hold Point Not Performed; February 1, 2005;

AR 00305116, U2 Steam Generator Secondary Side Cover ASME Code Issue,

February 24, 2005;

AR 00354493, U2 SG Tube Not Expanded; July 19, 2005;

AR 00377135, TRM Appendix I Table Does Not List Latest Revision of WCAP-14976,

September 23, 2005;

AR 00377795, Body to Bonnet Leakage 2RC8045D, September 25, 2005;

AR 00504902, Unit 2 ASME Section XI Pressure Test, April 8, 2004;

CR 276428, Ultrasonic Thickness Below Nominal Wall, November 24, 2004;

CR 313173, B1R13 LL 3/15/05 NRC ISI Audit Team Debrief Comments, March 15,

2005;

IR- 331095, Failure to Identify Thru-Wall FP Leak with an IR/WR, May 2, 2005

Corrective Action Program Documents as a Result of NRC Inspection

AR 00379823,Procedure ER-AP-335-1012 Needs Enhancement, September 29, 2005;

AR 00379827, Overly Conservative Use of Recordable Indication, September 29, 2005;

AR 00380389, Inadequate VT-2 Performed for EC 333251 Letdown Booster Pump,

September 30, 2005;

AR 00380444, Failure to Evaluate Past Operability, September 30, 2005;

AR 00380254, Potential Historical Missed TRM TLCO 3.4.F Entry, September 30, 2005;

IR-00380472, Improper Penetrameter Placement During Radiographic Test,

September 30, 2005;

Attachment

7

Corrective Action Program Documents With Engineering Evaluations for Boric Acid

Leakage

Evaluation No. 2004-315 for Component 2CV128, Minor Packing Leak; October 28,

2004;

Evaluation No. 2004-466 for Component 2RH029A, Valve Cap found Leaking at 1/2 Drop

per Second, November 9, 2004;

Evaluation No. 2004-404 for Component 2SI121A, Boric Acid Leak at Base of Relief

Valve, November 16, 2004;

Corrective Action Program Documents for Boric Acid Leakage

AR 00377795; Body-Bonnet Leakage from 2RC8045D; September 26, 2005.

AR 00377801; 2SI8956D Minor Dry Boron on B/B Flange; September 26, 2005.

AR 00379378; Boric Acid Packing Leak, Dry 2CV236; September 29, 2005.

AR 00379379; Boric Acid Leak at Body to Bonnet 2CV8160, Dry; September 29, 2005.

AR 00381103; Boric Acid Leakage at Check Valve Cap; October 3, 2005.

Documents Related to Pressure Boundary Welding

ASME Weld Data Record; 3"X16" weld-o-let; September 17, 2003.

ASME Weld Data Record; 2RH032AA-3; September 17, 2003.

ASME Weld Data Record; 2RH032AB-3; September 17, 2003.

Liquid Penetrant Examination Data Report 2003-244; FW-5; September 5, 2005.

Liquid Penetrant Examination Data Report 2003-287; FW-1; September 17, 2005.

Liquid Penetrant Examination Data Report 2003-289; FW-4&6; September 17, 2005.

Procedure ER-AA-335-005, Radiographic Examination, Revision 1.

PQR 1-51A; April 21, 2001.

PQR 4-51A; April 20, 2001.

PQR A-003; February 8, 2000.

PQR A-004; February 8, 2000.

Radiography Examination Report: 2003-216, welds W2 and W3 (and associated RT

Film.); September 3, 2003.

VT-2 Visual Examination Record, 2RH8703 B/A; March 23, 2004.

VT-2 Visual Examination Record, 2RH8703 B/A; September 18, 2003.

Work Order 00366731; Install Line 2RH032AA-3" and 2RH032AB-3"; September 17,

2003.

WPS 8.8-GTSM; GTAW, SMAW; Revision 1.

Documents Associated with the Visual Examination of The Vessel Head

ER-AP-335-1012; Visual Examination of PWR Reactor Vessel Head Penetrations;

Revision 1.

Documents Associated with Disposition of Relevant Indications

Data Sheet 2004-159; VT-3 examination of Support 2RC18001S, March 23, 2004.

Indication Data Sheet 2004-112, Ultrasonic Examination of Weld C30 on Line

2FW87CB-6"; March 30, 2004.

Attachment

8

Documents Associated with ASME Code Nondestructive Examinations Observed

Ultrasonic Calibration Data Sheet B2R12-UT-011; 2FW03DD-16", FW C01, C02;

September 27, 2005.

