IR 05000528/2020002

From kanterella
(Redirected from IR 05000530/2020002)
Jump to navigation Jump to search
Integrated Inspection Report 05000528/2020002, 05000529/2020002, and 05000530/2020002
ML20212M129
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 07/31/2020
From: John Dixon
NRC/RGN-IV/DRP/RPB-D
To: Lacal M
Arizona Public Service Co
References
EA-20-075 IR 2020002
Download: ML20212M129 (32)


Text

July 31, 2020

SUBJECT:

PALO VERDE NUCLEAR GENERATING STATION UNITS 1, 2, AND 3 -

INTEGRATED INSPECTION REPORT 05000528/2020002, 05000529/2020002, AND 05000530/2020002

Dear Mrs. Lacal:

On June 30, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Palo Verde Nuclear Generating Station Units 1, 2, and 3. On July 7, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. None of these findings involved a violation of NRC requirements.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 205550001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Palo Verde Nuclear Generating Station Units 1, 2, and 3. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, John L. Dixon, Jr., Chief Reactor Projects Branch D Division of Reactor Projects

Docket Nos. 05000528, 05000529, and 05000530 License Nos. NPF-41, NPF-51, and NPF-74

Enclosure:

Inspection Report 05000528/2020002, 05000529/2020002, and 05000530/2020002 w/Attachment: Detailed Risk Assessment

Inspection Report

Docket Numbers:

05000528, 05000529, and 05000530

License Numbers:

NPF-41, NPF-51, and NPF-74

Report Numbers:

05000528/2020002, 05000529/2020002 and 05000530/2020002

Enterprise Identifier: I-2020-002-0001

Licensee:

Arizona Public Service Company

Facility:

Palo Verde Nuclear Generating Station Units 1, 2, and 3

Location:

Tonopah, AZ

Inspection Dates:

April 1, 2020 to June 30, 2020

Inspectors:

C. Peabody, Senior Resident Inspector

R. Bywater, Resident Inspector

D. You, Resident Inspector

A. Athar, Resident Inspector

I. Anchondo-Lopez, Reactor Inspector

W. Cullum, Reactor Inspector

J. Drake, Senior Reactor Inspector

F. Thomas, Reactor Inspector

Approved By:

John L. Dixon, Jr., Chief

Reactor Projects Branch D

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Palo Verde Nuclear Generating Station Units 1, 2, and 3, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Incorrect Installation of Unit 3 Reactor Coolant Pump 1B Seal Assembly Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000530/2020002-01 Open/Closed

[H.6] - Design Margins 71152 A self-revealed Green finding was identified when the licensee failed to follow Procedure 31MT-9RC23, Reactor Coolant Pump Sulzer Bingham Seal Replacement,

Revision 41. Specifically, when installing the Unit 3 1B reactor coolant pump seal package during the fall 2019 refueling outage, the stage 2 to stage 3 drive pins were not installed properly causing the seal to leak and ultimately requiring a forced outage to replace the seal on February 8, 2020.

Failure to Adequately Evaluate or Test the Impact of a Design Modification to the Unit 2 Main Feedwater Lube Oil Control Panel Protective Relay System Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000529/2020002-02 Open/Closed EA-20-075 None 71153 A self-revealed Green finding was identified when the licensee failed to follow Procedure 81DP-0EE10, Design Change Process, Revision 30. Specifically, the licensee failed to adequately evaluate or test the impact of a design modification to the Unit 2 main feedwater lube oil control panel protective relay system, which resulted in a spurious loss of both main feedwater pumps and subsequent reactor trip on March 3, 2020.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000529/2020-001-00 LER 2020-001-00 for Palo Verde Nuclear Generating Station (PVNGS), Unit 2,

Reactor Trip on Low Steam Generator Level Signal 71153 Closed

PLANT STATUS

Unit 1 operated at or near full power for the duration of the inspection period.

Unit 2 entered the inspection period at full power. On April 4, 2020, Unit 2 shut down for a planned refueling outage. Unit 2 was restarted on May 4, 2020, and operated at or near full power for the remainder of the inspection period.

Unit 3 operated at or near full power for the duration of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities; and completed on site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (2 Samples)

(1) The inspectors evaluated summer readiness of offsite and alternating current (AC)power systems on May 8, 2020.
(2) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of the monsoon season on May 14, 2020.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 auxiliary feedwater system A following refueling outage testing on May 4, 2020
(2) Unit 3 low pressure safety injection B on May 8, 2020
(3) Unit 1 auxiliary feedwater system B on June 23, 2020

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the hydrogen recombiner system shared among the three units on June 8, 2020.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Unit 2 southwest of containment building, Fire Zone 66A, on April 6, 2020
(2) Unit 1 condensate transfer pump room and tunnel, Fire Zone 83, on April 9, 2020
(3) Unit 3 condensate transfer pump room and tunnel, Fire Zone 83, on April 20, 2020
(4) Unit 3 140 elevation fuel building, Fire Zone 29A, on May 28, 2020
(5) Unit 1 west piping penetration area, Fire Zone 37C, on June 3, 2020

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections in the class 1E electrical penetration rooms on May 21, 2020.

===71111.07T - Heat Sink Performance

Triennial Review (IP Section 03.02)===

(1) Unit 3 diesel generator A jacket water cooler, cooled by service water
(2) Unit 2 diesel generator A air intercooler, cooled by service water
(3) Unit 1 essential chiller B, cooled by essential cooling water
(4) Unit 3 control room essential air cooling unit A, cooled by essential chilled water

71111.08P - Inservice Inspection Activities (PWR) PWR Inservice Inspection Activities Sample (IP Section 03.01)

(1) The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined, and accepted by reviewing the following activities from April 6, 2020, to April 17, 2020. Due to the COVID 19 pandemic, only visual examinations were performed during this outage.

Therefore, one ultrasonic examination from the previous Unit 2 refueling outage was selected for review as allowed by the inspection procedure.

03.01.a - Nondestructive Examination and Welding Activities.

1. Ultrasonic examination

a. Steam Generator, Weld 54-10A, reducer to pipe

2. Visual examination

a. Reactor coolant system instrumentation connections 4-99 cold leg

connections b. Reactor coolant system instrumentation connections, 5-36 c. Reactor coolant system instrumentation connections, 6-99 cold leg connection d. Reactor coolant pump pressure taps (4 suction taps) 6-100-1, 6-100-3,

6-100-6, 6-100-7 e. Pressurizer heaters penetrations (36), 5-37 f. Essential cooling water, 2-ewa-eoi, pipe hanger g. Essential cooling water, ewa-e01-w, pipe hanger h. Essential cooling water, 2-ew-023-h-012, pipe hanger

03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities.

The inspectors reviewed 15 condition reports and associated boric acid evaluations.

03.01.d - Pressurized-Water Reactor Steam Generator Tube Examination Activities.

1. The licensee performed:

a. One hundred percent bobbin testing was performed in both steam generators.

2. No in-situ pressure testing was required.

The inspectors reviewed 18 notifications that dealt with inservice inspections issues and found that items were entered into the corrective action program at the appropriate level and addressed appropriately.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated Unit 3 operators conducting a controlled power ascension following turbine valve testing on June 12, 2020.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a simulator scenario for the steam generator tube rupture emergency operating procedure on June 24, 2020.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Unit 2 safety injection system B reliability performance monitoring criteria exceeded due to a blown fuse causing the shutdown cooling isolation valve SI-654 to be nonfunctional on March 21, 2020.

