ML052080485

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IR 05000263-05-003, on 04/01/2005, for Monticello Nuclear Generating Plant; Operability Evaluations and Event Follow-Up
ML052080485
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 07/27/2005
From: Satorius M
Division Reactor Projects III
To: Conway J
Nuclear Management Co
References
IR-05-003
Download: ML052080485 (52)


See also: IR 05000263/2005003

Text

July 27, 2005

Mr. J. Conway

Site Vice President

Monticello Nuclear Generating Plant

Nuclear Management Company, LLC

2807 West County Road 75

Monticello, MN 55362-9637

SUBJECT:

MONTICELLO NUCLEAR GENERATING PLANT

NRC INTEGRATED INSPECTION REPORT 05000263/2005003

AND NOTICE OF VIOLATION

Dear Mr. Conway:

On June 30, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Monticello Nuclear Generating Plant. The enclosed report documents the

inspection findings which were discussed on July 7, 2005, with Mr. Rick Jacobs and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, an issue was reviewed under the NRC traditional

enforcement process and determined to be a Severity Level IV violation of an NRC

requirement. The circumstances surrounding the violation is described in detail in the subject

inspection report. The violation was evaluated in accordance with the NRC Enforcement Policy.

The current Enforcement Policy is included on the NRCs web site at www.nrc.gov; select What

We Do, Enforcement, then Enforcement Policy. The violation was cited in the enclosed

Notice of Violation (Notice) because your staff failed to restore compliance and failed to place

the issue into the corrective action program.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. The NRC will use your response, in part, to

determine whether further enforcement action is necessary to ensure compliance with

regulatory requirements.

Additionally, there were one NRC-identified and two self-revealed findings of very low safety

significance, of which two involved violations of NRC requirements. However, because these

violations were of very low safety significance and because the issues were entered into the

licensees corrective action program, the NRC is treating these findings as Non-Cited Violations

in accordance with Section VI.A.1 of the NRCs Enforcement Policy. In addition, licensee

identified violations are listed in Section 4OA7 of this report.

J. Conway

-2-

If you contest the subject or severity of a Non-Cited Violation, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC

20555-0001; with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

Resident Inspector Office at the Monticello Nuclear Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Satorius, Director

Division of Reactor Projects

Docket No. 50-263

License No. DPR-22

Enclosure:

1.

Notice of Violation

2.

Inspection Report 05000263/2005003

w/Attachment: Supplemental Information

cc w/encl:

J. Cowan, Executive Vice President

and Chief Nuclear Officer

Manager, Regulatory Affairs

J. Rogoff, Vice President, Counsel, and Secretary

Nuclear Asset Manager, Xcel Energy, Inc.

Commissioner, Minnesota Department of Health

R. Nelson, President

Minnesota Environmental Control Citizens

Association (MECCA)

Commissioner, Minnesota Pollution Control Agency

D. Gruber, Auditor/Treasurer,

Wright County Government Center

Commissioner, Minnesota Department of Commerce

Manager - Environmental Protection Division

Minnesota Attorney Generals Office

DOCUMENT NAME: E:\\Filenet\\ML052080485.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

RIII

RIII

E RIII

NAME

BBurgess:dtp

CWeil for

KOBrien

Satorius

DATE

07/22/05

07/25/05

07/27/05

OFFICIAL RECORD COPY

J. Conway

-3-

ADAMS Distribution:

HKN

LMP

RidsNrrDipmIipb

GEG

KGO

SPR

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

NOTICE OF VIOLATION

Nuclear Management Company, LLC

Docket No. 50-263

Monticello Nuclear Generating Plant

License No. DPR-22

During an NRC inspection conducted from April 1, 2005, through June 30, 2005, a violation of

NRC requirements was identified. In accordance with the for NRC Enforcement Policy the

violations is listed below:

1.

Section (b)(3)(iv)(A) of 10 CFR 50.72 requires the licensee notify the NRC Operations

Center as soon as practical and in all cases within eight hours for any event or condition

that results in a valid actuation of certain specified systems.

Contrary to the above, on April 2, 2005, the licensee failed to make a required

notification to the NRC when it experienced a valid actuation of the reactor building

ventilation isolation system, the A standby gas treatment system, and the A control room

emergency filtration train and a partial primary containment group II isolation, systems

which were specified under 10 CFR 50.72 as being reportable upon a valid actuation.

As of June 30, 2005, the licensee failed to notify the NRC Operations Center, a period in

excess of eight hours.

This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Nuclear Management Company is hereby required

to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington DC 20555 with a copy to the Regional

Administrator, Region III, and a copy to the NRC Resident Inspector at the facility that is the

subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation

(Notice). This reply should be clearly marked as a Reply to a Notice of Violation and should

include: (1) the reason for the violation, or if contested, the basis for disputing the violation or

severity level, (2) the corrective steps that have been taken and the results achieved, (3) the

corrective steps that will be taken to avoid further violations, and (4) the date when full

compliance will be achieved. Your response may reference or include previous docketed

correspondence, if the correspondence adequately addresses the required response. If an

adequate reply is not received within the time specified in this Notice, an order or Demand for

Information may be issued as to why the license should not be modified, suspended, or

revoked, or why such other action as may be proper should not be taken. Where good cause is

shown, consideration will be given for extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington DC 20555-0001.

Notice of Violation

-2-

Because your response will be made available electronically for public inspection in

the NRC Public Document Room or from the Publically Available Records (PARS)

component of the NRCs document system (ADAMS), to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. ADAMS is accessible from the NRC Web site at

http://www.nec.gov/NRC/ADAMS/index.html (the Public Electronic Reading Room). If

personal privacy or proprietary information is necessary to provide an acceptable response,

then please provide a bracketed copy of your response that identifies the information that

should be protected and a redacted copy of response that deletes such information. If you

request withholding of such material, you must specifically identify the portions of your

response that you seek to have withheld and provide in detail the basis for your claim of

withholding (e.g., explain why the disclosure of information will create an unwarranted invasion

of personal privacy or provide the information required by 10 CFR 2.390(b) to support a request

for withholding confidential commercial or financial information). If safeguards information is

necessary to provide an acceptable response, please provide the level of protection described

in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days.

Dated this 27 day of July 2005

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-263

License No:

DPR-22

Report No:

05000263/2005003

Licensee:

Nuclear Management Company, LLC

Facility:

Monticello Nuclear Generating Plant

Location:

2807 West Highway 75

Monticello, MN 55362

Dates:

April 1 through June 30, 2005

Inspectors:

S. Burton, Senior Resident Inspector

S. Ray, Senior Resident Inspector

R. Orlikowski, Resident Inspector

C. Acosta Acevedo, Reactor Engineer

D. Eskins, Resident Inspector, Lasalle

M. Holmberg, Reactor Inspector

M. Jordan, Reactor Engineer

D. Karjala, Resident Inspector, Prairie Island

C. Zoia, Acting Project Engineer

Observers:

None

Approved by:

B. Burgess, Chief

Branch 2

Division of Reactor Projects

Enclosure

1

SUMMARY OF FINDINGS

IR 05000263/2005003; 04/01/2005 - 06/30/2005; Monticello Nuclear Generating Plant;

Operability Evaluations and Event Follow-up.

This report covers a 3-month period of baseline resident inspection, Temporary Instruction

(TI) 2515/163, Operational Readiness of Offsite Power, and an announced baseline

inspection of heat sink performance. The inspections were conducted by Region III reactor

inspectors and the resident inspectors. The significance of most findings is indicated by their

color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance

Determination Process (SDP). Findings for which the SDP does not apply may be Green or

be assigned a severity level after NRC management review. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. A finding of very low safety significance and Non-Cited Violation (NCV) was

identified on August 3, 2004, by the inspectors when the engineering and operations

groups failed to fully evaluate the availability of a vent path credited in the operability

evaluation for a degraded high energy line break (HELB) issue. Specifically, the

inspectors identified that the ventilation damper credited as a vent path for a feedwater

HELB failed in the shut position on a loss of service air, isolating the vent path. The

primary cause of this finding was related to the cross-cutting area of Human

Performance. The licensee entered this into their corrective action program (CAP) and

completed plant modifications to install HELB dampers to isolate the turbine building

mild environments from the turbine building harsh environments.

The inspectors determined that the issue was more than minor because it directly

impacted the equipment performance attribute for availability and reliability of the

mitigating systems. The finding was of very low safety significance because it was

considered a design deficiency which did not result in loss of function per Generic Letter 91-18, Information to Licensees Regarding NRC Inspection Manual Section on

Resolution of Degraded and Nonconforming Conditions, Revision 1. This issue was an

Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criteria III, Design Control.

(Sections 1R15, 4OA4.1, and 4OA5.2)

Green. A finding of very low safety significance was self-revealed on March 8, 2005,

when residual heat removal (RHR) flow to the shutdown reactor was lost for

approximately 13 minutes due to an inadequately written and reviewed isolation

procedure for outage work. The primary cause of this finding was related to the cross-

cutting area of Human Performance. Corrective actions included immediate restoration

of shutdown cooling, placing all outage isolations on hold for additional reviews and

impact assessments, an operations department stand down, and increased

management observations of equipment isolations. Additional corrective actions to

Enclosure

2

revise work control and outage processes were in progress and being tracked through

the corrective action program.

The inspectors evaluated the finding using the IMC 0609 Appendix G, Shutdown

Significance Determination Process (SDP). Using a Phase 3 SDP, the NRC

determined that the finding was of very low safety significance because multiple

systems were available for manual injection and recovery of RHR was uncomplicated.

Because procedures required by Technical Specifications for initiating isolations were

adequate and were followed, albeit inadequately, this finding was not considered a

violation of NRC requirements. (Sections 4OA3.4 and 4OA4.2)

Green. A finding of very low safety significance and Non-Cited Violation (NCV) was

self-revealed when, on April 2, 2005, with the reactor shutdown during a refueling

outage, performance of an inadequately written and reviewed post-maintenance test

(PMT) resulted in a temporary loss of electrical bus 16 and actuation of several

engineered safety features. The primary cause of this finding was related to the cross-

cutting area of Human Performance. Corrective actions included restoring the bus and

increasing technical and management reviews of PMTs. In addition, the licensee was in

the process of revising the PMT development process to strengthen the levels of review

in a graded approach.

The event was more than minor because it involved the Mitigating Systems Cornerstone

attribute of procedure quality and affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events. During

the time period that bus 16 was lost, one train of mitigating system equipment was not

available. The finding was determined to be of very low safety significance by

comparing it with the results of a Phase 3 SDP for a similar earlier event. Since, in this

case, shutdown cooling was not actually lost and other plant conditions were similar to

the previous event, the significance was no more than for the previous event which had

been categorized as of very low safety significance. This was an NCV of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a PMT procedure

that was not appropriate for the circumstances. (Sections 4OA3.6 and 4OA4.3)

Severity Level IV. The inspectors identified a Severity Level IV violation when the

licensee failed to make a notification, within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, to the NRC Operations Center, in

accordance with 10 CFR 50.72(b)(3)(iv)(A), for an event involving loss of bus 16 and

actuation of engineered safety features on April 2, 2005. The licensee did not restore

compliance or take any corrective actions.