Ultrasonic Calibration Data Sheet B2R12-UT-012; 2RC28A-3", FW J03, J04, J05;

September 27, 2005.

Ultrasonic Calibration Data Sheet B2R12-UT-013; 2FW87CA-6", FW C05, C06, C07,

C08, C09; September 27, 2005.

Surface Examination Data Sheet 2MS07AD-28", E-2; September 27, 2005.

Documents Associated with Steam Generator Examinations

Amendment No. 144 to NPF-66; September 19, 2005.

EC 349439; SG Pressure Test Evaluation B2R11; Revision 0.

ER-MW-335-1009; Site Specific Performance Demonstration Program; Revision 1.

ETSS CBE-001-0905; Bobbin 40(IPS); September 26, 2005.

ETSS CBE-002-0905; Bobbin 24(IPS); September 26, 2005.

ETSS CBE-003-0905; Bobbin 24(IPS); September 26, 2005.

ETSS CBE-004-0905; 3Coil, +PT; September 26, 2005.

ETSS CBE-005-0905; 3Coil, +PT Dent; September 26, 2005.

ETSS CBE-006-0905; 3Coil, +PT MagBias; September 26, 2005.

ETSS CBE-007-0905; Low Row U-bend +PT; September 26, 2005.

ETSS CBE-008-0905; High Row U-bend +PT; September 26, 2005.

Letter BYRON 2005-0089; Byron Unit 2 Inspection Degradation Assessment and

Condition Monitoring Checklist for B2R12; July 28, 2005.

Letter RS-04-159; Response to NRC Generic Letter 2004-01,Requirements for Steam

Generator Tube Inspection; October 29, 2004.

MRS 2.4.2 Gen-45; Standard In-Situ Pressure Test Using the Computerized Data

Acquisition System; Revision 3.

Tube Plugging and Stabilization List; SG 2C; October 3, 2005.

Tube Plugging and Stabilization List; SG 2B; October 3, 2005.

Tube Plugging and Stabilization List; SG 2D; October 4, 2005.

Tube Plugging and Stabilization List; SG 2D; October 5, 2005.

Westinghouse Document DDM-96-009; Documentation of Appendix H Compliance and

Equivalency, Pages 1-23; Revision 0.

Westinghouse Document SGS-02-013; Data Analysis Sizing Uncertainty of Volumetric

Indications; March 18, 2002.

Westinghouse Memorandum; Use of Appendix H Qualified Techniques at Byron Unit 2

B2R12; August 16, 2005.

Other Documents

Form NIS-1; Manufacturers Data Report for Nuclear Vessels, for A/B/C/D Steam

Generators; February 5, 1980.

EC-354172; B1R13 End of Cycle 13 Effective Degradation Years In Accordance with

NRC Order EA-03-009; Revision 1.

1R11

Licensed Operator Requalification Program (Quarterly)

1BOA-SEC-7; Auxiliary Feedwater Check Valve Leakage, Unit 1; Revision 102

1BOA-INST-2; Operation with a Failed Instrument Channel, Unit 2; Revision 103;

1BFR-S.1; Response to Nuclear Power Generation/ATWS, Unit 1; Revision 102;

1BEP-0; Reactor Trip or Safety Injection, Unit 1; Revision 107;

Attachment

9

1BEP; SI Termination, Unit 1; Revision 106;

1R12

Maintenance Effectiveness

CR 381127, RCP Motor Slipped Off Hydraulic Lifting Devices, October 03, 2005;

CR 381133, Spare 2D RCP Motor Lifting Event, October 03, 2005;

1R13

Maintenance Risk Assessments and Emergent Work Control

Unit 1 Risk Configurations, Week of November 07, 2005;

Unit 1 Risk Configurations, Week of November 28, 2005, Revision 5;

Unit 1 and 2 Risk Configurations, Week of October 10, 2005, Revision 5;

Unit 2 Risk Configurations, Week of December 12, 2005;

CR 385348, 2FW009C Would not go Open, October 12, 2005;

CR 435841, On-line Risk Incorrect for 1CS019A Work, December 21, 2005;

CR 436179, NRC Concerns in the 1B EDG Room, December 21, 2005;

Byrons Archival Operations Narrative Logs for October 12 and 13, 2005;

Byrons Active Operations Narrative Logs, December 21, 2005;

Unit 1 and 2 Risk Configurations, Week of October 24, 2005, Revision 0;