Quality Control (IP Section 03.02) (1 Sample)

The inspectors evaluated the effectiveness of maintenance and quality control activities to ensure the following SSC remains capable of performing its intended function:

(1) Review of commercial grade dedication of 15-amp fuses on April 27-28, 2020

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 2 refueling outage 22 plan on April 1, 2020
(2) Unit 3 emergent work for auxiliary feedwater pump B on April 27, 2020
(3) Unit 2 work controls for contingency freeze seal installation to repair valve 2PSIB-V532 on May 1, 2020
(4) Planned outage of 525 KV switchyard east bus for capacitive coupled voltage transformer replacement on May 8, 2020
(5) Unit 2 planned maintenance of containment spray pump B and low-pressure safety injection pump B on May 21, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (11 Samples)

The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 1 reactor coolant pump orbital vibration monitoring system on April 6, 2020
(2) Unit 2 startup transformer 3 high temperature on April 21, 2020
(3) Units 1, 2, and 3 GE Hitachi AKR-2B-50 breakers part 21 notification on April 22, 2020
(4) Unit 2 operability of safety injection system valve SIB-UV-275 on April 29, 2020
(5) Unit 2 evaluation of debris identified during core reload on April 29, 2020
(6) Unit 2 operability of the containment liner on April 30, 2020
(7) Unit 1 reactor trip circuit breaker B failed to reset multiple times on May 19, 2020
(8) Unit 2 operability of condensate storage tank in response to CST trouble - leakage alarm received on June 1, 2020
(9) Unit 2 operability impact of damaged conductors within AFW pump turbine temperature elements on June 2, 2020
(10) Unit 3 containment hydrogen analyzer isolation valve HPB-UV8 on June 4, 2020
(11) Units 1, 2, and 3 functionality of hydrogen recombiner B on June 10, 2020

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Design modification for the condensate low-low level trip defeat switch

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1)77ST-9SB13, Unit 2 core protection calculator channel A functional testing following planned maintenance loss and restoration of instrument power on April 25, 2020 (2)40OP-9AF01, Unit 3 essential auxiliary feedwater system after corrective maintenance on leaking oil sight glass on April 29, 2020 (3)32MT-9RC03, Unit 2 reactor coolant pump 1B testing following motor replacement on May 6, 2020

(4) Work order 5231052, startup transformer no. 2 NANX03 testing following planned maintenance and repairs on June 16, 2020 (5)73ST-9XI20, Unit 2 ADV-178 stroke after nitrogen check valve internals replaced on June 18, 2020

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated refueling outage 2R22 activities from April 4 to May 4, 2020.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) Unit 2 auxiliary feedwater pump B on April 29, 2020
(2) Unit 1 plant protection system functional testing on May 30, 2020
(3) Unit 3 diesel generator B 24-hour loaded run, load reject, and hot restart test on June 15, 2020

Inservice Testing (IP Section 03.01) (1 Sample)

(1) Unit 1 essential chill water pump B inservice test on April 20, 2020

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) Unit 2 quick opening closure device local leak rate test review on May 5,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05)===

(1) Unit 1 (April 1, 2019 through March 31, 2020)
(2) Unit 2 (April 1, 2019 through March 31, 2020)
(3) Unit 3 (April 1, 2019 through March 31, 2020)

MS07: High Pressure Injection Systems (IP Section 02.06) (3 Samples)

(1) Unit 1 (April 1, 2019 through March 31, 2020)
(2) Unit 2 (April 1, 2019 through March 31, 2020)
(3) Unit 3 (April 1, 2019 through March 31, 2020)

MS08: Heat Removal Systems (IP Section 02.07) (3 Samples)

(1) Unit 1 (April 1, 2019 through March 31, 2020)
(2) Unit 2 (April 1, 2019 through March 31, 2020)
(3) Unit 3 (April 1, 2019 through March 31, 2020)

MS09: Residual Heat Removal Systems (IP Section 02.08) (3 Samples)

(1) Unit 1 (April 1, 2019 through March 31, 2020)
(2) Unit 2 (April 1, 2019 through March 31, 2020)
(3) Unit 3 (April 1, 2019 through March 31, 2020)

MS10: Cooling Water Support Systems (IP Section 02.09) (3 Samples)

(1) Unit 1 (April 1, 2019 through March 31, 2020)
(2) Unit 2 (April 1, 2019 through March 31, 2020)
(3) Unit 3 (April 1, 2019 through March 31, 2020)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for trends in unplanned reactor scrams and shutdowns between February 2018 and March 2020 that might be indicative of a more significant safety issue. No significant trends were observed and no findings were identified.

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Incorrect installation of Unit 3 reactor coolant pump 1B seal assembly on November 22, 2019

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) Licensee Event Report 05000529/2020-001-00, Unit 2 Reactor Trip on Low Steam Generator Level Signal on March 3, 2020, LER 50-529-2020-001 (ADAMS Accession No. ML20121A285). The inspection conclusions associated with this LER are documented in this report under Inspection Results Section

INSPECTION RESULTS

Incorrect Installation of Unit 3 Reactor Coolant Pump 1B Seal Assembly Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events

Green FIN 05000530/2020002-01 Open/Closed

[H.6] - Design Margins 71152 A self-revealed Green finding was identified when the licensee failed to follow Procedure 31MT-9RC23, Reactor Coolant Pump Sulzer Bingham Seal Replacement, Revision 41. Specifically, when installing the Unit 3 1B reactor coolant pump seal package during the fall 2019 refueling outage, the stage 2 to stage 3 drive pins were not installed properly causing the seal to leak and ultimately requiring a forced outage to replace the seal on February 8, 2020.

Description:

On November 22, 2019, Unit 3 operators identified a degrading trend for reactor coolant pump 1B second and third stage seal pressures as well as an increasing flow trend into the reactor drain tank (RDT). An evaluation completed on November 25, 2019, determined that this was likely indicative of a reactor coolant pump 1B seal leak. By February 7, 2020, reactor coolant system unidentified leak rate had increased to 0.328 gallons per minute (gpm). Unit 3 was shut down on February 8, 2020, to replace the reactor coolant pump 1B seal assembly.

A visual inspection of the disassembled seal found damage to the seal assembly as well as a misalignment of the second and third stage shaft protection sleeves. A cause evaluation found that the installation of the seal assembly on November 5, 2019 (during the Unit 3 refueling outage) was not done in accordance with procedure. Station Procedure 31MT-9RC23, Reactor Coolant Pump Sulzer Bingham Seal Replacement, Section 6.17, outlines steps that indicate the stage 2 to stage 3 drive pins for the inner pins are to be installed before the outer pins. However, the investigation found that the outer pins were installed before the inner pins.

The procedure also requires measurement taken to verify seal running clearances (Kf). It was noted that the value for Kf was larger than the previous value (2.290 vs. 2.270).

Although the procedure does not have any specific acceptance criteria for this measurement, the discrepancy was brought to the attention of the engineering department. Interviews with maintenance personnel revealed a lack of understanding of the importance of the Kf value as well as what a good Kf value should be since no acceptance criteria existed in the procedure.