Because this issue affected the NRCs ability to perform its regulatory function, it was

evaluated using the traditional enforcement process. The violation of 10 CFR 50.72 is

categorized in accordance with the NRC Enforcement Policy at Severity Level IV. Since

the licensee failed to place the violation into a corrective action program to address

recurrence, the violation was cited. (Sections 4OA3.5 and 4OA4.3)

Enclosure

3

B.

Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

corrective action tracking numbers are listed in Section 4OA7 of this report.

Enclosure

4

REPORT DETAILS

Summary of Plant Status

Monticello started the inspection period in a shutdown condition for a refueling outage. The

reactor was made critical on April 10, 2005, the generator was placed on the grid on April 13,

and the plant reached full power on April 16. The plant operated at full power for the remainder

of the inspection period except for brief down-power maneuvers to accomplish rod pattern

adjustments.

1.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01

Adverse Weather Protection (71111.01)

Readiness for Seasonal Susceptibilities

a.

Inspection Scope

The inspectors performed a detailed review of the licensees procedures and a

walkdown of two systems to observe the licensees preparations for adverse weather,

including conditions that could result from high temperatures or high winds. The

inspectors focused on plant specific design features for the systems and implementation

of the procedures for responding to or mitigating the effects of adverse weather.

Inspection activities included, but were not limited to, a review of the licensees adverse

weather procedures, preparations for the summer season, and a review of analysis and

requirements identified in the Updated Safety Analysis Report (USAR). The inspectors

also verified that operator actions specified by plant specific procedures were

appropriate. As part of this inspection, the documents in the attachment were utilized to

evaluate the potential for an inspection finding.

The inspectors evaluated readiness for seasonal susceptibilities for the following

systems for a total of two samples:

emergency diesel generator - emergency service water (EDG-ESW); and

switchyard.

b.

Findings

No findings of significance were identified.

Enclosure

5

1R04

Equipment Alignment (71111.04)

Partial Walkdown

a.

Inspection Scope

The inspectors performed partial walkdowns of accessible portions of trains of

risk-significant mitigating systems equipment. The inspectors reviewed equipment

alignment to identify any discrepancies that could impact the function of the system and

potentially increase risk. Identified equipment alignment problems were verified by the

inspectors to be properly resolved. The inspectors selected redundant or backup

systems for inspection during times when equipment was of increased importance due

to unavailability of the redundant train or other related equipment. Inspection activities

included, but were not limited to, a review of the licensees procedures, verification of

equipment alignment, and an observation of material condition, including operating

parameters of equipment in-service. As part of this inspection, the documents in the

attachment were utilized to evaluate the potential for an inspection finding.

The inspectors selected the following equipment trains to assess operability and proper

equipment line-up for a total of three samples:

A residual heat removal (RHR) train with B RHR out-of-service for maintenance;

B residual heat removal service water (RHRSW) train with 12 control rod drive

(CRD) pump out-of-service for maintenance; and

B core spray (CS) train with A CS train out-of-service for maintenance.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05)

.1

Quarterly Fire Zone Walkdowns (71111.05Q)

a.

Inspection Scope

The inspectors walked down risk significant fire areas to assess fire protection

requirements. The inspectors reviewed areas to assess if the licensee had

implemented a fire protection program that adequately controlled combustibles and

ignition sources within the plant, effectively maintained fire detection and suppression

capability, maintained passive fire protection features in good material condition, and

had implemented adequate compensatory measures for out-of-service, degraded or

inoperable fire protection equipment, systems or features. The inspectors selected fire

areas based on their overall contribution to internal fire risk as documented in the plants

Individual Plant Examination of External Events (IPEEE), or the potential to impact

equipment which could initiate or mitigate a plant transient. The inspection activities

included, but were not limited to, the control of transient combustibles and ignition

sources, fire detection equipment, manual suppression capabilities, passive suppression

capabilities, automatic suppression capabilities, compensatory measures, and barriers

Enclosure

6

to fire propagation. As part of this inspection, the documents in the attachment were

utilized to evaluate the potential for an inspection finding.

The inspectors selected the following areas for review for a total of nine samples:

Fire Zone 24, diesel fire pump room;

Fire Zone 12-A, lower 4160 volt bus area (buses 11, 13, and 15);

Fire Zone 8, cable spreading room;

Fire Zone 23-A, intake structure pump room;

Fire Zone 34, 35, and 36, east electrical equipment room and 13 diesel

generator (DG);

Fire Zone 9, control room;

Fire Zone 13-B; main turbine lube oil reservoir and reactor feed pump area,

turbine building elevation 911;

Fire Zone 19-B, turbine building elevation 931 motor control center (MCC)

142 and 143 area; and

Fire Zone 31-B, first floor emergency filtration train (EFT) building (Division II).

b.

Findings

No findings of significance were identified.

.2

Annual Fire Drill Review (71111.05A)

a.

Inspection Scope

The inspectors reviewed fire drill activities to evaluate the licensees ability to control

combustibles and ignition sources, the use of fire fighting equipment, and their ability to

mitigate the event. The inspection activities included, but were not limited to, the fire

brigades use of fire fighting equipment, effectiveness in extinguishing the simulated fire,

effectiveness of communications amongst fire brigade members and the control room,

command and control of the fire commander, and observation of the post-drill critique.

As part of this inspection, the documents in the attachment were utilized to evaluate the

potential for an inspection finding.

The inspectors observed the following fire drill for a total of one sample:

the licensees fire brigade response to an announced fire drill at the 2R auxiliary

transformer.

b.

Findings

No findings of significance were identified.

Enclosure

7

1R06

Flood Protection Measures (71111.06)

a.

Inspection Scope

The inspectors performed an annual review of flood protection barriers and procedures

for coping with internal and external flooding. The inspection focused on determining

whether flood mitigation plans and equipment were consistent with design requirements

and risk analysis assumptions. The inspection activities included, but were not limited

to, a review and/or walkdown to assess design measures, seals, drain systems,

contingency equipment condition and availability of temporary equipment and barriers,

performance and surveillance tests, procedural adequacy, and compensatory

measures. The inspectors utilized the documents listed in the attachment to accomplish

the objectives of the inspection procedure.

The inspectors selected the following equipment for a total of two samples:

external flood protection measures; and

turbine building 931 east elevation and 125 volt battery rooms.

b.

Findings

No findings of significance were identified.

1R07

Heat Sink Performance (71111.07)

Biennial Review

a.

Inspection Scope

The inspectors reviewed the performance of the A and B RHRSW room coolers (a total

of two heat exchangers). These heat exchangers were chosen for review based on

their high risk assessment worth in the licensees probabilistic safety analysis. This

review resulted in the completion of two inspection samples. While on-site, the

inspectors verified that the inspection/maintenance were adequate to ensure proper

heat transfer. This was done by conducting independent heat transfer capability

calculations, reviewing the methods used to inspect the heat exchangers, and verifying

that the as-found results were appropriately dispositioned, such that the final condition

was acceptable. The inspectors also verified by review of procedures and test results

that chemical treatments, ultrasonic tests, and methods used to control biotic fouling

corrosion and macrofouling were sufficient to ensure required heat exchanger

performance.

The inspectors verified that the condition and operation were consistent with design

assumptions in heat transfer calculations by conducting a service water system

walkdown and reviewing related procedures and surveillance. The inspectors also

verified that redundant and infrequently used heat exchangers were flow tested

periodically at maximum design flow. This was performed by reviewing related

procedures and surveillance.

Enclosure

8

The inspectors verified the performance of the ultimate heat sink and its

sub-components, such as piping, intake screens, intake bays, pumps, valves, etc. by

reviewing procedures, surveillance, and inspections conducted on the system.

The inspectors verified that the licensee had entered significant heat exchanger/heat

sink problems into their corrective action program (CAP). The inspectors reviewed

issues entered to verify that the corrective actions taken were appropriate.

The documents that were reviewed as part of this inspection are listed in the

attachment.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification Program (71111.11)

Requalification Activities Review by Resident Staff

a.

Inspection Scope

The inspectors performed a quarterly review of licensed operator requalification training.

The inspection assessed the licensees effectiveness in evaluating the requalification

program, ensuring that licensed individuals operate the facility safely and within the

conditions of their license, and evaluated licensed operator mastery of high-risk operator

actions. The inspection activities included, but were not limited to, a review of high risk

activities, emergency plan performance, incorporation of lessons learned, clarity and

formality of communications, task prioritization, timeliness of actions, alarm response

actions, control board operations, procedural adequacy and implementation, supervisory

oversight, group dynamics, interpretations of Technical Specifications (TS), simulator

fidelity, and licensee critique of performance. As part of this inspection, the documents

in the attachment were utilized to evaluate the potential for an inspection finding.

The inspectors observed the following requalification activity for a total of one sample:

an operating crew during an evaluated simulator scenario that included a

recirculation pump runup, feedwater pump rupture, and stuck open safety relief

valve with a tailpipe rupture, which resulted in a manual reactor scram, entry into

emergency operating procedures, and emergency depressurization.

b.

Findings

No findings of significance were identified.

Enclosure

9

1R12

Maintenance Effectiveness (71111.12)

Routine Maintenance Effectiveness Inspection

a.

Inspection Scope

The inspectors reviewed systems to assess maintenance effectiveness, including

maintenance rule activities, work practices, and common cause issues. Inspection

activities included, but were not limited to, the licensee's categorization of specific issues

including evaluation of performance criteria, appropriate work practices, identification of

common cause errors, extent of condition, and trending of key parameters. Additionally,

the inspectors reviewed implementation of the Maintenance Rule (10 CFR 50.65)

requirements, including a review of scoping, goal-setting, performance monitoring,

short-term and long-term corrective actions, functional failure determinations associated

with reviewed CAP documents, and current equipment performance status. As part of

this inspection, the documents in the attachment were utilized to evaluate the potential

for an inspection finding.

The inspectors performed the following maintenance effectiveness reviews for a total of

two samples:

an issue/problem-oriented review of the RHRSW system because it was

designated as risk significant under the Maintenance Rule and the system

experienced a blockage of flow to the 12/14 RHRSW pump motor coolers due to

sand/grit build-up after long standing issues with debris/sand fouling in the

RHRSW system; and

an issue/problem-oriented review of the non-essential DG system because it was

designated as risk significant under the Maintenance Rule and the system

experienced performance problems which resulted in it being placed in the

Maintenance Rule (a)(1) category.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed maintenance activities to review risk assessments (RAs) and

emergent work control. The inspectors verified the performance and adequacy of RAs,

management of resultant risk, entry into the appropriate licensee-established risk bands,

and the effective planning and control of emergent work activities. The inspection

activities included, but were not limited to, a verification that licensee RA procedures

were followed and performed appropriately for routine and emergent maintenance, that

RAs for the scope of work performed were accurate and complete, that necessary

actions were taken to minimize the probability of initiating events, and that activities to

ensure that the functionality of mitigating systems and barriers were performed.

Reviews also assessed the licensee's evaluation of plant risk, risk management,

Enclosure

10

scheduling, configuration control, and coordination with other scheduled risk significant

work for these activities. Additionally, the assessment included an evaluation of external

factors, the licensee's control of work activities, and appropriate consideration of

baseline and cumulative risk. As part of this inspection, the documents in the

attachment were utilized to evaluate the potential for an inspection finding.