WC-AA-101, Protected Equipment Process and Methodology, Revision 11;

WC-AA-101, On-line Work Control Process, Revision 11;

WC-AA-101-1004, On-line Maintenance for Limiting Condition for Operation of Systems

or Components, Revision 3;

Policy No: 400-47, Byron Operating Department Policy Statement, Revision 8;

Shift Manager Daily Events, December 16, 2005;

Protected Equipment Log, December 21, 2005;

Unit 1 Risk Configurations, Week of December 19, 2005, Revision 2;

BAP 1100-3A3, Pre-evaluated Plant Barrier Matrix, Revision 17;

1R15

Operability Evaluations

CR 393772, 1B Diesel Generator Undervoltage Relay Failed Surveillance Criteria,

November 2, 2005;

1BOSR 8.1.2-2, Unit One 1B Diesel Generator Operability Surveillance; Revision 19;

1BOSR 8.1.14-2, Unit One 1B Diesel Generator 24 Hour Endurance Run and Hot

Restart Test, 18 Month; Revision 5;

License Event Report 89-001-01, Inadvertent Safety Injection During Generator

Operability Surveillance Due to Procedural Inadequacies, August 8, 1989;

Report 05-029; IST Valve Evaluation for 2FW009C; October 14, 2005;

CR 388199; 2FW009C Would Not Open; October 20, 2005;

CR 385902; 2FW009C Failed Stroke Time Test; October 14, 2005;

CR 385348; Apparent Cause Report for 2FW009C Failure to Open Following B2R12;

November 29, 2005;

Byron Station Logs for November 2, 2005;

WO 854993; 1B Diesel Generator Operability Monthly Surveillance

WO 697610; 1B Diesel Generator 24 Hour Endurance Run and Hot Restart Surveillance

1R16

Operator Workarounds

Adverse Condition Monitoring and Contingency Plan, 1D MSIV High Pressure Alarm,

May 20, 2005;

Issue Resolution Documentation, 1D MSIV High Pressure Alarm, SER 2005-13,

Revision 1

Attachment

10

CR 320649, High Pressure on 1MS001D Hydraulic System and Standby Accumulator,

April 04, 2005

1R17

Permanent Plant Modifications (Annual)

LS-AA-125-1001, Root Cause Report - Unit 2 Reactor Trip, Revision 5;

UFSAR Section 15.6.3.2, Steam Generator Tube Rupture, Revision 10;

CR 397646, Discrepancies Were Identified with the Unit 1 DEH Modification Tests,

November 11, 2005;

CR 399021, Issue Identified with 1/2 BOA SEC-1 Regarding Turbine Runback,

November 15, 2005;

Daily Orders, DEHC Update, November 15, 2005;

50.59 Review Coversheet, DEH Replacement, Revision 1;

SPP 05-003 Section 1, Moisture Reheat Separator (MSR) Modification Test, Revision 0

1R19

Post Maintenance Testing

CR 392142, Computer Point #P2302 is Failed to 51#, October 30, 2005;

CR 43607, 1A DG Large Swings in VARS During Monthly Surveillance

WO 610849, OP PMT - Cycle Breaker and Stroke 1SX033, December 15, 2005;

WO 676325, Limitorque Valve OPR Diagnostic test for 2B Containment Recirculation

Sump Outlet Isolation Valve, October 4, 2005;

WO 719874, VT-2 Examination of Discharge Head Connection,2B CV Pump,

October 21, 2005;

WO 862100, Computer Point #P2302 is Failed to 51#, October 30, 2005;

Issue 397232, B2R12 LL - Review and Evaluation of MOV Test Data,

November 10, 2005;

2BOSR 0.1-1,2,3, Unit Two Mode 1, 2, 3 Tech Spec Data Sheet Reactor Trip System

and ESFAS, October 30 and 31, 2005;

WO 697610, 1B DG 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Endurance Run and Hot Restart Surveillance,

November 1, 2005;

1BOSR 8.1.14-2, Unit One 1B Diesel Generator 24 Hour Endurance Run and Hot

Restart Test, 18 Month, Revision 5;

1BOSR 8.1.2-2, Unit One 1B Diesel Generator Operability Surveillance, Revision 19;

1R20

Refueling and Outage Activities

Unit Two Operations Narrative Logs, September 25 - October 13, 2005;

B2R12 Outage Control Center Turnover, September 26 - October 11, 2005;