Corrective Actions: Unit 3 reactor coolant pump seal assembly was replaced during the forced outage.

Corrective Action References: 20-01928

Performance Assessment:

Performance Deficiency: The licensees failure to follow Procedure 31MT-9RC23, Reactor Coolant Pump Sulzer Bingham Seal Replacement, Section 6.17, when installing the Unit 3 reactor coolant pump 1B seal assemblies during the fall 2019 refueling outage was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the human performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the installation sequence errors caused seal degradation which ultimately required an unplanned plant shutdown in order to replace the seal assembly.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined that the finding had very low safety significance (Green) because the finding could not result in exceeding the RCS leak rate for a small loss of coolant accident (LOCA) and would not have likely affected other systems used to mitigate a LOCA, resulting in a total loss of their function (Exhibit 1, Section A).

Cross-Cutting Aspect: H.6 - Design Margins: The organization operates and maintains equipment within design margins. Margins are carefully guarded and changed only through a systematic and rigorous process. Special attention is placed on maintaining fission product barriers, defense-in-depth, and safety-related equipment. The finding has a cross-cutting aspect in the area of human performance associated with the design margins component because the licensee failed to operate and maintain their equipment within design margins. Specifically, the licensees procedure did not have an acceptance criterion for the seal running clearance measurement. As a result, the licensee was not aware that a higher than normal value could be indicative of a seal assembly mis-alignment. Ultimately this caused a degradation of the reactor coolant pump seal assembly during normal plant operations.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

Failure to Adequately Evaluate or Test the Impact of a Design Modification to the Unit 2 Main Feedwater Lube Oil Control Panel Protective Relay System Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events

Green FIN 05000529/2020002-02 Open/Closed EA-20-075 None 71153 A self-revealed Green finding was identified when the licensee failed to follow Procedure 81DP-0EE10, Design Change Process, Revision 30. Specifically, the licensee failed to adequately evaluate or test the impact of a design modification to the Unit 2 main feedwater lube oil control panel protective relay system, which resulted in a spurious loss of both main feedwater pumps and subsequent reactor trip on March 3, 2020.

Description:

On March 3, 2020, at 3:25 p.m., an operator inadvertently opened the breaker that supplies the Unit 2 main feedwater pump lube oil control panel. At 8:49 p.m., power to the Unit 2 main feedwater pump lube oil control panel was restored by closing the supply breaker. Upon restoration of power, an erroneous low lube oil pressure signal tripped both main feedwater pumps, which resulted in an automatic reactor trip on low steam generator 1 water level.

The function of the main feedwater lube oil control panel protective relays is to monitor main feedwater bearing lube oil pressure and to take protective actions when a low-pressure condition is detected. The protective system consists of multiple digital relays and auxiliary relays configured to provide a 2 out of 3 logic on the low-pressure protection circuit. Per the vendor technical documents, the digital relays default to the tripped condition upon loss of power, whereas the auxiliary relays default to the non-tripped condition. The digital relays perform a power-on diagnostic routine, which takes approximately 10 seconds. The auxiliary relays do not have an initialization delay. Thus, during this event, when power was initially lost and then subsequently restored to the circuit, the auxiliary relays immediately actuated in response to the digital relay being tripped, providing an erroneous low lube oil pressure signal.

In 2013, the licensee modified the main feedwater pump lube oil system to address single point vulnerabilities and provide increased reliability. The original low-pressure switches were replaced with the current switching logic. However, while implementing this modification, the licensee failed to adequately evaluate the installation of the low-pressure switching logic under Design Modification Work Order ENG-DMWO 2512314. After the modification was installed, post-modification return-to-service testing should have revealed that the changes introduced a design vulnerability that could cause spurious tripping of the main feedwater pumps when power to the protective relay circuitry was cycled. However, the station failed to properly test the replacement logic system during or following this modification to determine whether the operational characteristics of the replacement system were fully compatible to support the systems functionality. The inspectors concluded that the post modification testing was inadequate and failed to identify the design vulnerability.

Procedure 81DP-0EE10, Design Change Process, Revision 30, step C.7.12.1.5, requires, in part, that design verification testing demonstrates that Failure logic will trip the component as expected (positive testing) and also that less than the expected failure will not trip the component (negative testing). Contrary to the above, on September 18, 2013, the licensees design verification testing of a main feedwater modification failed to demonstrate that less than the expected failure would not trip the component (negative testing). Specifically, design verification testing of the low-pressure switching logic installed in the main feedwater lube oil control panel protective relay system under design modification Work Order ENG-DMWO 2512314 failed to demonstrate that the component would not spuriously trip without an actual low-pressure signal. In particular, the switching logic response during a loss of power and subsequent restoration of power scenario for the associated electrical bus was not adequately tested at the time of the modification, which resulted in an unexpected trip of the main feedwater system during normal operations.

Corrective Actions: Place trip hazard labeling on the associated breakers to prevent future plant events by recognizing the reactor trip hazard of removing and restoring power to the main feedwater pump lube oil system at-power.

Corrective Action References: 20-02912

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to perform adequate design verification testing for modification Work Order ENG-DMWO 2512314 was a performance deficiency that was within the licensees ability to foresee and correct.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inadequate design verification resulted in a latent vulnerability upon restoration of electrical power to the system that resulted in an automatic trip on March 3, 2020.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. A detailed risk evaluation was required for this finding because it was a condition that caused an automatic reactor scram and the loss of main feedwater. A senior reactor analyst performed the detailed risk assessment and determined that the estimated increase in core damage frequency from the loss of main feedwater event at Palo Verde, Unit 2, on March 3, 2020, was 9.9E-7/year. The analyst applied qualitative factors to the results and to estimate that the significance was of very low safety significance (Green). The full Detailed Risk Assessment is provided as an attachment to this report.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance. The actions of the performance deficiency occurred in 2013 and are not able to be determined as a reliable indicator of current licensee performance.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 17, 2020, the inspectors presented the Unit 2 Inservice inspection results to Mr. Bruce Rash, Vice President, Nuclear Engineering and Regulatory, and other members of the licensee staff.
  • On June 18, 2020, the inspectors presented the Triennial Heat Sink inspection results to Mr. Bruce Rash, Vice President, Nuclear Engineering and Regulatory, and other members of the licensee staff.
  • On July 7, 2020, the inspectors presented the integrated inspection results to Mrs. Maria Lacal, Executive Vice President/Chief Nuclear Officer, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