The inspectors observed maintenance or planning for the following activities or risk

significant systems undergoing scheduled or emergent maintenance for a total of five

samples:

troubleshooting of an emergent reactor core isolation cooling (RCIC) system

operability problem while breaker 8N12 and the 12 service water pump were also

out-of-service;

routine scheduled maintenance and risk management during planned

maintenance on the 12 CRD pump;

routine scheduled maintenance and risk management during troubleshooting of

14 ESW pump for high vibrations;

routine scheduled maintenance and risk management during planned

maintenance on the high pressure coolant injection (HPCI) system and the

2R and 2RS transformers; and

troubleshooting of an emergent RHRSW pressure control valve problem while

the 2R and 2RS transformers were also out-of-service.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed operability evaluations which affected mitigating systems or

barrier integrity to ensure that operability was properly justified and that the component

or system remained available. The inspection activities included, but were not limited to,

a review of the technical adequacy of the operability evaluations to determine the impact

on TS, the significance of the evaluations to ensure that adequate justifications were

documented, and that risk was appropriately assessed. As part of this inspection, the

documents in the attachment were utilized to evaluate the potential for an inspection

finding.

The inspectors reviewed the following operability evaluations for a total of five samples:

indications of localized wall thickness reduction in the service water supply line to

the A RHR heat exchanger;

non-destructive examination thickness less than 87.5 percent of nominal

thickness on the B feedwater to reactor line;

inadvertent closure of AO-2886, condensate service water system cross-tie

header;

failure of Division l RHR torus cooling injection/test inboard valve to close; and

Enclosure

11

high energy line break (HELB) calculations for differential pressure challenge

turbine building wall qualification.

b.

Findings

Introduction: The inspectors identified a finding of very low safety significance involving

a Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion III, Design Control.

The inspectors identified that the engineering and operations groups failed to fully

evaluate the availability of a vent path credited in the operability evaluation for a

degraded HELB issue. Specifically, the inspectors identified that the ventilation damper

credited as a vent path for a feedwater HELB failed in the shut position on a loss of

service air, isolating the vent path. This item, previously discussed in Inspection Report 05000263/2004004, Section 1R15, was Unresolved Item (URI)05000263/2004004-01.

The URI is closed in Section 4OA5.2 of this report.

Description: On June 2, 2004, the engineering group identified that the GOTHIC

computer model used to analyze a turbine building HELB failed to include four flow

paths within the turbine building. The condition had the potential to affect the operability

of equipment associated with the 4160 volt system (bus 15 and bus 16), the 480 volt

system (LC-103 and LC-104), and the 125 volt system (D111 and D211). Specifically,

the engineering group identified three heating, ventilation, and air conditioning (HVAC)

flow paths that existed between a single turbine building mild environment and three

turbine building harsh environments. The turbine building mild environment included

both 4160 volt essential switchgear rooms, the 941 elevation cableway, and the

931 elevation Division II essential MCCs. The harsh environments included the

911 elevation condenser area, the 951 elevation turbine building operating floor, and the

911 elevation feedwater pump area. The unanalyzed flow paths might have allowed

steam to travel to the mild environment areas during a HELB via the existing HVAC

ductwork.

Upon discovery, the engineering department initiated CAP033462 to document the

issue. The operations department took compensatory measures to block shut three

dampers to isolate the flow paths between the turbine building harsh and mild

environments. An operability evaluation was performed documenting the operability of

the potentially affected equipment.

On August 3, 2004, the inspectors reviewed the operability evaluation and noted that it

took credit for a vent path in the ventilation system that would help mitigate the

consequences of a HELB by relieving steam and pressure. However, when the

inspectors raised questions about the design of a damper in the vent path, it was

identified that the damper failed shut on a loss of service air, thus isolating the vent

path. The engineering department initiated CAP034281 to document the issue.

Subsequently, compensatory measures were taken to ensure the vent path damper

remained open. A period of approximately 55 days passed from the time compensatory

measures were first taken to isolate the flow paths to when the licensee took

compensatory measures to block open the damper to ensure the vent path remained

open.

Enclosure

12

Analysis: The inspectors reviewed the finding and determined that a performance

deficiency existed because engineering and operations personnel failed to fully evaluate

the availability of a vent path credited in the operability evaluation for a degraded

HELB issue. The inspectors determined that the issue was more than minor because a

feedwater HELB had the potential to directly impact the equipment performance

attribute for availability and reliability of the mitigating systems as well as human

performance and the finding affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

The inspectors reviewed this finding in accordance with Inspection Manual Chapter (IMC) 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for

At-Power Situations." Using the Phase 1 Significance Determination Process (SDP)

worksheet for the Mitigation Systems Cornerstone, the inspectors determined that this

finding was considered a design deficiency which did not result in loss of function per

Generic Letter 91-18, Information to Licensees Regarding NRC Inspection Manual

Section on Resolution of Degraded and Nonconforming Conditions, Revision 1.

Therefore, this finding was considered to be of very low safety significance (Green).

This finding was assigned to the Mitigating Systems Cornerstone and also involved the

cross-cutting area of Human Performance.

Enforcement: Title 10 CFR 50, Appendix B, Criterion III, "Design Control," requires, in

part, that design changes, including field changes, shall be subject to design control

measures commensurate with those applied to the original design. Monticello USAR,

Appendix I, Postulated Pipe Failures Outside of Containment, states, in part, that both

4160 volt essential switchgear rooms, the 941 elevation cableway, and the 931 elevation

Division II essential MCCs were mild environments and were not adversely affected by

ruptures in pipes carrying high energy fluid.

Contrary to the above, on June 2, 2004, operations personnel implemented

compensatory field changes to the turbine building HVAC system. These changes were

intended to prevent interactions between a single turbine building mild environment and

three turbine building harsh environments through HVAC flow paths that existed in the

turbine building. On August 3, 2004, NRC inspectors identified that one of dampers

credited in the operability analysis (OPR000101) as providing a vent flow path would fail

shut on a loss of service air. The licensee took compensatory measures to ensure the

vent path damper remained open and initiated CAP034281 to document the issue.

Because this violation was of very low safety significance and it was entered into the

licensees corrective action program, the violation was being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy,

(NCV 05000263/2005003-01). The licensee subsequently completed plant

modifications to install HELB dampers to isolate the single turbine building mild

environment from the three turbine building harsh environments.

Enclosure

13

1R16

Operator Workarounds (71111.16)

.1

Operator Workaround Semiannual Review of Cumulative Effects

a.

Inspection Scope

The inspectors performed a semiannual review of the cumulative effects of operator

workarounds (OWAs). The inspectors reviewed OWAs to identify any potential effect

on the functionality of mitigating systems. The inspection activities included, but were

not limited to, a review of the cumulative effects of the OWAs on the availability and the

potential for improper operation of the system, for potential impacts on multiple systems,

and on the ability of operators to respond to plant transients or accidents. Additionally,

reviews were conducted to determine if the workarounds could increase the possibility of

an initiating event, if the workaround was contrary to training, required a change from

long standing operational practices, created the potential for inappropriate

compensatory actions, impaired access to equipment, or require equipment uses for

which the equipment was not designed. As part of this inspection, the documents in the

attachment were utilized to evaluate the potential for an inspection finding. This

inspection constituted one sample of the semiannual requirement.

b.

Findings

No findings of significance were identified.

.2

Quarterly Review of Selected Operator Workarounds

a.

Inspection Scope

The inspectors reviewed an operator workaround involving the operation of the

EDG-ESW during DG operation. The inspectors reviewed the workarounds potential to

impact the operators ability to isolate the ESW system from the service water system to

prevent deadheading the ESW pumps during operation of the EDG. As part of this

inspection, the documents in the attachment were utilized to evaluate the potential for

an inspection finding. This review represented one inspection sample.

b.

Findings

No findings of significance were identified.

1R19

Post-Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors verified that the post-maintenance testing (PMT) procedures and

activities were adequate to ensure system operability and functional capability. Activities

were selected based upon the structure, system, or component's ability to impact risk.

The inspection activities included, but were not limited to, witnessing or reviewing the

integration of testing activities, applicability of acceptance criteria, test equipment

calibration and control, procedural use and compliance, control of temporary

Enclosure

14

modifications or jumpers required for test performance, documentation of test data,

system restoration, and evaluation of test data. Also, the inspectors verified that

maintenance and PMT activities adequately ensured that the equipment met the

licensing basis, TS, and USAR design requirements. As part of this inspection, the

documents in the attachment were utilized to evaluate the potential for an inspection

finding.

The inspectors selected the following PMT activities for review for a total of seven

samples:

repair of CRD 38-31 insert line;

replace the screen wash fire pump with a rebuilt unit;

repair of the RCIC controller;

repair of bus 16 safeguards relay 97-31;

preventive maintenance and repair of the 12 CRD pump;

preventive maintenance and repairs on the HPCI system; and

RHRSW check valves SW-21-1 and SW-21-2 post-repair testing.

b.

Findings

No findings of significance were identified.

1R20

Outage Activities (71111.20)

a.

Inspection Scope

The inspectors evaluated outage activities for a refueling outage that was in progress at

the beginning of the inspection period and ended on April 13, 2005. The inspectors

reviewed activities to ensure that the licensee considered risk in developing, planning,

and implementing the outage schedule, developed mitigation strategies for loss of key

safety functions, and adhered to operating license and TS requirements to ensure

defense-in-depth. The inspection activities included, but were not limited to, a review of

the outage plan, control of outage activities and risk, observation of reduced inventory

operations, observations of startup and physics testing, and other maintenance and

refueling activities. This inspection constituted the completion of a sample that was

initiated and accounted for in NRC Inspection Report 05000263/2005002. As part of

this inspection, the documents in the attachment were utilized to evaluate the potential

for an inspection finding.

In addition to activities inspected utilizing specific procedures, the following represents a

partial list of the major outage activities the inspectors reviewed/observed, all or in part:

control room turnover meetings and selected pre-job briefings;

control room demeanor, communications, self/peer checking, and equipment

panel control;

outage management turnover meetings;

walkdowns of the reactor and turbine building to observe ongoing work activities;

walkdowns of the main control room to observe alignment of systems important

to shutdown risk;

Enclosure

15

leak rate testing activities;

outage equipment configuration and risk management;

electrical line-ups;

selected clearances;

control and monitoring of decay heat removal;

drywell closure;

startup and heatup activities, including criticality, feed pump startup, main turbine

generator startup and synchronization, and elements of power escalation to full

power; and

identification and resolution of problems associated with the outage.

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed surveillance testing activities to assess operational readiness

and to ensure that risk-significant structures, systems, and components were capable of

performing their intended safety function. Activities were selected based upon risk

significance and the potential risk impact from an unidentified deficiency or performance

degradation that a system, structure, or component could impose on the unit if the

condition was left unresolved. The inspection activities included, but were not limited to,

a review for preconditioning, integration of testing activities, applicability of acceptance

criteria, test equipment calibration and control, procedural use, control of temporary

modifications or jumpers required for test performance, documentation of test data,

TS applicability, impact of testing relative to performance indicator (PI) reporting, and

evaluation of test data. As part of this inspection, the documents in the attachment were

utilized to evaluate the potential for an inspection finding.

The inspectors selected the following surveillance testing activities for review for a total

of six samples:

drywell prestart inspection;

13 ESW quarterly pump and valve tests;

reactor coolant pressure boundary (RCPB) leakage test;

condenser low vacuum scram instruments test and calibration;

reactor high pressure scram functional test; and

RHR loop A quarterly pump and valve test.

b.

Findings

No findings of significance were identified.

