L-23-016, Twenty-Eighth Refueling Outage Inservice Inspection Summary Report

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Twenty-Eighth Refueling Outage Inservice Inspection Summary Report
ML23052A143
Person / Time
Site: Beaver Valley
Issue date: 02/21/2023
From: Blair B
Energy Harbor Nuclear Corp
To:
Office of Nuclear Reactor Regulation, Document Control Desk
References
L-23-016
Download: ML23052A143 (1)


Text

energy Energy Harbor Nuclear Corp.

harbor Beaver Valley Power Station P.O. Box 4 Shippingport, PA 15077 Barry N. Blair 724-682-5234 Site Vice President, Beaver Valley Nuclear February 21, 2023 L-23-016 10 CFR 50.55a(g)

ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001

Subject:

Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 Twenty-Eighth Refueling Outage lnservice Inspection Summary Report In accordance with 10 CFR 50.55a, "Codes and Standards," and the American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME Code) Case N-532-5, "Repair/Replacement Activity Documentation Requirements and lnservice Inspection Summary Report Preparation and Submission,Section XI, Division 1," enclosed pleased find the inservice inspection owner's activity report for examinations performed prior to and during the twenty-eighth refueling outage at Beaver Valley Power Station, Unit No. 1 (BVPS-1 ).

lnservice inspection activities addressed in the report were performed during the second period of the fifth ten-year interval in accordance with Section XI of the ASME Code, 2013 Edition. The inservice inspection term at BVPS-1 covered by this report includes the period from May 12, 2021 to November 18, 2022.

There are no regulatory commitments contained in this submittal. If there are any questions or if additional information is required, please contact Mr. Phil H. Lashley, Manager - Fleet Licensing, at (330) 696-7208.

Barry N. Blair

Beaver Valley Power Station, Unit No. 1 L-23-016 Page 2

Enclosure:

Beaver Valley Power Station, Unit No. 1, Twenty-Eighth Refueling Outage Inservice Inspection Owners Activity Report cc: NRC Region I Administrator NRC Resident Inspector NRR Project Manager Director BRP/DEP Site BRP/DEP Representative

Enclosure L-23-016 Beaver Valley Power Station, Unit No. 1 Twenty-Eighth Refueling Outage Inservice Inspection Owner's Activity Report (2 pages follow)

Beaver Valley Power Station Unit 1 energy Report No. BV1-OAR 1-1 R28 lnservice Inspection Program 1R28 Owner's Activity Report harbor 1 of 2 FORM OAR-1 OWNER'S ACJIYIIY REPORT Report Number BV1-OAR1-1R28 Plant Beaver Valley Power Station Unit No. Commercial Service Date September 30, 1976 Refueling Outage No. 1R28 (if applicable)

Current Inspection Interval 5th (1st, 2nd, 3"', 4th, other)

Current Inspection Period Edition and Addenda of Section XI applicable to the inspection plan 2013 Edition Date and Revision of inspection plans October 11, 2021, 1/2-ADM-2039, Rev. 19 Edition and Addenda of Section XI applicable to repair/replacement activities, if ~ifferent than the inspection plans _S_am_e_ _ _ _ __

Code Case Used: N-513-4, N-532-5, N-639, N-661-3, and N-716-1 (if applicable, including cases modified by Case N-532 and later revisions)

CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting completion of 1R28 (refueling outage number)

Signed L. Seaman-ISi Program Owner Date 61/-;;.r;/g 3 CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by Hartford Steam Boiler of Hartford, have inspected the items described in the Inspection and Insurance Connecticut Company Owner's Activity Report, and state that, to the best ofmy knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable i anner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

NB 15908 NIR (National Board Number and Endorsement)

Beaver Valley Power Station Unit 1 energy Report No. BV1-0AR 1-1 R28 lnservice Inspection Program 1R28 Owner's Activity Report harbor 2 of2 TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Category Item Description Evaluation Description and Item Number 0-8 02.10 24"-WR20-151-Q3 24 inch class 3 River water piping . A Code Case 513-4 evaluation was performed to continue operation into outaoe 1R28 when the pipinQ was repaired .

D-8 02.10 20"-WR-5-151-Q3 Class 3 River water piping reducer. A Code Case 513-4 evaluation was performed to continue operation into outage 1R28 when the pipinQ was repaired.

TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Date Repair/Replacement Class Item Description Description of Work Completed Plan Number 3 24" WR20-151-Q3 Pipeline repaired. 11-15-22 4404 Applied Code case 661-3 overlays in two 3 20"-WR-5-151-Q3 11-4-2022 4422 locations.

Notes:

(1) "Date Completed" is the date that the Repair Replacement Plan final signature was applied. This date may be after the end of the reporting period for work that was physically completed within the reporting period.

(2) Steam Generator activities are reported under separate correspondence in Technical Specification required reports.