Condition Reports 20-07013

71111.01

Miscellaneous

Updated Final Safety Analysis Report

71111.01

Miscellaneous

13-MS-A154

Tornado-Borne Missile Impact Analyses for Unprotected

Components

71111.01

Miscellaneous

MN-850-A00001

Design Basis Tornado-Generated Missile Impact Calculation

for U58 Containment Penetration

71111.01

Procedures

01DP-0XX01

Control and Monitoring of Potential Tornado Borne Missiles

71111.01

Procedures

40OP-9ZZ19

Hot Weather Protection

71111.04

Corrective Action

Documents

Condition Reports 20-07332, 20-07538, 20-07585, 20-07955

71111.04

Drawings

01-E-ZPL-002

Power Block Safe Shutdown Emergency Lighting

71111.04

Drawings

01-M-AF-001

P&I Diagram Auxiliary Feedwater System

71111.04

Drawings

01-M-HPP-001

Containment Hydrogen Control

71111.04

Drawings

01-M-SIP-001

P&I Safety Injection & Shutdown Cooling System

71111.04

Miscellaneous

HPDBM

Containment Hydrogen Control System

71111.04

Procedures

31MT-9HP01

Hydrogen Recombiner/Hydrogen Purge Exhaust Air

Filtration Unit Removal and Installation

71111.04

Procedures

2FT-9QD08

Annual Fire Protection Test for QDN-N08

71111.04

Procedures

36ST-9HP01

Hydrogen Recombiner Instrumentation Calibration and

Functional Test

71111.04

Procedures

40EP-9E003

Loss of Coolant Accident

71111.04

Procedures

40EP-9EO10-019

Appendix 19: Containment Hydrogen Control

71111.04

Procedures

40OP-9HP02

Containment Hydrogen Control and Hydrogen Purge

Exhaust System (HP)

71111.04

Procedures

40ST-9SI14

Train B LPSI and CS System Alignment Verification

71111.04

Procedures

41ST-1HP01

Hydrogen Recombiner Functional Test

71111.04

Work Orders

215025

71111.05

Drawings

13-A-ZYD-023

Fire Protection Auxiliary Building Floor Plan

71111.05

Miscellaneous

2-M-AFP-001

Auxiliary Feedwater System

71111.05

Miscellaneous

2-M-RDP-002

Radioactive Waste Drain System

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.05

Miscellaneous

UFSAR Sect 9B

Fire Hazards Analysis

71111.05

Procedures

PVGS Pre-Fire Strategies Manual

71111.05

Procedures

14DP-0FP33

Control of Transient Combustibles

71111.07T

Calculations

13-MC-DG-0411

Diesel Generator (DG) Heat Exchanger Minimum Flow Rate

vs. Inlet SP Water Temperature

71111.07T

Calculations

13-MC-HJ-0003

Control Building HVAC System (HJ) Heat Load and

Equipment Adequacy Calculation

71111.07T

Calibration

Records

Heat Exchanger Test Instrument Calibration - 3MHJAF04

71111.07T

Corrective Action

Documents

Condition Reports 17-14358, 18-01044, 19-02995, 19-03263, 19-10943,

19-11012, 19-12422, 19-13800, 19-13802, 19-13997,

20-01497, 20-05883, 20-07557

71111.07T

Corrective Action

Documents

Resulting from

Inspection

Condition Report

20-08094

71111.07T

Drawings

2-M-SPP-002

P & I Diagram Essential Spray Pond System

71111.07T

Drawings

03-M-HJP-001

P & I Diagram Control Building HVAC

71111.07T

Drawings

13-10407-M721B-

37-3

Cooling Coil for HJA(B) - F04

04/01/1983

71111.07T

Drawings

13-10407-M721B-

38-5

Cooling Coil for HJA(B)

03/09/1987

71111.07T

Drawings

13-M018-00500

Intercoolers & Piping Drawing

71111.07T

Drawings

13-M018-00501

Intercoolers & Piping DWG

71111.07T

Drawings

13-M018-00606

19R CPT Exchanger

71111.07T

Drawings

13-M018-00652

Intercooler Outline Drawing PERFEX 500-L-359

71111.07T

Drawings

13-M018-01298

Tube Layout For Diesel Generator Air Intercoolers

71111.07T

Drawings

M723-10

Refrigeration Machine Outline Drawing

71111.07T

Engineering

Evaluations

4757042

Engineering Evaluation

03/24/2016

71111.07T

Miscellaneous

Closed Cooling Water Chemistry Strategic Plan

71111.07T

Miscellaneous

Essential Spray Pond Water Chemistry Strategic Plan

71111.07T

Miscellaneous

13-MM-723

Water Chillers Specification

71111.07T

Miscellaneous

13-VTD-P162-

PERFEX Industrial Products Installation, Operation and

2/28/1992

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

0001-1

Maintenance Instructions for Heat Transfer Equipment

71111.07T

Miscellaneous

13-VTD-P162-

0002-1

PERFEX Industrial Products Data Sheets and Drawings for

Diesel Generator Intercoolers

2/28/1992

71111.07T

Miscellaneous

73DP-9ZZ21

Heat Exchanger Visual Inspection - Diesel Generator

Intercooler - Right Bank

09/24/2019

71111.07T

Miscellaneous

73DP-9ZZ21

Heat Exchanger Visual Inspection - Diesel Generator

Intercooler - Left Bank

09/23/2019

71111.07T

Miscellaneous

73DP-9ZZ21

3A Jacket Water Cooler Inspection Report

2/27/2017

71111.07T

Miscellaneous

73DP-9ZZ21

3A Jacket Water Cooler Inspection Report

03/04/2019

71111.07T

Miscellaneous

EC System

Design Basis

Manual

Essential Chilled Water System Design Basis Manual

71111.07T

Miscellaneous

ERET 2991102

Essential Chiller Maintenance Template

71111.07T

Miscellaneous

EW System

Design Basis

Manual

Essential Cooling Water System Design Basis Manual

71111.07T

Miscellaneous

Maintenance Rule

Performance

Criteria Basis

Worksheet

Maintenance Rule Performance Criteria Basis Worksheet -

Essential Spray Pond System (SP)

71111.07T

Miscellaneous

System Health

Report - Essential

Spray Pond (SP)

System

System Health Report for Essential Spray Pond (SP)

System from February 1, 2018 through July 31, 2018

2/01/2018 -

07/31/2018

71111.07T

Miscellaneous

System Health

Report - Essential

Spray Pond (SP)

System

System Health Report for Essential Spray Pond (SP)

System from August 1, 2018 through January 31, 2019

08/01/2018 -

01/31/2019

71111.07T

Miscellaneous

System Health

Report - Essential

Spray Pond (SP)

System

System Health Report for Essential Spray Pond (SP)

System from February 1, 2019 through July 31, 2019

2/01/2019 -

07/31/2019

71111.07T

Miscellaneous

System Health

Report - Essential

System Health Report for Essential Spray Pond (SP)

System from August 1, 2019 through January 31, 2020.