Enclosure

16

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed a temporary modification to assess the impact of the

modification on the safety function of the associated system. The inspection activities

included, but were not limited to, a review of design documents, safety screening

documents, USAR, and applicable TS to determine that the temporary modification was

consistent with modification documents, drawings and procedures. The inspectors also

reviewed the post-installation test results to confirm that tests were satisfactory and the

actual impact of the temporary modification on the permanent system and interfacing

systems were adequately verified. As part of this inspection, the documents in the

attachment were utilized to evaluate the potential for an inspection finding.

The inspectors selected the following temporary modification for review for a total of one

sample:

replace feeder cable for 11 recirculation pump motor generator (MG) set motor.

b.

Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope

The inspectors selected emergency preparedness exercises that the licensee had

scheduled as providing input to the Drill/Exercise PI. The inspection activities included,

but were not limited to, the classification of events, notifications to off-site agencies,

protective action recommendation development, and drill critiques. Observations were

compared with the licensees observations and CAP entries. The inspectors verified

that there were no discrepancies between observed performance and PI reported

statistics. As part of this inspection, the documents in the attachment were utilized to

evaluate the potential for an inspection finding.

The inspectors selected the following emergency preparedness activity for review for a

total of one sample:

an emergency response drill with a simulated reactor coolant leak that was

performed on May 16, 2005, in conjunction with licensed operator requalification

training, including simulated notifications to state, county, and local agencies for

an alert classification.

b.

Findings

No findings of significance were identified.

Enclosure

17

4.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems (71152)

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As part of the routine inspections documented in this report, the inspectors verified that

the licensee entered the problems identified during the inspection into its CAP.

Additionally, the inspectors verified that the licensee was identifying their issues at an

appropriate threshold and entering them in the CAP, and verified that problems included

in the licensee's CAP were properly addressed for resolution. Attributes reviewed

included: complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrence reviews were proper and

adequate; and that the classification, prioritization and focus were commensurate with

safety and sufficient to prevent recurrence of the issue.

b.

Findings

No findings of significance were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished by reviewing daily

CAP summary reports and attending corrective action review board meetings.

b.

Findings

No findings of significance were identified.

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors reviews were focused on radiation protection and procedural error issues,

but also considered the results of daily inspector CAP item screening discussed in

Enclosure

18

Section 4OA2.2 of this report, licensee trending efforts, and licensee human

performance results. The inspectors reviews nominally considered the period of

January 2005 through June 2005, although some examples expanded beyond those

dates when the scope of the trend warranted.

Inspectors reviewed adverse trend CAP items associated with various events that

occurred during the period. The review also included issues documented outside the

normal CAP in major equipment problem lists, repetitive and/or rework maintenance

lists, departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self assessment reports, and maintenance rule assessments.

The specific items reviewed are listed in the attachment to this report. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending documents. Corrective actions associated with a sample of the issues

identified in the licensees trend report were reviewed for adequacy.

The inspectors also evaluated the licensees trending report against the requirements of

the licensees CAP as specified in 4 AWI-10.01.01, Corrective Action Program, and

10 CFR 50, Appendix B. Additional documents reviewed are listed in the attachment to

this report.

b.

Assessment and Observations

There were no findings of significance identified. The inspectors evaluated the licensee

trending methodology and observed that the licensee had performed a detailed review.

The licensee routinely reviewed cause codes, involved organizations, key words, and

system links to identify potential trends in their CAP data. The inspectors compared the

licensee process results with the results of the inspectors daily screening and did not

identify any discrepancies.

.4

Selected Issue Follow up (Annual Sample): RHRSW System Motor Cooling Issues

a.

Inspection Scope

On June 14, 2005, the licensee entered an unplanned limiting condition for operations

(LCO) action requirement for Division II CS due to sand intrusion within the B RHRSW

system. The inspectors chose to perform a more in-depth review of the licensees

corrective actions for this issue. Previous CAPs and work orders (WOs) pertaining to

the RHRSW system were also reviewed to ensure that the licensees corrective actions

were commensurate with the significance of previously identified issues. The inspectors

reviewed CAPs and WOs looking for any previous history of sand intrusion, previous

instances of reduced motor cooler flow, or repeat equipment issues related to the A and

B RHRSW system motor coolers.

b.

Issues

The inspectors identified a discrepancy between the corrective actions associated with

two similar CAPs. On November 4, 2004, CAP035620 was written to document that

flow through the 12 and 14 RHRSW motor coolers was within the procedures

acceptance band but required an air flush. Operators performed an air flush of the

Enclosure

19

system and then measured the as-left motor cooler flow. The as-left flow measurement

again met the requirement for pump operability, but was outside the as-left flow range of

the procedure. The licensee wrote WO0403809 to perform a cleaning of the 12 and

14 RHRSW motor coolers.

On May 6, 2005, CAP038945 was written to document that the 12 and 14 RHRSW

as-found combined motor cooler flow was within the procedures acceptance band but

required an air flush. After the air flush was performed, the as-left motor cooler flow was

greater than the minimum required for pump operability but was still outside the as-left

acceptance band, the same condition following the licensees November 4, 2004, air

flush activity. The CAP was closed to trend and no cleaning of the 12 and 14 motor

coolers was performed.

The 12 and 14 RHRSW pump motor cooler flows were never measured to be less than

the minimum required for operability. However, after the May 6, 2005, quarterly

surveillance was performed, CAP038945 was closed to trend and no work order was

written to perform a motor cooler cleaning as had been done for CAP035620. While

there is no regulatory requirement to perform a motor cooler cleaning, it was generally

considered a good practice.

The inspectors also discussed with the system engineer the possibility that the degraded

flow identified on November 4, 2004, and May 6, 2005, could have been an indication

that the 12 and 14 RHRSW system line was fouling and that is what led to the

B RHRSW system being declared inoperable on June 14, 2005, due to insufficient

motor cooler flow. The system engineer provided the inspectors with the results from

the surveillance performed during the first quarter of 2005 that found the 12 and

14 RHRSW motor cooler flows to be within the acceptance band of the procedure. This

led the inspectors to conclude that there was not a declining trend in the 12 and

14 RHRSW motor cooler flow that could have alerted licensee personnel to a degraded

condition of the B RHRSW motor cooler flow.

No findings of significance were identified.

4OA3 Event Follow-up (71153)

.1

(Closed) Licensee Event Report (LER) 05000263/2004-002-00: Cable Separation Issue

Identified During Appendix R Re-analysis.

On September 1, 2004, during a reconstitution review of the Monticello 10 CFR 50,

Appendix R, Safe Shutdown Analysis (SSDA) Program, the licensee discovered a

nonconformance with 10 CFR 50, Appendix R, III.G.2 divisional criteria. The licensee

determined that the 4160 volt motor power cables for the Division I RHR and CS pumps

passed through a Division II area without an adequate barrier. The cause of this issue

was a failure by personnel to recognize a 10 CFR 50, Appendix R, compliance issue

with the cable routing in the original SSDA. Corrective actions include a modification to

provide a 3-hour rated fire barrier for the Division I RHR and CS cables. The licensee

entered this into their corrective action program as CAP033003. A licensee-identified

violation is discussed in Section 4OA7.1.

Enclosure

20

.2

(Closed) LER 05000263/2005-001-00 and (Closed) LER 05000263/2005-001-01:

Single Failure Identified That Could Prevent Energizing Buses 15 and 16.

Some of the issues described in this LER were previously discussed in Inspection

Report 05000263/2005002, Section 1R14. On February 4, 2005, the licensee identified

a single point vulnerability between the 4160 volt vital bus circuit breakers 152-610 and

152-511 overcurrent relays. Activation of the supply circuits overcurrent relays due to a

hot smart short could initiate a respective bus (15/16) lockout. The licensee attributed

the apparent cause of the single point vulnerability issue to a failure to recognize an

original plant construction design which was noncompliant to 10 CFR 50, Appendix A,

General Design Criteria. Corrective actions included design modifications to remove

the 4160 volt vital bus relaying and metering single point vulnerability. The licensee

entered this into their corrective action program as CAP036987.

On February 23, 2005, upon further evaluation, the licensee identified a previously

undiscovered Appendix R non-compliance related to the 1AR transformer breaker

152-610 to safeguards bus 16 current transformers. During a postulated fire in the

control room and/or cable spreading room, this noncompliance could have caused a

lockout of bus 16 that would not be able to be overridden during a transfer to the

alternate shutdown system (ASDS), preventing Division II equipment operation from the

control room and ASDS panel. The apparent cause of the Appendix R vulnerability was

a failure to completely implement the original ASDS design recommendation by General

Electric (GE) Safe Shutdown Analysis reports. Corrective actions included

disconnecting the cable to isolate the ASDS Appendix R vulnerability. The licensee also

performed an engineering review of the ASDS design to validate compliance with the

originally proposed General Electric ASDS design recommendation. The licensee

entered this into their corrective action program as CAP037264.

On April 5, 2005, as an additional result of the review discussed above, the licensee

discovered that the bus 16 source to load center 104 had a similar potential vulnerability

with the ASDS isolation design that could result in load center 104 being locked out in

the event of a control room or cable spreading room fire. The licensee reported this

latest issue in Revision 1 of the original LER. Plant modifications were performed to

remove the vulnerabilities.

A licensee-identified violation is discussed in Section 4OA7.2.

.3

(Closed) LER 05000263/2005-002-00: Failure of #11 Reactor Protection System

Motor-Generator Set Results in an Engineered Safety Feature Actuation.

This event, which occurred on February 24, 2005, was previously discussed in

Inspection Report 05000263/2005002, Section 4OA3.2. The licensee issued the

LER on April 25, 2005, within the required time frame. Based on an evaluation by a

vendor, the licensee attributed the MG set failure to a winding short due to age-related

degradation of the winding insulation. The inspectors determined that the event did not

involve a performance deficiency and that it was of minor safety significance, for the

reasons discussed in the LER. In addition to repairing the motor, licensee corrective

actions consisted of an extent of condition review looking for other motors with extended

duty times and a planned evaluation to determine the frequency for re-winding or

Enclosure

21

replacing various motors on the plant critical equipment list. The LER was reviewed by

the inspectors and no findings of significance were identified. In addition to the LER,

other documents reviewed during this inspection are listed in the attachment. The

licensee entered this issue into its corrective action program as CAP037306.

.4

(Closed) LER 05000263/2005-003-00: Loss of Shutdown Cooling Due to #12 Residual

Heat Removal Pump Trip.

Introduction: A finding of very low safety significance was self-revealed on

March 8, 2005, when RHR flow to the shutdown reactor was lost for approximately

13 minutes due to an inadequately written and reviewed isolation procedure for outage

work.

Description: On March 8, 2005, while performing an isolation for outage work on safety

relief valves, de-energizing the electrical supply breakers designated on the isolation

caused the unexpected loss of a large number of logic circuits for various pieces of

equipment and initiated several annunciators in the control room. Operations

supervision ordered the isolation to be restored, and while it was being restored, the

running 12 RHR pump spuriously sensed a closure of its suction valve, and tripped as

designed. After a few minutes, operators recognized the loss of shutdown cooling and

initiated actions to restart the pump. Shutdown cooling had been lost for a total of about

13 minutes. Reactor coolant temperature and level did not change measurably during

the time cooling was lost. The licensee reported the event to the NRC in accordance

with 10 CFR 50.72 as Event Number 41468 and entered it into its corrective action

program as CAP037567.