Shutdown Safety Equipment Status Checklist, various dates;

1R22

Surveillance Testing

IST-BYR-BDOC-V-25; Inservice Testing bases Document, February 21, 2005

2BOSR 0.5-2.SI.2-2.2; Unit Two 2SI18802B, 2SI18809B, 2SI18811B and 2SI18923B

Stroke Test and Position Indication Test, Revision 7

2BVSR 5.c.2-1; Unit Two Flow Balance of the Charging/Safety Injection System To The

Cold Legs (CM 7.6.5), Revision 1

WO 00751528; CV Pump ECCS Flow Balance Test After System Alteration,

September 16, 2005

EC 357553; Flo-Series Evaluation of 2B CV Pump During B2R12, Revision 000

Attachment

11

CR 425626, 2RF008 Calibration Procedure Enhancement Needed, November 18, 2005;

WO 686521, Perform Calibration of 2FT0RF008 Containment Floor Drain Leak Detector

Flow Transmitter, December 13, 2005;

BAP 400-17, Partial Procedure Record; Revision 2

BISR 4.15.3-200, Surveillance Calibration of Containment Floor/Equipment Drain and

Reactor Cavity Leak Detection Loop, Revision 4;

1R23

Temporary Modification

Engineering Change 353724, Removal of Tachometer Pickup Protective Guard from the

Unit 1 B Train Diesel Generator

1EP4

Emergency Action Level and Emergency Plan Changes

Braidwood Station Emergency Plan; Revisions 15 and 16

1EP6

EP Drill Evaluation

Byron 2005 Fourth Quarter Security PI Drill Scenario Information

Fourth Quarter EP/LLEA Drill Findings and Observation Report, December 20, 2005

2OS1 Access Control to Radiologically Significant Areas; and

2OS2 ALARA Planning And Controls

NF-AA-390; Spent Fuel Pool Material Control; Revision 1

B2R12 Cobalt Release Data

CR327893; Request PM ID Frequency Change to Semi-Annual Observation; dated

April 22, 2005

AR341834341834 Elevated Radiation Background Level at AB 401' Exit; dated June 7, 2005

AR272663272663 Radiation Protection Post Outage ALARA Assessment; dated November 11,

2004

IR316023; Alloy 600 Westinghouse RP/ALARA Lessons Learned; dated March 22, 2005

CR315005; B1R13 LL OCC Intervention Causing RWP Violations; dated March 19, 2005

CR342233; RXS Technicians on Wrong RWP; dated June 8, 2005

AR256482-02; Apparent Cause Evaluation: Electronic Dosimeter Not Responding to

Neutron Radiation; dated December 23, 2004

AR318930318930 Common Cause Analysis: Rad Worker Practices; dated May 13, 2005

Monthly Data Elements for NRC Occupational Exposure Control Effectiveness

Individual Dose Report (TE011); dated October 7, 2005

Environmental Lower Limits of Detection

ATI 279546-04; ALARA Readiness Check-In; dated August 22, 2005

ATI 279546-05; Access Control Check-In; dated October 2, 2005

B2R12 ALARA Index

RWP 10005473; S/G Eddy Current and Tube Repairs; Revision 1

RWP 10005463; Lead Shielding - Install, Maintain, and Remove; Revision 1

2PS3

Radiological Environmental Monitoring and Radioactive Material Control Programs

2004 Annual Radioactive Effluent Release Report and Addendum to 2003 Annual

Radioactive Effluent Release Report; dated April 30, 2005

2003 Annual Radioactive Effluent Release Report; dated April 30, 2004

2003 Annual Radiological Environmental Operating Report; dated May 15, 2004

2004 Annual Radiological Environmental Operating Report and Current Revision of The

Attachment

12

Byron Station Off-site Dose Calculation Manual (ODCM); dated May 15, 2005

AR 00324066; U1 and U2 Exceed ODCM Projection for Organ Dose in March; dated

April 13, 2005

AR 00325266; Reporting Errors in The 2003 Annual Radiological Environmental Report;

dated April 15,2005

AR 00165050; Issues Identified During REMP FASA; dated June 26, 2003

AR 00319730; ODCM LLDs Are Incorrect/Iodine Sampling Varies from NUREG; dated

March 31, 2005

AR 00178862; QATR Appendix A R/70 Versus RG 4.15 Discrepancies; dated October 2,

2003

AR 00179892; NOS Identified Met Tower Contractor Not Audited; dated October 8, 2003