08/01/2019 -

01/31/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Spray Pond (SP)

System

71111.07T

Miscellaneous

VTD-1982-00001

ITT Standard Storage, Installation, Operation and

Maintenance of Heat Exchangers

71111.07T

Miscellaneous

VTD-C150-0014

Carrier Application Data for the Condenser and Economizer

71111.07T

Miscellaneous

VTD-C725-00004

Cryogenics Engineering Co. (Formerly CTI Nuclear)

Instructional Manual for the Control Room Essential Air

Handling Units

71111.07T

NDE Reports

19-0783

Eddy Current Examination Report - Unit 2 DGA Intercooler

B

09/23/2019

71111.07T

NDE Reports19-784

Eddy Current Examination Report - Unit 2 DGA Intercooler

A

09/23/19

71111.07T

Work Orders

4660907/0

Testing of the Control Room Emergency Air Temperature

Control System Train A

03/09/2017

71111.07T

Work Orders

4866373/0

Testing of the Control Room Emergency Air Temperature

Control System Train A

11/08/2018

71111.08P` Corrective Action

Documents

Condition Reports 14-00265, 15-00956, 16-18718, 18-10764, 18-12437,

19-09766, 19-10498, 19-10558, 19-11147, 19-11505,

19-11971, 19-11976, 19-12237, 19-13479, 19-13515,

19-13561, 19-13648, 19-14482, 19-14972, 19-15012,

19-15458, 19-15585, 19-17818, 20-00172, 20-02472,

20-02917, 20-03007, 20-03339, 20-03343

71111.08P

Corrective Action

Documents

Resulting from

Inspection

20-05244

71111.08P

Engineering

Changes

DMWO 2513813

Pressurizer Heater Sleeve Replacement

71111.08P

Miscellaneous

20_03 U2M22

BAW Waiver

U2M22 Boric Acid Walk Down Requirements

71111.08P

Miscellaneous

EPID L-2018-

LLR-0028

Safety Evaluation By The Office Of Nuclear Reactor

Regulation Relief Request No. 58

Regarding Certain Class 1 And 2 Welds For The Third 10-

Year Inservice Inspection Interval

2/19/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Arizona Public Service Company Palo Verde Nuclear

Generating Station, Unit 2

Docket No. STN 50-529

71111.08P

Miscellaneous

MRP-058

Materials Reliability Program: Boric Acid Corrosion

Guidebook, Revision 2: Managing Boric Acid Corrosion

Issues at PWR Power Stations

71111.08P

NDE Reports

2-054-010A - 18-

UTE-2014

Ultrasonic Examination Report for Steam Generator

Reducer to Pipe 54-10A

10/17/2018

71111.08P

NDE Reports

20-VE-2024

Visual Examination of Reactor Coolant Instrumentation

Connection 4-99 Cold Leg Connections

04/05/2020

71111.08P

NDE Reports

20-VE-2025

Visual Examination of Reactor Coolant System

Instrumentation Connections

5-36 PZR Heaters Penetrations (36), 5-37 PZR Instrument

Connections (7)

04/05/2020

71111.08P

NDE Reports

20-VE-2026

Visual Examination of Reactor Coolant System

Instrumentation Connections

6-99 Cold Leg Connections, 6-100 RCP Pressure Taps (4

suction Taps) 6-100-1, 6-100-3, 6-100-6, 6-100-7 and 6-101

Hot Leg Instrument Connections (27)

04/05/2020

71111.08P

NDE Reports

20-VT-2027

Visual Examination Report for 2-EWA-E01

04/06/2020

71111.08P

NDE Reports

20-VT-2028

Visual Examination for EWA-E01-W

04/06/2020

71111.08P

NDE Reports

20-VT-2029

Visual Examination of 2-EW-023-H-012

04/06/2020

71111.08P

Procedures

70TI-9ZC01

Boric Acid Walkdown Leak Detection

71111.08P

Procedures

73DP-9WP04

Welding and Brazing Control

71111.08P

Procedures

73DP-9WP05

Welding Filler Material Control

71111.08P

Procedures

73DP-9ZC01

Boric Acid Corrosion Control Program

71111.08P

Procedures

73TI-9ZZ05

Dry Magnetic Particle Examination

71111.08P

Procedures

73TI-9ZZ07

Liquid Penetrant Examination

71111.08P

Procedures

73TI-9ZZ07

Liquid Penetrant Exam

71111.08P

Procedures

73TI-9ZZ10

Ultrasonic Weld Examinations in Ferritic Components

71111.08P

Procedures

73TI-9ZZ17

Visual Examination of Welds, Bolting, and Components

71111.08P

Procedures

73TI-9ZZ18 Rev

Visual Examination of Components Supports

71111.08P

Procedures

73TI-9ZZ19

Visual Examination of Pump and Valve Internal Surfaces

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.08P

Procedures

73TI-9ZZ20

Visual Examination of Reactor Vessel Internals

71111.08P

Procedures

73TI-9ZZ82

Visual Examination of Metal Containment Building Surfaces

71111.08P

Procedures

73WP-0ZZ07

Welding Of Stainless And Nickel Alloys

71111.08P

Procedures

EPRI-PIPE-MPA-

Procedure for Manual Phased Array of Austenitic and

Ferritic Pipe Welds

71111.08P

Procedures

EPRI-PIPE-TWS-

MPA-1

Procedure for Manual Phased Array of Through wall sizing

in Pipe Welds

71111.08P

Self-Assessments 18-14430-002

ISI Self Assessment

04/02/2019

71111.11Q

Corrective Action

Documents

Condition Reports 20-07885, 20-08356

71111.11Q

Miscellaneous

NLR20S030200

Licensed Operator Continuing Training Simulator Scenario

04/22/2020

71111.11Q

Procedures

40DP-9AP09

SG Tube Rupture Technical Guideline

71111.11Q

Procedures

40EP-9EO04

Steam Generator Tube Rupture

71111.11Q

Procedures

40OP-9ZZ05

Power Operations

150

71111.12

Corrective Action

Documents

Condition Reports 20-04986, 20-05952, 18-17794, 20-03809, 20-04152

71111.12

Miscellaneous

0547-20

Quality Receiving Checklist for APN 44400996

71111.12

Miscellaneous

0549-20

Quality Receiving Checklist for APN 44400996

71111.12

Miscellaneous

1836-17

Quality Receiving Checklist for APN 44400996

71111.12

Miscellaneous

20-04152

Maintenance Rule Expert Panel Action Record

05/28/2020

71111.12

Miscellaneous

500614161

Purchase Order Number for APN 44400996

71111.12

Procedures

2DP-0MC46

Receipt Inspection

71111.12

Procedures

2MT-9ZZ74

Molded Case Circuit Breaker Test

71111.12

Procedures

2ST-9ZZ74

Molded Case Circuit Breaker Surveillance Test

71111.12

Procedures

87DP-0MC39

Commercial Grade Dedication (CGD) Process

71111.12

Procedures

93DP-0LC18

Part 21 Reporting Process

71111.12

Work Orders

233686

71111.13

Corrective Action

Documents

Condition Reports 20-05805, 20-05983

71111.13

Drawings

2-P-SIF-105

Containment Building Isometric Safety Injection System

Shutdown Cooling Lines

71111.13

Miscellaneous

Integrated Risk Assessment for CM 5180151

71111.13

Miscellaneous

Switchyard System Health Report Q1-2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.13