As part of the CAP review, the licensee performed a root cause evaluation and initiated

extensive corrective actions. The cause of the event was determined to be an

inadequately planned isolation. The outage isolation was written in advance of the

outage but due to manpower shortages, pre-outage milestone pressures, inadequate

change management, inadequate management oversight, and personnel performance

issues, this isolation specified isolation of 125 volt supply breakers, which supplied

numerous circuits in addition to the ones that needed to be de-energized. Had the

isolation writer made a more careful review of the electrical prints or used pre-approved

isolation points in the maintenance procedure, individual circuit fuses would have been

used as isolation points and power would have been maintained on the rest of the

circuits.

Additional opportunities to prevent this event were missed during the review, approval,

and pre-job briefing processes for the isolation when the reviewer did not ask for help

when he had trouble reading the prints, when questions regarding the potential effect of

the isolation on shutdown cooling were not pursued, and when the pre-job briefing

concentrated almost exclusively on personnel safety and not on the adequacy of the

isolation itself.

Corrective actions included immediate restoration of shutdown cooling, placing all

outage isolations on hold for additional reviews and impact assessments, an operations

department stand down, and increased management observations of equipment

Enclosure

22

isolations. Additional corrective actions to revise work control and outage processes

were in progress and being tracked through the corrective action program.

Analysis: The inspectors evaluated the finding using the IMC 0609 Appendix G,

Shutdown Significance Determination Process. Based on checklist 6, the inspectors

determined that this finding required a Phase 2 analysis because it resulted in a loss of

the decay heat removal system. The NRC Region III Senior Reactor Analyst (SRA)

evaluated the finding using the worksheet for the Loss of an Operating Train of RHR in

Plant Operating State 2. Because the finding resulted in a loss of RHR and the loss of

all automatic emergency core cooling system (ECCS) injection capability, no credit was

initially given for these functions. A credit of 3 was given for recovery of RHR because

the system was restored quickly and because a large amount of time was available to

recover RHR prior to reactor coolant system boiling and subsequent core uncovery. A

credit of 2 was given for manual injection of other available injection systems. This

Phase 2 result was determined to be Yellow with a dominant sequence of the loss of

RHR, failure to recover RHR, and the failure to manually inject to the reactor coolant

system with other systems. The SRA determined that this result was overly

conservative given that multiple systems were available for manual injection, and

recovery of RHR and automatic injection systems was not difficult. The Phase 2

worksheets assumed a low dependence between the recovery of RHR and the operator

action to manually inject using other systems. For this particular scenario, the SRA

determined that no dependence existed between these two operator actions because

they would not be close in location or time and the operators would have many

indications, including reactor low level alarms, to determine that manual injection was

necessary. Therefore, a Phase 3 analysis was performed and additional credit for

manual injection was given. This resulted in a finding of very low safety significance

(Green) (Finding (FIN)05000263/2005003-02). This finding was assigned to the

Mitigating Systems Cornerstone and also involved the cross-cutting area of Human

Performance.

Enforcement: This event was primarily caused by human performance errors in the

writing and review of an isolation for outage work. Procedures required by TS for

initiating isolations were adequate and were followed, but performed inadequately.

Therefore, this finding was not considered a violation of NRC requirements.

.5

(Closed) LER 05000263/2005-005-00: Inadvertent Engineered Safety Function

Actuations During Testing.

Introduction: A finding of very low safety significance and NCV was self-revealed when,

on April 2, 2005, performance of an inadequately written and reviewed PMT resulted in

a temporary loss of the electrical bus 16 and actuation of several engineered safety

features (ESFs). In addition, the inspectors identified that the licensee failed to report

the event in accordance with 10 CFR 50.72. This failure to report was dispositioned as

a Severity Level IV violation under the traditional enforcement program.

Description: On April 2, 2005, with the reactor shutdown during a refueling outage,

operators were performing a PMT following a relay replacement. As described in the

LER, due to an inadequate procedure, the essential bus transfer logic sensed a loss of

bus 16 voltage and tried to transfer to an alternate source. However, the alternate

Enclosure

23

sources were out-of-service as part of the outage, resulting in the loss of bus 16. Loss

of bus 16 caused a loss of its loads, including reactor protection system (RPS) bus B.

When RPS bus B was lost, several safety systems actuated as designed. The

actuations were isolation of reactor building ventilation, initiation of the A standby gas

treatment system, initiation of the A control room EFT, tripping of the reactor water

cleanup (RWCU) system, a partial primary containment group II isolation, and initiation

of a half scram. Shutdown cooling was not lost and the actuations did not cause any

significant complications. Power was restored to bus 16 expeditiously.

The licensee did not make an 8-hour notification to the NRC in accordance with 10 CFR 50.72 because the licensee determined that the actuation was invalid because the

initial sensed loss of power signal was invalid (bus 16 was still energized at the time).

However, the inspectors informed the licensee that the NRC position was that the ESF

actuations were caused by the subsequent actual loss of bus 16 and the associated

RPS bus. The NRC position was that the systems actuated as designed due to valid

plant conditions, even though the cause of the loss of voltage was an invalid signal to

the bus transfer logic. Despite being given the NRC position, the licensee failed to notify

the NRC Operations Center of the event, in accordance with 10 CFR 50.72. The

licensee did issue the LER in a timely manner in accordance with 10 CFR 50.73, but still

maintained in the LER that the actuation was invalid.

Analysis: For the event itself, the inspectors determined that the failure to adequately

write and review the PMT in sufficient detail to avoid the unintended loss of a vital bus

and a challenge to the engineered safety systems was a human performance deficiency

requiring an evaluation using the SDP. The event was more than minor because it

involved the Mitigating Systems Cornerstone attribute of Procedure Quality and affected

the cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events. During the time period that bus 16 was lost, one train

of mitigating system equipment was not available. The inspectors used IMC 0609,

Appendix GProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix G" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Shutdown Significance Determination Process, Checklist 6 and screened

the issue as very low safety significance in Phase 1. As an alternative, the inspectors

also reviewed the results of the Phase 3 SDP conducted in response to the event

described in Section 4OA3.4 of this report and determined that, since shutdown cooling

was not actually lost and other plant conditions were similar, the significance was no

more than for the previous event (very low safety significance) and the finding was

Green. The finding was assigned to the Mitigating Systems Cornerstone and also

involved the cross-cutting area of Human Performance.

Enforcement: Criterion V, of Appendix B, or 10 CFR 50, requires, in part, that activities

affecting quality shall be prescribed by documented instruction, procedures, or drawings

of a type appropriate to the circumstances. Contrary to this requirement, on

April 2, 2005, a marked up copy of Procedure 0036-01, ECCS Emergency Bus

Undervoltage Test and ECCS Loss of Normal Auxiliary Power Test, was used to

perform a post-maintenance test, an activity affecting quality. As described in the LER,

the procedure was not appropriate for the circumstances because one necessary step

was not specified to be accomplished, resulting in an unexpected loss of power to a vital

bus and actuation of ESF equipment. However, because the event was of very low

safety significance and because the issue was entered into the licensees corrective

action program, this violation is being treated as an NCV, consistent with Section VI.A.1

Enclosure

24

of the Enforcement Policy (NCV 05000263/2005003-04). The licensee entered the

event into its corrective action program as CAP0038433. Corrective action included

restoring the bus and increasing technical and management reviews of PMTs. In

addition, the licensee was in the process of revising the PMT development process to

strengthen the levels of review in a graded approach.

Section (b)(3)(iv)(A) of 10 CFR 50.72 required an 8-hour report to the NRC for any event

or condition that results in valid actuation of certain specified systems. On April 2, 2005,

the licensee experienced a valid actuation of the reactor building ventilation isolation,

A standby gas treatment system, A control room EFT, a partial primary containment

group II isolation, tripping of the RWCU system, and a half scram. The first three of

those systems are specified under 10 CFR 50.72 as being reportable upon a valid

actuation. The licensee did not make an 8-hour report to the NRC for this event. The

failure to properly report was considered to be a violation that potentially impeded or

impacted the regulatory process and such issues are dispositioned using the traditional

enforcement process instead of the SDP. The failure to notify the NRC Operations

Center within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of occurrence of a valid actuation of specified systems is

categorized as a Severity Level IV violation in accordance with the NRC Enforcement

Policy. The licensee position, as stated in the LER, was that the event was not

reportable under 10 CFR 50.72 because it was not a valid actuation. Thus, the

reportability issue was not entered into the licensees CAP to address recurrence. The

violation was assigned to the Mitigating Systems Cornerstone.

4OA4 Cross-Cutting Aspects of Findings

.1

A NRC-identified finding described in Section 1R15 of this report had, as its primary

cause, human performance deficiencies, in that the engineering and operations groups

failed to fully evaluate the availability of a vent path credited in the operability evaluation

for a degraded HELB issue, such that the ventilation damper in the vent path would fail

shut on a loss of service air.

.2

A self-revealed finding described in Section 4OA3.4 of this report had, as its primary

cause, human performance deficiencies, in that the isolation for an outage work item

was inadequately written and reviewed, such that a brief loss of shutdown cooling

occurred when it was executed.

.3

A self-revealed finding described in Section 4OA3.6 of this report had, as its primary

cause, human performance deficiencies, in that the procedure used for a PMT was not

adequately written and reviewed, resulting in an unexpected loss of a vital electrical bus.

4OA5 Other Activities

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

.1

Operational Readiness of Offsite Power (Temporary Instruction (TI) 2515/163)

The objective of TI2515/163, Operational Readiness of Offsite Power, was to confirm,

through inspections and interviews, the operational readiness of offsite power (OSP)

Enclosure

25

systems in accordance with NRC requirements. The inspectors reviewed licensee

procedures and discuss the attributes identified in TI2515/163 with licensee personnel.

In accordance with the requirements of TI2515/163, inspectors evaluated licensee

procedures against the attributes discussed below.

The operating procedures that the control room operator uses to assure the operability

of the OSP have the following attributes:

1.

Identify the required control room operator actions to take when notified by the

transmission system operator (TSO) that post-trip voltage of the OSP at the

nuclear power plant will not be acceptable to assure the continued operation of

the safety-related loads without transferring to the onsite power supply.

2.

Identify the compensatory actions the control room operator is required to

perform if the TSO is not able to predict the post-trip voltage at the nuclear

power plant for the current grid conditions.

3.

Identify the notifications required by 10 CFR 50.72 for an inoperable offsite

power system when the nuclear station is either informed by its TSO or when an

actual degraded voltage condition is identified.

The procedures to ensure compliance with 10 CFR 50.65(a)(4) have the following

attributes:

1.

Direct the plant staff to perform grid reliability evaluations as part of the required

maintenance risk assessment before taking a risk-significant piece of equipment

out-of-service to do maintenance activities.

2.

Direct the plant staff to ensure that the current status of the OSP system has

been included in the risk management actions and compensatory actions to

reduce the risk when performing risk-significant maintenance activities or when

loss of offsite power or station blackout mitigating equipment are taken

out-of-service.

3.

Direct the control room staff to address degrading grid conditions that may

emerge during a maintenance activity.

4.

Direct the plant staff to notify the TSO of risk changes that emerge during

ongoing maintenance at the nuclear power plant.

The procedure to ensure compliance with 10 CFR 50.63 has the following attribute:

Direct the control room operators on the steps to be taken to try to recover offsite

power within the station blackout coping time.