CY-AA-170-1000; Radiological Environmental Monitoring Program and Meteorological

Program Implementation; Revision 0

RP-BY-503; Unconditional Release Survey Method; Revision 0

EIML-SPM-1; [REMP] Sampling Procedures Manual - Environmental Incorporated

Midwest Laboratory; Revision 9 (June 6, 2005)

Exelon Audit No. NOSA-BYR-03-08; REMP, ODCM, Non-Radiological Monitoring

/NPDES Audit Report; dated November 11, 2003

Nuclear Utilities Procurement Issues Committee (NUPIC) Joint Quality Assurance

Program Audit Report - Environmental Incorporated Midwest Laboratory; NUPIC Audit

Number 18558; dated June 3, 2003

State of New York, Department of Health Assessment Report for Teledyne Brown

Engineering - Environmental Service; dated September 7, 2004

Toxco Materials Management Centers Quality Assurance Audit of Teledyne Brown

Engineering; Vendor Audit A05-01; dated June 24, 2005

Focus Area Self-Assessment (Check-In) Report: Radiological Environmental Monitoring

Program; dated February 15 - 23, 2005

Monthly Report on the Meteorological Monitoring Program at the Byron Nuclear Station;

dated January 2005 through July 2005

REMP-6; Pump Maintenance Data; dated January 2004 through March 2005

REMP-3; Pump Field Check Data; dated May 2004 through September, 2005

REMP-9-1; Land Use Census - Milch Animals; dated August 9, 2005

REMP-9-2; Land Use Census - Nearest Livestock; dated August 13 an 14, 2005

REMP-9-3; Land Use Census - Nearest Residence; dated August 13, 2005

4OA2 Identification and Resolution of Problems

Common Cause Analysis 351213, NRC Identified Human Performance Cross-cutting

Issue for Byron Station and Station Event Free Clock Resets, dated December 8, 2005;

Focused Area Self-Assessment 350127, Byron Station Human Performance and

Technical Human Performance, dated August 20, 2005;

Byron Site Policy Memo 200.26; Human Performance Task Force; dated November 3,

2005;

Byron Site Policy Memo 200.51, Guidance for Integrated Performance Management

System; dated November 2, 2005

100 day plan, dated December 13, 2005;

Departmental Human Performance Improvement Plan for Electrical Maintenance,

date fourth Quarter 2005;

Attachment

13

Operations Trend Improvement Initiatives; Time Period; 2005 second and third Quarter;

Chemistry Trend Improvement Initiatives; Time Period; 2005 second and third Quarter;

Maintenance Rule - Performance Criteria, Ultimate Heat Sink Temperature Control;

CR 111838, Void Discovered in SX Cooling Tower Concrete During Repairs,

June 13, 2003

CR 227277, Void Identified in SX Cooling Tower Fill Support Beam, June 09, 2004;

AR 227277227277 Extent of Condition review, October 15, 2004;

CR 357066, 0A SX Cooling Tower Concrete Degradation, July 27, 2005;

CR 432671, Some Fill Damage in Unit 1 NDCT, December 10, 2005

CR 437338, Unit 1 W Outfall Screen Coming Loose From Concrete,

December 29, 2005;

Issue 356940, Expanded Scope for Grout Repairs on SXCT D Cell, July 26, 2005;

WR 970114175 01, Perform Minor Concrete Repairs to B Cell Structure;

WR 970129710 01, Perform Minor Concrete Repairs to F Cell Structure

WR 980019429 01, Perform Concrete Repairs to A Cell Structure;

WR 980033192 01, Perform Minor Concrete Repairs to C Cell Structure;

WR 980033713 01, Perform Minor Concrete Repairs to G Cell Structure;

WR 980033718 01, Perform Minor Concrete Repairs to H Cell Structure;

WR 980011671 01, Perform Concrete Repairs to B Cell Structure;

WR 980033714 01, Perform Minor Concrete Repairs to D Cell Structure

4OA3 Event Followup

LER 2005-005-00, Both Trains of the Ultimate Hear Sink Water Makeup Trains

Exceeded TS Required Action Completion Time Due to Contaminated fuel Oil Resulting

From Inadequate Tank cleaning Procedure;

October 14, 2005

Unit 2 Reactor Trip Lessons Learned, Log No 05-033, Revision 0;

Prompt Investigation Report, Unit 2 Reactor Trip on Loss of 2A Condensate;