Miscellaneous

Schedulers Evaluation for PV Unit 2

05/21/2020

71111.13

Miscellaneous

Palo Verde Unit 2 Operator Logs

05/21/2020

71111.13

Miscellaneous

Unit TWO 22 Refueling Outage Final Shutdown Risk

Assessment

04/02/2020

71111.13

Miscellaneous

EEOS Risk Evaluation for Unit 1, Unit 2, and Unit 3

05/08/2020

71111.13

Miscellaneous

16-15545-004

Engineering Evaluation

11/02/2016

71111.13

Miscellaneous

20-05805

Unit 3 B AFW Pump Risk Evaluation

04/26/2020

71111.13

Procedures

33MT-9ZZ02

Freeze Sealing

71111.13

Procedures

40DP-9OP34

Switchyard Administrative Control

71111.13

Work Orders

4802216, 5180151

71111.15

Corrective Action

Documents

Condition Reports 19-10645, 20-04986, 20-04216, 20-05961, 20-05173,

20-05143, 20-04374, 20-04787, 20-05961, 20-06959,

20-07538, 20-07585, 20-07491, 20-07438

71111.15

Drawings

2-E-CTB-001

Elementary Diagram Condensate Transfer and Storage

System

71111.15

Drawings

2-J-RKS-001

Annunciator / Electronic Isolation List

71111.15

Drawings

2-M-AFP-001

P&I Diagram Auxiliary Feedwater System

71111.15

Drawings

2-M-CTP-001

P&I Diagram Condensate Transfer and Storage System

71111.15

Miscellaneous

Decision Making Basis Summary: Repair Options for

Startup Transformer NAN-X03

04/07/2020

71111.15

Miscellaneous

Zircaloy Fines and the U2 C2 Fuel Receipt

2/26/1988

71111.15

Miscellaneous

13-CN-0393

Technical Specification for the Evaluation and Repair of

Containment Building Liner Plate

04/23/2015

71111.15

Miscellaneous

20-04218-002

Engineering Evaluation

04/24/2020

71111.15

Miscellaneous

20-VT-2072

Visual Examination Report

04/21/2020

71111.15

Miscellaneous

3011469

Palo Verde Action Request

71111.15

Miscellaneous

3017378

Condition Report Disposition Request

71111.15

Miscellaneous

3017381

Condition Report Action Item

71111.15

Miscellaneous

7675R

Product Specification: M5 Zirconium alloy cladding tubes

3.0

71111.15

Miscellaneous

MATBZL09

Westinghouse Electric Company Nuclear Fuel Material

Specification

07/03/2013

71111.15

Miscellaneous

SC 20-03

Safety Communication 20-03 from GE Hitachi

71111.15

Procedures

40DP-9OP26

Operations Condition Reporting Process and Operability

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Determination/Functional Assessment

71111.15

Work Orders

233686, 5235384, 5110882, 5134706

71111.18

Miscellaneous

4689510

Engineering Disposition for CD-1675

71111.18

Miscellaneous

S-16-0094

CFR 50.59 Screening/ Evaluation

71111.18

Procedures

40EP-9EO10-044

Appendix 44: Feeding with the Condensate Pumps

71111.18

Procedures

40OP-9ZZ14

Feedwater and Condensate

71111.18

Work Orders

4689510

71111.19

Corrective Action

Documents

Condition Reports 20-05888, 20-05352

71111.19

Miscellaneous

2309ER.19

Engineering Examination on Clutch - Torque Arm Assembly

P/N CL42030-2 S/N-8

71111.19

Procedures

2MT-9RC03

Reactor Coolant Pump Motor Testing

71111.19

Procedures

36MT-9SG04

Calibrate the Atmospheric Dump Valve (ADV) SG-HV-178

Loop (I&C Portion)

71111.19

Procedures

40OP-9AF01

Essential Auxiliary Feedwater System

71111.19

Procedures

40OP-9RC01

Reactor Coolant Pump Operation

71111.19

Procedures

73DP-0XI03

Check Valve Predictive Maintenance and Monitoring

Program

71111.19

Procedures

73ST-9XI20

ADVs Inservice Test

71111.19

Procedures

73ST-9ZZ25

Check Valve Disassembly, Inspection, and Manual Exercise

71111.19

Procedures

73ST-9ZZ25

Check Valve Disassembly, Inspection, and Manual Exercise

71111.19

Procedures

77ST-9SB13

CPCS Channel A Calibration

71111.19

Work Orders

237596, 5235384, 5231052, 5088215, 5082346, 5188738,

5119759

71111.20

Corrective Action

Documents

Condition Reports 20-04382, 20-04463, 20-04595, 20-04374, 20-04522,

20-04751, 20-04799, 20-04780, 20-04840

71111.20

Miscellaneous

Unit TWO 22 Refueling Outage Shutdown Risk Assessment

Final Report

04/02/2020

71111.20

Miscellaneous

7675R

Letter: Zircaloy Fines and the U2 C2 Fuel Receipt

2/26/1988

71111.20

Miscellaneous

MATBZL09

Seamless low-tin and optimized Zirlo Tubing

71111.20

Procedures

40ST-9ZZ09

Containment Cleanliness Inspection

71111.22

Corrective Action

Documents

Condition Reports 20-07979, 20-07343, 20-07377

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.22

Procedures

36ST-9SB04

PPS Functional Test - RPS/ESFAS Logic

71111.22

Procedures

73ST-9AF05

Auxiliary Feedwater Pump B - Comprehensive Pump Test

71111.22

Procedures

73ST-9CL01

73ST-9CL01

71111.22

Procedures

73ST-9DG08

Class 1E Diesel Generator Load Rejection, 24 Hour Rated

Load and Hot Start Test Train B

71111.22

Procedures

73ST-9EC01

Essential Chilled Water Pumps - Inservice Test

71111.22

Work Orders

5091207, 5087521, 5086899, 5104952

71152

Corrective Action

Documents

Condition Reports 20-01928, 18-02605, 18-08748, 18-10686, 19-11892,

20-01928, 20-02912

71152

Procedures

31MT-9RC23

Reactor Coolant Pump Sulzer Bingham Seal Replacement

71152

Procedures

81DP-0CC28

Classification of Structures, Systems, and Components

71152

Work Orders

5042701

71153

Calculations

Calculation

Number 03-MC-

FP-0008

Hydraulic Analysis of Fire Protection Water System to Unit 3

Power Block Vendor Sprinkler Systems

71153

Engineering

Evaluations

ENG WO #: 20-

2912-015

Perform Risk Assessment of Unit 2 Trip Following

Restoration of Main Feed Pump Lube Oil Control Panel to

Address Safety Significance

04/12/2020

71153

Miscellaneous

Palo Verde Nuclear Generating Station, System Training

Manual, Volume 21, Auxiliary Feedwater (AF)

71153

Miscellaneous

Palo Verde Nuclear Generating Station, System Training

Manual, Volume 41, Chemical and Volume Control System

(CH)

71153

Miscellaneous

Palo Verde Nuclear Generating Station, System Training

Manual, Volume 19, Condensate System (CD)

71153

Miscellaneous

Palo Verde Nuclear Generating Station, System Training

Manual, Volume 20, Feedwater/Feedwater Pump Turbine

System (FW/FT)

71153

Miscellaneous

13-NS-B062

At-Power PRA Study for Human Reliability Analysis

13, 15

71153

Procedures

40EP-9EO01

Standard Post Trip Actions

71153

Procedures

40EP-9EO02

Reactor Trip

71153

Procedures

40EP-9EO06

Loss of All Feedwater

71153

Procedures

40EP-9EO10-038

Appendix 38: Resetting AFA-P01

71153

Procedures

40EP-9EO10-039

Appendix 39: Local Operation of AFB-P01

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71153

Procedures

40EP-9EO10-040

Appendix 40: Local Operation of AFA-P01 Using Main

Steam

71153

Procedures

40EP-9EO10-041

Appendix 41: Local Operation of AFN-P01

71153

Procedures

40EP-9EO10-042

Appendix 42: Aligning Essential Aux Feedwater Pumps

Suction to RMWT

71153

Procedures

40EP-9EO10-043

Appendix 43: Restarting MFPs

71153

Procedures

40EP-9EO10-044

Appendix 44: Feeding With the Condensate Pumps

71153

Procedures

40EP-9EO10-112

Appendix 112: Manual Operation of AFA-P01 During a

Security Event

2

71153

Procedures

40EP-9EO10-118

Appendix 118: Cross-Connect FP to AF

Detailed Risk Evaluation

Palo Verde, Unit 2, Loss of Main Feedwater

Conclusion: The estimated increase in core damage frequency from the loss of main

feedwater event at Palo Verde, Unit 2, on March 3, 2020, was 9.9E-7/year. The analyst applied

qualitative factors to the results and to estimate that the significance was of very low safety

significance (Green). This detailed risk evaluation was reviewed by a reliability and risk analyst

from the Office of Nuclear Reactor Regulation.