The results of the inspectors review were forwarded to the Office of Nuclear Reactor

Regulation for further review and evaluation.

Enclosure

26

.2

(Closed) URI 05000263/2004004-01: Feedwater Line HELB Could Potentially Impact

Multiple Safety Related Systems.

This item was reviewed in Section 1R15 and 4OA4.1 of this report and a Green finding

and associated NCV was identified.

4OA6 Meetings

.1

Exit Meeting

The inspectors presented the inspection results to Mr. Rick Jacobs and other members

of licensee management on July 7, 2005. The licensee acknowledged the findings

presented. The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. One proprietary letter was identified

and returned to the licensee.

.2

Interim Exit Meetings

Interim exits were conducted for:

Heat Sink Biennial Inspection with Mr. B. Sawatzke and other members of

licensee management on May 20, 2005.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the

licensee and are violations of NRC requirements which meet the criteria of Section VI of

NRC Enforcement Policy, NUREG-1600, for being dispositioned as Non-Cited

Violations.

Cornerstone: Mitigating Systems

.1

This issue relates to LER 05000263/2004-002-00 discussed in Section 4OA3.1 of this

report. Section III.G.2 of 10 CFR 50 Appendix R, Divisional Separation Criteria,

stated, in part, that cables or equipment of redundant trains of systems necessary to

achieve and maintain hot shutdown conditions that are located in the same fire area,

shall have means provided to ensure that one of the redundant trains remains free of

fire damage. Contrary to this requirement, as discussed in the LER, the licensee

determined that the 4160 volt motor power cables for the Division I RHR and CS pumps

passed through a Division II fire area without an adequate barrier.

The inspectors and the Region III SRA evaluated the finding using IMC 0609

Appendix FProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix F" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Fire Protection Significance Determination Process. The inspectors

determined that the finding category was localized cable or component protection

because the finding was a deficiency in the licensees compliance with 10 CFR 50,

Appendix R, III.G.2. The degradation rating assigned to the finding was moderate and

the duration was greater than 30 days. The Phase 1 initial quantitative screening

determined that a Phase 2 analysis was required. The Region III SRA reviewed the

Enclosure

27

finding and determined that no credible fire scenario could be developed which would

impact both the Division I RHR and CS cables and the Division II safe shutdown

equipment because the cables were on two separate elevations in the fire area and

were separated by more than 30 feet. In Step 2.3 of the Phase 2 SDP, the SRA

determined that there was no basis for defining a fire spread that could encompass both

sets of cables beyond the fire ignition sources considered. Additionally, there were no

scenarios of sufficient intensity to result in a hot gas layer that could damage both

Division I and Division II cables. Based on the above, this finding was determined to be

of very low safety significance (Green). Corrective actions include a modification to

provide a 3-hour rated fire barrier for the Division I RHR and CS cables. The licensee

entered this into their corrective action program as CAP033003.

.2

This finding relates to LERs 05000263/2005-001-00 and 05000263/2005-001-01,

discussed in Section 4OA3.2 of this report. Section XVI of 10 CFR 50 Appendix B,

Corrective Action, states, in part, that measures shall be established to assure that

conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations,

defective material and equipment, and nonconformances are promptly identified and

corrected. Contrary to this requirement, the licensee failed to identify and correct an

ASDS design issue during an engineering review performed in 2001 under CAP002941.

The finding was identified by the licensee through its external event review process.

Since the finding only affected the ability to reach and maintain cold shutdown

conditions and the probability of the specific hot short that would cause the problem was

extremely low, the Region III SRA screened it as having very low safety significance

(Green) per Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance

Determination Process. The licensee entered this into their corrective action program

as CAP037264.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

J. Conway, Site Director for Operations

R. Jacobs, Plant Manager

R. Baumer, Regulatory Compliance

K. Jepsen, Radiation Protection Manager

J. Fields, Regulatory Affairs Manager (Acting)

B. Sawatzke, Plant Manager (Acting)

S. Kibler, Principal Engineer

J. Ohotto, System Engineer

Nuclear Regulatory Commission

B. Burgess, Chief, Reactor Projects Branch 2

A. M. Stone, Chief, Engineering Branch 2

S. Burgess, Senior Reactor Analyst

L. Kozak, Senior Reactor Analyst

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000263/2005003-01

NCV

Failure to Fully Evaluate the Availability of a Vent Path

Credited in the Operability Evaluation for a Degraded

HELB Issue (Sections 1R15, 4OA4.1, and 4OA5.2)05000263/2005003-02

FIN

Loss of Shutdown Cooling Due to #12 Residual Heat

Removal Pump Trip (Sections 4OA3.4 and 4OA4.2)05000263/2005003-04

NCV

Inadvertent Engineered Safety System Actuations During

Testing (Sections 4OA3.5 and 4OA4.3)05000263/2005003-05

VIO

Failure to Report Inadvertent Engineered Safety System

Actuations during Testing (Sections 4OA3.5 and 4OA4.3)

Closed

05000263/2004-002-00

LER

Cable Separation Issue Identified During Appendix R

Re-analysis (Sections 4OA3.1 and 4OA7.1)

05000263/2005-001-00

LER

Single Failure Identified That Could Prevent Energizing

Buses 15 and 16 (Sections 4OA3.2, and 4OA7.2)

05000263/2005-001-01

LER

Single Failure Identified That Could Prevent Energizing

Buses 15 and 16 (Sections 4OA3.2, and 4OA7.2)

Attachment

Attachment

2

05000263/2005-002-00

LER

Failure of #11 Reactor Protection System Motor-Generator

Set Results in an Engineered Safety Feature Actuation

(Section 4OA3.3)

05000263/2005-003-00

LER

Loss of Shutdown Cooling Due to #12 Residual Heat

Removal Pump Trip (Sections 4OA3.4 and 4OA4.2)

05000263/2005-004-00

LER

Voluntary LER Control Rod Drive Insert Line Leakage

(Sections 4OA3.5 and 4OA5.3)

05000263/2005-005-00

LER

Inadvertent Engineered Safety System Actuations During

Testing (Sections 4OA3.6 and 4OA4.3)05000263/2005003-01

NCV

Failure to Fully Evaluate the Availability of a Vent Path

Credited in the Operability Evaluation for a Degraded

HELB Issue (Sections 1R15, 4OA4.1, and 4OA5.2)05000263/2005003-02

FIN

Loss of Shutdown Cooling Due to #12 Residual Heat

Removal Pump Trip (Sections 4OA3.4 and 4OA4.2)05000263/2005003-04

NCV

Inadvertent Engineered Safety System Actuations During

Testing (Sections 4OA3.6 and 4OA4.3)05000263/2004004-01

URI

Feedwater Line HELB Could Potentially Impact Multiple

Safety Related Systems (Sections 1R15 and 4OA5.2)05000263/2005002-02

URI

Reactor Coolant Leakage Identified at the Insert Line and

Flange Interface for Control Rod 38-31 (Sections 4OA3.5

and 4OA5.3)

Discussed

05000263/2001-006-00

LER

Alternate Shutdown System Design Deficiencies Result in

Vulnerability to Single Hot shorts During Postulated Control

Room or Cable Spreading Room Fire (Section 4OA3.1)

Attachment

Attachment

3

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection reports.

1R01

Adverse Weather

Documents and Procedures:

2206 Plant Prestart Checklist EDG - ESW System; Revision 3

1150 Summer Checklist; Revision 35

2154-22 EDG - ESW Prestart Valve Checklist; Revision 20

4 AWI-04.02.01; Housekeeping; Revision 11

Corrective Action Program Documents:

CE010725; Further Review of NRC Questions Concerning Wind Generated Missiles Is

Required (NRC-Identified)

CAP033894; Further Review of NRC Questions Concerning Wind Generated Missiles Is

Required (NRC-Identified)

CAP021998; Revise 4 AWI-04.02.01, Housekeeping to Recognize Periodic Inspection

Requirement (NRC-Identified)

1R04

Equipment Alignment

Documents and Procedures:

2154-11; CS System Prestart Valve Checklist; Revision 18

2154-12; RHR System Prestart Valve Checklist; Revision 40

2154-23; RHR Service Water System Prestart Valve Checklist; Revision 26

Corrective Action Program Documents:

CAP038535; Past Operability Issues Not Addressed in CAP038041 and CAP037627

1R05

Fire Protection

Pre-Fire Fighting Procedures and Strategies:

A.3-12-A; Lower 4160 Volt Bus Area (Busses 11, 13, and 15); Revision 9

A.3-24; Diesel Fire Pump Room; Revision 6

A.3-08; Cable Spreading Room; Revision 9

A.3-23-A; Intake Structure Pump Room; Revision 7

A.3-34; East Electrical Equipment Room; Revision 7

Attachment

Attachment

4

A.3-09; Control Room; Revision 5

A.3-13-B; Reactor Feedpump and Lube Oil Reservoir Room; Revision 7

A.3-19-B; Essential MCC Area (No. 142 & 143) 931' Elevation; Revision 8

A.3-31-B; EFT Building 1st Floor (Division II); Revision 10

A.3-37; Transformers; Revision 4

Documents and Procedures:

NSPLMI-95001; Monticello Individual Plant Examination of External Events - Appendix B

- Internal Fires Analysis; Revision 1

Corrective Action Program Documents:

CAP038786; Loose Metallic Tape in Diesel Fire Pump Room

CAP038820; Small Holes in Cable Spreading Room Ceiling & Wall, Not Through Barrier

(NRC-Identified)

1R06

Flood Protection Measures

Documents and Procedures:

Modification 02Q085; Modify Doors in the Hot Shop; Revision 2

Corrective Action Program Documents:

CAP023293; Perform a Flood Analysis for Internal Flooding Scenarios

CAP029566; Document the Focused Self-Assessment of the Monticello Nuclear

Generating Plant Internal Flooding Program Which was Conducted September 8th

through 11th, 2003

CAP020306; Document All Postulated Internal Flooding Scenarios Affecting Safe

Shutdown Equipment in Vital Plant Areas

1R07

Heat Sink Performance

Documents and Procedures:

Design Basis Document; ESW System; Revision 3

Drawing 112; RHR Service Water and ESW Systems; Revision BM

Drawing 811; Service Water System and Make-up Intake Structure; Revision CF

Drawing NF-36458; Intake Structure Sections and Details, Sheet 1 of 3; Revision A

Drawing NF-36461; Intake Structure Wing Walls and Apron; Revision O

Drawing NF-93492; Service Water Supply From Pump-111D to VEAC-14B (Intake

Structure and Access Tunnel); Revision C

Drawing NX-8763-23; V-AC-4 Air Cooling Unit; Revision C

Drawing NX-8763-24; V-AC-5 Cooling Unit; Revision C

Letter; Response to Generic Letter 89-13, Service Water Problems Affecting

Safety-Related Equipment; January 29, 1990

Attachment

Attachment

5

Letter; Follow-up Response to Generic Letter 89-013, Service Water Problems

Affecting Safety-Related Equipment; June 27, 1991

MOD 99Q050; ESW Flow Improvement; Revision 0

Ops Man B.06.04-05; Circulating Water System; Revision 34

Ops Man B.08.01.05-01; Biocide Injection; Revision 1

Procedure 20-A-10; Southwest Equip Rm V-AC-4; Revision 6

Procedure 20-A-17; Southeast Equip Rm V-AC-5 High Temp; Revision 5

Procedure 242-A-37; 13-14 ESW Pump Trouble; Revision 3

Procedure 0255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; January 4, 2005

