05-09-2005 | reactor head was removed and the reactor was flooded up to the flange with the main steam-line plugs installed. At 0454, the station was in the process of performing an equipment isolation to support replacement of the Safety Relief Valve solenoids. While performing the isolation several unexpected alarms annunciated in the Control Room. Operations Shift Supervision decided to remove the isolation and re-evaluate the tagged components. When the isolation was removed the #12 RHR pump sensed a loss of suction flow path. The sensed loss of suction flow path caused the pump to trip and resulted in the loss of the in-service Shutdown Cooling train. Based on the loss of shutdown cooling, an NRC Event Notification Report (#41468) was made on March 8, 2005 at 1041 under 10 CFR Part 72(b)(3)(v)(B) "Event or Condition that could have Prevented Fulfillment of a Safety Function.
The Root Cause was determined to be failure of Operations Management and Station Management to effectively oversee implementation of the outage isolation process. |
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Description On March 8, 2005 the Monticello Nuclear Generating plant was shutdown in a refueling outage, with the reactor head [RPV] removed, and the reactor pressure vessel (RPV) [RPV] flooded up to the flange with the main steam-line plugs installed. The reactor water temperature was 98 degrees F and being cooled by #12 Residual Heat Removal (RHR) [BO] pump [P] aligned in shutdown cooling (SDC) mode.
At 0454, the station was in the process of performing an equipment isolation to support replacement of the Safety Relief Valve (SRV) [RV] solenoids [SOL]. While performing the isolation several unexpected alarms [ALM] annunciated in the Control Room. Operations Shift Supervision decided to remove the isolation and re-evaluate the tagged components. When the isolation was removed the running pump logic sensed a loss of suction flow path to the operating #12 RHR because the position indication for the RHR pump shutdown cooling suction valves [VLV] had been lost due to the equipment isolation.
The indicated loss of suction flow path caused the pump to trip and resulted in the loss of the in-service SDC train.
Operators restored SDC to the unit at 0507 by restarting the #12 RHR pump. The RPV water level remained stable at 651 inches and RPV water temperature remained stable at 98 degrees F.
Based on the loss of shutdown cooling, an NRC Event Notification Report (#41468) was made on March 8, 2005 at 1041.
Event Analysis
In accordance with 10 CFR 50.72 (b)(3)(v)(B), "Event or Condition that could have Prevented Fulfillment of a Safety Function," an eight-hour event notification was made to the USNRC, due to the loss of shutdown cooling which is required to remove residual heat. Per 10 CFR 50.73 (a)(2)(v)(B), a Licensee Event report is required for this event.
The event is classified as a safety system functional failure.
Safety Significance
A review for event significance was performed for the loss of SDC. During the event the RHR and core spray (CS) [BM] injection paths remained available. In addition, Reactor Water Cleanup (RWCU) [CE] was in operation throughout the event. The safety significance of this event with regards to the potential for core damage from the loss of shutdown cooling was determined to be minimal. Several alternative systems and sources of coolant were available and operable, and fully capable of keeping the reactor core covered/cooled.
Operations control room personal identified the loss of SDC and restored it to service in approximately 13 minutes after confirming that the removal of the isolation on the 125 VDC system [EJ] had resulted in the #12 RHR pump trip causing the loss of SDC.
Station procedures provide a means to establish alternate SDC if Operations personnel are unable to restore normal SDC. These procedures assume that the RHR system in SDC mode is either unavailable or incapable of maintaining reactor water temperature, a condition more severe than the actual occurrence. The procedure describes the systems available and how they are to be used to augment SDC in the event of a complete failure of the RHR system. The following alternate systems would be available: RWCU, the CST, Residual Heat Removal Service Water (RHRSW) "A" [BI] cross tie to Low Pressure Coolant Injection (LPCI) [BO], Service water crosstie to condensate [SD]/feedwater [SJ], Firewater [FP] crosstie to LPCI, and SBLC.
Cause
The Root Cause was determined to be failure of Operations and Station Management to effectively oversee implementation of the outage isolation process.
The contributing causes identified several weaknesses in the preparation, review and approval of outage isolations. These weaknesses included failure to require impact statements (e.g.; the effect on safety systems) in outage work packages and isolations, deficiencies in isolation preparations, and inadequate verification of isolations.
Corrective Action Immediate Actions Taken:
1. The SDC system was restored to service.
2. All outage isolations were placed on hold. Each of the outage isolations received an additional review to determine if the isolation had the potential to affect safety related components. If the potential existed, then the work package documentation was reviewed and an impact statement was developed and noted in the isolation placement instructions. The impact statement identified the affected safety related systems or components, and the potential impact on the plant.
3. A stand down was performed with the operations staff to review the event and actions taken.
4. Plant management increased observations during the outage to monitor equipment isolation performance.
Additional Corrective Actions to be taken:
A root cause investigation was completed and corrective actions were identified to revise the work control and outage processes. These actions are being tracked through the corrective action program process.
Failed Component Identification N/A
Previous Similar Events
A review of the station corrective action program database found the following similar event:
November 26, 2001: During Refuel Outage 20, SDC was lost due to an error in a modification installation procedure. The wrong studs for installing a jumper were listed in the procedure causing the "A" LPCI injection valve to close interrupting SDC. The cause was inadequate review of modification installation procedures. Corrective actions were appropriate but limited to the Design Engineering Department's reviews of modification documents.
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Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000362/LER-2005-001 | Emergency Diesel Generator (EDG) 3G003 Declared Inoperable Due to Loose Wiring Connection on Emergency Supply Fan | | 05000263/LER-2005-001 | | | 05000456/LER-2005-001 | Potential Technical Specification (TS) 3.9.4 Violation Due to Imprecise Original TS and TS Bases Wording | | 05000454/LER-2005-001 | Failed Technical Specification Ventilation Surveillance Requirements During Surveillance Requirement 3.0.3 Delay Period | | 05000282/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2005-001 | Plant in a Condition Prohibited by Technical Specifications due to Error Making Control Room Ventilation System Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000400/LER-2005-001 | Reactor Auxiliary Building Emergency Exhaust System Single Failure Vulnerability | | 05000395/LER-2005-001 | Emergency Diesel Generator Start and Load Due To A Loss Of Vital Bus | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2005-001 | RCS Pressure Boundary Leakage Due to Primary Water Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000305/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2005-001 | Reactor Coolant System Leakage Detection Instrumentation Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2005-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000255/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-002 | Missing Taper Pins on CCW Valve Cause Technical Specification Required Shutdown | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000370/LER-2005-002 | Ice Condenser Lower Inlet Door Failed Surveillance Testing | | 05000353/LER-2005-002 | High Pressure Coolant Injection System Inoperable due to a Degraded Control Power Fuse Clip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000263/LER-2005-002 | | | 05000454/LER-2005-002 | One of Two Trains of Hydrogen Recombiners Inoperable Longer Than Allowed by Technical Specifications Due to Inadequate Procedure | | 05000244/LER-2005-002 | Emergency Diesel Generator Start Resulting From Loss of Off-Site Power Circuit 751 | | 05000362/LER-2005-002 | Emergency Containment Cooling Inoperable for Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2005-002 | DTechnical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by Gas Intrusion from a Leaking Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000265/LER-2005-002 | Main Steam Relief Valve Actuator Degradation Due to Failure to Correct Vibration Levels Exceeding Equipment Design Capacities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000286/LER-2005-002 | • Entergy Nuclear Northeast Indian Point Energy Center 450 Broadway, GSB P.O. Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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