A. NRC Internal Events Analysis

Influential Assumptions: The following are model inputs which were discovered during conduct

of the detailed risk evaluation, which the licensee raised, or were assumptions which the final

risk estimate was sensitive to:

1. Recovery of the Main Feedwater (MFW) System

For the March 3, 2020, loss of MFW (LOMFW) event at Palo Verde, Unit 2, the analyst

determined that the failure was recoverable. The analyst, along with a license examiner,

reviewed the applicable procedures and interviewed three senior reactor operators at the

station. The analyst also reviewed the applicable human reliability analysis (HRA)

calculation performed by Palo Verde personnel and documented in Engineering Work

Order 20-02912-015, Perform risk assessment of Unit 2 trip following restoration of

Main Feed Pump Lube Oil Control Panel to address safety significance, dated April 12,

20. In this HRA calculation, Basic Event 1MFW-RECOVERHR, Operations fails to

recover Main Feedwater after an uncomplicated reactor trip, licensee PRA personnel

estimated a failure probability of 5.64E-2 (or a success rate of 94.4 percent) of

operators.

Since the SPAR model did not contain a recovery event, the analyst consulted with INL

to modify the Palo Verde SPAR model to incorporate recovery of the MFW pumps. The

analyst then performed an independent HRA calculation using the SPAR-H HRA

methodology. By procedure, recovery of MFW would be the first choice of operators for

the case where auxiliary feedwater (AFW) was unavailable due to random failures.

Operators would be tasked with performing enough troubleshooting to gain confidence

that recovering the MFW system was a viable strategy. The analyst applied an available

but poor rating to the performance shaping factors (PSF) for diagnosis and kept all other

PSFs as nominal. These factors yielded a failure probability of 5.1E-2 for MFW recovery

via the SPAR-H methodology.

2. Failure rate of Class 1E bus failures

Two of the basic events (ACP-ICC-FC-ESFA, Spurious Electrical Protection on Train A

ESF Bus Locks Out All Power Sources, and ACP-ICC-FC-ESFB, Spurious Electrical

Protection on Train B ESF Bus Locks Out All Power Sources) which were present in

some of the core damage cutsets are instrumentation and control failures associated

with the Class 1E buses. The licensees PRA model contains these failure events which

represent an occurrence at Palo Verde where the load sequencer load shed feature

locked in and would not allow any electrical equipment to be loaded and powered from a

Class 1E bus. The licensee modeled the failure probability at 6.5E-6.

The SPAR model contains a similar event estimated at 1.70E-3. The analyst noted that

the failure probability of 1.70E-3 of these events was derived from data from a 1989

Westinghouse Savannah River Site parameter report for generic failures of

instrumentation and controls equipment. The analyst discussed with INL the possibility

of a more representative value and so based on the failure occurrence and operating

history, a value of 2.61E-5 was used.

3. Condensate system dependency on the Condensate Storage Tank (CST)

The analyst noted that the SPAR model failed the condensate system and therefore

MFW recovery and condensate injection mitigative strategies when the CST failed. The

licensee noted that these strategies would remain available in this case because their

inventory source would be the main condenser which remained available for LOMFW

events. To remove this dependency, the analyst removed the pertinent cutset(s) from

the results.

Core Damage Risk Metric Estimate: The analyst incorporated these changes and estimated the

incremental conditional core damage probability (ICCDP) in accordance with Section 08.02,

Treatment of Degraded Conditions and Initiating Events, of NRC Inspection Manual Chapter 0308, Attachment 3, Significance Determination Process Technical Basis, Issue date June 16,

2016. The manual chapter prescribes estimating ICCDP using the following formula:

ICCDP = CCDP - Baseline CDP

To estimate the CCDP, the analyst ran an initiating event analysis in accordance with

Section 8.0, Initiating Events Analyses, from the Risk Assessment of Operational Events

Handbook, Volume 1, Internal Events, Revision 2.02. Specifically, for analyst referred to

Section 8.2, Case 1 - Initiating Event Only, and set the loss of main feedwater event to 1.0

and all other initiating events to 0.0. From this run, the CCDP was estimated as:

CCDP = 1.06E-6

The baseline core damage probability was estimated using the nominal initiating event

frequency and nominal failure probabilities of all other components. The baseline CDP was

estimated as:

Baseline CDP = 7.0E-8

The analyst then obtained the ICCDP as follows:

ICCDP = CCDP - Baseline CDP

ICCDP = 1.06E-6 - 7.0E-8

ICCDP = 9.9E-7

This ICCDP value was multiplied by one inverse year to equate the ICCDP to an increase in

core damage frequency of 9.9E-7/year.

Analysis Data: The analyst used Palo Verde SPAR model version PVNG-EQK-HWD-FLEX-

LOMFW-DEESE, which contains modifications described in the sections above to model

version 8.61, run on SAPHIRE, software version 8.2.1, for the evaluation. Truncation of 1E-11

was used in all analyses.

B. Licensees Internal Events Results

The analyst requested that the licensee perform a LOMFW analysis with and without MFW

recovery on their model(s). The results are shown in the table below:

LOMFW without MFW recovery

LOMFW with MFW recovery

All hazards model

1.3E-7

3.8E-8

EOOS model (fire water

injection not credited)

9.1E-7

7.8E-8

The SPAR model can replace INL derived industry failure rates data with the failure rates that

Palo Verde uses in their model. The analyst exercised this option as a sensitivity with the same

assumptions related to recovery events and the SPAR model estimated the CCDP to be 1.5E-7.

Also, the licensee has a copy of the NRCs SPAR model which they reviewed and submitted

paper, Recommended SPAR model Adjustments, Palo Verde Unit 2 March 2020 LOMFW

Event, to the analyst on May 15, 2020. The probabilistic risk assessment group at Palo Verde

reviewed the SPAR model results and provided recommended adjustments to the SPAR model

to better reflect the LOMFW event and the systems they considered available to respond to the

event. These adjustments were:

Crediting MFW recovery: Like the influential assumption in the NRC internal events

analysis, the licensee considered that the MFW was recoverable after the March

LOMFW event. The licensee estimated a human error probability for MFW of 5.64E-2

using their human reliability analysis tool. The analyst estimated a similar value of

5.1E-2 in the NRC internal events section above.