Procedure 0255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; October 4, 2004

Procedure 0255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; June 10, 2003

Procedure 0255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; May 17, 2003

Procedure 0255-11-III-4; 14 ESW Quarterly Pump and Valve Tests; April 1, 2005

Procedure 0255-11-III-4; 14 ESW Quarterly Pump and Valve Tests; January 17, 2005

Procedure 0255-11-III-4; 14 ESW Quarterly Pump and Valve Tests; October 18, 2004

Procedure 0255-11-III-4; 14 ESW Quarterly Pump and Valve Tests; May 17, 2003

Procedure 3590; Service Water Component Inspection; Revision 4

Procedure 40-57-PM; Intake Bay/Traveling Screen Forebay Inspection;

September 1, 2004

Procedure 40-57-PM; Intake Bay/Traveling Screen Forebay Inspection; July 1, 2003

Procedure 40-57-PM; Intake Bay/Traveling Screen Forebay Inspection; April 30, 2002

Procedure 40-57-PM; Intake Bay/Traveling Screen Forebay Inspection;

November 28, 2001

Procedure 40-57-PM; Intake Bay/Traveling Screen Forebay Inspection; June 16, 2000

Procedure 4058-05-PM; A RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; March 12, 2005

Procedure 4058-05-PM; A RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; May 12, 2003

Procedure 4058-05-PM; A RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; November 14, 2001

Procedure 4058-05-PM; A RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; January 26, 2000

Procedure 4058-06-PM; B RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; March 30, 2005

Procedure 4058-06-PM; B RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; May 5, 2003

Procedure 4058-06-PM; B RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; November 28, 2001

Procedure 4058-06-PM; B RHR Room Air Cooling Unit V-AC-5 Internal, External

Cleaning and Visual Inspection; January, 14, 2000

Procedure 4125-PM; East Service Water Bay Inspection/Dredging; May 13, 2003

Procedure 4125-PM; East Service Water Bay Inspection/Dredging; November 15, 2001

Procedure 4125-PM; East Service Water Bay Inspection/Dredging; January 25, 2000

Procedure 4126-PM; West Service Water Bay Inspection/Dredging; May 5, 2003

Procedure 4126-PM; West Service Water Bay Inspection/Dredging;

November 28, 2001

Procedure 4126-PM; West Service Water Bay Inspection/Dredging; January 14, 2000

Procedure A.6; Acts of Nature; Revision 19

Procedure EWI-08.22.01; Generic Letter 89-013; Revision 0

Attachment

Attachment

6

Procedure I.05.29; Operation of the Sodium Hypochlorite System Equipment;

Revision 14

Procedure I.05.31; Operation of the Non-Oxidizing Biocide System; Revision 6

Procedure FP-PE-SW-01; Service Water and Fire Protection Inspection Program;

Revision 1

Corrective Action Program Documents:

CAP039098; Minimum Dredging Criteria for Service Water Bays Not Provided in

Predictive Maintenance Procedures; (NRC-Identified)

SA023227; Snapshot Assessment SA0223227, Preparation for Upcoming 2004

NRC Ultimate Heat Sink Inspection; December 1, 2004

1R11

Licensed Operator Requalification Program

Documents and Procedures:

Simulator Exercise Guide RQ-SS-62; Recirculation Pump Runup, Feedwater Rupture,

Stuck Open Safety Relief Valve with Tailpipe Rupture and Emergency Depressurization;

Revision 1

1R12

Maintenance Effectiveness

Documents and Procedures:

Monticello Maintenance Rule Periodic Update for February 2005; March 3, 2005

Monticello Maintenance Rule Program System Basis Document; Non-Essential DG;

June 18, 1996

Monticello Maintenance Rule Program System Basis Document; RHRSW System;

October 23, 1997

Maintenance Rule Performance Data for RHRSW; January 2003 to June 2005

Corrective Action Program Documents:

CAP031758; Received 86 Lockout on 52-710 While Trying to Synchronize 13 DG to

LC-107 During Monthly Operability Test

CAP032199; Received 86 Lockout on 52-710 While Trying to Synchronize 13 DG to

LC-107 During Monthly Operability Test

CAP032246; Bracket on 52-710 Used to Ensure Breaker is Tripped Prior to Racking it In

or Out Bent Up

CAP032979; 13 Diesel Maintenance Rule Status Changed to Red (a)(1)

CAP033222; Lack of Spare Breaker Will Challenge Maintenance Rule Availability for

13 DG

CAP034785; 11 RHRSW Pump Motor Cooling SV-4937A Leaks

CAP035622; SV 4937D Fails to Close after Being Cycled

CAP036114; RHRSW Motor Cooling Solenoid Supply Valves Not Well Suited for the

Application

CAP038720; SV-4937B Leakage Will Not Allow RHRSW Loop B to Proper Pressure

When Shutdown

Attachment

Attachment

7

CAP038945; #12 & #14 RHRSW Combined Motor Cooler Flow Outside of As Left

Acceptance Band

CAP039503; Unplanned 7 Day LCOs entered for Division II Containment Spray for the

Failure of PCV-3005

1R13

Maintenance Risk Assessments and Emergent Work Control

Documents and Procedures:

0255-08-1A-1; RCIC Quarterly Pump and Valve Tests; Revision 60 (with additional

Temporary Change on May 10, 2005)

3334; IST Program Surveillance Test Frequency Notification for Pump P-111D;

Revision 4; May 16, 2005

3108; Pump/Valve/Instrument Record of Corrective Action for Pump P-111D;

Revision 13; May 16, 2005

3108; Pump/Valve/Instrument Record of Corrective Action for Pump P-111D;

Revision 7; July 19, 2000

Maintenance Schedule for Work Week 5512; May 22 through 28, 2005

Maintenance Schedule for Work Week 5302; June 12 through June 18, 2005

Corrective Action Program Documents:

CAP038969; Entered Unplanned LCO for RCIC During the Performance of

0255-08-1A-1

CAP038972; Anomalous Behavior of RCIC System During April 16, 2005, Surveillance

Not Captured in CAP

CAP038991; RCIC Speed Signal Cable Shield Not Grounded

CAP039065; 14 ESW Motor Vibration Levels Elevated in Alert and Required Actions

Range

OPR000104; Operability Recommendation for P-111D, 14 ESW Pump

CAP039172; 12 CRD Pump Motor is Missing Its Dust Shield on the Outboard Bearing

CAP039177; Rigging Point for 12 CRD Pump Motor Challenged Motor Removal

Schedule

CAP039187; 12 CRD Pump Check Valve Leaks

CAP039479; HPCI Aux Oil Pump Alignment Criteria Specified by PM Could Not Be

Obtained

CAP039490; Shim Was Missing Underneath Motor Foot of HPCI Aux Oil Pump P-217

CAP039491; No Jacking Bolts on Motor

CAP039503; Unplanned 7 Day LCOs Entered for Division II Containment Spray for the

Failure of PCV-3005

CAP039507; Unplanned Core Damage Failure Color Change From Green to Yellow

Due to Equipment Failure

Work Orders:

0307083; PM 12 CRD Pump Motor (P-201B)

0108318; Minor Oil Leak on 12 CRD Motor Outboard Bearing

0506222; Isolate HPCI for Maintenance Activities

Attachment

Attachment

8

1R15

Operability Evaluations

Documents and Procedures:

Electrical Power Research Institute (EPRI) Sourcebook for Microbiologically Influenced

Corrosion in Nuclear Power Plants

CA-05-091; Evaluate Line RHRSW SW9-18-GF for Thinning Found While Performing

Nondestructive Examination

FAC-05-032; Flow Accelerated Corrosion (FAC) Program Thickness Data Report

FAC-05-048; FAC Program Thickness Data Report

QC-101; Engineers Receiving Report for Feedwater System Line FW2B-10"

645-3601; Tensile Test and Chemical Analysis of Steel Pipe Sections; Job Number

5828; Twin Cities Testing and Engineering Laboratories, Inc.

CA-05-108; Evaluation of Wall Thinning on FW2B-10-ED

CA05-005; Motor Control Center MCC-143 Internal Temperature Rise from a Feedwater

Break at the Feedpumps, Past Operability Analysis

Corrective Action Program Documents:

CAP038226; Indications of Localized Wall Thickness Reduction in Line SW9-18"

CAP024051; Conduct a Technical Challenge Board Prior to Startup

CE012151; Condition Evaluation for Indications of Localized Wall Thickness Reduction

in Line SW9-18"

CAP038177; Nondestructive Examination Thickness <87.5% on Nominal Wall

Thickness on FW2B-10"-ED, B Feedwater to Reactor Line

CAP037389; Opening of Breaker B4117 for WO0403632 Caused an Inadvertent

Closure of AO-2886

CAP035390; Hot Inboard Bearing on P-4 Condensate Service Jockey Pump

CAP033462; Winter Mode of HVAC Operation May Challenge HELB Analysis of Record

EWR023489; Formally Document the Thermal Lag Analysis Performed for MCC-143

Past Operability Using the Results of Calculation 04-200

Work Orders:

0403632; Perform MC2 Testing on P-4 Motor at Breaker

1R16

Operator Workarounds

Documents and Procedures:

Safety Review Item 92-020; Demonstration of Procedure for Loss of Alternating Current

Power Concurrent with a HELB

OWI-01.07; Operations Department Self-Assessment; Section 4.9 Operational

Challenges; Revision 24 & 25

OWA/Non-Transient OWA Impact Factor Report; 06/21/05

Probabilistic Risk Analysis Review of OWAs; 1/04/05, 2/21/05, 4/21/05 and 6/02/05

Acceptable As-Is Report (List of Operational Challenges Closed by Completing

Procedure 2220); 06/07/05

Operational Challenges List; 06/07/05

Attachment

Attachment

9

Operations Manual B.08.1.2-01; EDG ESW; Revision 6

Operations Manual B.09.08-05; EDG Operations; Revision 19

Operations Manual B.02.02-05; RWCU System Operations; Revision 25

Operations Manual C.4-B.01.03.A; Response to Loss of CRD Pump Flow; Revision 6

Corrective Action Program Documents:

CAP039612; ESW Pump Operation in Parallel with Service Water Creates Potential to

Degrade ESW Pump (NRC-Identified)

1R19

Post-Maintenance Testing

Documents and Procedures:

0266; Fire Pumps Simulated Auto-Actuation and Capability Test; Revision 41

0255-08-1A-1; RCIC Quarterly Pump and Valve Tests; Revision 60 (with Temporary

Change dated May 11, 2005)

0036-01; ECCS Bus Undervoltage Test and ECCS Loss of Normal Auxiliary Power Test;

Revision 21; April 2, 2005

Ops Manual B.01.03-05; CRD Hydraulic System; Revision 18

0255-06-IA-1; HPCI Quarterly Pump and Valve Tests; Revision 72

0255-05-1A-1-1; A RHRSW Quarterly Pump and Valve Tests; Revision 55

Corrective Action Program Documents:

CAP036415; Seal Leakage Noted to be Greater than Drain Line Capacity on P-104, the

