IR 05000424/1980015
| ML19290G678 | |
| Person / Time | |
|---|---|
| Site: | Vogtle |
| Issue date: | 10/28/1980 |
| From: | Bryant J, Hunt M, Vandoorn P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML19290G677 | List: |
| References | |
| 50-424-80-15, 50-425-80-15, NUDOCS 8012180289 | |
| Download: ML19290G678 (3) | |
Text
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pm alcug'o UNITED STATES
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s REGION 11
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101 M ARlETTA ST.. N W.. SUITE 3100
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ATLANTA, GEORGI A 30303
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Report Nos. 50-424 and 50-425 Licensee:
Georgia Power Company 270 Peachtree Street Atlanta, GA 30303 Facility Name:
Plant Vogtje Docket Nos. 50-424 and 50-425 License Nos. CPPR-108 and CPPR-109 Inspection at Vogtle site near Waynesboro, GA Inspectors:
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M. D. Hunt D6te digned
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Date,6igned
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's Approved by:
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J.,0 (Bryhnt, Sec don Chief, BRC&ES Branch Date Signed d
j SDiMARY Inspection on September 29 - October 1, 1980 Areas Inspected This routine announced inspection involved 36 inspector-hours onsite in the areas of equipment storage, piping contractor facilities, nonconforming reports and surface water control.
Results Of the four areas inspected, no items of noncompliance or deviations were iden-tified.
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DETAILE 1.
Perso-atacted Licensee Employees
- D. M. Fiquett, Manager of Field Operations
- E. D. Groover, QA Site Supervisor
- M. H. Googe, Mechanical QC Supervisor Other licensee employees contacted included 6 construction craftsmen and 3 office personnel.
Other Organizations Bechtel Power Corporation (BPC)
- D. P. Armstrong, Resident Engineer - Civil
- D. M. Ryan, Resident Engineer, Plant Design Walsh Construction Company (WCC)
G. S. Wisen, QC Coordinator
- F. R. McCarty, Project Manager
- Attended exit interview.
2.
Exit Interview The inspection scope and findings were summarized on October 1, 1980 with those persons indicated in Paragraph I above.
3.
Licensee Action on Previous Inspection Findings Not inspected.
4.
Unresolved Items Unresolved items were not identified during this inspection.
5.
Independent Inspection Effort The inspectors toured the vessel storage, rebar storage and piping storage areas to examine the condition of equipment stored in these areas. These areas appear to be well maintained and the drainage is adequate. The reactor vessels for both units are adequately protected. The vessel heads are stored in specially constructed sheds well above ground level.
Equipment stored at the various levels in the warehouse was examined. The storage requirements for levels A, B, and C were being me.
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Prior to and during this inspection, several inches of rain had fallen. In view of the licensee's difficulties with surface water runoff and resulting damage to Class I backfill, the inspectors examined various areas where backfill had been placed to determine that adequate control of surface water was being maintained.
There were no areas along the slopes that appeared to be dislodging due to surface water runof f.
The inspectors reviewed mechanical contractor's plae for coordination with GPC's A-E to insure that all data required for installation drawings is entered and reviewed before the drawings are released to the field. A tour of the weld test facilities was made.
The facility appears adequately staffed to insure proper evaluation of welders.
Within the areas examined no items of noncompliance or deviations were identified.
6.
Review of Nonconforming Reports The inspectors reviewed various nonconformance Reports (NCR's) to determine if adequate and timely corrective actions were taken and if adequate review had been provided to determine reportability in accordance with 10 CFR 50.55(e).
NCR's reviewed included CD-830, 839, 924, 935, 937, 938, 948, 986, 988, 1000, 1008, 1009, 1013, and 1030; and MD-457, 458, 461, 462, 468, 480, 491, 495, 503, 508, 509, 510, 513, 519, 539, 581, 599, 606, 607, and 654.
During this review, the inspectors noted that at least 16 NCR's had been written concerning defects in structural steel received from Ingalls Iron Works.
The inspectors questioced whether these defects were indicative of a breakdown in the vendor's QA program and should be reported in accordance with 10 CFR 50.55(e).
Site personnel indicated that an audit would be performed at the vendor's facility during November 1980, to determine the cause of the defects.
Until completed licensee actions concerning this item can be fully reviewed by NRC this will be Inspector Followup Item No.
50-424/425/80-15-01 " Review of licensee actions concerning defective struc-tural steel".
7.
Licensee Identified Items (LII) 10 CFR 50.55(e)
(Open) LII 424/80-15-02, Hydrogen recombiner power transformer. The licensee received a letter from the NSSS supplier that advised them that one power supply for the H2 recombiner contained an unqualified transformer.
The letter advised GPC that this was the only unit shipped and action is under-way to replace the unqualified unit and to correct the quality assurance plan in the area of equipment specifications.
(Closed) LII, 424/80-12-02, Collapse of Cooling Tower 1A Rebar Steel. The inspectors reviewed the actions taken by the licensee to prevent the recur-rence of the activities leading to this type of problem. The repair proce-dures have been outlined with hold points established.