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MONTHYEARML0209405042002-04-0303 April 2002 Attachment to Letter Crystal River Unit 3 - Table for OTSG Post-Inspection Phone Call and Drawings Project stage: Other ML0209307962002-04-0303 April 2002 Summary of Conference Call with Florida Power Corp. Regarding 2001 Steam Generator Tube Inspection Results 9TAC MB3015) Project stage: Other ML0410508232004-04-13013 April 2004 Steam Generator Tube Inservice Inspection Summary Reports from the Fall 2001 Outage Project stage: Other 2002-04-03
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Category:Letter
MONTHYEARML23342A0942024-01-0909 January 2024 Independent Spent Fuel Storage Installation Security Inspection Plan ML23354A0632023-12-22022 December 2023 Cover Letter - Crystal River License Termination Plan Request for Additional Information ML23345A1882023-12-0606 December 2023 Fws to NRC Crystal River Species List of Threatened and Endangered Species That May Occur in Your Proposed Project Location or May Be Affected by Your Proposed Project ML23320A2592023-11-17017 November 2023 STC-23 077 Notification of the Crystal River Unit 3 Generating Plant License Termination Plan Public Meeting and Federal Register Notice ML23313A1322023-11-15015 November 2023 Request for Additional Information for the Environmental Assessment of the License Termination Plan for Crystal River Unit 3 Nuclear Generating Plant ML23310A0712023-11-0707 November 2023 Audit Plan Cover Letter - Crystal River Unit 3 Nuclear Generating Plant LTP ML23187A1112023-07-25025 July 2023 Acceptance of Requested Licensing Action License Request to Add License Condition to Include License Termination Plan Requirements ML23107A2722023-06-13013 June 2023 Letter Transmitting NRC Survey Results for East Settling Pond ML23160A2962023-06-0909 June 2023 Response to Crystal River, Unit 3 Supplemental Information Needed for Acceptance on the Application for a License Amendment Regarding Approval of the License Termination Plan ML23107A2732023-06-0707 June 2023 Orise Independent Survey Report Dcn 5366-SR-01-0 IR 05000302/20220032023-05-25025 May 2023 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report No. 05000302/2022003 ML23103A1902023-04-19019 April 2023 Request for Supplemental Information Cover Letter ML23058A2532023-03-22022 March 2023 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River, Unit 3 - NRC Inspection Report No. 05000302/2022003 ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities ML22265A0192022-09-26026 September 2022 Nuclear Generating Plant - U.S. Nuclear Regulatory Commission'S Analysis of ADP CR3, Llc'S Decommissioning Funding Status Report (License No. DPR-72, Docket Nos. 50-302 and 72-1035) IR 05000302/20220022022-08-0909 August 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report 05000302/2022002 IR 05000302/20220012022-05-0303 May 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report 05000302/2022001 ML22116A1752022-04-27027 April 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3- Independent Spent Fuel Storage Installation Security Inspection Report 07201035/2022401 ML22105A3992022-04-18018 April 2022 Nuclear Generating Plant - Change in NRC Project Manager ML22011A1362022-01-31031 January 2022 Independent Spent Fuel Storage Installation Security Inspection Plan IR 05000302/20210042022-01-24024 January 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report No. 05000302/2021004 ML22024A2142022-01-24024 January 2022 Nuclear Generating Plant - NMFS NRC Letter - Crystal River Energy Complex Biological Opinion Status (License No. DPR-72, Docket Nos. 50-302 and 72-1035) ML21351A0052021-12-20020 December 2021 NRC Analysis of ADP CR3, LLC Decommissioning Funding Status Report for the Crystal River Unit 3 Nuclear Generating Plant (License No. DPR-72, Docket Nos. 50-302 and 72-1035) ML21322A2702021-11-24024 November 2021 Nuclear Generating Plant - Issuance of Amendment No. 260 Approving the Independent Spent Fuel Storage Installation Only Security Plan, Rev 3 IR 05000302/20210032021-11-0909 November 2021 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report Nos. 05000302/2021003 and 07201035/2021001 ML21288A4292021-10-18018 October 2021 Letter - Crystal River Unit 3 Nuclear Generating Plant - Correction to Safety Evaluation Related to the Issuance of Amendment No. 259 Approving the Independent Spent Fuel Storage Installation Only Emergency Plan ML21238A0952021-10-13013 October 2021 Issuance of Amendment No. 259 Approving the ISFSI-Only