CR 387581, Unit 2 Reactor Trip on Loss of CD/CB PP2A, October 19, 2005;

CR 387431, Unit 2 NRC 88-08 Temperature Monitoring Data Evaluation,

October 18, 2005;

CR 387579, 2FW009D FWI Monitor Light Did Not Illuminate as Required,

October 19, 2005;

CR 387582, 2A CD/CB Trip, October 19, 2005;

CR 387583, Unit 2 DEHC Panel Shows Dual Indication for #4 Governor Valve,

October 19, 2005;

CR 387590, 2E MPT Combustible Gas Alarm During Unit 2 Reactor Trip,

October 19, 2005;

CR 387603, 2FW520 Did Not Full Close Following Unit 2 Reactor Trip,

October 19, 2005;

CR 387698, Missing DEHC Page 10 from Controller, October 19, 2005

OP-AA-108-114, Post Transient Review, October 19, 2005;

PORC 05-038 & 05-039, Byron Plant Operating Review Committee Minutes, October 19,

2005;

Startup of Byron Unit 2 Following Runback Failure of DEH System Drop 3/53,

October 19, 2005;

4OA5 Pressurizer Penetration Nozzles and Steam Space Piping Connections in U. S.

Pressurized Water Reactors (TI 2515/160)

Attachment

14

Exelon Letter; Initial Response to NRC Bulletin 2004-01, Inspection of Alloy 82/182/600

Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping

Connections at Pressurized-Water Reactors; dated July 27, 2004.

Work Order 00745675; Examine DM Welds Pressurizer Top Nozzles; August 24, 2005.

Level III VT-2 Certification Record; Robert G McBride; February 21, 2005.

TQ-AA-122; Qualification and Certification of Nondestructive(NDE) Personnel;

Revision 1.

Visual Examination Report, VT-2, September 28, 2005.

ER-AA-335-015; VT-2 Visual Examination; Revision 4.

Drawing EDSK379550/B; Spray Nozzle; Revision B.

Drawing EDSK379445/B, Safety Relief Nozzle; Revision B.

ER-AP-331-1001; Boric Acid Corrosion Control (BACC) Inspection Locations,

Implementation and Inspection Guidelines; Revision 1.

ER-AP-331-1002; Boric Acid Corrosion Control Program Identification, Assessment, and

Evaluation; Revision 2.

Attachment

15

LIST OF ACRONYMS USED

ACE

Apparent Cause Evaluation

ADAMS

Agency wide Documents Access and Management System

AFW

Auxiliary Feedwater

AR

Action Request

ASME

American Society of Mechanical Engineers

BACC

Boric Acid Corrosion Control

CFR

Code of Federal Regulations

CR

Condition Report

DD

Diesel Driven

DRP

Division of Reactor Projects; Region RIII

EAL

Emergency Action Level

EDY

Effective Degradation Years

EH

Turbo Electro-Hydraulic Control

EPRI

Electric Power Research Institute

ESF

Engineered Safety Feature

ET

Eddy Current

GL

Generic Letter

IMC

Inspection Manual Chapter

IR

Inspection Report

ISI

Inservice Inspection

LCOAR

Limiting Condition for Operation Action Requirement

LER

Licensee Event Report

MSIV

Main Steam Isolation Valve

NCV

Non-Cited Violation

NDE

Nondestructive Examination

No.

Number

NPP

Nuclear Power Plants

NRC

United States Nuclear Regulatory Commission

NRR

Office of Nuclear Reactor Regulation

ODCM

Offsite Dose Calculation Manual

OSP

Offsite Power

PARS

Public Availability Records

PI

Performance Indicator

PSIG

Pounds Per Square Inch Gage

PWR

Pressurized Water Reactor

RCS

Reactor Coolant System

REMP

Radiological Environmental Monitoring Program

RETS

Radiological Environmental Technical Specifications

RP

Radiation Protection

RWST

Refueling Water Storage Tank

SBO

Station Blackout

SDP

Significance Determination Process

SG

Steam Generator

SSC

Structures, Systems for Components

SSPS

Solid State Protection System

SX

Essential Service Water

Attachment

16

TI

Temporary Inspection

TR

Technical Requirement

TRM

Technical Requirements Manual

TS

Technical Specification

TSO

Transmission System Operator

U

Unit

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

UT

Ultrasonic Examination

VCT

Volume Control Tank

WO

Work Order

WR

Work Request

WS

Non-Essential Service Water