Screenwash Fire Pump

CAP038099; Insulation on Motor Pigtails for 12 CRD Pump is Degraded

CAP038257; 12 CRD Pump Placed in Emergency Status Only

CAP038433; Loss of Power to Bus 16 During PMT for WO0505600

CAP039176; Motor Leads Swollen From Oil Infiltration

CAP039483; Emergency Operating Procedure Entry of 90 Degrees Torus Temperature

Reached During HPCI Testing (Expected)

CAP039485; Noisy Environment Caused Individual to Not Hear Dose Rate Alarm During

HPCI Run

CAP039494; Loose Nuts Found Around HPCI Stop Valve

Work Orders:

0403787; Replace Screenwash Fire Pump with Rebuilt Unit

0505600; 152-610 Breaker Tripped Early During ECCS Bus Undervoltage Test and

ECCS Loss of Normal Auxiliary Power Testing

0401719; Repack 11 RHRSW Pump

1R20

Outage Activities

Documents and Procedures:

2005 Refueling Outage Daily Risk Data Sheets

Attachment

Attachment

10

2005 Outage Daily Shift Turnover Reports

Monticello Nuclear Generating Plant 2005 Refuel Outage Critical Path Schedule

1R22

Surveillance Testing

Documents and Procedures:

0006-A; Condenser Low Vacuum Scram Instruments Test and Calibration Procedure

(>600 PSIG [pounds per square inch gauge]); Revision 13

1371; Drywell Prestart Inspection; Revision 6

0255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; Revision 31

0255-20-IIC-1; Reactor Coolant Pressure Boundary Leakage Test; Revision 22

0255-20-IIC-2; Reactor Coolant Pressure Boundary Leakage Test; Revision 18

CA-94-141; Stem Thrust Assessment of 10 inch Anchor Darling Globe Valves:

MO-2008 and MO-2009; April 1, 2005

3108; Pump/Valve/Instrument Record of Corrective Action for MO-2008

Altran Corporation Letter 0404-L-001; Transmittal of Final Weak Link Calculation;

March 23, 2005

0002; Reactor High Pressure Scram Instrument Test and Calibration Procedure;

Revision 18

CA-95-047; Instrument Setpoint Calculation, High Reactor Pressure Scram; Revision 1

0255-04-1A-1-1; RHR Loop A Quarterly Pump and Valve Testing; Revision 67

2145; RHR System Discharge Venting; Revision 8

Corrective Action Program Documents:

CAP037415; 24 Hour Cold Shutdown LCO Entry May Be Needed to Perform IST Pump

Test

CAP038713; Unplanned LCO Entry Due to Failure of MO-2008 to Close

CAP038732; MO-2008 Actuator Made Unusual Noises During Setup

CAP038722; MO-2008 VIPER Diagnostic Testing Preparations Result in Overthrust in

the Open Direction

CAP038730; MO-2008 Limit Switch Wiring Discrepancies Discovered

1R23

Temporary Plant Modifications

Documents and Procedures:

Product Data Sheet for Okonite Company C-L-X Okoguard Shielded Power Cable

3352; Generic Cable Replacement Worksheet; Revision 3

3278; NMC Standard 10 CFR 50.59 Screening Form; Revision 3

8040; Generic Cable Replacement Procedure; Revision 6

3279; Test Report for Hypotential D.C. Testing of 5kv and 15kv Cable; Revision 2

ECN 2005-105; Engineering Change Notice; Revision 0

QF-0520 (FP-E-MOD-05); Plant Impact List for Contingency Replacement of 11 Reactor

Recirculation Pump MG Drive Motor Cables

LF-31AC; Load Study Report for 11 Recirculation MG Set Cable Replacement

QF-0532 (FP-E-MOD-010); Turnover and Closeout Control Form for

Modification 03T075C

Attachment

Attachment

11

QF-0530 (FP-E-MOD-10); Modification Turnover Punchlist for Modification 03T075C

3722; Combustible Loading Change Request for Modification 03T075C

Corrective Action Program Documents:

CAP037776; Anomalous Results Produced by Megger Test of #11 Recirculation

Pump MG

CE012033; Anomalous Results Produced by Megger Test of #11 Recirculation

Pump MG

CAP038326; Temporary Cable for Recirculation MG Set Motor Damaged During Armor

Removal

CE012178; Temporary Cable for Recirculation MG Set Motor Damaged During Armor

Removal

Work Orders:

0505345; (Contingency) Replace Feeder Cable for 11 MG Set Drive Motor

1EP6 Drill Evaluation

Documents and Procedures:

5790-102-02; Monticello Emergency Notification Report Form; Revision 30

4OA2 Identification and Resolution of Problems

Documents and Procedures:

1456-02; RHRSW Pump 12 and 14 Motor Cooler Flush Quarterly Surveillance

0255-05-IA-1-2; B RHRSW Quarterly Pump and Valve Tests

Work Orders:

WO0403809; Clean 12 RHRSW Pump Motor Cooler

Corrective Action Program Documents:

CAP038655; HPCI Jib Crane found Extended (NRC-Identified)

CAP038786; Loose Metallic Tape in Diesel Fire Pump Room (NRC-Identified)

CAP038820; Small Holes in Cable Spreading Room Ceiling and Wall, Not Through

Barrier (NRC-Identified)

CAP038842; NRC Inspector Identifies Housekeeping/Severe Weather Concerns on

Plant Grounds (NRC-Identified)

CAP039612; ESW Pump Operation in Parallel with SW Creates Potential to Degrade

ESW Pump (NRC-Identified)

CAP039464; Balance Of Plant Testing Methodology of Pat May Not Meet 2003 Fitness

For Duty Order (NRC-Identified)

Attachment

Attachment

12

List of CAPs between the period of January 1, 2005, through June 30, 2005, with a

CAP Hot Button Designator of Procedural Adherence Issue - Non-Administrative

Control Procedures

List of CAPs between the period of January 1, 2005, through June 30, 2005, with a

CAP Hot Button Designator of Administrative Control Procedure Adherence

List of CAPs between the period of January 1, 2005, through June 30, 2005, with a

CAP Hot Button Designator of Radiation Protection, Respiratory Protection

CAP035620; B RHRSW Cooling Flow not Acceptable

CAP038945; #12 and #14 RHRSW Combined Motor Cooler Flow Outside of As-Left

Acceptance Band

CAP039503; Unplanned 7 Day LCO Entered for Division II Containment Spray for the

Failure of Valve Pressure Control Valve PCV-3005

CAP038785; Solenoid Valve SV-4937A, #11 RHRSW Pump Motor Cooling Water Valve

is Stuck Open

CAP036114; RHRSW Motor Cooling Supply Solenoids Not Well Suited for the

Application

CAP038720; Solenoid Valve SV-4937B Leakage will not Allow RHRSW Loop B to

Proper Pressure when Shutdown

4OA3 Event Follow-up

Documents and Procedures:

NRC Event 41441; Engineered Safety Feature Actuation Following Trip

of Reactor Protection MG Set; February 24, 2005

NRC Event 41374; 4160 Volt Relaying and Metering Single Failure

Vulnerability; February 4, 2005

NRC Event 41436; Potential Vulnerability with ASDS Isolation Design;

February 23, 2005

NRC Event 41468; RHR Pump Tripped Due to Loss of Valve Position

Indication; March 8, 2005

LER 05000263/2004-002-00; Cable Separation Issue Identified During Appendix R

Re-analysis; November 1, 2004

LER 05000263/2005-001-00; Single Failure Identified That Could Prevent Energizing

Buses 15 and 16; April 4, 2005

LER 05000263/2005-001-01; Single Failure Identified That Could Prevent Energizing

Buses 15 and 16; June 6, 2005

LER 05000263/2005-002-00; Failure of #11 Reactor Protection System Motor-Generator

Set Results in an Engineered Safety Feature Actuation; April 25, 2005

LER 05000263/2005-003-00; Loss of Shutdown Cooling Due to #12 RHR Pump Trip;

May 9, 2005

LER 05000263/2005-004-00; Voluntary Report CRD Insert Line Leakage;

March 9, 2005

LER 05000263/2005-005-00; Inadvertent Engineered Safety Function Actuations During

Testing; June 1, 2005

Attachment

Attachment

13

Corrective Action Program Documents:

CAP037306; Failure of 11 Reactor Protection System MG Set Causes Engineered

Safety Features Actuation

CAP036987; Single Failure Identified That Could Prevent Energizing Bus 15 and 16

ACE004303; Single Failure Identified That Could Prevent Energizing Bus 15 and 16

CAP037264; ASDS Isolation Design Issue Could Prevent Bus 16 from Energizing

CAP037567; Loss of Shutdown Cooling During the Isolation to Replace Safety Relief

Valve Solenoid Valves

CAP038433; Loss of Power to Bus 16 During PMT for WO0505600

4OA5 Other Activities

Documents and Procedures:

Operations Manual E.5; Electrical Manual: System Electrical Blackout

Operations Manual E.2; Electrical Manual: Master Power Restoration Procedure

Operations Manual C.4-B.09.02.A; Abnormal Procedures: Station Blackout

Operations Manual B.09.03-05; 345 kV Substation - System Operation

Operations Manual B.09.06-05; 4.16 kV Station Auxiliary - System Operation

Operations Manual B.09.05-05; 115 kV Substation - System Operation

4AWI-08.15.01; Risk Management for Outage and On-Line Activities; Revision 0

4AWI-04.08.01; Event Notifications; Revision 20

4AWI-04.08.02; 10 CFR 50.72 and 10 CFR 73.71 Immediate Notifications; Revision 14

Operations Manual A.2; Emergency Implementing Procedures

Attachment

Attachment

14

LIST OF ACRONYMS USED

ASDS

Alternate Shutdown System

ASME

American Society of Mechanical Engineers

BWR

Boiling Water Reactor

CAP

Corrective Action Program

CRD

Control Rod Drive

CRDM

Control Rod Drive Mechanism

CS

Core Spray

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EFT

Emergency Filtration Train

EPRI

Electrical Power Research Institute

ESF

Engineered Safety Feature

ESW

Emergency Service Water

FAC

Flow Accelerated Corrosion

GE

General Electric

FIN

Finding

HCU

Hydraulic Control Unit

HELB

High Energy Line Break

HPCI

High Pressure Core Injection

HVAC

Heating, Ventilation, and Air Conditioning

IMC

Inspection Manual Chapter

IR

Inspection Report

IST

Inservice Testing

kV

Kilovolt

LCO

Limiting Condition for Operation

LER

Licensee Event Report

MCC

Motor Control Center

MG

Motor-Generator

NCV

Non-Cited Violation

NMC

Nuclear Management Company

NRC

U.S. Nuclear Regulatory Commission

NRR

Office of Nuclear Reactor Regulation

OSP

Offsite Power

OWA

Operator Workaround

PARS

Publicly Available Records

PI

Performance Indicator

PMT

Post-Maintenance Testing

PSIG

Pounds per Square Inch Guage

RA

Risk Assessment

RCIC

Reactor Core Isolation Cooling

RCPB

Reactor Coolant Pressure Boundary

RHR

Residual Heat Removal

RHRSW

Residual Heat Removal Service Water

RPS

Reactor Protection System

RWCU

Reactor Water Cleanup

Attachment

Attachment

15

SDP

Significance Determination Process

SRA

Senior Reactor Analyst

SSDA

Safe Shutdown Analysis

TI

Temporary Instruction

TS

Technical Specification

TSO

Transmission System Operator

URI

Unresolved Item

USAR

Updated Safety Analysis Report

VIO

Violation

WO

Work Order