Emergency Plan, Revision Draft a IR 05000302/20210012021-08-12012 August 2021 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report Nos. 05000302/2021001 and 05000302/2021002 ML21182A1032021-07-0606 July 2021 Request for Additional Information (RAI) Related to the ISFSI-Only Emergency Plan ML21159A0422021-06-28028 June 2021 VY and CR Indirect License Transfer Package ML21060B4142021-04-12012 April 2021 U.S. Nuclear Regulatory Commission Analysis of Duke Energy Florida, Llc'S Initial Decommissioning Funding Plan for the Crystal River Independent Spent Fuel Storage Installation ML21028A5912021-03-0202 March 2021 Letter to Reid Forwarding Exemption from 10 CFR Part 20, Appendix G, Section Iii.E ML21055A7832021-02-25025 February 2021 Letter to Reid, Change in NRC Staff Project Management for Crystal River Unit 3 Nuclear Generating Plant ML21012A3142021-01-13013 January 2021 Independent Spent Fuel Storage Installation Security Inspection Plan IR 05000302/20200012020-11-19019 November 2020 NRC Inspection Report No. 05000302/2020001, Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3, Crystal River, Florida ML20269A2922020-10-0707 October 2020 NRC Form 311 QA Program Approval Revision 10 Related to Crystal River 3 ML20101G5822020-04-10010 April 2020 CR-3 License Transfer SE Corrected Cover Letter ML20069A0232020-04-0101 April 2020 Order Approving Transfer of Licensed Authority from Duke Energy Florida, LLC, to ADP CR3, LLC, and Draft Conforming Administrative License Amendment ML20050D0142020-02-19019 February 2020 NRC Independent Spent Fuel Storage Installation Inspection Report No. 07201035/2020001, Duke Energy Florida, LLC, Crystal River Unit 3, Crystal River, Florida ML20050F7702020-02-14014 February 2020 30-Day Notice of Payment from the City of Tallahassee Trust Fund Non-Qualified Nuclear Decommissioning Trust Fund for Crystal River Unit 3 ML20015A5672020-01-15015 January 2020 Independent Spent Fuel Storage Installation Security Inspection Plan ML20009D0432020-01-10010 January 2020 Letter to Hobbs, Crystal River Unit 3 Nuclear Generating Plant - Corrected Safety Evaluation for Approval of Partial Site Release for Facility Operating License No. DPR-72 ML19339G5092020-01-0202 January 2020 Letter to Hobbs, Crystal River Unit 3 Nuclear Generating Plant - Approval of Partial Site Release for Facility Operating License No. DPR-72 ML19343A8252019-12-0606 December 2019 Letter from Erika Bailey, Oak Ridge Institute for Science and Education, to John Hickman, NRC, Forwarding Independent Confirmatory Survey Summary and Results for the 3,854-Acre Area Partial Site Release at the Crystal River Energy Complex IR 05000302/20190022019-11-20020 November 2019 NRC Inspection Report No. 05000302/2019002 and Independent Spent Fuel Storage Installation Inspection Report No. 07201035/2019002, Duke Energy Florida, LLC, Crystal River Unit 3, Crystal River, Florida ML19317D0932019-10-25025 October 2019 Engine Systems, Inc., 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10 CFR21-0127, Rev. 0, Emd Fuel Injectors - Seized Plunger and Bushing ML19261A0702019-09-19019 September 2019 VEGP U3 Proficiency Watches Prior to Fuel Load ML19177A0802019-06-26026 June 2019 Nuclear Generating Plant (CR-3) - Notification of Revised Post-Shutdown Decommissioning Activities Report (Revised PSDAR) ML19170A1942019-06-14014 June 2019 Application for Order Consenting to Direct Transfer of Control of Licenses and Approving Conforming License Amendment ML19129A1402019-05-15015 May 2019 Letter to Hobbs, Correction to Amendment No. 257 Approving Independent Spent Fuel Storage Installation (ISFSI)-Only Emergency Plan, Revision 1 2024-01-09
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Text
April 3, 2002 Mr. Dale E. Young, Vice President Crystal River Nuclear Plant (NA1B)
ATTN: Supervisor, Licensing & Regulatory Programs 15760 W. Power Line Street Crystal River, Florida 34428-6708
SUBJECT:
CRYSTAL RIVER UNIT 3
SUMMARY
OF CONFERENCE CALL WITH FLORIDA POWER CORPORATION REGARDING 2001 STEAM GENERATOR TUBE INSPECTION RESULTS (TAC NO. MB3015)
Dear Mr. Young:
On October 17, 2001, the Nuclear Regulatory Commission staff (NRC) participated in a conference call with Florida Power Corporation (FPC) regarding the steam generator tube inspection activities during Refueling Outage 12 at Crystal River Unit 3. Enclosed is a summary of the conference call. Also enclosed are materials provided by FPC to support the call.
Participants included myself, John Tsao, Ken Karwoski, and Mark Lesser.