Changing the failure probability of Basis Event AFW-XHE-XM-XFRRMWTTK: This basic

event models the failure of operators to transfer AFW pumps suction to the reactor

makeup water tank (RMWT) on loss of the CST. Its human error probability in the SPAR

model was 1.0E-1. The licensee proposed changing the value to the product of the

MFW recovery human error probability (5.64E-2) and the condensate injection human

error probability (3.0E-1) which was 1.69E-2. The licensee cited that these strategies

would still be available because they are dependent on the condenser hotwell, not the

CST as their inventory source.

The analyst reviewed this dependency and made the change describe in Item (3) of the

Influential Assumptions section of the NRCs internal events analysis described above

in lieu of the licensees proposed change.

Setting Basic Event CDS-XHE-XM-2HRs to 0.0: This event assumes that the MFW

system trips and no longer feeds the steam generators 30 minutes after the reactor trip.

The licensee proposed that since for the event on March 3, 2020, MFW was lost at the

time of the reactor trip, this basic event should be set to 0.0 thereby eliminating a

condition that did not occur.

The analyst consulted with INL on Basic Event CDS-XHE-XM-2HRS and the overall

recovery of a LOMFW condition in the SPAR model. From this a model change was

incorporated and new model version PVNG-EQK-HWD-FLEX-LOMFW-DEESE was

created changing this basic event to CDS-XHE-XM-LATE to reflect that this term was

also for late recovery of AFW pumps failing to run. Thus, this change was not made for

this evaluation.

Finally, in conversations with the licensee during the estimation of the ICCDP for this event, the

analyst noted the following topics which the analyst subsequently reviewed.

Use of fire water injection into a depressurized steam generator: The final available

method of feeding water into a steam generator is using a diesel driven fire water pump

to feed a depressurized steam generator. This steam generator feeding strategy is

modeled in the licensees model, but not in the SPAR model. Of note, the licensee did

credit this strategy in their risk evaluation for the 62-day emergency diesel generator

allowed outage time amendment in December 2016. The analyst noted two HRA events

in licensee documentation, 1AF-FP-BACKUP-HL, Operator Fails to Align FP to feed

SGs via AFN flowpath, from calculation 13-NS-B062, At-Power PRA Study for Human

Reliability Analysis, and 1AF-FLEX-SGHR-HL, Operator Fails to Align FP to AF cross-

connect to feed SG, from Letter 102-07411-MLL/TNW, Emergency License

Amendment Request to Extend Diesel Generator 3B Completion Time. When asked by

the analyst, the licensee replied these HRA events reflected the same action. The

analyst therefore reviewed the information from 1AF-FLEX-SGHR-HL since it was the

more recent of the two when analyzing. The calculation documents a 38 minute delay

time, a 20 minute execution time, and an available time window of 75 minutes. The

analyst considered these and judged that there would be barely enough time when

analyzing per the SPAR-H methodology. Also, the analyst considered that stress would

be high because this strategy would be the last available method of feeding steam

generators. The SPAR-H analysis estimated a failure rate of 5.05E-1. Next, the analyst

considered that the actions were close in time by the same crew which would yield at

least high dependency. These factors yielded a failure rate of 7.5E-1. Because this was

such a high failure rate and because dependency could have been considered complete,

the analyst did not credit this strategy. The analyst did however consider the possibility

of some success as a qualitative factor.

C. External Events Analysis

The analyst noted that this detailed risk assessment evaluates an actual event in which no

external events occurred. Additionally, the period of time that the events impacted plant

equipment was small enough that the probability of an external initiator occurring during this

time would be negligible. Therefore, the analyst assumed that the risk from external events,

given the subject performance deficiency was essentially zero. The licensee came to the same

conclusion external events analysis.

D. Large Early Release Frequency

The increase in large early release frequency from this finding was determined to be of very low

safety significance using Manual Chapter 0609, Appendix H, Containment Integrity Significance

Determination Process, because LOMFW sequences screen as having low safety significance

in pressurized water reactors with large dry containments.

Also, the analyst considered the possibility of consequential steam generator tube ruptures

using the draft guidance of Volume 5, Risk Analysis of Containment-Related Events (LERF), of

the RASP Handbook. Applying this guidance, the analyst estimated that the ICLERP was

1.4E-7. This value contains known conservatisms and is realistically lower when risk-informing

with qualitative factors. First, the same qualitative factors discussed for the estimate of the

increase in core damage frequency in section G below would also be relevant to the ICLERP

estimate. Additionally, the assumption of the release path to the environment in Volume 5 of the

RASP Handbook is conservative. Finally, the evaluation does not consider evacuation

effectiveness or differentiate between early and late releases which would qualitatively lower the

ICLERP estimate. Given the performance deficiency does not challenge or question the steam

generator tube integrity, further evaluation of the consequential steam generator tube rupture

results would support a very low safety significance.

E. Uncertainties

The analyst performed an uncertainties analysis on the results of the SPAR model in SAPHIRE

by running 5000 cases in a Monte Carlo analysis as allowed by SAPHIRE. The results

produced a distribution of outcomes with a point estimate of ICCDP of 1.0E-6. The median

case had an estimate of 5.5E-7. The analyst considered this skew towards lower values in the

determination of final significance.

F. Sensitivities

The analyst performed the sensitivity runs in the table below to evaluate potentially influential

factors of the evaluation.

Sensitivity

Action

Result

Removing possibility of a

consequential LOOP

Set OEP-VCF-LP-CLOPT equal to 0.0

3.7E-7

Class 1E bus lockout frequency

set to licensees value

Set ACP-ICC-FC-ESFA and -ESFB equal to

6.5E-6

1.0E-6

Class 1E bus lockout frequency

set to SAPR baseline value

Set ACP-ICC-FC-ESFA and -ESFB equal to

1.7E-3

2.0E-6

Zero test and maintenance

Ran events and condition assessment with

no test and maintenance selected

4.7E-7

Give higher success rate for

TDAFW pump operation

without DC power

Set AFW-XHE-XM-CNTRL equal to 1.0E-1

8.9E-7

Use only motor driven pumps in

common cause failure group for

AFW pumps

Set AFW-PMP-CF-FR equal to 0.0

9.6E-7

G. Qualitative Considerations

The analyst noted several qualitative considerations which were unable to be quantified and that

were used to inform the numerical estimate. They were:

Some credit for fire water injection into a depressurized steam generator could be given.

While the timing for accomplishing fire water injection was barely adequate for scenarios

where all AFW was unavailable at the beginning of the postulated core damage

sequences used in this evaluation, some credit could be considered for scenarios where

the AFW pumps run for part of their 24-hour mission time. This AFW run time would

allow more time to align fire water injection and increase the probability of its success as

a mitigative strategy.

The licensee, like many licensees, typically does not perform current maintenance

activities on similar systems. This would lower the likelihood of the licensee attempting

the recovery of the MFW panel restoration concurrently with AFW system maintenance.

Several cutsets in the results with AFW test and maintenance terms could eliminated,

lowering the increase in core damage frequency for this event.

Long-term failures-to-run of the AFW pumps were not fully modeled. For example, if an

AFW pump failed to run at 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, an additional 1 to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> would be available for

operators to employ the condensate injection strategy and therefore the failure rate of

this strategy would be lower. This effect would lower the overall increase in core

damage frequency.