By letter dated October 19, 2001, FPC submitted a special inspection report prior to ascension to MODE 4. FPC will be submitting a comprehensive inspection report in accordance with the plant technical specifications. We appreciate your support in this matter. If you have any questions, please give me a call at (301) 415-1437.
Sincerely,
/RA/
John M. Goshen, Project Manager, Section 2 Project Directorate II Division of Licensing Project Management Office of Nuclear Reactor Regulation Docket No. 50-302
Enclosures:
- 1. Summary of 10/17/01 Conference Call
- 2. FPC Supporting Documentation cc w/enclosures: See next page
ML020930796 OFFICE PDII-2/PM PDII-2/LA PSDII-2/SC NAME JGoshen BClayton RCorreia DATE 3/27/2002 3/27/2002 3/27/2002
SUMMARY
OF OCTOBER 17, 2001, CONFERENCE CALL WITH FLORIDA POWER CORPORATION REGARDING CURRENT STEAM GENERATOR INSPECTION RESULTS AT CRYSTAL RIVER UNIT 3 On October 17, 2001, staff from the Materials and Chemical Engineering Branch of the Division of Engineering participated in conference calls with Florida Power Corporation (FPC) representatives to discuss the results of the steam generator tube inspections during Refueling Outage 12 at Crystal River Unit 3.
FPC representatives discussed the following topics: initial eddy current testing scope, scope expansion plans, indications identified to-date, repair/plugging plans, new inspection findings, in situ pressure test plans and actions taken in response to lessons learned from the Indian Point Unit 2 tube failure.
In accordance with Regulatory Commitments specified in License Amendment No. 198 for the reroll joint repair, dated September 10, 2001, FPC reported that several circumferential indications were detected in the original roll joints and rerolled joints in the tubesheet. These tubes were plugged. As a part of the Regulatory Commitments, FPC reported that the estimated leakage from the reroll joints under large break loss-of-coolant accident conditions for steam generators A and B were within the allowable limits. Additional details may be found in FPCs letter dated October 19, 2001 (Adams Accession No. ML013610008).
FPC also reported observing the following degradation as a result of the steam generator tube inspection: volumetric indications in the transition regions of the roll and reroll joints; axial indications in the tube end regions; volumetric/intergranular attack indications at the first span; and circumferential, axial, and volumetric indications in various locations.
FPC plugged approximately 40 tubes, including a tube that was not expanded in the tubesheet, and a tube with a circumferential indication. This latter indication was located 0.78 inch below the top of the eighth tube support plate, which has a thickness of 1.5 inches. The indication was 0.23-inch in circumferential extent and exhibited a voltage of 0.57 volts. The indication was detected initially by the bobbin probe and subsequently confirmed by a plus point coil as a circumferential indication. The indication had axial branching and was in reality a mixed-mode indication. No other indications were detected in similar locations in other tube support plate locations. The indication was analyzed to be within the conditioning monitoring limits.
On the basis of the information discussed during the calls, the staff did not identify any issues requiring further discussion.
ENCLOSURE 1
Mr. Dale E. Young CRYSTAL RIVER UNIT NO. 3 Florida Power Corporation cc:
Mr. R. Alexander Glenn Chairman Associate General Counsel (MAC-BT15A) Board of County Commissioners Florida Power Corporation Citrus County P.O. Box 14042 110 North Apopka Avenue St. Petersburg, Florida 33733-4042 Inverness, Florida 34450-4245 Mr. Daniel L. Roderick Ms. Sherry L. Bernhoft Plant General Manager Manager Regulatory Affairs Crystal River Nuclear Plant (NA2C) Crystal River Nuclear Plant (NA2H) 15760 W. Power Line Street 15760 W. Power Line Street Crystal River, Florida 34428-6708 Crystal River, Florida 34428-6708 Mr. Michael A. Schoppman Senior Resident Inspector Framatome ANP Crystal River Unit 3 1911 North Ft. Myer Drive, Suite 705 U.S. Nuclear Regulatory Commission Rosslyn, Virginia 22209 6745 N. Tallahassee Road Crystal River, Florida 34428 Mr. William A. Passetti, Chief Department of Health Mr. Richard L. Warden Bureau of Radiation Control Manager Nuclear Assessment 2020 Capital Circle, SE, Bin #C21 Crystal River Nuclear Plant (NA2C)
Tallahassee, Florida 32399-1741 15760 W. Power Line Street Crystal River, Florida 34428-6708 Attorney General Department of Legal Affairs The Capitol Tallahassee, Florida 32304 Mr. Craig Fugate, Director Division of Emergency Preparedness Department of Community Affairs 2740 Centerview Drive Tallahassee, Florida 32399-2100